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Category:Letter
MONTHYEARIR 05000327/20240102024-12-19019 December 2024 Design Basis Assurance Inspection (Programs) Inspection Report 05000327/2024010 and 05000328/2024010 CNL-24-009, Brown Ferry Nuclear Plant, Units 1, 2 & 3; Sequoyah Nuclear Plant, Units 1 & 2 and Watts Bar Plant, Units 1 & 2 - Triennial Decommission Funding Plans for Independent Spent Fuel Storage Installations2024-12-17017 December 2024 Brown Ferry Nuclear Plant, Units 1, 2 & 3; Sequoyah Nuclear Plant, Units 1 & 2 and Watts Bar Plant, Units 1 & 2 - Triennial Decommission Funding Plans for Independent Spent Fuel Storage Installations CNL-24-082, Central Emergency Control Center Emergency Plan Implementing Procedure Revision2024-12-17017 December 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revision ML24337A1922024-12-0202 December 2024 Discharge Monitoring Report (Dmr), May 2024 ML24337A1952024-12-0202 December 2024 Discharge Monitoring Report (Dmr), August 2024 ML24337A1942024-12-0202 December 2024 Discharge Monitoring Report (Dmr), July 2024 ML24337A1972024-12-0202 December 2024 Discharge Monitoring Report (Dmr), October 2024 CNL-24-075, Response to Request for Additional Information for Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah and Watts Bar (SQN-TSTS-23-02 and W2024-11-27027 November 2024 Response to Request for Additional Information for Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah and Watts Bar (SQN-TSTS-23-02 and WBN CNL-24-073, Request for Exemption from Requirements of 10 CFR 26.205, Fitness for Duty Programs - Work Hours2024-11-27027 November 2024 Request for Exemption from Requirements of 10 CFR 26.205, Fitness for Duty Programs - Work Hours CNL-24-071, Expedited Application to Revise Technical Specifications to Revise the Reactor Coolant System Pressure Isolation Valve Leakage Testing Frequency for the (SQN-TS-24-04)2024-11-26026 November 2024 Expedited Application to Revise Technical Specifications to Revise the Reactor Coolant System Pressure Isolation Valve Leakage Testing Frequency for the (SQN-TS-24-04) 05000327/LER-2024-002, Reactor Trip Due to a Turbine Trip2024-11-20020 November 2024 Reactor Trip Due to a Turbine Trip CNL-24-021, Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020)2024-11-12012 November 2024 Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020) ML24312A1552024-11-0606 November 2024 Cycle 27 Core Operating Limits Report, Revision 1 IR 05000327/20240032024-11-0606 November 2024 Integrated Inspection Report 05000327/2024003 and 05000328/2024003 CNL-24-014, License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22)2024-11-0404 November 2024 License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22) ML24304A8492024-10-31031 October 2024 December 2024 Requalification Inspection Notification Letter IR 05000327/20250102024-10-29029 October 2024 Notification of Sequoyah, Units 1 and 2 - Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000327/2025010 and 05000328/2025010 ML24298A1172024-10-24024 October 2024 Cycle 26, 180-Day Steam Generator Tube Inspection Report CNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000327/LER-2024-001, Reactor Trip Due to a Turbine Trip2024-10-17017 October 2024 Reactor Trip Due to a Turbine Trip ML24282B0412024-10-15015 October 2024 Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 ML24260A1682024-10-0404 October 2024 Regulatory Audit Summary Related to Request to Add and Revise Notes Related to Technical Specification Table 3.3.2-1, Function 5 ML24284A1072024-09-26026 September 2024 Affidavit for Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2 05000328/LER-2024-001, Reactor Trip Due to an Electrical Trouble Turbine Trip2024-09-25025 September 2024 Reactor Trip Due to an Electrical Trouble Turbine Trip CNL-24-047, Decommitment of Flood Mode Mitigation Improvement Systems2024-09-24024 September 2024 Decommitment of Flood Mode Mitigation Improvement Systems CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan ML24267A0402024-09-19019 September 2024 Cycle 27 Core Operating Limits Report Revision 0 ML24185A1742024-09-18018 September 2024 Cover Letter - Issuance of Exemption Related to Non-Destructive Examination Compliance Regarding Sequoyah Nuclear Plant Independent Spent Fuel Storage Installation CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24253A0152024-09-0808 September 2024 Emergency Plan Implementing Procedure Revisions ML24247A2212024-08-29029 August 2024 Notification of Deviation from Pressurized Water Reactor Owners Group (PWROG) Letter OG-21-160, NEI 03-08 Needed Guidance: PWR Lower Radial Support Clevis Insert X-750 Bolt Inspection Requirements, September 1, 2021 ML24247A1802024-08-28028 August 2024 Application to Revise the Fuel Handling Accident Analysis, to Delete Technical Specification 3.9.4, Containment Penetrations, and to Modify Technical Specification 3.3.6, Containment Ventilation Isolation Instrumentation for Sequoyah Nuclea IR 05000327/20240052024-08-26026 August 2024 Updated Inspection Plan for Sequoyah Nuclear Plant, Units 1 and 2 - Report 05000327/2024005 and 05000328/2024005 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 CNL-24-061, Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08),2024-08-19019 August 2024 Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08), IR 05000327/20240022024-07-31031 July 2024 Integrated Inspection Report 05000327/2024002 and 05000328/2024002 ML24211A0572024-07-29029 July 2024 Submittal of Emergency Plan Implementing Procedure Revision ML24211A0542024-07-29029 July 2024 Operator License Examination Report ML24211A0412024-07-26026 July 2024 Unit 1 Cycle 26 Refueling Outage - 90-Day Inservice Inspection Summary Report ML24199A0012024-07-22022 July 2024 Clarification and Correction to Exemption from Requirement of 10 CFR 37.11(c)(2) ML24172A1342024-07-15015 July 2024 Exemptions from 10 CFR 37.11(C)(2) (EPID L-2023-LLE-0024) - Letter ML24191A4652024-07-0909 July 2024 Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24177A0282024-06-25025 June 2024 Emergency Plan Implementing Procedure Revisions ML24176A0222024-06-24024 June 2024 Retraction of Interim Report of a Deviation or Failure to Comply – Transducer Model 8005N ML24089A1152024-06-21021 June 2024 Transmittal Letter, Environmental Assessments and Findings of No Significant Impact Related to Exemption Requests from 10 CFR 37.11(c)(2) ML24145A0852024-05-30030 May 2024 1B-B Diesel Generator Failure - Final Significance Determination Letter ML24145A1052024-05-29029 May 2024 301 Exam Approval Letter ML24134A1762024-05-13013 May 2024 Submittal of 2023 Annual Radiological Environmental Operating Report CNL-24-040, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-05-0808 May 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 2024-09-08
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000327/LER-2024-002, Reactor Trip Due to a Turbine Trip2024-11-20020 November 2024 Reactor Trip Due to a Turbine Trip 05000327/LER-2024-001, Reactor Trip Due to a Turbine Trip2024-10-17017 October 2024 Reactor Trip Due to a Turbine Trip 05000328/LER-2024-001, Reactor Trip Due to an Electrical Trouble Turbine Trip2024-09-25025 September 2024 Reactor Trip Due to an Electrical Trouble Turbine Trip 05000328/LER-2023-001, Inoperable Ice Condenser Intermediate Deck Doors Results in Condition Prohibited by Technical Specifications2023-06-0707 June 2023 Inoperable Ice Condenser Intermediate Deck Doors Results in Condition Prohibited by Technical Specifications 05000327/LER-2022-002, Turbine Trip Function Inoperable Due to Slow to Close Turbine Throttle Valve2022-12-15015 December 2022 Turbine Trip Function Inoperable Due to Slow to Close Turbine Throttle Valve 05000327/LER-2022-001, Regarding Failure of 1B-B Centrifugal Charging Pump Results in Condition Prohibited by Technical Specifications2022-09-15015 September 2022 Regarding Failure of 1B-B Centrifugal Charging Pump Results in Condition Prohibited by Technical Specifications 05000328/LER-2021-002, Turbine Trio Function Inoperable Due to Slow to Close Turbine Throttle Valve2022-01-0606 January 2022 Turbine Trio Function Inoperable Due to Slow to Close Turbine Throttle Valve 05000327/LER-2021-003, Exceeded Breach Margin Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable2021-10-19019 October 2021 Exceeded Breach Margin Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable 05000328/LER-2021-001, Ice Bed Inoperable Due to Exceeding Surveillance Requirement Frequency2021-09-22022 September 2021 Ice Bed Inoperable Due to Exceeding Surveillance Requirement Frequency 05000327/LER-2021-001, Sequoya Nuclear Plant, Unit 1, Reactor Trip on High Neutron Flux Rate Due to Dropped Control Rods2021-07-21021 July 2021 Sequoya Nuclear Plant, Unit 1, Reactor Trip on High Neutron Flux Rate Due to Dropped Control Rods 05000328/LER-2020-001, Ice Bed Inoperable Due to Exceeding Maximum Allowed Ice Bed Temperature2020-09-16016 September 2020 Ice Bed Inoperable Due to Exceeding Maximum Allowed Ice Bed Temperature 05000327/LER-2020-002, Safety Injection Signal with Reactor Trip Caused by a Failure with the Main Turbine Control System2020-07-0101 July 2020 Safety Injection Signal with Reactor Trip Caused by a Failure with the Main Turbine Control System 05000327/LER-2019-003-01, 1 for Sequoyah Nuclear Plant, Unit 1, Automatic Reactor Trio Due to Negative Rate Trip as a Result of a Dropped Control Rod2020-04-25025 April 2020 1 for Sequoyah Nuclear Plant, Unit 1, Automatic Reactor Trio Due to Negative Rate Trip as a Result of a Dropped Control Rod 05000327/LER-2020-001-01, 1 for Sequoyah Nuclear Plant, Unit 1, Containment Vacuum Relief Lines Found Isolated2020-03-20020 March 2020 1 for Sequoyah Nuclear Plant, Unit 1, Containment Vacuum Relief Lines Found Isolated 05000327/LER-2019-004, Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board2020-02-13013 February 2020 Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board 05000328/LER-2019-002, Loss of Heater Drain Tank Flow Causes Turbine Runback and Manual Reactor Trip2020-02-0707 February 2020 Loss of Heater Drain Tank Flow Causes Turbine Runback and Manual Reactor Trip 05000328/LER-2019-001, Component Cooling Water System Train a Inoperable Longer than Allowed by Technical Specifications2019-11-15015 November 2019 Component Cooling Water System Train a Inoperable Longer than Allowed by Technical Specifications 05000327/LER-2019-003, Automatic Reactor Trip Due to Negative Rate Trip as a Result of a Dropped Control Rod2019-10-23023 October 2019 Automatic Reactor Trip Due to Negative Rate Trip as a Result of a Dropped Control Rod 05000327/LER-2019-002, Regarding Steam Generator Pressure Transmitter Degraded Sensing Line Causes Condition Prohibited by Technical Specifications2019-07-26026 July 2019 Regarding Steam Generator Pressure Transmitter Degraded Sensing Line Causes Condition Prohibited by Technical Specifications 05000327/LER-2019-001, Reactor Trip on Low-Low Steam Generator Level Due to the Loss of a Main Feedwater Pump2019-06-11011 June 2019 Reactor Trip on Low-Low Steam Generator Level Due to the Loss of a Main Feedwater Pump 05000327/LER-2018-002, Exceeded Breach Margin Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable2019-01-22022 January 2019 Exceeded Breach Margin Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable 05000327/LER-2018-001, Inadequate Post Maintenance Testing Results in Condition Prohibited by Technical Specifications2018-09-18018 September 2018 Inadequate Post Maintenance Testing Results in Condition Prohibited by Technical Specifications 05000327/LER-1917-002, Regarding Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board2017-07-14014 July 2017 Regarding Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board 05000327/LER-1916-009-01, Regarding Manual Reactor Trip During Startup Due to a Control Rod Misalignment2017-05-0505 May 2017 Regarding Manual Reactor Trip During Startup Due to a Control Rod Misalignment 05000327/LER-1917-001, Regarding Breached Door Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable2017-04-26026 April 2017 Regarding Breached Door Renders Both Trains of the Auxiliary Building Gas Treatment System Inoperable 05000327/LER-2016-009, Regarding Manual Reactor Trip During Startup Due to a Control Rod Misalignment2017-02-27027 February 2017 Regarding Manual Reactor Trip During Startup Due to a Control Rod Misalignment 05000327/LER-2016-008, Regarding Closed Fire Damper Renders Both Trains of the Control Room Emergency Ventilation System Inoperable2016-10-0707 October 2016 Regarding Closed Fire Damper Renders Both Trains of the Control Room Emergency Ventilation System Inoperable 05000327/LER-2016-004-01, Regarding Emergency Diesel Generator Fire Dampers and Crankcase Pressure Switches Not Analyzed for Withstanding the Effects of a Tornado2016-10-0303 October 2016 Regarding Emergency Diesel Generator Fire Dampers and Crankcase Pressure Switches Not Analyzed for Withstanding the Effects of a Tornado 05000327/LER-2016-007, Regarding Unanalyzed Condition Due to Emergency Gas Treatment System Not Meeting Single Failure Criteria2016-10-0303 October 2016 Regarding Unanalyzed Condition Due to Emergency Gas Treatment System Not Meeting Single Failure Criteria 05000327/LER-2016-006, Regarding Improper Calibration of Reactor Trip Instrumentation Results in Condition Prohibited by Technical Specifications2016-09-12012 September 2016 Regarding Improper Calibration of Reactor Trip Instrumentation Results in Condition Prohibited by Technical Specifications 05000327/LER-2016-005, Regarding Hydrogen Mitigation System Train a Inoperable Longer than Allowed by Technical Specifications2016-08-17017 August 2016 Regarding Hydrogen Mitigation System Train a Inoperable Longer than Allowed by Technical Specifications 05000327/LER-2016-004, Regarding Emergency Diesel Generator Fire Dampers and Crankcase Pressure Switches Not Analyzed for Withstanding the Effects of a Tornado2016-07-15015 July 2016 Regarding Emergency Diesel Generator Fire Dampers and Crankcase Pressure Switches Not Analyzed for Withstanding the Effects of a Tornado 05000327/LER-2016-003, Regarding Control Room Door Unable to Close Causes Inoperable Control Room Envelope2016-07-0505 July 2016 Regarding Control Room Door Unable to Close Causes Inoperable Control Room Envelope 05000327/LER-2016-001, Regarding Automatic Safety Injection Due to Low Steam Line Pressure on Loop 2 Main Steam2016-04-11011 April 2016 Regarding Automatic Safety Injection Due to Low Steam Line Pressure on Loop 2 Main Steam 05000327/LER-2015-004, Regarding Manual Reactor Trip Due to Main Steam Isolation Valve Drifting in the Closed Direction2016-01-22022 January 2016 Regarding Manual Reactor Trip Due to Main Steam Isolation Valve Drifting in the Closed Direction 05000328/LER-2015-002, Regarding Unanalyzed Condition Due to Inoperable Containment Recirculation Drains2016-01-0606 January 2016 Regarding Unanalyzed Condition Due to Inoperable Containment Recirculation Drains 05000327/LER-2015-003, Regarding Manual Reactor Trip Due to Loss of Power to the Vital Instrument Power Board 1-II2015-11-13013 November 2015 Regarding Manual Reactor Trip Due to Loss of Power to the Vital Instrument Power Board 1-II 05000327/LER-2015-002, Regarding Automatic Reactor Trips Due to Improper Wire Termination in Main Generator Voltage Regulator Circuit2015-09-22022 September 2015 Regarding Automatic Reactor Trips Due to Improper Wire Termination in Main Generator Voltage Regulator Circuit 05000327/LER-2015-001, Regarding Automatic Reactor Trip Due to Negative Rate Trip as a Result of a Dropped Control Rod2015-05-11011 May 2015 Regarding Automatic Reactor Trip Due to Negative Rate Trip as a Result of a Dropped Control Rod 05000328/LER-2015-001, Regarding Automatic Reactor Trip Due to Failure of Main Generator C-Phase Neutral Current Transformer Cable2015-05-0101 May 2015 Regarding Automatic Reactor Trip Due to Failure of Main Generator C-Phase Neutral Current Transformer Cable 05000328/LER-2014-002, Regarding Containment Vacuum Relief Valve Inoperable Resulting in a Condition Prohibited by Technical Specifications2014-08-22022 August 2014 Regarding Containment Vacuum Relief Valve Inoperable Resulting in a Condition Prohibited by Technical Specifications 05000327/LER-2014-002, Regarding Lack of Administrative Controls for Some Containment Penetrations During Fuel Movement Results in Condition Prohibited by Technical Specifications2014-08-0505 August 2014 Regarding Lack of Administrative Controls for Some Containment Penetrations During Fuel Movement Results in Condition Prohibited by Technical Specifications 05000328/LER-2014-001, From Sequoyah Nuclear Plant, Unit 2 Regarding Misalignment of Containment Purge Radiation Monitors Results in Condition Prohibited by Technical Specifications2014-06-29029 June 2014 From Sequoyah Nuclear Plant, Unit 2 Regarding Misalignment of Containment Purge Radiation Monitors Results in Condition Prohibited by Technical Specifications 05000327/LER-2014-001, Regarding Never Performed Technical Specification Surveillance for Common Spare Component Cooling System Pump2014-03-26026 March 2014 Regarding Never Performed Technical Specification Surveillance for Common Spare Component Cooling System Pump 05000327/LER-2013-004, Regarding Failure to Comply with Technical Specifications for Containment Penetrations During Fuel Movement Resulting from Ineffective Procedures2013-12-24024 December 2013 Regarding Failure to Comply with Technical Specifications for Containment Penetrations During Fuel Movement Resulting from Ineffective Procedures 05000327/LER-2013-003, Regarding Limiting Conditions for Operation Exceeded for Emergency Core Cooling System2013-10-21021 October 2013 Regarding Limiting Conditions for Operation Exceeded for Emergency Core Cooling System 05000327/LER-2012-002, Regarding Loss of Auxiliary Control Room Instrumentation2013-04-29029 April 2013 Regarding Loss of Auxiliary Control Room Instrumentation 05000328/LER-2013-001, Manual Reactor Trip Due to Loss of Hotwell Level2013-04-25025 April 2013 Manual Reactor Trip Due to Loss of Hotwell Level 05000327/LER-2013-001, Regarding Latent Design Input Inconsistencies Adversely Affect Probable Maximum Flood Analysis2013-04-0808 April 2013 Regarding Latent Design Input Inconsistencies Adversely Affect Probable Maximum Flood Analysis 05000327/LER-2012-001, Regarding Unanalyzed Condition Affecting Essential Raw Cooling Water System Due to External Flooding2013-02-0808 February 2013 Regarding Unanalyzed Condition Affecting Essential Raw Cooling Water System Due to External Flooding 2024-09-25
[Table view] |
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Tennessee Valley Authority, Sequoyah Nuclear Plant, P.O. Box 2000, Soddy Daisy, Tennessee 37384 November 15, 2019 10 CFR 50.73 ATTN:
Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001 Sequoyah Nuclear Plant, Unit 2 Renewed Facility Operating License No. DPR-79 NRC Docket No. 50-328
Subject:
Licensee Event Report 50-328/2019-001 -00, Component Cooling Water System Train A Inoperable Longer Than Allowed by Technical Specifications The enclosed licensee event report provides details concerning the inoperability of one train of the Component Cooling Water System for longer than allowed by Technical Specifications.
This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B), as any operation or condition which was prohibited by the unit's Technical Specification. Additionally, this event is being reported in accordance 10 CFR 50.73(a)(2)(v), as an event or condition that could have prevented the fulfillment of a safety function of structures or systems that are needed to:
(B) remove residual heat and (D) mitigate the consequences of an accident.
There are no regulatory commitments contained in this letter. Should you have any questions concerning this submittal, please contact Mr. Andrew McNeil, acting Site Licensing Manager, at (423) 843-8098.
Respectfully, Matthew Rasmussen Site Vice President Sequoyah Nuclear Plant Enclosure: Licensee Event Report 50-328/2019-001-00 cc:
NRC Regional Administrator-Region II NRC Senior Resident Inspector-Sequoyah Nuclear Plant printed on recycled paper
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 (04-2018)
, the NRC may not conduct or sponsor, anda person is notrequired to respond to,the informationcollection.
3.LERNUMBB*
Sequoyah Nuclear Plant Unit 2 05000-328 YEAR SEQUENTIAL NUMBER REV NO.
- - 00 B.
2019 001 train of the CCS was inoperable for approximately 72 days and 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> without completing Required Action A.1 or C.1, this is a condition prohibited by TS and is therefore being reported in accordance with 10 CFR 50.73(a)(2)(i)(B), as any operation or condition which was prohibited by the unit's TS.
Additionally, a review of redundant equipment in the opposite train was performed for the timeframe between June 17, 2019, at 1723 EDT and August 28, 2019, at 2330 EDT. The review considered occurrences when Train B of the Unit 2 CCS and other equipment or systems redundant to Train A were inoperable. The review found there were forty occurrences when redundant equipment or systems in the opposite train, which included the Emergency Diesel Generators [EMS: DG], Emergency Core Cooling System (ECCS)
[EMS: CB], and the Containment Spray System [EMS: BE], were declared inoperable. As a result, this event is reportable as a Condition that Could Have Prevented the Fulfillment of a Safety Function in accordance with 10 CFR 50.73(a)(2)(v)(B) and (D).
Status of structures, components, or systems that were inoperable at the start of the event and contributed to the event:
No inoperable structures, components, or systems contributed to this event.
C.
Dates and approximate times of occurrences
Date/Time (EDT)
Description
June 17, 2019, 1723 The temporary modification was implemented that provided incorrect specified throttling positions for manual valve, 2-VLV-67-551.
TS LCO 3.3.7.A became applicable.
August 24, 2019 During the flush of a CCS heat exchanger, manual valve 2-VLV-67-551 was placed in one of the specified throttled positions.
Shortly thereafter, CCS alarms were received in the MCR which caused operators to terminate the flush and restore ERCW flows.
August 28, 2019 Section XI test data were evaluated and it was determined that the throttled positions implemented by the modification did not allow the required flow.
August 28, 2019, 2330 A flow balance was conducted and the correct positions were determined. TS LCO 3.3.7.A was no longer applicable.
September 20, 2019 A past operability evaluation determined that Unit 2 Train A of CCS was inoperable from June 17, 2019, at 1723 EDT until August 28, 2019, at 2330 EDT.Page 3 of 7(04-2018)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 Estimated burden perresponse to comply with this mandatory collection request 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated intothe licensing process and fed backto industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001,or bye-mail to lnfocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, anda person is notrequired to respond to,the informationcollection.
& LER NUMBER Sequoyah Nuclear Plant Unit 2 05000-328 YEAR 2019 SEQUENTIAL NUMBER
- - 001 REV NO.
- - 00 D.
Manufacturer and model number of each component that failed during the event
There was no component that failed during the event.
E.
Other systems or secondary functions affected
The ECCS and Containment Spray System are systems supported by the CCS.
F.
Method of discovery of each component or system failure or procedural error
During the flush of a CCS heat exchanger, manual valve 2-VLV-67-551 was placed in one of the throttled positions determined as part of the temporary modification. Shortly after beginning the flush, CCS alarms were received in the MCR which caused operators to terminate the flush and restore ERCW flows. Subsequently,Section XI test data were evaluated and it was determined that the throttled positions implemented by the modification did not allow the required flow.
G.
Failure mode, mechanism, and effect of each failed component:
There was no component that failed during the event.
H.
Operator actions
After receiving CCS alarms in the MCR during CCS heat exchanger flushing, operators terminated the flush and restored ERCW flows I.
Automatically and manually initiated safety system responses
There were no automatic or manually initiated safety system responses associated with this event.
Cause of the Event
A.
Cause of each component or system failure or personnel error
The cause of this event is the failure to adequately recognize the risk of relying on an indirect method (counting number of turns vice performance of a flow balance) to determine the throttle valve positions. The assumption that counting the number of turns would be adequate was not challenged during design reviews.Page 4 of 7(04-2018)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET
<?'
7 APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 Estimated burden perresponseto comply with this mandatory collection request. 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated intothe licensing process and fed backto industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001,or bye-mail to lnfocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conductor sponsor,anda personis notrequired to respondto,the informationcollection.
- 3. LER NUMBER Sequoyah Nuclear Plant Unit 2 05000-328 YEAR 2019 SEQUENTIAL NUMBER 001 REV NO.
- - 00 B.
Cause(s) and circumstances for each human performance related root cause
1)
The causes of this human performance event were:
a.
There was an assumption that the internals of MOV 2-FCV-67-146 and manual valve 2-VLV-67-551 were the same such that the throttle positions could be derived based on the equivalent number of turns between the two valves. Additionally, there was an assumption that the actuator's characteristic curve for manual valve 2-VLV-67-551 was linear.
It was later determined that the valve's actuator characteristic curve was non linear. These incorrect assumptions resulted in the determination of incorrect throttle positions.
b.
The draft version of the temporary modification required a flow balance; however, during review itwas requested that the flow balance not be performed due to the impact to the plant. There was a misunderstanding that the flowtest would have been required during the outage (the temporary modificationwas developed during an ongoing outage) which would have impacted the outage schedule. Because of this misunderstanding the decision was made to revise the temporary modification to no longer require a flow balance.
2)
The circumstances associated with this human performance event were:
a.
The individuals involved were utility personnel in the Engineering department and they were not licensed.
b.
The temporary modificationwas developed during the Unit2 fall outage of 2018 in a short period of time with 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> shift coverage. The fast track schedule and the miscommunication that a flow balance test would be required during the outage contributed to the decision to not perform the flow test.
IV.
Analysis of the Event
The CCS provides a heat sink for the removal of process and operating heat from safety related components during a Design Basis Accident (DBA) or transient. During normal operation, the CCS also provides this function for various nonessential components, as well as the spent fuel storage pool. The CCS serves as a barrier to the release of radioactive byproducts between potentially radioactive systems and the ERCW System, and thus to the environment. Some of the systems served by the CCS are: (1) Reactor Coolant System, (2) Residual Heat Removal System, (3) Chemical and Volume Control System, (4) Safety injection System, and (5) Containment Spray System.Page 5 of 7(04-2018)
- " 0 U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 Estimated burden perresponse to comply with this mandatory collection request 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated intothe licensing process and fed backto industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001,or bye-mail to lnfocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, anda person is notrequired to respond to,the informationcollection.
- 3. LER NUMBER Sequoyah Nuclear Plant Unit 2 05000-328 YEAR 2019 SEQUENTIAL NUMBER 001 REV NO.
- - 00 The CCS trains are independent of each other to the degree that each has separate controls and power supplies and the operation of one does not depend on the other. In the event of a DBA, one CCS train is required to provide the minimum heat removal capability assumed in the safety analysis for the systems to which it supplies cooling water. To ensure this requirement is met, two trains of CCS must be operable. At least one CCS train will operate assuming the worst case single active failure occurs coincident with a loss of offsite power.
The design basis of the CCS is for one train to remove the post loss of coolant accident (LOCA) heat load from the containment sump fluid during the recirculation phase. This provides a gradual reduction in the temperature of the fluid as the fluid is supplied to the Reactor Coolant System by the ECCS pumps.
An Engineering evaluation determined that had a Unit 2 LOCA occurred (or any transient requiring Unit 2 Safety Injection [SI]), the ERCW System and CCS would have been able to perform their UFSAR required functions of core cooling and containment vessel protection for the accident unit.
Additionally, the ERCW System and CCS would have been able to provide the required equipment cooling functions for the non-accident unit (Unit 1).
The evaluation also determined that had a Unit 1 LOCA occurred (or any transient requiring Unit 1 SI), the Unit 2 A Train of CCS would not have been able to perform its required equipment cooling function for the non-accident unit (Unit 2) without intervention from Operations. Based on this determination, Unit 2 A Train of CCS was declared inoperable from June 17, 2019, to August 28, 2019.
V.
Assessment of Safety Consequences
There were no actual safety consequences as a result of this event.
A Probabilistic Risk Assessment evaluation of this condition determined there was no risk increase for Unit 1, and the risk increase for Unit 2 during the time this condition existed was very small.
A.
Availability of systems or components that could have performed the same function as the components and systems that failed during the event:
None.
B.
For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident:
The event did not occur when the reactor was shut down.Page 6 of 7(04-2018)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET 7
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020
, the NRC may not conduct or sponsor,anda personis notrequired to respondto, the informationcollection.
- 3. LB?NUMBER Sequoyah Nuclear Plant Unit 2 05000-328 YEAR 2019 SEQUENTIAL NUMBER
- - 001 REV NO.
- - 00 C.
For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:
Initially, the Unit 2 A Train of the ERCW System was declared inoperable at 1658 EDT on August 28, 2019. After performance of a flow balance test, the Unit 2 A Train of the ERCW System was declared operable at 2330 EDT on August 28, 2019. The elapsed time was approximately 6.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. After completion of the past operability evaluation it was determined that the event affected the Unit 2 A Train of the CCS vice the ERCW System.
VI.
Corrective Actions
The reactor trip event was entered into the Tennessee Valley Authority Corrective Action Program (CAP) under CR 1544846.
A.
Immediate Corrective Actions
Once the issue was identified a flow balance test was completed to determine the correct throttle positions for manual valve 2-VLV-67-551.
B.
Corrective Actions to Prevent Recurrence or to reduce probability of similar events occurring in the future:
Corrective actions include completing a required reading and lessons learned for the Engineering Department regarding the event and the circumstances associated with the event. The lessons learned will include: (1) adequately identifying risks and actions to mitigate error precursors when developing design changes, (2) the importance of documenting critical thinking and challenges to designs formerly on comment sheets, (3) the compensating actions that should be implemented when there is time pressure to perform a task, and (4) properly identifying and validating assumptions when developing design changes.
VII.
Previous Similar Events at the Same Site
There were no previous similar events at SQN occurring within the last three years.
VIII.
Additional Information
There is no additional information.
IX.
Commitments
There are no commitments.Page 7 of 7
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05000328/LER-2019-001, Component Cooling Water System Train a Inoperable Longer than Allowed by Technical Specifications | Component Cooling Water System Train a Inoperable Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000327/LER-2019-001, Reactor Trip on Low-Low Steam Generator Level Due to the Loss of a Main Feedwater Pump | Reactor Trip on Low-Low Steam Generator Level Due to the Loss of a Main Feedwater Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000328/LER-2019-002, Loss of Heater Drain Tank Flow Causes Turbine Runback and Manual Reactor Trip | Loss of Heater Drain Tank Flow Causes Turbine Runback and Manual Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000327/LER-2019-002, Regarding Steam Generator Pressure Transmitter Degraded Sensing Line Causes Condition Prohibited by Technical Specifications | Regarding Steam Generator Pressure Transmitter Degraded Sensing Line Causes Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000327/LER-2019-003-01, 1 for Sequoyah Nuclear Plant, Unit 1, Automatic Reactor Trio Due to Negative Rate Trip as a Result of a Dropped Control Rod | 1 for Sequoyah Nuclear Plant, Unit 1, Automatic Reactor Trio Due to Negative Rate Trip as a Result of a Dropped Control Rod | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000327/LER-2019-003, Automatic Reactor Trip Due to Negative Rate Trip as a Result of a Dropped Control Rod | Automatic Reactor Trip Due to Negative Rate Trip as a Result of a Dropped Control Rod | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000327/LER-2019-004, Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board | Automatic Actuation of Emergency Diesel Generators Due to Loss of Power to 6.9kV Shutdown Board | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
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