The inspectors reviewed a Green,self-revealed non-cited violation of
Technical Specification 5.4.1.a Procedures, because
PG&E personnel failed to follow the requirements of MA1.DC54, Conduct of Maintenance, Revision 15. Specifically, on March 20, 2018, with the reactor in Mode 3 during informal troubleshooting of high background count rate on source range nuclear instrument (NI) NI-32,
PG&E personnel caused a short in NI cabinet B resulting in a blown fuse and the loss of power to the cabinet. This resulted in the loss of power to power range NI-42, intermediate range NI-36, source range NI-32, a
reactor trip signal, a
turbine trip signal, and all associated reactor protection interlocks. Power was automatically removed from the remaining source range NI due to reactor protection interlock P-10, resulting in no safety-related source range NI indication being available for control room operators.