05000323/FIN-2009009-01
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Finding | |
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Title | Failure to Follow Design and Configuration Control Requirements |
Description | The inspection team identified a noncited violation of 10 CFR 50, Appendix B, Criterion III, Design Control, which requires licensees to implement measures to assure that applicable regulatory requirements and the design basis are correctly translated into specifications, drawings, procedures, and ins ructions. These design control measures include verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculation methods, or by the performance of a suitable testing program. Specifically, on February 16, 2008, plant engineering personnel failed to implement the design control process for a modification to the Unit 2 residual heat removal containment sump valves when they inappropriately used maintenance procedures to reduce the valve stroke leng1hs from 15.5 to 13.8 inches. The invalid design change resulted in the inoperability of both emergency core cooling trains between April 8, 2008, (when the plant entered Mode 4) and October 22,2009. The reduced sump valve stroke length also caused a portion of the sump valve disc to remain in the residual heat removal suction flow path, reducing the available residual heat removal pump net positive suction head. The licensee entered this condition into their corrective action program as Notification 50277252. The inspection team concluded that the failure of plant engineering to use the design control process was a performance deficiency within the licensees ability to foresee and correct. The finding is more than minor because it affected the Mitigating Systems Cornerstone initial design control attribute and objective to ensure the availability, reliability, and capability of systems that respond to initiating events. Using Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of Findings, the finding required a Phase 2 analysis because the finding represented the loss of a safety system function. The Phase 2 analysis determined that this finding was potentially greater than Green; therefore, a Phase 3 analysis was completed by a regional senior reactor analyst. The Phase 3 analysis determined that this issue was of very low safety significance (Green), owing principally to the fact that operators could have opened the affected valves locally with a very high probability of success. This finding had a crosscutting aspect in the area of problem identification and resolution associated with the corrective action program component because the licensee did not thoroughly evaluate the failure of the valves to meet the specified stroke time to ensure that the resolution fully addressed the causes and extent of condition, as necessary P.1(c) |
Site: | Diablo Canyon |
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Report | IR 05000323/2009009 Section 1R02 |
Date counted | Mar 31, 2010 (2010Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.02 |
Inspectors (proximate) | M Peck P Elkmann M Runyan R Caniano M Williams |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
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Finding - Diablo Canyon - IR 05000323/2009009 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Diablo Canyon) @ 2010Q1
Self-Identified List (Diablo Canyon)
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