05000275/FIN-2009004-02
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Finding | |
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Title | Failure to Perform Corrective Actions Resulted in an Unplanned Trip |
Description | A self-revealing finding was identified after Pacific Gas and Electric failed to implement planned corrective actions resulting in the loss of cooling to a main transformer, a rapid shutdown and a manual reactor trip of Unit 2. On June 30, 2009, cooling to a main transformer was lost because a fuse opened in the 480 volt power circuit due to loose terminal connections in the cooling control panel. Plant operators rapidly shut-down the unit from full power after transformer cooling was lost. A previous failure of transformer cooling due to loose terminal connections occurred on Unit 1, also resulting in a reactor trip. Corrective actions to prevent recurrence following the previous event included replacement of the main transformer terminations in the cooling control panels. Review of the work orders revealed that these corrective actions were not completed and the work documents were closed. While the failure to complete the corrective actions was a latent issue, the inspectors concluded that the licensee had a recent opportunity to identify the issue. Plant technicians implemented thermograph monitoring of main transformer cooling circuits and identified hot 480 volt power terminations in the Unit 2 main transformer cooling disconnect box in April 2009. These hot terminations should have prompted Pacific Gas and Electric to review internal operating experience related to main transformer cooling issues. The licensee entered this finding into corrective program as Notification 50260721. The inspectors concluded that the finding is greater than minor because it is associated with the equipment performance attribute of the initiating events cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that interrupt plant stability and challenge critical safety functions during shutdown as well as power operations. The inspectors determined the finding to have very low safety significance because the condition did not contribute to both the likelihood of a reactor trip and the unavailability of mitigation equipment or functions. This finding has a crosscutting aspect in the area of problem identification and resolution, associated with the operating - 3 - Enclosure experience component because Pacific Gas and Electric failed to perform an adequate internal operating experience review following the discovery of hot terminations on Unit 2 main transformer in April 2009 P.2(a) |
Site: | Diablo Canyon |
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Report | IR 05000275/2009004 Section 1R12 |
Date counted | Sep 30, 2009 (2009Q3) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.12 |
Inspectors (proximate) | G Guerra M Brown M Peck S Garchow V Gaddy G Apger B Larson J Braisted |
CCA | P.5, Operating Experience |
INPO aspect | CL.1 |
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Finding - Diablo Canyon - IR 05000275/2009004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Diablo Canyon) @ 2009Q3
Self-Identified List (Diablo Canyon)
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