05000313/FIN-2011004-03
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Finding | |
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| Title | Failure to Provide Adequate Work Instruction Results in Failed Bearing on Motor Generator Set |
| Description | The inspectors documented a self-revealing finding for an inadequate work instruction for the 2-02 control element motor generator set flywheel bearing replacement that resulted in a failure of that bearing. Specifically, the licensee failed to provide instructions to obtain flywheel shaft dimensions to ensure adequate interference fit between the bearing and the shaft during corrective maintenance. This bearing subsequently failed on April 6, 2011. The licensee placed the issue into the corrective action program as Condition Report ANO-CR-2-2011-1817. The licensee replaced the failed bearing and shaft assembly and the system was returned to service. The failure to provide adequate maintenance work instruction to verify dimensional fit up between the flywheel shaft and bearing for the Unit 2, 2-02 motor generator set prior to reassembly was determined to be a performance deficiency. Specifically, it was within the licensees ability to foresee and correct and was a failure to meet station requirements to provide adequate maintenance work instruction to maintenance personnel. The performance deficiency was determined to be more than minor because it was associated with the procedure quality attribute of the Initiating Event Cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during power operations. Specifically, due to both control element motor generator sets being in the same room, the failure of the motor generator flywheel bearing caused the failure of that motor generator shaft and could have affected the only operating motor generator set and resulted in a reactor trip. Using Manual Chapter 0609, Exhibit 1, Phase 1 Initial Screening and Characterization of Finding, the finding was determined to be of very low safety significance because it did not contribute to both the likelihood of a reactor trip and that mitigation equipment or function would not be available. The inspectors determined that the finding did not have a crosscutting aspect because the performance deficiency is not indicative of current plant performance as the cause of not developing adequate work instructions stems from the late 1990s. |
| Site: | Arkansas Nuclear |
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| Report | IR 05000313/2011004 Section 4OA2 |
| Date counted | Sep 30, 2011 (2011Q3) |
| Type: | Finding: Green |
| cornerstone | Initiating Events |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71152 |
| Inspectors (proximate) | A Sanchez J Rotton K Clayton L Ricketson R Azua R Kumana W Schaup |
| INPO aspect | |
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Finding - Arkansas Nuclear - IR 05000313/2011004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2011Q3
Self-Identified List (Arkansas Nuclear)
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