05000311/FIN-2016004-02
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Finding | |
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Title | Inadequate Surveillance Test Procedure Results in Water Hammer and Reactor Trip |
Description | Green. The inspectors determined there was a self-revealing Green non-cited violation (NCV) of Technical Specification (TS) 6.8.1.c, Surveillance and test activities of safety-related equipment, when PSEG did not establish adequate procedures for restoring service water (SW) to a drained section of discharge piping from the containment fan coil unit (CFCU) following surveillance test activities. Consequently, during restoration of SW to 22 CFCU following testing on August 31, 2016, refilling the voided SW piping created a pressure pulse sufficient to extrude the motor cooler cover plate spacer gasket inside primary containment, resulting in leakage that caused a 21 reactor coolant pump (RCP) cable fault and subsequent reactor trip. PSEG entered the issue in the corrective action program (CAP), performed a root cause evaluation (RCE), and revised applicable procedures for filling and venting SW to the CFCUs on September 19, 2016. This issue was more than minor since it was associated with the procedure quality attribute of the Initiating Events cornerstone and adversely impacted its objective to limit the likelihood of events that upset plant stability and challenge critical safety functions. Using IMC 0609, Attachment 4 and Appendix A, Exhibit 1, the inspectors determined that this finding was of very low safety significance, or Green, since mitigating equipment relied upon to transition the plant to stable shutdown remained available. The finding had a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because PSEG did not thoroughly evaluate previous CFCU motor cooler gasket leaks such that the resolution addressed the cause. [P.2] |
Site: | Salem |
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Report | IR 05000311/2016004 Section 4OA3 |
Date counted | Dec 31, 2016 (2016Q4) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | A Ziedonis F Bower J Deboer J Hawkins J Kulp P Finney P Ott |
Violation of: | Technical Specification |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
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Finding - Salem - IR 05000311/2016004 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Salem) @ 2016Q4
Self-Identified List (Salem)
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