05000286/FIN-2015002-01
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Finding | |
|---|---|
| Title | Inadequate Corrective Action for Main Steam Safety Valve 46-3 Failure to Lift at Required Setpoint |
| Description | The inspectors identified a Green NCV of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action, for Entergys failure to take corrective actions for a condition adverse to quality involving Unit 3 Main Steam Safety Valve (MSSV) 46-3. Specifically, MSSV 46-3 failed to meet its Technical Specification (TS) required lift setting during a surveillance test on March 22, 2015. This failure was documented in a condition report (CR) but closed for trending purposes. Additionally, Entergy personnel did not correct the failure of MSSV 46-3 to meet its TS required lift setting after it failed its as-found lift setting test on March 1, 2013. The inspectors determined the performance deficiency was more than minor because it is associated with the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, Entergy did not take corrective actions following the March 22, 2015, failure of MSSV 46-3, and previous corrective actions in 2013 were not effective in ensuring it would remain capable of lifting at its TS required setpoint. The inspectors determined that this finding is of very low safety significance (Green) because the finding does not represent an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant in accordance with Entergys maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Specifically, of the 20 valves tested in 2015, 16 passed the as-found lift test and there was no loss of safety function. The inspectors determined that this finding had a Problem Identification and Resolution cross-cutting aspect related to Evaluation, because Entergy did not thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the CR documenting the MSSV 46-3 failure was closed for trending purposes and as a result, a thorough evaluation of the cause was not completed. |
| Site: | Indian Point |
|---|---|
| Report | IR 05000286/2015002 Section 1R22 |
| Date counted | Jun 30, 2015 (2015Q2) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.22 |
| Inspectors (proximate) | A Bolger A Burritt B Pinson G Newman J Bream J Furia J Stewart R Barkley R Montgomery S Rich T Setzer |
| Violation of: | 10 CFR 50 Appendix B Criterion XVI Technical Specification |
| CCA | P.2, Evaluation |
| INPO aspect | PI.2 |
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Finding - Indian Point - IR 05000286/2015002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Indian Point) @ 2015Q2
Self-Identified List (Indian Point)
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