IR 05000247/2015010
| ML15204A499 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 07/23/2015 |
| From: | Burritt A L Reactor Projects Branch 2 |
| To: | Coyle L Entergy Nuclear Operations |
| Burritt A L | |
| References | |
| IR 2015010 | |
| Download: ML15204A499 (28) | |
Text
July 23, 2015
Mr. Larry Coyle Site Vice President Entergy Nuclear Operations, Inc.
Indian Point Energy Center 450 Broadway, GSB Buchanan, NY 10511-0249
SUBJECT: INDIAN POINT NUCLEAR GENERATING - SPECIAL INSPECTION REPORT 05000286/2015010
Dear Mr. Coyle:
On June 24, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed a Special Inspection Team (SIT) review of the circumstances surrounding the May 9, 2015, water accumulation in the Unit 3 safety-related switchgear room following the 31 main transformer failure and reactor trip event at your Indian Point Nuclear Generating (Indian Point) Unit 3. This event satisfied the criteria in NRC Inspection Manual Chapter 0309, "Reactive Inspection Decision Basis for Reactors," for conducting a special inspection. As a result, the NRC sent a SIT to your site on May 19, 2015. The SIT Charter (Attachment 1 of the enclosed report)
provides the basis and additional details concerning the scope of the inspection. The enclosed report documents the inspection team's activities and observations conducted in accordance with the SIT Charter. On June 24, 2015, the SIT discussed the results of the inspection with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with Commission rules and regulations and with conditions of your license. The team reviewed selected procedures and records and interviewed personnel. In particular, the SIT reviewed technical analyses, hydraulic flow models, and causal investigations to assess the significance and potential consequences of the water accumulation in the Unit 3 safety-related switchgear room. This report documents one NRC-identified finding of very low safety significance (Green). This finding involved a violation of NRC requirements. However, because of the very low safety significance, and because it has been entered into your corrective action program, the NRC is treating this finding as a non-cited violation (NCV), consistent with Section 2.3.2.a of the NRC Enforcement Policy. If you contest the NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident Inspector at Indian Point. In addition, if you disagree with the cross-cutting aspect assigned to the NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector at Indian Point.
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/ Arthur L. Burritt, Chief Reactor Projects Branch 2 Division of Reactor Projects Docket No. 50-286 License No. DPR-64
Enclosure:
Inspection Report 05000286/2015010 w/Attachments 1, 2, and 3
cc w/encl: Distribution via ListServ
SUMMARY OF FINDINGS
........................................................................................................... 3
REPORT DETAILS
....................................................................................................................... 51.Summary and Chronology of Event ................................................................................... 52.Equipment Response to Fire Resulting in Water in Switchgear Room .............................. 63.Operator and Fire Brigade Performance in Identifying and Isolating the Source of Water into the Switchgear Room ................................................................................................ 134.Effectiveness of Entergy Response to Water Intrusion .................................................... 155.Evaluation of Pertinent Industry Operating Experience ................................................... 166.Risk Significance of the Event .......................................................................................... 177.Exit Meetings .................................................................................................................... 17ATTACHMENT 1: SPECIAL INSPECTION TEAM CHARTER .............................................. A1-1ATTACHMENT 2: DETAILED SEQUENCE OF EVENTS ..................................................... A2-1ATTACHMENT 3:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
............................................................................................... A3-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
.................................................. A3-1
LIST OF DOCUMENTS REVIEWED
................................................................................... A3-1
LIST OF ACRONYMS
- ...... ................................................................................................... A3-4
- OF [[]]
- FINDIN [[]]
GS Inspection Report 05000286/2015010; 05/19/2015 - 06/24/2015; Indian Point Nuclear Generating (Indian Point) Unit 3; Special Inspection Team (SIT) review of the May 9, 2015, water accumulation in the Unit 3 safety-related switchgear room following 31 main transformer
failure and reactor trip event; Inspection Procedure 93812, "Special Inspection."
A four-person
NRC) team, comprised of regional
inspectors, a Resident Inspector, and a regional Senior Reactor Analyst (SRA), conducted this Special Inspection. The team identified one non-cited violation (NCV) of very low safety significance (Green). The significance of most findings is indicated by their color (i.e., greater than Green, Green, White, Yellow, Red) and determined using Inspection Manual Chapter
(IMC) 0609, "Significance Determination Process," dated April 29, 2015. Cross-cutting aspects
are determined using
NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in
- NUR [[]]
EG-1649, "Reactor Oversight Process," Revision 5, dated February 2014.
Cornerstone: Mitigating Systems Green. The inspectors identified a Green
DPR-64, "Fire Protection Program," for failure to promptly identify, report, and correct a condition adverse to fire protection. Specifically, solenoid valve (SOV)-230-1, associated with the deluge valve for the 32 main
transformer (MT), was documented to have opened during its 2-year deluge activation
tests on April 7, 2011, April 2, 2013, and March 24, 2015, but did not close as designed after the deluge system actuated. This condition was not corrected, and recurred on May 9, 2015, when the deluge system actuated in response to a fire on the 31 MT.
Entergy entered this issue into the corrective action program (CAP) (condition report
(CR)-IP3-2015-02921), and determined a clogged orifice in the SOV pressure switch
prevented the SOV from de-energizing and going closed. The performance deficiency was determined to be more than minor because it is
associated with the Protection Against External Factors attribute of the Mitigating
Systems cornerstone and adversely affected the cornerstone's objective to ensure the availability, reliability, and capability of systems that respond to initiating events to
prevent undesirable consequences. Specifically, water intrusion into the switchgear room can challenge the reliability of the safety-related electrical equipment required to respond to a reactor transient. The inspectors screened the finding for significance
using the screening questions in IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems,"
and Exhibit 4, "External Events," and determined that this performance deficiency
required a Detailed Risk Evaluation because the potential existed for enough water leakage into the switchgear room to cause a loss of all safety-related power and station blackout (SBO) condition. The Detailed Risk Evaluation determined that this finding was
of very low safety significance (Green) with an estimated increase in core damage
frequency in the low E-7 per reactor year range (an increase of 1 in 10 million reactor
years). The inspectors determined the finding had a cross-cutting aspect in the Human Performance cross-cutting area, "Challenge the Unknown," because Entergy did not stop and fully explore an uncertain condition with SOV-230-1 when it failed to closed on
three occasions since April 2011. Entergy replaced the
- SOV , but did not determine that the cause was a clogged pressure switch orifice until after the May 9, 2015, 31
MT fire
event. [H.11] (Section 2.c)
- REPORT [[]]
DETAILS 1. Summary and Chronology of Event In accordance with the SIT Charter (Attachment 1), the team conducted a detailed
review of the events regarding water accumulation found in the Unit 3 safety-related
480V switchgear room following a 31 MT failure and reactor trip event on May 9, 2015.
The team gathered information from operator narrative logs, the plant process computer, sequence of events printouts, and interviews with plant operators and engineering staff to develop a detailed timeline of the event (Attachment 2). The following summary
highlights the events and challenges encountered by the Indian Point staff.
On May 9, 2015, at 5:50 p.m., Indian Point Unit 3 experienced a main turbine-generator lockout, main turbine trip, and automatic reactor trip as a result of an explosion and fire on the 31 MT. The reactor trip was uncomplicated. All control rods inserted into the
reactor core and all safety systems responded as designed.
The heat from the transformer fire caused activation of the
MT, unit auxiliary transformer (UAT), and curtain wall fire protection water deluge systems. At 5:52 p.m., the site fire brigade was activated and notified the Control Room that a fire was present
on the 31 MT. At 5:53 p.m., Verplanck and Montrose Fire Departments were called for
assistance, and arrived at the site's front gate approximately 9 minutes later. At
6:01 p.m., Entergy declared a Notification of Unusual Event for an explosion within the
station's Protected Area. At 6:12 p.m., with the majority of the fire out, the fire brigade leader ordered securing the
deluge system in order to apply foam to the transformer in accordance with station pre-
fire plans and oil fire-fighting strategies. Also at this time, water had been reported on
the floor in the Unit 3 480V switchgear room. The Unit 3 480V switchgear room houses breakers that power safety-related equipment. Operators attempted to isolate the deluge system; however, the yoke on an isolation valve was broken during operation,
which caused the system to leak-by. An alternate valve was used to isolate deluge
water to all four deluge systems.
The fire was initially extinguished at 6:15 p.m.; however, it reflashed at 6:37 p.m., at which time Entergy brought Verplanck fire engines into the Protected Area. Additionally, a request for a tower ladder truck was made to Montrose Fire Department, which arrived
at approximately 7:00 p.m. The fire brigade continued to fight the fire with foam and
declared the fire extinguished at 8:05 p.m.
The water that accumulated on the floor of the Unit 3 480V switchgear room was initially reported to be approximately 1 to 2 inches in depth. The source of this water was
determined to be deluge system water that had come from a deluge valve room, which is
adjacent to the 480V switchgear room. The deluge valve room houses four deluge
system valves; specifically,
- UAT , and station auxiliary transformer deluge valves. The deluge valve associated with the curtain wall system is located in the turbine building. In order for a deluge valve to open, an
SOV associated with each deluge valve opens and bleeds water pressure off a diaphragm assembly. This water is
bled to the floor towards a drain. Entergy determined that the water bled from the 31
- UAT [[]]
SOVs was unable to completely drain through a floor drain due to
its limited capacity, and consequently made its way into the 480V switchgear room where it pooled to approximately 1-inch in depth. Operators reported that all the water
drained completely within 30 minutes after the deluge system had been isolated. 2. Equipment Response to Fire Resulting in Water in Switchgear Room a. Inspection Scope During on-site inspections on May 19-22 and June 3-4, the inspectors evaluated the equipment response to the fire that resulted in water accumulation in the switchgear room. Specifically, the inspectors reviewed Entergy drawings, calculations, procedures,
and analyses that describe the operation and design of the station deluge valves and
their associated subcomponents. The inspectors reviewed Entergy's hydraulic analyses
of flows through the transformer yard storm drain system and Unit 3 switchgear room floor drain system, and performed independent confirmatory calculations. The inspectors conducted plant walkdowns of the systems and components to verify their condition and configuration in accordance with plant design basis documents. The
inspectors reviewed preventive maintenance records, work orders, and CAP documents
(CRs) for the deluge, floor drain, and storm drain systems to understand the history of the system and its proper operation. The inspectors viewed videos of boroscopic inspections of the floor and storm drain systems to verify that conditions aligned with
those described in the analyses. The documents reviewed during the inspection are
listed in Attachment 3.
b. Assessment and Observations .1 Fire Protection Deluge Valves On May 9, 2015, at 5:50 p.m., Indian Point Unit 3 control room received indications and
alarms associated with an automatic turbine and reactor shutdown. Following the shutdown, the control room received alarms on the Fire Display Control Panel, alerting operators that the main transformer deluge system had activated due to a fire on the 31
MT. Based on the design of the deluge system for the transformer yard, only one deluge
system actuation is anticipated. However, the heat generated from the fire also caused
activation of the adjacent deluge systems on the
UAT. Additionally, the
curtain wall deluge system, which is a fire protection system designed to protect the turbine building from a fire in close proximity, activated and provided sprays along the turbine building outer wall. The deluge systems are activated by one or more heat
detectors that are installed on each associated transformer, with a valid turbine trip
signal. The inspectors reviewed the system response and determined that the
UAT deluge valves, and curtain wall deluge system activated as designed to provide water to the sprays for each transformer and turbine building wall. .2 Fire Protection Deluge Valve Solenoid Valve and Pressure Switch
The deluge valves and associated SOVs are located in a room adjacent to the Unit 3
switchgear room on 15'-0" elevation. The switchgear room and deluge valve room are separated by a single door. When both a valid turbine trip signal is present and one or more
SOV for the respective
deluge valve is energized to open. By opening, the SOV ports water to the floor towards
a drain, which causes water pressure within a diaphragm assembly to bleed off. This
results in the retraction of a hold down pin, and system pressure is then able to force open a clapper and allow water to flow through piping and out the spray heads around
each affected transformer. Once water pressure in the spray header reaches 6 pounds per square inch gauge (psig), a pressure switch de-energizes the SOV and closes it, which stops water from being continuously ported to the floor.
The
UAT deluge valves opened as
designed to allow deluge initiation. However, they did not close once system pressure
reached 6 psig, and continued to port water to the floor. Water from the SOVs flowed to the floor at approximately 50 gallons per minute (gpm). This water began to flood the deluge valve room to a height of 4 to 6 inches, and flowed underneath the door to the
switchgear room because the floor drain in the room could drain only 6 gpm. At
6:12 p.m., operators reported observing water in switchgear room. The operators also
reported observing water flowing out of hub drains near the instrument air compressors within the switchgear room. At this time, the fire brigade leader ordered the securing of the deluge system.
At 6:16 p.m., operators attempted to isolate the deluge valves by closing each of the
isolation valves for the
FP-2-2) during operation, causing the system to leak-by. The main system isolation, FP-75, was closed to aid in the isolation. At 6:20 p.m.,
water to the deluge system had been completely isolated. The estimated water level in
the switchgear room was reported to be 1 to 2 inches, varying at different locations in the
room. Operators reported that all the water drained completely within 30 minutes after
the deluge system had been isolated. The inspectors performed a review of historical CAP documents and found three
instances where plant operators had identified a SOV failure to close during its 2-year
deluge system surveillance tests. Specifically, in April 2011, operators identified the
MT (SOV-230-1) deluge valve was failing to close (CR-IP3-2011-02177). Additionally, the pressure switch was noted to have severely corroded internals. Entergy replaced SOV-230-1, but did not troubleshoot the pressure switch. In
April 2013,
CR-IP3-2015-02133). Work orders were
created to investigate the issue but were not completed before the event on May 9, when the
CRs which documented a failure to close during testing. However, the inspectors
concluded that adverse conditions with these SOVs should have been discovered by
Entergy had an extent of condition review been completed. Following the May 9 event, Entergy reviewed the operation of the SOV and its failure to
close at the appropriate system pressure and determined that orifices for the pressure
switches were clogged with system debris, which prevented them from sensing system pressure and closing the
NCV of Condition 2.H of the Indian Point Unit
Facility Operating License
- DPR -64, "Fire Protection Program," is discussed below in Section 2.c because Entergy did not promptly identify, report, and correct a condition adverse to fire protection associated with
SOV-230-1 failure to close.
.3 Deluge Valve Room and Switchgear Room Floor Drains The deluge valve room and switchgear room have both hub and floor drains that are connected underground by 4-inch cast iron piping. During the event, operators observed water flowing out of hub drains in the switchgear room located near the instrument air
compressors. Entergy performed a boroscopic inspection of the floor drains and found
restrictions and standing water downstream of the instrument air compressor hub drains
(CR-IP3-2015-03025). Entergy determined the water that flowed from the deluge valve
room to the switchgear room was unable to completely drain due to these restrictions, and consequently flowed out through the path of least resistance, which was the hub drains nearest the instrument air compressors. Entergy performed flow tests and
determined that the floor drains, as restricted, could pass a maximum of 25 gpm. After
testing, the drains were cleaned (CR-IP3-2015-03121).
The inspectors reviewed the preventive maintenance program for the floor drains and determined that the testing methodology to determine the capability of the drains did not
ensure they were clear of restrictions. Entergy's test of the floor drains included pouring
gallons of water down the floor drain. If the water drained within one minute, the
drain was considered satisfactory. Given the restrictions found during the boroscopic inspection, and the volume of piping in the drain system that could absorb 10 gallons of water while being restricted downstream, the inspectors concluded this approach may
not consistently reveal whether the floor drains were clear of restrictions. Entergy
entered an item into their CAP to enhance the preventive maintenance practices on the
floor drain system for both Unit 2 and Unit 3 (Action Request 228018). Additionally, as
an interim corrective action, Entergy installed a temporary modification and procedure change to direct operators to open doors between the switchgear room and the emergency diesel generator (EDG) room, so that water would be directed to the EDG
room's large capacity sump in the event of a water intrusion event. .4 Transformer Yard Storm Drains The storm drain piping system in the Unit 3 transformer yard is a series of eight
manholes (MHs) that are connected by underground corrugated metal pipe. The MHs
begin in the transformer yard at 18'-0" elevation, and drain to a single outlet into the
discharge canal. MH B3 receives normal water runoff from the transformer yard, and is
also connected to the outlet of the Unit 3 switchgear room floor drains located at 15'-0" elevation. The inspectors questioned whether water observed in the switchgear room during the event had originated from the storm drain system, since there is nothing to
prevent a back-up of water from MH B3 to the switchgear room other than a difference in
elevation (3'-0").
Entergy performed a hydraulic analysis (PIPE-FLO) of the storm drain system to determine if water from the storm drain system could have been the source of water
observed in the switchgear room. Additionally, Entergy retained an engineering firm to
perform a separate analysis. The three deluge systems that activated during the event
had a combined flow of 4300 gpm. The 4300 gpm deluge flow eventually overwhelmed the transformer yard moat, and resulted in water accumulation in the transformer yard. Based on field observations from Entergy fire brigade members, this water accumulation may have been as high as 3 inches above the transformer yard ground level in some
places.
In a bounding analysis, Entergy assumed that the entire volume of deluge water (4300 gpm) would flow into MH B3, which is the closest manhole connected to the switchgear
room floor drain piping. This is considered a conservative assumption, since the maximum drainage capability through the MH B3 grate with 3 inches of available water height over the entire drain is approximately 1500 gpm. Additionally, during the event, a
portion of the water flowed downhill and away from MH B3 and entered the storm drain
system through manholes located at a lower hydraulic grade. Based on the maximum
drainage capability exiting
MH
B3 would rise to a maximum, equilibrium level of 10'-4" elevation. Since this level is below the level of the switchgear room (15'-0"), Entergy concluded that the source of the water observed in the switchgear room could not have originated from transformer yard storm drain system.
To further support their conclusion, a model of the drainage system utilizing
- FLO was created to determine what the maximum flow rate into MH B3 must be to cause an influx of water from the yard storm drains to the switchgear room. The result of the
FLO analysis indicated that a flow rate of approximately 6200 gpm would be needed to flow into MH B3 to cause water to backup into the switchgear room. This
exceeds both the maximum drainage capability of the MH B3 grate and the maximum possible flowrate the fire protection system could deliver.
The inspectors reviewed the Entergy
FLO and supporting engineering firm's
analysis and determined it was reasonable with supported conclusions. However, the
inspectors determined that the analysis for the maximum flow rate into
- MH B3 did not consider damage and a restriction in the storm drain system that was discovered by Entergy during a robotic inspection (
CR-IP3-2015-03090). This restriction produced a 36 percent resistance to the flow out of the storm drain system, and would potentially
result in lower flowrates needed to cause a backup of water into the switchgear room. Entergy performed the analysis applying a 36 percent resistance and determined that
the maximum flow rate into MH B3 decreased to 5600 gpm. This did not change the conclusion that water from the transformer yard storm drains did not flow into the switchgear room. Entergy further supported this conclusion based on the observation
that the water flowing out of the hub drain next to the 31 instrument air compressor was
clear with no oil sheen. Additionally, no water was seen flowing from the floor drains at
even lower elevations than the switchgear room (5'-0" elevation of the turbine building).
Considering the damage identified in the storm drain system, and the risk of a potential storm drain collapse, the inspectors questioned whether rain water could overcome the
storm drain system and cause water to potentially flow to the switchgear room. Entergy
entered the condition in the
CR-IP3-2015-03328) to request vendor support in
evaluating costs and repairs to the restricted or damaged portions of the storm drain piping. Additionally, Entergy instituted a Special Log to check MHs for unusually high water levels, and hourly firewatch tours in the switchgear room to determine if water was
flowing out of the floor drains. Entergy concluded that the degraded conditions in the
storm drain system did not significantly alter its capability. The inspectors determined
that Entergy had an adequate basis for this conclusion.
c. Findings Introduction. The inspectors identified a Green
DPR-64, "Fire Protection Program," for failure to
promptly identify, report, and correct a condition adverse to fire protection. Specifically,
MT, was documented to have
opened during its 2-year deluge activation tests on April 7, 2011, April 2, 2013, and
March 24, 2015, but did not close as designed after the deluge system actuated. This
condition was not corrected, and recurred on May 9, 2015, when the deluge system actuated in response to a fire on the
CAP (CR-IP3-2015-02921), and determined a clogged orifice in the SOV pressure switch
prevented the
- SOV from de-energizing and going closed. Description. On May 9, 2015, at 5:50 p.m., a fire on the 31
system. In order for a deluge valve to open, a SOV associated with each deluge valve opens and bleeds water pressure off a diaphragm assembly. This water is bled to the
deluge valve room floor towards a drain. As designed,
- SOV s ported water from each deluge valve diaphragm chamber onto the floor at approximately 50 gpm. The
SOVs are designed to de-energize and close after a pressure switch
senses 6 psig in the spray header. However, a buildup of corrosion products in the
pressure switch orifices prevented the pressure switch from closing the SOVs. As a
result, all three SOVs remained open and continued to discharge water to the floor at a
rate of 50 gpm for approximately 30 minutes. The inspectors performed a review of historical CAP documents and found three
instances where plant operators had identified SOV-230-1 failure to close during its 2-
year deluge system surveillance tests. Specifically, in April 2011, operators identified
- CR -IP3-2011-02177). Additionally, the pressure switch was noted to have severely corroded internals. Entergy replaced
SOV-230-1 failed to close during its
2-year surveillance test (CR-IP3-2013-02214), but the issue was not investigated nor
were corrective actions taken. In March 2015, SOV-230-1 failed to close for a third time
(CR-IP3-2015-02133). Work orders were created to investigate the issue but were not
completed before the event on May 9, when the
SOVs had no CRs which documented a failure to close during testing.
However, the inspectors concluded that adverse conditions with these SOVs should
have been discovered by Entergy had an extent of condition review been completed.
Analysis. The inspectors determined that the failure to promptly identify, report, and correct a condition adverse to fire protection associated with SOV-230-1 failure to close on April 7, 2011, April 2, 2013, and March 24, 2015, was a performance deficiency that
was reasonably within Entergy's ability to foresee and correct, and should have been
prevented. The performance deficiency was determined to be more than minor,
because it is associated with the Protection Against External Factors attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone's objective to ensure the availability, reliability, and capability of systems that respond to initiating
events to prevent undesirable consequences. Specifically, water intrusion into the
switchgear room can challenge the reliability of the safety-related electrical equipment required to respond to a reactor transient.
The inspectors screened the finding for significance using the screening questions in IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems," and Exhibit 4, "External Events," and determined that this performance deficiency required a Detailed Risk Evaluation
because the potential existed for enough water leakage into the switchgear room to
cause a loss of all safety-related power and SBO condition.
The actual water accumulation in the switchgear room was not measured. Entergy performed as-found testing and determined the combined leakage from the three deluge
valve
UAT was approximately 12 gpm. This
flowrate would not have resulted in a sufficient volume of water in the room to challenge
the critical height (flooding electrical switchgear cabinets) and therefore, did not result in any increase in core damage frequency. Absent a measured leakage rate, the Region I SRA conducted a bounding Detailed Risk Evaluation using conservative assumptions, to
approximate the potential increase in risk associated with this performance deficiency.
The SRA developed a condition specific event tree and used the following assumptions
in the Detailed Risk Evaluation: If the deluge valve SOV leakage was not isolated, the switchgear room would fill to the critical height of 4.875 inches in six hours. This was based on the licensee determined maximum, as found, drainage system flowrate of 25 gpm and the
approximate 30 minutes elapsed time for water to drain from the room after the
deluge
SRA used a 50 gpm maximum
flowrate into the room for the bounding analysis, representing a flowrate
approximately four times the 12 gpm licensee estimate (See Section 3.b below for the basis of the assumed 50 gpm flowrate). An exposure period of one year. A fire frequency of 6.6E-3 per reactor year, was taken from
- NUREG -2169, representing switchyard large transformer catastrophic failure. Not all large transformer catastrophic failures result in three deluge valves actuating. A 50/50 split was assumed. Successful deluge
- EDG room or use portable pumps) within 6 hours, results in no increase in core damage probability. Flooding of the switchgear room results in a
- SBO with subsequent emergency operating procedure entry and operators taking manual control of the turbine-driven auxiliary feedwater (TDAFW) pump and use the alternate safe shutdown methodology powered via
- MCC 312A. Maintaining Reactor Coolant System Inventory: One charging pump has a capacity of 100 gpm. In the event of a reactor coolant pump (
- RCP [[) seal leakage exceeding 25 gpm per pump (>100 gpm total), one pump would not be sufficient. Standard split fraction for Westinghouse high temperature]]
RCPs on a complete loss of seal cooling following the SBO would result in a 480 gpm
leak per pump. Assuming a complete loss of seal cooling and successful tripping of the RCPs, 0.8 chance of 21 gpm per pump and 0.2 chance of greater than 21 gpm per pump was used.
Maintaining Decay Heat Removal: manual local operation of the
- SRA used Standardized Plant Analysis Risk (SPAR) H to develop the following conservative Operator Action human failure probabilities: Isolate the deluge valve and the
- SOV was contained in the fire response procedure and was specific on operation of these two valves for each deluge system. Human Reliability Analysis (
was estimated assuming a procedurally driven action with high stress and
low experience and training. Secure the fire system, open the doors to the
- HRA -OPS-ISO-MIT-FLD - 1E-2 with expansive time, high stress, low experience and training, and poor procedures. Manual operation of the
- HRA -OPS-TDAFW-MAN) assigned a 1E-2 failure probability (conservatively high given the lower decay heat rate after 6 hours). Trip the
NUREG-1921 for outside the control room remote shutdown actions. In core damage sequences where the combined HRA valve was less than 1E-5, the 1E-5 limit, in accordance with the Risk Assessment Standardization Project manual, was used.
The Detailed Risk Evaluation determined that this performance deficiency was of very low safety significance (Green) with an estimated increase in core damage frequency in
the low E-7 per reactor year range (an increase of 1 in 10 million reactor years). The
Detailed Risk Evaluation dominant core damage sequence for this condition involves:
operators failing to isolate the
- SOV leakage in accordance with the fire protection procedures, the loss of the 480V switchgear in approximately six hours and the resultant
RCPs on the
loss of all seal cooling, and the subsequent RCP seal failures greater than 25 gpm each. The inspectors determined the finding had a cross-cutting aspect in the Human
Performance cross-cutting area, "Challenge the Unknown," because Entergy did not stop and fully explore an uncertain condition with
SOV, but did not determine that
the cause was a clogged pressure switch orifice until after the May 9, 2015, 31 MT fire
event. [H.11] Enforcement. Condition
DPR-64 requires Entergy to implement and maintain in effect all provisions of the approved Fire Protection Program as described in the Final Safety Analysis Report for Indian Point Nuclear Generating Unit
No. 3, and as approved in the
SEs) dated
September 21, 1973; March 6, 1979; May 2, 1980; November 18, 1982; December 30,
1982; February 2, 1984; April 16, 1984; January 7, 1987; September 9, 1988; October 21, 1991; April 20, 1994; January 5, 1995; and supplements thereto.
The
- NRC [[]]
SE dated May 2, 1980, Section 2.5.6, Quality Assurance, Subsection 6.1
states, "The design, procurement, installation, testing, and administrative control
activities for fire protection will be controlled in accordance with the quality assurance program criteria of Appendix A to BTP 9.5-1."
Appendix A to BTP 9.5-1, Section C.8, "Corrective Action," requires measures to be established to assure that conditions adverse to fire protection, such as failures,
malfunctions, deficiencies, deviations, defective components, uncontrolled combustible
materials, and non-conformances are promptly identified, reported, and corrected.
Contrary to the above, on April 7, 2011, April 2, 2013, and March 24, 2015, Entergy did not implement all provisions of the approved Fire Protection Program; in that, Entergy did not assure that a condition adverse to fire protection was promptly identified,
reported, and corrected. Specifically,
MT did not close after energizing to actuate the deluge system. This condition
was not corrected, and recurred on May 9, 2015, when the deluge system actuated in response to a fire on the
- 31 MT. Because the violation was of very low safety significance (Green) and it was entered into the
CAP (CR-IP3-2015-02921), this violation
is being treated as a
NRC Enforcement
Policy. (NCV 05000286/2015010-01, Failure to Correct a Degraded Condition of Fire Protection System Solenoid Valve SOV-230-1) 3. Operator and Fire Brigade Performance in Identifying and Isolating the Source of Water into the Switchgear Room a. Inspection Scope During on-site inspections on May 19-22, the inspectors reviewed the operator and fire brigade performance in identifying and isolating the source of water into the switchgear
room. Specifically, the inspectors reviewed operator logs, written event recollections, procedures, and CRs to assess the actions of licensed operators and fire brigade
members taken in response to the identification of water on the floor of the switchgear room. The inspectors performed walkdowns of the switchgear room and deluge valve room both independently and with members of the fire brigade to verify observations and
recollections from the event. The inspectors interviewed fire brigade members and the
fire brigade leader to understand the actions they took while fighting the fire on 31 MT.
The inspectors interviewed licensed operators to understand their perspective on the
event and their actions taken. The inspectors reviewed Entergy hydraulic analyses of water flow into and out of the switchgear room, and interviewed the engineers who performed the calculations to verify the calculations corresponded with the conditions
observed in the room. The inspectors reviewed design documents of the safety-related
switchgear to verify the height (4.875 inches) at which the water level would adversely
affect the electrical components. b. Assessment and Observations
Fire brigade members who traversed the room during the event identified water
approximately 1 to 2 inches in depth on the floor of the switchgear room. After the door
between the deluge valve room and switchgear room was opened, operators reported that approximately 4 to 6 inches of water had flooded the deluge valve room and flowed out to the switchgear room. Additionally, water was observed to be flowing out of a hub
drain near the instrument air compressor, and from the
UAT deluge valves. This was reported to the fire brigade leader, who at
6:12 p.m., ordered securing of the deluge system. Operators began isolating each deluge valve by closing the local upstream isolation valve, but were unsuccessful when
a yoke on one of the isolation valves (FP-2-2) broke while being operated. Operators then closed the main stop valve to the deluge room (FP-75), which isolated deluge water to all four deluge systems. The water that accumulated in the switchgear room was
reported to have drained completely within 30 minutes after the deluge system had been
isolated. The inspectors determined that Entergy had appropriately identified the source
of water, and performed the proper activities to ensure the water intrusion into the
switchgear room was isolated. The inspectors questioned the actual water level in the room, since reports were not all
consistent (varying from 1 to 2 inches). As discussed in Section 2.b.3, Entergy
performed flow tests and determined that the floor drains, as restricted, could pass a
maximum of 25 gpm. Operators reported the water that accumulated in the switchgear room had completely drained within 30 minutes after the deluge system had been isolated. Assuming the water took 30 minutes to drain, this would have yielded
approximately 750 gallons of water in the switchgear room, which based on the room
volume would equate to 0.4 inches of water level. Therefore, the inspectors determined
that the actual water level in the room could not have substantially exceeded 0.4 inches, and would have been less than the 1 to 2 inches reported. This is further supported by the observation that water did not flood into an area beneath the 32 instrument air
compressor, as this area is effectively sealed around its perimeter by steel angle-iron
that is approximately 1-inch in height.
Entergy performed a calculation (Engineering Calculation 58061) and determined the flowrate through one
SOVs remained open during the event, this would produce approximately 75 gpm of water being ported to the floor of the deluge valve room, for 30 minutes. The inspectors
questioned whether these flowrates could have been the actual flowrates during the
event, since the 75 gpm SOV flow would produce a volume of water in the switchgear room that could not have drained completely in 30 minutes. Specifically, given an input of water of 75 gpm, and subtracting the known drain rate of 25 gpm, a net flowrate of 50
gpm would have flooded the room for 30 minutes and produced approximately 1500
gallons of water in the switchgear room. Given the known drain rate of 25 gpm, this
volume could not have drained completely within the 30 minutes reported by the
operators. In response to the inspectors concerns regarding the SOV flowrates, Entergy performed
as-found flowrate tests of each
- SOV -237-1 produced 5 gpm, 3.6 gpm, and 3.7 gpm, respectively. This would equate to a total of approximately 12 gpm of
SOV flow during the event. The inspectors determined this could not have been the actual flowrates during the event, since this was within the drainage capability of the floor drain system (25 gpm), and therefore would not
have produced significant water accumulation in the switchgear room.
After further evaluation, the inspectors concluded the total combined SOV flowrate
during the event would have had to be approximately 50 gpm. Subtracting the drainage capability of 25 gpm, a net flow of 25 gpm would have entered the switchgear room for 30 minutes. This would have produced approximately 750 gallons of water (0.4 inches
of level), and would have been able to drain completely within 30 minutes. The safety-
related switchgear equipment was not adversely affected by 0.4 inches of water since the electrical components are 4.875 inches off the ground.
The inspectors determined that y-strainers in the piping leading to each SOV had never been cleaned or inspected, and concluded that clogging from debris known to be in the
system may have produced a low as-found flowrate (12 gpm). The initial flowrate during the event reduced to 12 gpm as this debris clogged the y-strainer. Entergy entered this
issue into the CAP to create a preventive maintenance item to open, inspect, and clean
the y-strainers (CR-IP3-2015-02921). c. Findings
No findings were identified.
4. Effectiveness of Entergy Response to Water Intrusion a. Inspection Scope The inspectors reviewed the effectiveness of Entergy's response to the water accumulation in the switchgear room. Specifically, the inspectors reviewed corrective actions taken in response to the water intrusion both during and following the event to
verify they would effectively address the issue. The inspectors reviewed the design of a
temporary modification intended to divert water away from the safety-related switchgear
room, and reviewed a standing order issued to site operators to ensure they would
properly address the water intrusion event without introducing new safety concerns or challenges. The inspectors reviewed records associated with the repair and post-maintenance testing of the deluge valves. The inspectors reviewed documentation for
cleaning of the transformer yard storm drains and switchgear room floor drains. b. Assessment and Observations In response to the water intrusion, Entergy immediately secured the deluges and took
action to remove the water from the room. Following the event, Entergy implemented a
temporary modification to provide a pathway for the water to drain from the Unit 3 480V switchgear room. The room is connected to the 31 EDG room, which contains a large
sump and drain line to mitigate potential service water pipe breaks. The temporary modification included a berm to direct water from the switchgear room to the sump, pre-staged chocks to hold two fire doors open, and steps added to the plant fire response
and alarm response procedures to direct a plant operator to open the doors and institute
a firewatch. To address extent of condition, a standing order was issued to Unit 2 that
directed a plant operator to respond to the Unit 2 480V switchgear room in the event the transformer deluge systems actuate, who would then monitor for leakage or open the door between the deluge room and the turbine building to allow water to drain.
Entergy also took action to inspect the floor drain lines for blockages. Several blockages
were identified downstream of the floor drains. Entergy performed troubleshooting
activities and determined that the drain next to the deluge valves could drain a steady-state flow rate of only 6 gpm. As stated earlier, further testing showed that the entire floor drain system for the room could drain a maximum of 25 gpm. Entergy cleaned the
floor drains and the post-maintenance testing verified the floor drains could drain
approximately 100 gpm.
Through troubleshooting, Entergy identified that the pressure switches associated with
each SOV were unable to sense downstream pressure accurately due to plugged orifices. Entergy cleaned the orifices, replaced one pressure switch, and performed post-maintenance testing to verify that the system would close the solenoid valves as
designed. The inspectors concluded the actions taken by Entergy in response to the
water intrusion were reasonable to prevent the event from recurring.
c. Findings
No findings were identified.
5. Evaluation of Pertinent Industry Operating Experience a. Inspection Scope The inspectors reviewed Entergy's evaluation of pertinent operating experience.
Specifically, inspectors searched Entergy's CAP database for previous similar events at Indian Point to determine whether those events should have driven Entergy to reduce the likelihood of the May 9 water accumulation event before it occurred. The inspectors also reviewed actions taken by the site in response to an industry operating experience
event that involved a switchgear room flooding event. b. Assessment and Observations In 1996, New York Power Authority, then-owner of Indian Point Unit 3, evaluated an industry operating experience event, Significant Event Report (SER) 95-8, where
unexpected service water leakage flooded a switchgear room and required the plant to
de-energize electrical busses in the room. As part of their evaluation, New York Power
Authority identified that the sources of water in the Unit 3 480V switchgear room included the fire protection piping and two service water relief valves. They calculated that the expected flow rate from the service water relief valves was 58 gpm. They did
not quantify the postulated leak rate from the fire protection piping in their evaluation, but
concluded that it was bounded by the expected drain rate of the floor drains, which was
calculated to be approximately 100 gpm. Entergy's periodic maintenance program
included testing the 480V switchgear room floor drains every 2 years to verify that they could drain 10 gallons of water in less than one minute, which was a substantially lower flowrate than that assumed in the operating experience analysis. The inspectors
determined that had the floor drain system been rigorously tested and maintained clean,
the May 9 event would not have resulted in as much water accumulation on the floor.
The inspectors also reviewed Entergy's corrective actions taken in response to water accumulation in the Unit 2 switchgear room during a severe weather event in August
2011 (see NRC Inspection Report 05000247/2012002). As a corrective action, Entergy
implemented a surveillance program for the Unit 2 switchgear room floor drains that mirrored the existing surveillance program on Unit 3, because at that time Unit 2 had not
been performing preventive maintenance on the Unit 2 floor drain system. c. Findings
No findings were identified.
6. Risk Significance of the Event Initial Assessment The initial risk assessment for this event is documented in the enclosed SIT Inspection
Team Charter (Attachment 1).
Final Assessment While there was no actual reactor core damage consequence of the May 9, 2015,
SRA used the model and assumptions developed to evaluate the risk
significance of the performance deficiency discussed above in Section 2.c, to estimate
the chance that such a fire could have progressed to core damage. This bounding
conditional core damage probability estimate was in the range of low E-5 per event (1 in 100,000 such events).
7. Exit Meetings On June 24, 2015, the team presented their overall assessment and observations to Mr. Larry Coyle, Site Vice President, and other members of his staff. The inspectors confirmed that any proprietary information reviewed during the inspection was returned
to Entergy.
- ATTACH [[]]
- TEAM [[]]
- ATTACH [[]]
- DETAIL [[]]
- ED [[]]
- SEQUEN [[]]
- CE [[]]
- OF [[]]
- EVENTS [[]]
- ATTACH [[]]
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- TEAM [[]]
CHARTER Indian Point Nuclear Generating Unit No. 3 Water Accumulation in Safety-Related Switchgear Room Following Deluge of a #31 Main Transformer Fire May 9, 2015 Background: On May 9, 2015, at 5:50 p.m., Indian Point Unit 3 experienced an automatic reactor trip as a result of a failure of the #31 main transformer. A Notification of Unusual Event (UE) was
declared at 6:01 p.m. for an explosion or fire within the station's Protected Area. The fire was
initially extinguished by the station's deluge system. The fire then reignited and was extinguished by both the site fire brigade and two offsite fire departments who responded to the event. The UE was exited at 9:03 p.m.
The reactor trip was uncomplicated. All control rods inserted into the reactor core, and all safety
systems responded as designed. The NRC Resident Inspectors responded to the site and
independently confirmed that the plant was in a stable, safe condition. After the reactor trip, Unit 3 was placed in Mode 4, Hot Shutdown, with normal offsite electrical
power available and decay heat being removed by the residual heat removal system. Unit 2
continues to operate at 100 percent power.
During the event, approximately 1" to 2" of water accumulated in the safety-related switchgear room. The switchgear room is risk significant as it contains all trains of safety-related 480 volt power. If the switchgear is lost, other alternate sources of power can be used to safely maintain
the plant shutdown.
Basis for the Formation of the SIT: Brief Description of the Basis for the Assessment:
The Inspection Manual Chapter (IMC) 0309 review concluded that one of the deterministic
criteria in Enclosure 1 of IMC 0309 was met. The criterion met was for the significant,
unexpected system interaction between the fire protection deluge system and the safety-related switchgear room.
Using the Indian Point Standardized Plant Analysis Risk (SPAR) models, a Region I Senior
Reactor Analyst conducted a preliminary risk analysis. The estimated conditional core damage probability (CCDP) for Unit 3 was in the 4 E-6 to 2 E-5 range. Based upon satisfying the deterministic criterion and the estimated
- CC [[]]
DP values for Unit 3
being in the 4 E-6 to 2 E-5 range per the
- SP [[]]
AR models, the reactive inspection response is
within the "No Additional Inspection to Special Inspection" overlap to the "Special Inspection to
Augmented Inspection Team" overlap range for Unit 3. A SIT is being initiated to gather
information available from the event and to verify that immediate corrective actions were appropriate.
Objectives of the Special Inspection: The SIT will expand on the inspection activities started by the resident inspectors immediately after the event. The team will review Entergy's organizational and operator response to the event, equipment performance and design, and the licensee casual analyses, as applicable.
The team will collect data, as necessary, to refine the preliminary risk analysis. The team will also assess whether the SIT should be upgraded to an Augmented Inspection Team.
To accomplish these objectives, the team will: 1. Develop a complete sequence of events including follow-up actions taken by Entergy; 2. Review and assess the equipment response to the fire resulting in water accumulation in the switchgear room. This assessment should evaluate the system response against the plant's design and regulatory requirements to assess the
adequacy of the equipment design and maintenance; 3. Review and assess operator and fire brigade performance in identifying and isolating the sources of water into the switchgear room, including review of procedures, logs, and communications (internal and external); 4. Review and assess the effectiveness of Entergy's response to the water intrusion. This includes overall organizational response, failure modes and effect analysis
developed for the equipment challenges, and interim and proposed longer term corrective actions; 5. Review Entergy's evaluations of pertinent industry fire-fighting operating experience and evaluation of potential precursors relating to the potential for water
accumulation, including the effectiveness of any actions taken; and 6. Collect data necessary to refine the existing risk analysis and document the final risk analysis in the
- SIT report. Guidance: Inspection Procedure 93812, "Special Inspection," provides additional guidance to be used by the
SIT. Team duties will be as described in Inspection Procedure 93812. The inspection
should emphasize fact-finding in its review of the circumstances surrounding the event. Safety
concerns identified that are not directly related to the event should be reported to the Region I
office for action. The Team will conduct an entrance meeting and begin the inspection on May 19, 2015. While
on site, the Team Leader will provide daily briefings to Region I management, who will coordinate with the Office of Nuclear Reactor Regulation to ensure that all other parties are kept
informed. A report documenting the results of the inspection will be issued within 45 days
following the final exit meeting for the inspection. This Charter may be modified should the team develop significant new information that warrants
review.
Attachment
- 2 DETAIL [[]]
- ED [[]]
- SEQUEN [[]]
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- OF [[]]
EVENTS This sequence of events was constructed by the team from review of the Control Room Narrative Log, corrective action program condition reports, process plant computer data, and plant personnel interviews. 5/9/15 1750 Unit 3 Main Generator lockout, turbine trip, reactor trip. #31 and #32 main transformer, unit auxiliary transformer, and curtain wall deluge systems activate. Motor driven fire pump automatically starts. Control Room enters E-0, "Reactor Trip of Safety Injection." 5/9/15 1752 Unit 3 control room acknowledges alarms on the Fire Display Control Panel alerting operators that the transformer deluge and wall curtain fire suppression systems had activated. Control
room enters 3-ONOP-FP-1, "Plant Fires." Fire Brigade is activated.
5/9/15 1753 Fire at #31 main transformer reported from the field. Verplanck Fire Department is called for assistance. Montrose Fire Department is also notified for mutual aid to Verplanck. 5/9/15 1757 Control Room air conditioning is placed in 100 percent recirculation mode in accordance with 3-ONOP-FP-1.
5/9/15 1759 Control room transitions from E-0 to
- ES -0.1, "Reactor Trip Response." 5/9/15 1800 Diesel driven fire pump automatically starts. 5/9/15 1801 Notification of Unusual Event (
- EAL [[]]
HU2.2 "Report of Explosion in the Protected Area Resulting in Damage to Plant Equipment."
5/9/15 1802 Verplanck Fire Department fire engines (2) arrive at Indian Point and are kept in standby at the front gate. 5/9/15 1807 Security reports that there is oil in the discharge canal. 5/9/15 1808 Fire Brigade Leader reports that fire on bushing will be attacked with foam. Offsite agencies notified via NYS Radiological Emergency Communications System.
5/9/15 1812 Fire Brigade orders securing deluge system as water is reported in the Unit 3 480V switchgear room. 5/9/15 1815 Fire Brigade Leader reports fire is extinguished. 5/9/15 1816 Deluge system is attempted to be isolated but leak-by is reported. 5/9/16 1819 Entergy notifies the
FP-75 is closed to aid in the isolation of the deluge system. This isolates fire water to all four deluge systems.
5/9/15 1837 Fire Brigade Leader reports that the fire on #31 main transformer has reflashed. Entergy processes Verplanck Fire Department engines into the Protected Area. Requests are made for
a tower ladder from Montrose Fire Department. 5/9/15 1847 Control Room transitions from
POP-3.2, "Plant Recovery from Trip, Hot Standby." 5/9/15 1850 Operators report that all the water in the switchgear room has drained completely (30 minutes after the deluge system had been isolated). 5/9/15 1851 Entergy notifies NY State Public Service Commission.
5/9/15 1900 Montrose Fire Department tower ladder arrives on scene. 5/9/15 1945 Entergy calls National Response Center as a result of oil spilled and making its way to the Hudson River. 5/9/15 1953 Entergy calls Westchester
- DEC. 5/9/15 2005 Fire Brigade Leader reports that the fire is extinguished. 5/9/15 2100 Entergy calls an environmental cleanup contractor. 5/9/15 2103
NOUE exited based on the fact that the fire is out and transformer indicates cooling is successful.
5/9/15 2135 Verplanck and Montrose fire companies depart site.
Attachment 3
- SUPPLE [[]]
- MENTAL [[]]
- INFORM [[]]
- ATION [[]]
- KEY [[]]
- POINTS [[]]
- OF [[]]
CONTACT
Licensee Personnel Contacted S. Radomski, Fire Brigade Leader
R. Burroni, Director, Engineering M. Kempski, Manager, Engineering J. Bridges, Fire Brigade Member
G. Grimes, Fire Brigade Member
A. Zastrow, Shift Manager
J. Johnson, Fire Brigade Leader J. Pineda, Design Engineering Supervisor T. Chan, Design Engineering Supervisor
- LIST [[]]
- OF [[]]
- ITEMS [[]]
- AND [[]]
- DISCUS [[]]
SED
Opened/Closed 05000286/2015010-01 NCV Failure to Correct a Degraded Condition of Fire Protection System
Solenoid Valve SOV-230-1 (Section
2.c).
- LIST [[]]
- OF [[]]
- DOCUME [[]]
- NTS [[]]
- REVIEW [[]]
ED In addition to the documents identified in the body of this report, the inspectors reviewed the following documents and records.
Condition Reports
IP3-2015-03090 Work Orders WO 00346693, "Valve Leaking One Drop Per Second, and Gland Stud Is Broken"
WO 00273284, "Valve Does Not Close When De-Energized By Normal Means"
AOP-SEISMIC-1, "Seismic Event," Revision 7
3-AOP-FLOOD-1, "Flooding," Revision 9
OAP-008, "Severe Weather Preparations," Revision 22
3-ONOP-FP-1, "Plant Fires," Revision 38 3-ONOP-FP-1, "Plant Fires," Revision 39 3-PT-R040, "Transformer Yard Water Deluge Systems Testing," Revision 19
3-PT-R040, "Transformer Yard Water Deluge Systems Testing," Revision 20, completed 3/24/15
AOP-FLOOD-1, Flooding, Revision 09 2-AOP-FLOOD-1, Flooding, Revision 10
3-PT-R040, Transformer Yard Water Deluge Systems Testing, Revision 20
0-MET-402-GEN, Location of Sandbags in Flood Warning Conditions, Revision 3
Miscellaneous Indian Point Unit 3 Final Safety Analysis Report, Revision 05, 2013 Indian Point Unit 3 Technical Requirements Manual
Indian Point Unit 3 Operations Log
PFP-380, "Main Transformer Yard," Revision 3 Standing Order 15-04
Event Recollections from 5/9/15
Mod No. 93-03-433
- LER 93-51-00, "A Seismically Induced Failure of a Fire Main, Caused by Personnel Error, Can Place the Plant Outside Design Basis"
LPI Inc. Report F15202-LR-002, Drainage Flows - 31 MT Incident of May 9th 2015, Revision 0 Post Transient Evaluation: Unit 3 Trip Due To Fire/Explosion on 31 Main Transformer Event Recollection Form, Nuclear Plant Operator (1) Event Recollection Form, Nuclear Plant Operator (2) Event Recollection Form, Nuclear Plant Operator (3)
Event Recollection Form, Nuclear Plant Operator (4)
Event Recollection Form, Fire Brigade Member
Event Recollection Form, Control Room Supervisor/Shift Technical Advisor Event Recollection Form, Fire Brigade Leader
CALC-FD-01821, G45-0126 Floor Drains Response to SER 95-8, Revision 0
480V Water Intrusion Position Paper, Revision 1
480V Water Intrusion Position Paper, Revision 0
Event Notification 51060, Unusual Event Declared Due to Main Transformer Fire
Tyco Fire Suppression and Building Products Catalog
- TD 117G, Deluge Valves, Vertical - 4&6 Inch, Model A-4 Multimatic, dated 3-87 Tyco Fire Suppression and Building Products Catalog
TFP1630, Model A-1 Automatic Drin Valve Trim Component for Dry Pipe, Deluge, and Preaction Valves, dated July 2010 NRC Safety Evaluation Report dated May 2, 1980
Fire Drill Report, Fire Brigade timeline of May 9, 2015 event A/R 228018228018Calculations
EC 58061, dated 06/03/15
Drawings 9321-F-40633-10, "Turbine and Control Building Floor and Hub Drains - El 15'-0"," Revision 10 9321-LL-30420-18, "Schematic Diagram Fire Protection Water System, Main, Unit Aux and Station Aux Transformers," Revision 3 9321-F-40033-11, "Turbine Building and Heater Bay Floor and Hub Drains - El 15'-0"," Revision 11 9321-F-40913, Sh. 1, "Flow Diagram of Plant Fire Protection System Sheet No. 2," Revision 29 9321-F-40913, Sh. 2, "Flow Diagram of Plant Fire Protection System Sheet No. 3," Revision 5 9321-LL-30420, Sh. 18, Schematic Diagram Fire Protection Water System Main Unit and Station Aux Transformers, Revision 3 154D938, Consolidated Edison Co. Indian Point Station,
- LVME [[]]
- SW [[]]
GR 31&32, Unit No. 3, Revision 10 9321-F-30893, Conduit Layout, Control Building, Revision 86 A202612, Turbine & Control Building Floor and Hub Drains, Plan El. 15'-0", Revision 10
21-F-40913, Sh. 1, Flow Diagram of Plant Fire Protection System, Sheet No. 2, Revision 29
21-F-40913, Sh. 2, Flow Diagram of Plant Fire Protection System Sheet No. 3, Revision 5
A202494, Yard Storm Drains Plan, Revision 14
5651D72, Logic Diagram Turbine Trip Signals, Revision 10 Fire Brigade Training Documents Fire Brigade Training Lesson
- VI [[]]
II, Water and Foam Application
Fire Brigade Training Outline Lesson
OPS-FBT003, Fire Brigade Annual Retraining, Revision 2014 Fire Brigade Training Lesson IX, Electricity and Fire
Fire Brigade Training Lesson XIV, Site Specific Training
Design Basis Documents
- LIST [[]]
- OF [[]]
- ACRONY [[]]
- MS [[]]
CR condition report DRP Division of Reactor Projects
DRS Division of Reactor Safety
EDG emergency diesel generator
gpm gallons per minute
IMC Inspection Manual Chapter MH manhole
RCP reactor coolant pump
SBO station blackout
- SP [[]]
AR Standardized Plant Analysis Risk
- TDA [[]]
FW turbine-driven auxiliary feedwater