05000285/LER-2012-012, Regarding Multiple Safety Injection Tanks Rendered Inoperable

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Regarding Multiple Safety Injection Tanks Rendered Inoperable
ML12227A289
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 08/13/2012
From: Bannister D
Omaha Public Power District
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LIC-12-0112 LER 12-012-00
Download: ML12227A289 (5)


LER-2012-012, Regarding Multiple Safety Injection Tanks Rendered Inoperable
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
2852012012R00 - NRC Website

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Omaha Public PowBrOlslrlcl 444 South 16th Street Mall Omaha, NE 68102-2247 LlC-12-0112 August 13, 2012 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001

Reference:

Docket No. 50-285

Subject:

Licensee Event Report 2012-012, Revision 0, for the Fort Calhoun Station Please find attached Licensee Event Report 2012-012, Revision 0, dated August 13,2012. This report is being submitted pursuant to 10 CFR 50.73(a)(2)(i)(B),

10 CFR 50.73(a)(2)(v)(D), and 10 CFR 50.73(a)(2)(vii)(D).

No commitments are being made in this letter.

If you should have any questions, please contact me.

Sincerely,

/J~

D. i Bannister Vice President and CNO DJB Irjrlsds Attachment c:

E. E. Collins, Jr., NRC Regional Administrator, Region IV L. E. Wilkins, NRC Project Manager J. C. Kirkland, NRC Senior Resident Inspector INPO Records Center Employment with Equal Opportunity

NRC FORM 366 (10-2010)

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (10-2010)

LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME Fort Calhoun Station
2. DOCKET NUMBER 05000285
3. PAGE 1 OF 4
4. TITLE Multiple Safety Injection Tanks Rendered Inoperable
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.

MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 03 19 2012 2012 - 012 -

0 08 13 2012 FACILITY NAME DOCKET NUMBER 05000

9. OPERATING MODE 5
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D)

Specify in Abstract below or in LICENSEE EVENT REPORT (LER)

CONTINUATION SHEET CONCLUSION A cause analysis is in progress. The results of the analysis will be published in a supplement to this LER.

CORRECTIVE ACTIONS

A cause analysis is in progress. The corrective actions will be published in a supplement to this LER.

SAFETY SIGNIFICANCE

A cause analysis is in progress. The results of the analysis will be published in a supplement to this LER.

SAFETY SYSTEM FUNCTIONAL FAILURE This event does result in a safety system functional failure in accordance with NEI-99-02.

PREVIOUS EVENTS A cause analysis is in progress. Previous events will be determined from the results of the cause analysis.