Letter Sequence Request |
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Initiation
- Request, Request, Request, Request, Request, Request, Request
- Acceptance...
- Supplement, Supplement, Supplement, Supplement, Supplement, Supplement
Results
Other: L-MT-05-089, Documentation of Responses to Aging Management Program and Aging Management Review Audits for the Monticello License Renewal Application, L-MT-05-096, Additional Information in Response to Aging Management Program and Aging Management Review Audits of the Monticello License Renewal Application, L-MT-05-099, Response to Three Requests for Additional Information Regarding the Monticello License Renewal Application, L-MT-05-108, Response to Two Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application, L-MT-05-115, Response to Two Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application, L-MT-06-015, Confirmatory Items Response Regarding the Monticello Nuclear Generating Plant License Renewal Application, L-MT-06-018, License Renewal Application Annual Update, L-MT-06-049, (Mngp), Comments Regarding the Safety Evaluation Report for MNGP License Renewal Application, L-MT-06-060, License Renewal Application Update, ML051580005, ML051600008, ML051600081, ML051990091, ML060340200, ML070450211
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MONTHYEARL-MT-05-014, Transmittal of Monticello Nuclear Generating Plant Application for Renewed Operating License2005-03-16016 March 2005 Transmittal of Monticello Nuclear Generating Plant Application for Renewed Operating License Project stage: Request SBK-L-05062, License Amendment Request 04-05 Changes to Spent Fuel Assembly Storage Technical Specifications2005-03-28028 March 2005 License Amendment Request 04-05 Changes to Spent Fuel Assembly Storage Technical Specifications Project stage: Request ML0513802172005-05-11011 May 2005 Presentation Slides Used at Meeting on May 11, 2005, Between the NRC and NMC to Discuss Monticello LRA Project stage: Meeting 05000263/LER-1950-004, Regarding Voluntary LER for Control Rod Drive Insert Line Leakage2005-05-12012 May 2005 Regarding Voluntary LER for Control Rod Drive Insert Line Leakage Project stage: Request ML0514001152005-05-18018 May 2005 Summary of 05/11/2005 Meeting Between the U.S. Nuclear Regulatory Commission and the Nuclear Management Company, LLC Representatives to Discuss the Monticello Nuclear Generating Plant License Renewal Application Project stage: Meeting ML0514002342005-05-18018 May 2005 Revision of Schedule for the Conduct of Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: Approval ML0516000082005-06-0202 June 2005 Audit & Review Plan for Plant Aging Management Reviews & Programs for Monticello Nuclear Generating Plant Project stage: Other ML0515800052005-06-0202 June 2005 Audit and Review Plan for Plant Aging Management Reviews and Programs for the Monticello Generating Plant Project stage: Other ML0516000812005-06-0909 June 2005 Memo Issuing Audit and Review Plan for Plant Aging Management Reviews and Programs for the Monticello Nuclear Generating Plant Project stage: Other L-MT-05-052, Monticello. Response to Request for Additional Information and Submittal of Additional Information in Support of the Plant License Renewal Application2005-06-10010 June 2005 Monticello. Response to Request for Additional Information and Submittal of Additional Information in Support of the Plant License Renewal Application Project stage: Response to RAI ML0519900912005-07-18018 July 2005 Audit Trip Report Regarding the Nuclear Management Company Application for License Renewal for the Monticello Nuclear Generating Plant Dated 03/16/05 Project stage: Other L-MT-05-082, Response to Request for Additional Information Regarding the Monticello License Renewal Application2005-07-21021 July 2005 Response to Request for Additional Information Regarding the Monticello License Renewal Application Project stage: Response to RAI L-MT-05-089, Documentation of Responses to Aging Management Program and Aging Management Review Audits for the Monticello License Renewal Application2005-08-11011 August 2005 Documentation of Responses to Aging Management Program and Aging Management Review Audits for the Monticello License Renewal Application Project stage: Other L-MT-05-092, Response to Request for Additional Information Regarding the Monticello License Renewal Application2005-08-16016 August 2005 Response to Request for Additional Information Regarding the Monticello License Renewal Application Project stage: Response to RAI ML0523100552005-08-18018 August 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI ML0523100442005-08-18018 August 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI ML0523100132005-08-18018 August 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI L-MT-05-096, Additional Information in Response to Aging Management Program and Aging Management Review Audits of the Monticello License Renewal Application2005-08-31031 August 2005 Additional Information in Response to Aging Management Program and Aging Management Review Audits of the Monticello License Renewal Application Project stage: Other L-MT-05-093, License Amendment Request - Full Scope Application of an Alternative Source Term2005-09-15015 September 2005 License Amendment Request - Full Scope Application of an Alternative Source Term Project stage: Request ML0526206222005-09-15015 September 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI L-MT-05-099, Response to Three Requests for Additional Information Regarding the Monticello License Renewal Application2005-09-16016 September 2005 Response to Three Requests for Additional Information Regarding the Monticello License Renewal Application Project stage: Other L-MT-05-086, Update Monticello Nuclear Generating Plant Technical Specification Bases Change2005-09-16016 September 2005 Update Monticello Nuclear Generating Plant Technical Specification Bases Change Project stage: Request ML0526206092005-09-16016 September 2005 9/16/05 - Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI ML0527301752005-09-28028 September 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI L-MT-05-108, Response to Two Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application2005-10-14014 October 2005 Response to Two Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Other L-MT-05-111, Response to Requests for Additional Information Regarding the Plant License Renewal Application2005-10-28028 October 2005 Response to Requests for Additional Information Regarding the Plant License Renewal Application Project stage: Response to RAI ML0530504362005-10-31031 October 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI ML0531200032005-11-0707 November 2005 Request for Additional Information for the Review of the Monticello Nuclear Generating Plant License Renewal Application Project stage: RAI ML0531200692005-11-15015 November 2005 Safety Evaluation Report on the Scoping and Screening Results for Monticello License Renewal Application Project stage: Approval L-MT-05-114, Supplement to Responses to Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application2005-11-17017 November 2005 Supplement to Responses to Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Supplement L-MT-05-115, Response to Two Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application2005-11-22022 November 2005 Response to Two Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Other ML0532603592005-11-22022 November 2005 Safety Evaluation Report Input for the Monticello Nuclear Generating Plant License Renewal Application Project stage: Approval ML0532605042005-11-22022 November 2005 Memo Issuing, Safety Evaluation Report Input for the Monticello Nuclear Generating Plant License Renewal Application Project stage: Approval L-MT-05-117, Response to Request for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application2005-12-0707 December 2005 Response to Request for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Response to RAI ML0534802162005-12-12012 December 2005 Safety Evaluation Report Regarding the License Renewal Application for Monticello Nuclear Generating Plant Project stage: Approval L-MT-05-121, Supplement to Responses to Requests for Additional Information Regarding the License Renewal Application2005-12-16016 December 2005 Supplement to Responses to Requests for Additional Information Regarding the License Renewal Application Project stage: Supplement ML0603402002006-01-30030 January 2006 Summary of a Telephone Conference Call Held on 01/12/ 2006, Between the U.S. Nuclear Regulatory Commission and Nuclear Management Company, LLC, Concerning Information Pertaining to the Monticello Nuclear Generating Plant License Renewal App Project stage: Other L-HU-06-009, Units 1 and 2 - Fitness for Duty Performance Data2006-02-27027 February 2006 Units 1 and 2 - Fitness for Duty Performance Data Project stage: Request L-MT-06-014, Supplement to Responses to Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application2006-02-27027 February 2006 Supplement to Responses to Requests for Additional Information Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Supplement L-MT-06-015, Confirmatory Items Response Regarding the Monticello Nuclear Generating Plant License Renewal Application2006-02-28028 February 2006 Confirmatory Items Response Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Other L-MT-06-018, License Renewal Application Annual Update2006-03-15015 March 2006 License Renewal Application Annual Update Project stage: Other 05000263/LER-2006-001, Unplanned LCO Due to Emergency Filter Flexible Connector Failure2006-03-31031 March 2006 Unplanned LCO Due to Emergency Filter Flexible Connector Failure Project stage: Request L-MT-06-019, Supplemental Information and Response to Requests for Additional Information Regarding Monticello Nuclear Generating Plant License Renewal Application2006-03-31031 March 2006 Supplemental Information and Response to Requests for Additional Information Regarding Monticello Nuclear Generating Plant License Renewal Application Project stage: Supplement L-MT-06-029, Supplemental Information Regarding Monticello Nuclear Generating Plant License Renewal Application2006-04-10010 April 2006 Supplemental Information Regarding Monticello Nuclear Generating Plant License Renewal Application Project stage: Supplement L-MT-06-037, Comments Regarding the Draft Plant-Specify Supplement 26 to the Generic Environmental Impact Statement for Plant License Renewal Application2006-04-26026 April 2006 Comments Regarding the Draft Plant-Specify Supplement 26 to the Generic Environmental Impact Statement for Plant License Renewal Application L-MT-06-049, (Mngp), Comments Regarding the Safety Evaluation Report for MNGP License Renewal Application2006-06-15015 June 2006 (Mngp), Comments Regarding the Safety Evaluation Report for MNGP License Renewal Application Project stage: Other ML0617805322006-06-23023 June 2006 Supplemental Information Regarding the Monticello Nuclear Generating Plant License Renewal Application Project stage: Supplement L-MT-06-060, License Renewal Application Update2006-08-18018 August 2006 License Renewal Application Update Project stage: Other ML0704502112007-02-23023 February 2007 Letter Correcting Errors in Renewed Facility Operating License Project stage: Other 2005-07-18
[Table View] |
LER-1950-004, Regarding Voluntary LER for Control Rod Drive Insert Line Leakage |
| Event date: |
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| Report date: |
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| Reporting criterion: |
10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(ix)(A)
10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(x)
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)(viii)(A)
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(viii)(B) |
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| 2631950004R00 - NRC Website |
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text
Monticello Nuclear Generating Plant Operated by Nuclear Management Company, LLC May 12, 2005 L-MT-05-035 10 CFR Part 50.73 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 Monticello Nuclear Generating Plant Docket No. 50-263 License No. DPR-22 LER 2005-004, - Voluntary LER for Control Rod Drive Insert Line Leakage A Voluntary Licensee Event Report for this occurrence is attached.
This letter makes no new commitments or changes any existing commitments.
Thomas J. Palmisano Site Vice President, Monticello Nuclear Generating Plant Nuclear Management Company, LLC Enclosure cc:
Administrator, Region III, USNRC Project Manager, Monticello, USNRC Resident Inspector, Monticello, USNRC 2807 West County Road 75
- Monticello, Minnesota 55362-9637 Telephone: 763-295-5151
NRC FORM 366 U.S. NUCLEAR REGULATORY (6-2004)
COMMISSION LICENSEE EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
APPROVED BY OMB NO. 3150-0104 EXPIRES 6-30-2007
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
FACILITY NAME (1)
DOCKET NUMBER (2)
PAGE (3)
Monticello Nuclear Generating Plant 05000263 1 of 2 TITLE (4) Voluntary LER for Control Rod Drive Insert Line Leakage EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
MO DAY YEAR YEAR SEQUENTIAL NUMBER REV NO MO DAY YEAR FACILITY NAME DOCKET NUMBER 05000 03 09 2005 2005
- - 004
- - 00 05 12 2005 FACILITY NAME DOCKET NUMBER 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) (11)
MODE (9)
N 20.2201(b) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(B) 50.73(a)(2)(ix)(A)
POWER 20.2201(d) 20.2203(a)(4) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LEVEL (10) 0 20.2203(a)(1) 50.36(c)(1)(i)(A) 50.73(a)(2)(iv)(A) 73.71(a)(4) 20.2203(a)(2)(i) 50.36(c)(1)(ii)(A) 50.73(a)(2)(v)(A) 73.71(a)(5) 20.2203(a)(2)(ii) 50.36(c)(2) 50.73(a)(2)(v)(B)
X 20.2203(a)(2)(iii) 50.46(a)(3)(ii) 50.73(a)(2)(v)(C) 20.2203(a)(2)(iv) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(D)
Voluntary 20.2203(a)(2)(v) 50.73(a)(2)(i)(B) 50.73(a)(2)(vii) 20.2203(a)(2)(vi) 50.73(a)(2)(i)(C) 50.73(a)(2)(viii)(A) 20.2203(a)(3)(i) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(B)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
Ron Baumer 763-295-1357 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX
CAUSE
SYSTEM COMPONENT MANU-FACTURER REPORTABLE TO EPIX B
AA PSP No SUPPLEMENTAL REPORT EXPECTED (14)
MONTH DAY YEAR YES (If yes, complete EXPECTED SUBMISSION DATE).
X NO EXPECTED SUBMISSION DATE (15)
ABSTRACT A voluntary License Event Report is being provided for the following event:
On March 5, 2005 with the Monticello Nuclear Generating plant in a refueling outage, during a scheduled under-vessel walk down, a small water leak was noted on a control rod drive flange. On March 9, Nuclear Management Company (NMC) determined that the leakage was from the top surface of the flange adjacent to the Control Rod Drive (CRD) insert line. The leakage was determined to be active and the result of a flaw in the insert line to CRD flange weld. Metallurgical examination determined that the leak initiated at a small weld void in the weld between the insert line and the CRD housing flange created during original construction. Corrective action taken included performance of a metallurgical, chemical and visual examination of the leaking section of the CRD insert line, replacement of a section of the insert line to re-make the weld at the CRD flange, and a 100 percent visual inspection of the other control rod drive flanges for leakage.
OTHER Specify in Abstract below or in NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION (1-2001)
LICENSEE EVENT REPORT (LER)
FACILITY NAME (1)
DOCKET (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL NUMBER REVISION NUMBER Monticello Nuclear Generating Plant 05000263 2005 004 00 2 of 2 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) Description On March 5, 2005 with the Monticello Nuclear Generating plant in a refueling outage, during a scheduled primary containment under vessel [RPV] walk down, a small water leak was noted on a control rod drive (CRD) [AA] flange. On March 9, Nuclear Management Company (NMC) determined that the leakage was from the top surface of the flange adjacent to the CRD insert line [PSP]. The leakage was determined to be active and the result of a flaw in the insert line to flange weld. The CRD was isolated to prevent movement and the drive was considered inoperable until the leak was repaired.
A portion of the insert piping was removed for examination and replaced under a station modification.
Following repairs, the CRD was tested and restored to service.
Event Analysis
The event was not reportable in accordance with 10 CFR 50.72 or 10 CFR 50.73, however in accordance with NUREG-1022 revision 2, a voluntary Licensee Event Report is being made for this event. The event is not classified as a safety system functional failure.
Safety Significance
The safety significance of this issue was low since the CRD was always capable of inserting into the reactor. In the event that the insert line severed at reactor power, the CRD could be inserted by using reactor pressure alone. The safety function of the CRD system would not be affected. The CRD insert lines are not part of the reactor coolant pressure boundary. A risk analysis determined that the effect on the Core Damage Frequency is less than 1 X 10-7 per year. This event had no adverse affect on the health and safety of the pubic.
Cause
Metallurgical examination of the pipe determined that the leak was the result of a small weld void in the weld between the insert line and the CRD housing flange created during original construction.
Corrective Action
A short section of pipe was removed and replaced under a station modification. A visual inspection of all CRD insert and withdrawal piping connections at the CRD flange was performed and no other leakage was observed.
Failed Component Identification Pipe Manufacturer: Greenville Tubes, Inc (Greenville, PA)
Previous Similar Events
A review of the station corrective action program and industry databases found the following similar events: Monticello (LER 1998-03), Brunswick (LER 2-88-007), and Duane Arnold (LER 88-019). Each of these events involved leakage from either the CRD insert or withdrawal lines, however in each case, the leakage was attributed to a corrosion failure mechanism of the pipe. The event discussed in LER 2005-04 was due to a weld void created during original construction.
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| | | Reporting criterion |
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| 05000263/LER-1950-004, Regarding Voluntary LER for Control Rod Drive Insert Line Leakage | Regarding Voluntary LER for Control Rod Drive Insert Line Leakage | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
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