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Category:Graphics incl Charts and Tables
MONTHYEARML16056A1392016-03-11011 March 2016 Correction to the U.S. Nuclear Regulatory Commission Analysis of Licensees' Decommissioning Funding Status Reports RA-13-012, Capability to Perform Multi-Unit Dose Assessment2013-06-26026 June 2013 Capability to Perform Multi-Unit Dose Assessment ML13037A2042013-01-31031 January 2013 Response to Second Request for Additional Information to Support NRC Reactor Systems Branch (Srxb) Technical Review of the CR-3 Extended Power Uprate LAR ML1214500142012-05-23023 May 2012 NFPA 805 LAR Status Matrix - May 2012 ML11112A1222011-06-10010 June 2011 Request for Additional Information and Schedule Revision for the Review of the Crystal River Unit 3 Nuclear Generating Plant License Renewal Application (TAC Nos. ME0274 and ME0278) ML1029107172010-10-20020 October 2010 Horizontal Tendons Pages 26-39 ML1013901262010-05-17017 May 2010 Table of Expiration Dates for Permits Associated with Crystal River Unit 3 for Draft Supplemental Environmental Impact Statement ML1029200902010-03-17017 March 2010 9.2 Seismic Events ML1029200892010-03-17017 March 2010 9.1 Hurricanes or Tornadoes ML1029200882010-03-17017 March 2010 8.4 Inadequate Concrete Structure ML1029200932010-03-17017 March 2010 9.3 Ground Movement ML1028703312010-01-30030 January 2010 5.7 Exhibit 7 Winter 2002-2010 ML1028703432010-01-29029 January 2010 Email - Subject: Detensioning Sequence Spreadsheets ML1027201562010-01-22022 January 2010 Email from Chou, Rich to Morrissey, Thomas, Dated Friday, January 22, 2010, 5:01 PM Cc Lake, Louis, Sykes, Marvin, Franke, Mark and Reyes, Rogerio; Subject: FW: Ctr Level II Schedule, Attachments: 01-25-10 Level 2 Rev E - 11x17.pdf ML1028706302010-01-22022 January 2010 Detensioning Sequence - Case 10 ML1028711742010-01-21021 January 2010 FW: Ctr Level II Schedule ML1028708112010-01-21021 January 2010 Email - from: Miller, Craig L (Craig.Miller@Pgnmail.Com) to Lake, Louis; Thomas, George; Carrion, Robert; 'Nausdj@Ornl.Gov'; Souther, Martin; 'Trowe@Wje.Com' Cc: Williams, Charles R. Dated Friday, January 22, 2010 8:53 Am Subject: FW: Failu ML1028711752010-01-21021 January 2010 5.3 Maintenance ML1028711762010-01-20020 January 2010 from: Williams, Charles R. (Charles.Williams@Pgnmail.Com) to: Lake, Louis; Thomas, George Dated Wednesday, January 20, 2010 5:16 PM Subject: FW: 01-21-10 Containment Repair Project Level 3 Schedule Attachments: 01 -21-10 Level 3 Rev D... At ML1028805012010-01-18018 January 2010 Email - from: Williams, Charles R., to: Lake, Louis; Thomas, George Dated Monday, January 18, 2010 4:18 PM, FW: 01-19-10 Containment Repair Project Level 3 Schedule, Attachments: 01-19-10 Level 3 Rev D - 11x17.pdf ML1028805092010-01-17017 January 2010 Email - from: Williams, Charles R. to: Lake, Louis, Thomas, George, Dated Sunday, January 17, 2010 9:28 Am, FW: 01-18-10 Containment Repair Prokect Level 3 Schedule, Attachments: 01-18-10 Level 3 Rev D - 11x17.pdf ML1028805132010-01-16016 January 2010 Email - from: Miller, Craig L (Craig.Miller@Pgnmail.Com) to: Lake, Louis; Thomas, George; Carrion, Robert; 'Trowe@Wje.Com'; Sealey, Mac Cc: Williams, Charles R. Dated Saturday, January 16, 2010 1:24 PM, Failure Mode 2.6 for Review .. ML1028805242010-01-16016 January 2010 Email - from: Miller, Craig L (Craig.Miller@Pgnmail.Com) to: Miller, Craig L; Lake, Louis; Thomas, George; Carrion, Robert; 'Trowe@Wje.Com' Cc: Williams, Charles R. Dated Saturday, January 16, 2010 1:15 PM Subject: Failure Mode 5.1 for Revi ML1028709172010-01-14014 January 2010 Email - from: Williams, Charles R. (Charles.Williams@Pgnmail.Com) to: Lake, Louis; Thomas, George Dated Thursday, January 14, 2010 7:16 Am Subject: FW: 01-14-10 Containment Repair Project Level 3 Schedule ML1028709162010-01-14014 January 2010 Email - from: Williams, Charles R. (Charles.Williams@Pgnmail.Com) to Lake, Louis; Thomas, George Dated Thursday, January 14, 2010 3:28 PM Subject: FW: 01-15-10 Containment Repair Project Level 3 Schedule ML1028709202010-01-13013 January 2010 5.1 Contamination During Construction ML1028709262010-01-13013 January 2010 Email - from: Williams, Charles R. to Lake, Louis; Thomas, George (Charles.Williams@Pgnmail.Com) Dated Wednesday, January 13, 2010 10:46 Am Subject: FW: 01-13-10 Containment Repair Project Level 3 Schedule ML1029105832009-12-28028 December 2009 Engg Repair Work Flow 12-28-09.pdf ML1029106132009-12-22022 December 2009 Email-From: Orf, Tracy to Lake, Louis Dated Tuesday, December 22, 2009 6:31 Am Subject:Fw CR3 Updated Root Cause Information Attachments: 2009 Dec 18 - Root Cause Update for Nrc. Pptx ML1027204462009-12-0808 December 2009 3.4 Exhibit 7, Petrographic Report ML1027204522009-12-0303 December 2009 2.2 Exhibit 3, Concrete Pour Data ML1027204452009-12-0303 December 2009 2.11 Concrete Pour Data ML1011708192009-12-0303 December 2009 Root Cause Analysis - PII Metrics as of Dec 3rd 2009 ML1028804872009-11-23023 November 2009 3.1 Inadequate Air Content ML1028711772009-11-23023 November 2009 8.1 and 8.5 ML1029106712009-10-30030 October 2009 2009 Oct 30 - Root Cause Analysis Metrics.Pptx ML1027300782009-01-25025 January 2009 2.5 Exhibit 1, Ambient and Concrete Temp in Buttresses 3-4 ML0728203072007-10-11011 October 2007 Electronic Distribtion Initiative Letter, Licensee List, Electronic Distribution Input Information, Division Plant Mailing Lists ML0529902932005-10-19019 October 2005 FAQ Log 10/19/2005 ML0613806832005-09-30030 September 2005 Operating Revenues Vs. Operating Expenses; Intergovernmental Transfers; Long-Term Debt; General Fuel Mix; Customer Class Composition; Total Retail Sales; Total Energy Sales 3F1104-05, 10CFR50.46 Loss-Of-Coolant Accident Evaluation Model Change and Peak Cladding Temperature Change Report2004-11-17017 November 2004 10CFR50.46 Loss-Of-Coolant Accident Evaluation Model Change and Peak Cladding Temperature Change Report ML0209405042002-04-0303 April 2002 Attachment to Letter Crystal River Unit 3 - Table for OTSG Post-Inspection Phone Call and Drawings 2016-03-11
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8.1 Prior spray event leading to low pressure inside containment IP re n a y May identify additional perspective on this issue as RCA related efforts proceeds
Description:
The containment spray event of October, 1992 resulted in an injection of about 9400 gallons of borated water into the reactor building (RB) atmosphere.
The event resulted in a decrease in RB internal pressure.Data to be Collected and Analyzed: 1. Review problem report of October 16, 1992 and associated containment atmosphere pressure graph.(Exhibit 1)2. Review Design bases for containment, FSAR Chapter 5. (Exhibit 2)Verified Refuting Evidence:
Verified Supporting Evidence: The RB pressure excursion from the 1992 containment spray event did not result in the containment pressure exceeding the design criteria for the RB.Reviewed by: Marci Cooper, 352-795-6486, ext 1030 -PII CR3 Team Office 11/23/2009 pI' P-rope anid Cc..... elldI, 2_009. Du not relea-c-tcd-fird pary with'out-11/23/200 1 r I 8.5 Containment depressurization due to inadequate purging operation Da May identify additional perspective on this issue as RCA related efforts proceeds
Description:
It was reported by a former CR3 operator (Dave Jones) that an event occurred in the late 1980's or early 1990's during which a purge exhaust fan was operating with the inlet purge valve closed. This resulted in a vacuum in the containment building.Data to be Collected and Analyzed:
Review event data, equipment information, and conduct personnel interviews if possible.1. Dave Jones (former CR3 operator) interview documented November 10, 2009 placed the event to the late 1980s to early 1990's. (Exhibit 1)2. No NCR to document the event has been found. CR3 self-evaluation unit has exhausted all databases in their document search. Estimate maximum vacuum achievable with purge fan operation. (Exhibit 1, pg 1)3. Purge fan vender manuals: VTMA 231 (Exhibit 2, pgs 2-5)4. Make/model of the purge fan: Joy Manufacturing Model 36-26.5-1770 axial vane fan. (Exhibit 1, pgs 2-5)5. Review containment design bases, FSAR Section 5. (Exhibit 3)Verified Refuting Evidence:
A calculation of a Verified Supporting Evidence: postulated worse-case vacuum generated by the purge fan demonstrated that a vacuum of 1 psi is less than the design bases for containment.
Reviewed.by Dr. Patrick Berbon, 352-795-6486 ext.1030- P11 CR3 Team Office I P4IM PF upL, and Confid.nti.l, 200.. D, 11/23/2009 nzet-release t..a third party ,ithout 1 8.5 Containment depressurization due to inadequate purging operation D na May identify additional perspective on this issue as RCA related efforts proceeds
Description:
It was reported by a former CR3 operator (Dave Jones) that an event occurred in the late 1980's or early 1990's during which a purge exhaust fan was operating with the inlet purge valve closed. This resulted in a vacuum in the containment building.Data to be Collected and Analyzed:
Review event data, equipment information, and conduct personnel interviews if possible.1. Dave Jones (former CR3 operator) interview documented November 10, 2009'placed the event to the late 1980s to early 1990's. (Exhibit 1)2. No NCR to document the event has been found. CR3 self-evaluation unit has exhausted all databases in their document search. Estimate maximum vacuum achievable with purge fan operation. (Exhibit 1, pg 1)3. Purge fan vender manuals: VTMA 231 (Exhibit 2, pgs 2-5)4. Make/model of the purge fan: Joy Manufacturing Model 36-26.5-1770 axial vane fan. (Exhibit 1, pgs 2-5)5. Review containment design bases, FSAR Section 5. Exhibit 3)Verified Refuting Evidence:
A calculation of a Verified Supporting Evidence: postulated worse-case vacuum generated by the purge fan demonstrated that a vacuum of 1 psi is less than the design bases for containment.
Reviewed by Dr. Patrick Berbon, 352-795-6486 ext.1030 -P11 CR3 Team Office 11/23/2009retr'and Csnfidcntial, 2000. Do h-oti .to.. t d "u 1 l 1 u ... ....y .....pemisin.1