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COOPER NUCLEAR ET ATION Nebraska Public Power District
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.e CNSS933054 March 18, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C.
20555
Dear Sir:
Cooper Nuclear Station Licensee Event Report 93-001, Revision 0, is forwarded as an attachment to this letter.
Sincerely,
. L. Gardner Plant Manager RLG/ju Attachment ec:
J. L. Milhoan G. R. Horn J. M. Meacham R. E. Wilbur i
V. L. Wolstenholm l
D. A. Whitman l
INPO Records Center NRC Resident Inspector R. J. Singer CNS Training CNS Quality Assurance j
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ANi a Rt PORTS MANAGEME NT SR ANCH (P430), U.S. NUCLE AR REGULA DRY COMMIEErON.14 ACHINGTON. DC 2D%5 AND TO THE PAPE Rwopet Rf DUCTION PROJECT (31b00104), OFFICE i
OF MANAGEME NT AND BUDGET, WASHINGTON.DC 20bO3.
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During ongoing efforts associated with the Design Basis Reconstitution Program for
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Cooper Nuclear Station (CNS), several design discrepancies in the Service Water (SW) and Reactor Equipment Cooling (REC) Systems were identified. These discrepancies l
affected the ability to achieve the minimum required SW and REC flows to essential equipment requiring cooling during and following a design basis accident (DBA).
On February 25, at 12:30 pm, both systems were declared inoperable and the 2411our LCO requiring plant shutdown specified in Technical Specifications was entered. At the time of entry into the LCO, the plant was operating at approximately 85 percent
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power (nearly 700 MWe) on end of cycle coastdown with all rods fully withdrawn.
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Review of design and construction documentation revealed that a SW piping
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configuration error was made during original plant construction, resulting in Division 1 SW being supplied to the Division II REC Heat Exchanger, and vice-versa.
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While subsequent evaluations were performed by the Architect / Engineer resulting in system operational ch'nges to compensate for the as-built condition, apparently the i
analyses were not sufficiently thorough to identify and resolve these concerns.
Compensatory measures taken to restore the SW and REC Systems to an operable status included interim procedure changes providing operator guidance and system valve alignment restrictions. Additionally, operators were briefed regarding the scenarios of concern and the necessary compensatory actions requircd. These actions were in effect until the plant achieved cold shutdown for the 1993 Refueling Outage which began on March 5.
Prior to startup from the outage, pertinent mechanical and electrical modifications will be made to resolve the identified concerns.
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I A.
Event Description
1 During ongoing efforts associated with the Nebraska Public Power District's Design Basis Reconstitution Program for Cooper Nuclear Station (CNS), several design discrepancies in_the Service Water _(SW)-
and Reactor Equipment Cooling (REC) Systems were identified. These i
j discrepancies involved the ability to a.:hieve the minimum required'SW and REC flows to the essential equipment requiring cooling during and following a design basis accident (DBA). On February 25, at 12:15 pm, an evaluation of the discrepancies was conducted by the Station Operations Review Committee (SORC). A recommendation was then inade to i
the Shift Supervisor to declare the SW and REC Systems inoperable and l
enter the 2411our LCO requiring plant shutdown specified in s4ctions i
3.12.B.4 (REC System) and 3.12.C 3 (SW System) of the Technica.1 Specifications.
Both systems were subsequently declared inoperable at 12:30 pm and the 24 Ilour LCO was entered.
DBA conditions include a loss-of-coolant accident (LOCA) with a concurrent loss-of-offsite power (IAOP) and a worst case single failure.
The postulated worst case single failure is a failure of one emergency diesel generator (DC), since this causes the failure of the most SW and REC components.
Under these conditions, if both REC IIeat Exchangers are -
in service prior to the accident, _It may not be possibic to remotely isolate the heat exchanger in the loop that serves the Core Standby.
Cooling Systems (CSCS) equipment in the failed electrical division.
For example, if DG No. I fails and all off-site power is lost, valve REC-MOV-711MV (the South Critical Loop Supply Valve) will not;open since it is powered by Division 1.
Thus, only REC lleat Exchanger B is available for critical loop component cooling. With both heat exchangers in service at the start of the event and both SW outlet' valves open, it would not be possible without manual operator action to isolate the SW flow to llent Exchanger A since the REC A Heat Exchanger SW System outlet valve (SU-MOV-651MV) is a Division I valve.
Consequently, a flow diversion proportional to the flow established prior to the accident would be directed to the "A" REC Heat Exchanger which would be non-functional; i.e.,
providing no useful accident response purpose. With this flow diversion, it may not be possible to-provide the minimum required flow to the operable DG, the functional REC liest Exchanger, the Residual lleat Removal (RHR) SW Booster Pump and j
other. cooling loads.
The REC System is also not single failure proof in the accomplishment of its safety function. The automatic isolation valves that isolate the i
noncritical header of REC from the critical header are all powered from
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Division I electrical power.
In the case of a Design Basis LOCA, IDOP and failure of DG No. 1 (DG No. 1 only), the noncritical header does not automatien11y isolate. _As a result, REC flow would be diverted to the nonessential evoling loads.
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With only one REC pump in operation, the essential CSCS area coolers and the RHR Pump seal coolers might not receive the required cooling flow.
In the event of a LOCA, LOOP and loss of DG No. 2, REC flow will be diverted to the noncritical header since REC-MOV-702MV, the Noncritical Header Drywell Supply Isolation Valve, does not receive the low header pressure isolation signal that is received by the other two noncritical loop isolation valves.
Thus, remote manual action from the Control Room i
must be taken to isolate the valves on the suction side of the REC Pumps to prevent diversion of the REC flow through the noncritical header.
i B.
flant Status Operating at approximately 85 percent power, at nearly 700 MWe, on end of cycle coastdown with all rods fully withdrawn.
4 C.
Basis for Report 1
A condition alone that could have prevented the fulfillment of the j
safety function of systems needed to mitigate the consequences of an accident, reportable in accordance with 10CFR50.73(a)(2)(v).
D.
Cnuse A review of documentation associated with the design and construction of the associated systems revealed that a SW piping configuration error
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during original plant construction occurred, resulting in Division I SW being supplied to the Division II REC Heat Exchanger, and vice-versa.
While subsequent failure modes and effects analyses performed by the Architect / Engineer resulted in system operational changes to compensate for the as-built condition, apparently the analyses were not t
sufficiently thorough to identify and resolve these concerns.
E.
Safetv Sinnificance The safety objective of the SW System is to provide a heat sink for the REC, RHR, and DG cooling systems under transient and accident conditions. However, adequate SW flow to all of the required cooling l
loads was not assured under postulated LOCA, LOOP and concurrent worst case single f allure conditions, without operator action from the Control Room.
Existing operating procedures direct the operator to start a second SW pump in the event that the SW header pressure.is low, as it could be under the postulated accident scenario.
Calculations show'that adequate power is available from a DG to support operation of this second pump. Also, calculations show that the operator has at least ten minutes to accomplish this remote manual action from the' Control Room.-
I which is within the.CNS licensing basis-and is a reasonable. response time.
Consequently, the safety objective of the SW System would have been achieved.
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.sm~ wc ram, swamn E.The safety objective of the REC System is to provide cooling to the CSCS area coolers and the RER pumps seal coolers, liowever, in the event of a LOCA, LOOP and worst caso single failure condition, the noncritical header will not be automatically isolated from the critical header as a result of low header pressure, an expected condition with only one pump in service. Adequate system flow to the CSCS area coolers and the RllR pumps seal coolers still might not be sufficient even if a second REC pump were started. Therefore, the safety objective of the REC System was jeopardized.
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Safety Imnlications I
l The event which must occur in order for the SW and REC Systems to be of concern is a Design Basis LOCA, which assumes a concurrent LOOP and a simultaneous failure of one DC.
The probability of these-three i
unrelated events occurring simultaneously is extremely remote (on the i
order of 10-8 per year of reactor operation).
C.
Corrective Actiqn Compensatory measures taken to restore the SW and-REC Systems to an operable status included interim procedure changes which provided operator guidance and valve alignment restrictions associated with the SW and REC Systems, along with operator briefings regarding the scenarios of concern and necessary compensatory actions that would be required upon their occurrence. At approximately 10:00 pm on February 25, SORC reviewed and approved the basis for continued aparation uithin the hour, the required compensatory measures were in place and both the SW and REC Systems were declared operable. Thesc 1
compensatory actions were in effect until the plant achieved cold shutdown for the 1993 Refueling Outage which commenced on March 5.
Prior to startup from the refueling outage, necessary mechanical and electrical modifications will be made to resolve the identified concerns.
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Similar Eventa j
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| | | Reporting criterion |
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| 05000298/LER-1993-001, :on 930225,several Design Discrepancies in SW & Reactor Equipment Cooling Sys Identified.Caused by Piping Configuration Error During Plant Const.Mechanical & Electrical Mods Will Be Made |
- on 930225,several Design Discrepancies in SW & Reactor Equipment Cooling Sys Identified.Caused by Piping Configuration Error During Plant Const.Mechanical & Electrical Mods Will Be Made
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-002, :on 930202,NRC Inspector Discovered That Fire Watchman Unaware That Thermo-Lag Fire in Assigned Area Declared Inoperable on 920625,during Interview.Personnel re-familiarized w/Thermo-Lag Areas of Concern |
- on 930202,NRC Inspector Discovered That Fire Watchman Unaware That Thermo-Lag Fire in Assigned Area Declared Inoperable on 920625,during Interview.Personnel re-familiarized w/Thermo-Lag Areas of Concern
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-003, :on 930306,Group Isolation & Loss of Shutdown Cooling Due to Inadvertent 4160 Vac Breaker Trip.Caused by Personnel error.Self-checking Training Will Be Enhanced & Addl Labeling & Visual Identification Aids Being Evaluated |
- on 930306,Group Isolation & Loss of Shutdown Cooling Due to Inadvertent 4160 Vac Breaker Trip.Caused by Personnel error.Self-checking Training Will Be Enhanced & Addl Labeling & Visual Identification Aids Being Evaluated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000298/LER-1993-004, :on 930308,discovered That Documentation for Installation of Temporary Seals in RB Exterior Wall on 930306 Incomplete Due to Procedural Deficiencies.Procedures Revised to Ensure Guidance Re Temporary Seal Installation |
- on 930308,discovered That Documentation for Installation of Temporary Seals in RB Exterior Wall on 930306 Incomplete Due to Procedural Deficiencies.Procedures Revised to Ensure Guidance Re Temporary Seal Installation
| | | 05000298/LER-1993-005, :on 930310,excessive Primary Containment Leakage Discovered During Local Leak Rate Testing of Reactor Check Valves.Caused by Equipment Deficiency.Valve Body & Disc Being Precision line-bored |
- on 930310,excessive Primary Containment Leakage Discovered During Local Leak Rate Testing of Reactor Check Valves.Caused by Equipment Deficiency.Valve Body & Disc Being Precision line-bored
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-006, :on 930316,two Fire Barrier Doors in RB Found Open & Obstructed W/No Fire Watch Assigned.Caused by Personnel Error.Review of Fire Watch Implementation Process Will Be Conducted to Prevent Recurrence |
- on 930316,two Fire Barrier Doors in RB Found Open & Obstructed W/No Fire Watch Assigned.Caused by Personnel Error.Review of Fire Watch Implementation Process Will Be Conducted to Prevent Recurrence
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-007, :on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection Cooling |
- on 930326,determined That ECCS Pump Compartment Cooler Power Supply Design Defect Could Have Prevented Adequate Containment Heat Removal.Caused by Design Errors.Mods Planned to Provide Convection Cooling
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-008, :on 930328,4,160-volt Breakers 1BG,1GB & 1GE Tripped Due to Actuation of 1GS Breaker Lockout Relay.Caused by Oversight in Design Change Installation Instructions. Work Stopped & Design Change Implemented |
- on 930328,4,160-volt Breakers 1BG,1GB & 1GE Tripped Due to Actuation of 1GS Breaker Lockout Relay.Caused by Oversight in Design Change Installation Instructions. Work Stopped & Design Change Implemented
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000298/LER-1993-009, :on 920329,discovered Potential for Inoperability of solenoid-operated Valves During Evaluation Per GL 91-15.Caused by Failure to Anticipate Problems of Overpressurization.Valves Replaced |
- on 920329,discovered Potential for Inoperability of solenoid-operated Valves During Evaluation Per GL 91-15.Caused by Failure to Anticipate Problems of Overpressurization.Valves Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-010, :on 930331 & 0621,RPS Bus B Deenergized Due to Defective Under Frequency (Uf) Trip Unit Resulting in Unplanned Actuations of Several Esfs.Action Initiated to Permanently Remove Uf Feature |
- on 930331 & 0621,RPS Bus B Deenergized Due to Defective Under Frequency (Uf) Trip Unit Resulting in Unplanned Actuations of Several Esfs.Action Initiated to Permanently Remove Uf Feature
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000298/LER-1993-011, :on 930308,max Differential Pressure Between Reactor Bldg & External Environ of -0.22-inches Water Gauge Exceeded TS Required Min.Caused by Lack of Loop Seal on Rupture Seal Drain Line.Seals Replaced |
- on 930308,max Differential Pressure Between Reactor Bldg & External Environ of -0.22-inches Water Gauge Exceeded TS Required Min.Caused by Lack of Loop Seal on Rupture Seal Drain Line.Seals Replaced
| | | 05000298/LER-1993-012, :on 930414,violation of Primary Containment Integrity Occurred.Caused by Personnel Error.Procedure Change Being Made to Eliminate Test Return Line Venting When Primary Containment Integrity Required |
- on 930414,violation of Primary Containment Integrity Occurred.Caused by Personnel Error.Procedure Change Being Made to Eliminate Test Return Line Venting When Primary Containment Integrity Required
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-013, :on 930415,determined That as-found Setpoint for Seven SRVs Not within TS Limit.Caused by Lift Setpoint Discrepancies of Srvs.Review of Setpoint Data Will Be Performed |
- on 930415,determined That as-found Setpoint for Seven SRVs Not within TS Limit.Caused by Lift Setpoint Discrepancies of Srvs.Review of Setpoint Data Will Be Performed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000298/LER-1993-014, :on 930316,small through-wall Leak Developed on High Pressure Side of SW Throttle Valve.Caused by Inadequate Valve Design.Frequency of Visual Insp of Valve Internals Will Be Increased to Once Per Cycle |
- on 930316,small through-wall Leak Developed on High Pressure Side of SW Throttle Valve.Caused by Inadequate Valve Design.Frequency of Visual Insp of Valve Internals Will Be Increased to Once Per Cycle
| | | 05000298/LER-1993-015, :on 930420,design Discrepancy in HPCI Sys Identified.Caused by Design Deficiency in Original Design. Mods Will Be Made to Startup from Current Refueling Outage to Correct Design Discrepancy |
- on 930420,design Discrepancy in HPCI Sys Identified.Caused by Design Deficiency in Original Design. Mods Will Be Made to Startup from Current Refueling Outage to Correct Design Discrepancy
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-016, :on 930422,during Performance of Surveillance Test on CR HVAC Sys Radiation Monitor RMV-RM-1,CR HVAC Sys Did Not Isolate & Transfer to Emergency Bypass Mode.Caused by Personnel Error.Wiring Error Corrected |
- on 930422,during Performance of Surveillance Test on CR HVAC Sys Radiation Monitor RMV-RM-1,CR HVAC Sys Did Not Isolate & Transfer to Emergency Bypass Mode.Caused by Personnel Error.Wiring Error Corrected
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-017, :on 930428,discovered That Hourly Fire Watch Patrol for RB Per TS Had Not Been Performed.Caused by Personnel Error.Review of Fire Watch Patrol Implementation Process Will Be Conducted |
- on 930428,discovered That Hourly Fire Watch Patrol for RB Per TS Had Not Been Performed.Caused by Personnel Error.Review of Fire Watch Patrol Implementation Process Will Be Conducted
| | | 05000298/LER-1993-018, :on 930430,potential Single Failure Vulnerability Noted W/Single Inlet Damper in Common Supply Duct.Caused by Faulty Original Design.Inlet Damper Sealed Open to Eliminate Single Failure |
- on 930430,potential Single Failure Vulnerability Noted W/Single Inlet Damper in Common Supply Duct.Caused by Faulty Original Design.Inlet Damper Sealed Open to Eliminate Single Failure
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-019, :on 930501,nonconservative Testing Methodology Discovered During LLRT Due to Nonconservative Interpretation of Info Supplied by Valve Mfg.Testing Conducted for Valves Not Previously Tested |
- on 930501,nonconservative Testing Methodology Discovered During LLRT Due to Nonconservative Interpretation of Info Supplied by Valve Mfg.Testing Conducted for Valves Not Previously Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) | | 05000298/LER-1993-020, :on 930507,determined That H2/O2 Sys Not Leak Tested to Verify Primary Containment Integrity During Testing of Sys.Caused by Failure to Have Administrative Controls in Place.Pressure Testing Conducted |
- on 930507,determined That H2/O2 Sys Not Leak Tested to Verify Primary Containment Integrity During Testing of Sys.Caused by Failure to Have Administrative Controls in Place.Pressure Testing Conducted
| 10 CFR 50.73(a)(2)(i) | | 05000298/LER-1993-021, :on 930611,determined That RB Ventilation Exhaust Inboard Isolation Valve HV-AOV-261AV Inoperable & Open Due to Personnel Error.Subj Valve Manually Closed. Proposed Change to TS Will Be Submitted |
- on 930611,determined That RB Ventilation Exhaust Inboard Isolation Valve HV-AOV-261AV Inoperable & Open Due to Personnel Error.Subj Valve Manually Closed. Proposed Change to TS Will Be Submitted
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-022, :on 930514,emergency Transformer Low Voltage Alarm Received & Actual Low Voltage Condition Did Not Exist.Caused by Human Factors & Unanticipated Design Problems.Addl Input Provided to Window |
- on 930514,emergency Transformer Low Voltage Alarm Received & Actual Low Voltage Condition Did Not Exist.Caused by Human Factors & Unanticipated Design Problems.Addl Input Provided to Window
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000298/LER-1993-023, :on 930528,fuel Assemblies Loaded Into Reactor Core Without Control Rods Fully Inserted,In Violation of TS 3.10.A.2.Caused by Need to Reposition Fuel Support Piece. Training Will Be Revised |
- on 930528,fuel Assemblies Loaded Into Reactor Core Without Control Rods Fully Inserted,In Violation of TS 3.10.A.2.Caused by Need to Reposition Fuel Support Piece. Training Will Be Revised
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-024, :on 930527,discovered That Testing of Four Reactor Vessel Low Water Level RPS Sensors Not Completed as Scheduled.Caused by Personnel Error.Stroke Testing Suspended & Surveillance Testing Completed |
- on 930527,discovered That Testing of Four Reactor Vessel Low Water Level RPS Sensors Not Completed as Scheduled.Caused by Personnel Error.Stroke Testing Suspended & Surveillance Testing Completed
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-025, :on 930618,hydrogen/oxygen Monitoring Sys Operability Concerns Discovered Due to Moisture & Accumulation & Sample Pump Reliability.Design Change Implemented During 1993 Refueling Outage |
- on 930618,hydrogen/oxygen Monitoring Sys Operability Concerns Discovered Due to Moisture & Accumulation & Sample Pump Reliability.Design Change Implemented During 1993 Refueling Outage
| 10 CFR 50.73(a)(2)(i) | | 05000298/LER-1993-026, :on 930618,determined That Safety Related Portions of SW & Reactor Equipment Cooling Sys Piping Not Included in ASME Code Section XI ISI Program.Portions Will Be Included by Next Refueling Outage |
- on 930618,determined That Safety Related Portions of SW & Reactor Equipment Cooling Sys Piping Not Included in ASME Code Section XI ISI Program.Portions Will Be Included by Next Refueling Outage
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-027, :on 930308,standby Gas Treatment Sys Unable to Establish & Maintain Reactor Bldg Pressure + or - 0.25 Inches Water Gauge Under Calm Wind Conditions.Evaluation of Secondary Containment Operability in Progress |
- on 930308,standby Gas Treatment Sys Unable to Establish & Maintain Reactor Bldg Pressure + or - 0.25 Inches Water Gauge Under Calm Wind Conditions.Evaluation of Secondary Containment Operability in Progress
| | | 05000298/LER-1993-027-01, :on 930618,potential Degradation of Secondary Containment Was Undetected Due to Preconditioning & Test Methodology Deficiencies.Review of Test Procedures Underway |
- on 930618,potential Degradation of Secondary Containment Was Undetected Due to Preconditioning & Test Methodology Deficiencies.Review of Test Procedures Underway
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000298/LER-1993-028, :on 930630,two Potentially Valves Were Inoperable Due to Inadequate Design of Valve Operators by Manufacturer.Modified Valve Operators |
- on 930630,two Potentially Valves Were Inoperable Due to Inadequate Design of Valve Operators by Manufacturer.Modified Valve Operators
| 10 CFR 50.73(a)(2)(i) | | 05000298/LER-1993-029, :on 930708,partially Withdrawn Control Rod 26-31 Scrammed.Caused by RPS Scram Signal from Two of Four Reactor Pressure Scram Switches.Scram Reset & Pressure Testing Completed |
- on 930708,partially Withdrawn Control Rod 26-31 Scrammed.Caused by RPS Scram Signal from Two of Four Reactor Pressure Scram Switches.Scram Reset & Pressure Testing Completed
| | | 05000298/LER-1993-030, :on 930708,discovered Inadequate Inservice Testing of Svc Water Sys Check Valves Due to Flow Instrument Calibr Error & Personnel Error in Specifying Sys Flow Requirement.Revised Calibr Factor Developed |
- on 930708,discovered Inadequate Inservice Testing of Svc Water Sys Check Valves Due to Flow Instrument Calibr Error & Personnel Error in Specifying Sys Flow Requirement.Revised Calibr Factor Developed
| 10 CFR 50.73(a)(2)(1) | | 05000298/LER-1993-032, :on 930708,B 125 Volt Battery Disconnect Switch Fuse Failed.Caused by Defective Fuse.Defective Fuses Replaced & Battery Returned to Svc |
- on 930708,B 125 Volt Battery Disconnect Switch Fuse Failed.Caused by Defective Fuse.Defective Fuses Replaced & Battery Returned to Svc
| | | 05000298/LER-1993-033, :on 931011,primary Containment Declared Inoperable & Plant Placed in Lco,Per TS 3.7.A.2,loss of Containment Integrity.Caused by Design Deficiency.Design Mods & Licensing Basis Revs Evaluated |
- on 931011,primary Containment Declared Inoperable & Plant Placed in Lco,Per TS 3.7.A.2,loss of Containment Integrity.Caused by Design Deficiency.Design Mods & Licensing Basis Revs Evaluated
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000298/LER-1993-034, :on 931028,identified That Fire Brigade Members from Support Groups Had Not Received Quarterly Fire Brigade Training Due to Misunderstanding.Quarterly Fire Brigade Training Provided to Appropriate Personnel |
- on 931028,identified That Fire Brigade Members from Support Groups Had Not Received Quarterly Fire Brigade Training Due to Misunderstanding.Quarterly Fire Brigade Training Provided to Appropriate Personnel
| | | 05000298/LER-1993-037, :on 931118,fire Door Declared Inoperable. Caused by Programmatic Deficiency.C/A:Procedures & Programs Will Be Revised to Ensure Clear Identification of Functions Each Door Performs |
- on 931118,fire Door Declared Inoperable. Caused by Programmatic Deficiency.C/A:Procedures & Programs Will Be Revised to Ensure Clear Identification of Functions Each Door Performs
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000298/LER-1993-038, :on 931214,unplanned Automatic Reactor Scram & ESF Actuations Occurred Due to Feedwater Controller Failure. Caused by Age Degradation.Master Controller Replaced |
- on 931214,unplanned Automatic Reactor Scram & ESF Actuations Occurred Due to Feedwater Controller Failure. Caused by Age Degradation.Master Controller Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000298/LER-1993-039, :on 931214,discovered Two Instrument Line Orifices Not Installed Due to Original Contruction Deficiencies.Caused by Mod Error.Orifices Installed & Tested |
- on 931214,discovered Two Instrument Line Orifices Not Installed Due to Original Contruction Deficiencies.Caused by Mod Error.Orifices Installed & Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function |
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