05000254/LER-1997-013, Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed

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Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed
ML20141A197
Person / Time
Site: Quad Cities 
Issue date: 05/08/1997
From: Pearce L
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML20141A200 List:
References
LWP-97-054, LWP-97-54, NUDOCS 9705140179
Download: ML20141A197 (1)


LER-1997-013, Forwards LER 97-013-00 Re Any Single Cause of Inoperable Independent Train or Channel in Single Sys Designed to Remove Residual Heat.Commitments Made by Ltr,Listed
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
2541997013R00 - NRC Website

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Quad Citics Generating Station a

22 10 2tkith Mcnue North cordova. iu,i 2 e4> in Tri.um,w22 4 i LWP-97-054 May 8, 1997 United States Nuclear Regulatory Commission Washington, DC 20555 Attention: Document Control Desk Reference: Quad Cities Nuclear Power Station Docket Number 50-254, DPR-29, Unit One Enclosed is Licensee Event Report (LER)97-013, Revision 00, for Quad Cities Nuclear Power Station.

This report is submitted in accordance with the requirements of the Code of Federal Regulations, Title 10, Part 50.73(a)(2)(vii)B. The licensee shall report any single cause of inoperable independent train or channel in a single system designed to remove residual heat.

The following ammitment is being made by this letter: A change will be made to QCIS 1300-05 and QCIS 2300-07, " Refuel HPCI Turbine Area High Temperature Isolation Calibration and Functional Test", to add a caution on the amount of sealing varnish applied to set screws and to include a requirement to bench test switches if and after varnish has been applied after calibration adjustments; (expected completion date 040198).

If there are any questions or comments concerning this letter, please refer them to Charles Peterson, Regulatory Affairs Manager at 309-654-2241, ext. 3609.

Respectfully, COMMONWEALTH EDIS0N COMPANY QUAD CITIES NUCLEAR POWER STATION

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\\l L. W. Pearce Station Manager

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A. B. Beach, Regional Administrator, Region III R. M. Pulsifer, Project Manager, NRR C. G. Miller, Senior Resident Inspector, Quad Cities W. D. Leech, MidAmerican Energy Company D. C. Tubbs, MidAmerican Energy Company

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