PY-CEI-NRR-0600, Annual ECCS Outage Rept,860318-1231

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Annual ECCS Outage Rept,860318-1231
ML20212G191
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 12/31/1986
From: Edelman M, Kensichi S, Stratman R
CLEVELAND ELECTRIC ILLUMINATING CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
RTR-NUREG-0887, RTR-NUREG-887, TASK-2.K.3.01, TASK-TM PY-CEI-NRR-0600, PY-CEI-NRR-600, NUDOCS 8703050284
Download: ML20212G191 (4)


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CLEVEUdO EMC1RIC IIUMDETING OCMPANY PERRY 10CEAR POWER PIANP March 18 - Decenber 31, 1986 AIGERL BOCS OLEAGE REPORP DOCKET NUMBER: 50-440 LICENSE NUMBER: NPF-58 Subnitted By: h/%e J2, 2- f/SkM!87 Plant Technical Mana er tY l1 NA

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I- INIRODUCTION This-information comprises the 1986 Annual ECC Systes Outage Report, which is submitted in accordance'with FSAR - IMI Action.

Plan Item Nmber II.K.3.17 (Appendix 1A) and NUREG-0887 section 6.3.3. The report covers the period fr m receipt of~ operating license-until December 31, 1986.

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NEE Tm Tm i yDI SPEC SYS/CCD@. ENFERED CMMtED IIRATIN REFERDCE DESCRIPYIN 3.5.2 4 E12/E21 12:07 13:10 2 days, SVI-P45- Bnergency Service Water (P45)

LPCI 'A' 6-20 6-22 1 hr., T2002 SvI failed (pump flow rates LPCS 3 min. fell outside the acceptable range) resulting in loss of P42. Loss of Bnergency Closed Cooling (P42) INOPS LPCI 'A' &

LPCS. Surveillance data was subsequently evaluated and accepted.

3.3.3 4 E22 HPCS 01:10 01:25 1 day, NO HPCS Suppression pool level 8-20 8-21 15 min. 11815 transmitter was discovered not

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working properly. Recalibrated instr. law SVI-E22-T0196C & G.

3.5.1 2 E12 LPCI 'A' 22:05 19:30 21 hrs., NO LPCI 'A' INOP due to valve 9-13 9-14 25 min. 12525 status. Valve opened for trouble-shooting - won't ' seal-in' in the closed direction. Torque switch contacts cleaned.

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3.5.1 2 E22 HPCS 18:30 12:20 17 hrs. , NO Bkr. Hil304 trip relay not set 9-38 9-19 32 min. 12560 properly. Relay IK65K 50/51A HPCS pump initial calibration per Setpoint Change Request 1-86-1320.

3.4.9.2 5 E12/E21 04:40 06:40 7 days, DCP 86-224 Bnergency Service Water (P45)

LPCI 'A' 11-3 11-10 2 hrs. NO pump 'A' tagged out for DCP LPCS 9347 implementation INOPS LPCI 'A' &

LPCS. DCP installs Bnergency Closed Cooling (P42) heat ex-changer outlet valve bypass valve for throttling purposes.

3.4.9.2 5 E12 LPCI 'B' 05:00 05:53 1 day, NO Maintenance on valve F024B.

11-13 11-14 53 min. 14748 Wires in MJC found terminated incorrectly. Corrected and applicable steps of SVI-E12-T2002 performed.

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THE CLEVELAND ELECTRIC !LLUMINATING COMPANY P.O. BOX 5000 - CLEVELAND, OHIO 44101 - TELEPHONE (216) 522-9800 - ILLUMINATING BLDG. - 55 PUBLICSQUARE Sewing The Best Location in the Nation MURRAY R. EDELMAN sa vice passoeur NUCLEAR February 27, 1987 PY-CEI/NRR-0600 L Document Control Desk U.S. Nuclear Regulatory Commission Washington D.C. 20555 I

Perry Nuclear Power Plant Docket No. 50-440 Annual ECCS Outage Report

Dear Sir:

Attached is the 1986 Annual ECCS Outage Report for Perry Unit 1. This report is submitted in accordance with NUREG-0887 Section 6.3.3 and our FSAR Appendix 1A - TMI Action Plan Item No. II.K.3.1.17.

Please feel free to contact me if you have any questions.

Very truly yours, Murray R. Edelman Senior Vice President Nuclear Group Enclosure MRE:njc cc: Jay Silberg, Esq.

Paul Leech (2)

K. Connaughton L. Hiller (Office of Management & Program Analysis)

J. G. Keppler, Region III adh IF.y