ML20141K764

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Forwards Category B Rept Re Util Forwarding First Semiannual Operating Rept for May-Dec 1969
ML20141K764
Person / Time
Site: Oyster Creek
Issue date: 04/21/1970
From: Mckinley J
Advisory Committee on Reactor Safeguards
To: Bush S, Stratton W
Advisory Committee on Reactor Safeguards
Shared Package
ML20091A092 List: ... further results
References
FOIA-91-282 NUDOCS 9203250131
Download: ML20141K764 (4)


Text

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4ril 21, 1970 4 7

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W. R. Strattco. Chairman Oyster Creek Subcoratittee

8. B. Bush, Vice Chairman, Acts .

CATEGORY B REPORTS - CTITER CREEr, - JERREY CENTRAL POWER & LICHT Cm WANY LETTER DATED AFRIL 2, 1970

! Attached is a brief susesary of the information presented in the esbject corresponder.co. No ACES rett:m appears warranted.

! This item may be destroyed when you have completed your w aluation of t.his matter.

0ricInol SI asd

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v. C. L'en1oy J. C. McKinley 8taf f Assistant l- Attachments:

1 1) Suessary l 2) Jersey Central Power & Light

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Caespany letter dated April 2,1970 cct ACRS Members i

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a OTSTER,CRENT Jarsay C.fatral poser & Limht * '- ,

letter dated April 2.1970 forwesde  ?

the first semi-eansal operettag report for the period May 1969 thru tesseber 1969. W ". . *

, The operations 4setag this first reporting period for Dait No.1 of ths Oyster Creek Reclear Generating Staties of the Jersey Central power and Light Campany esasisted primarily of events related to the step-wise approach to semanarcial operaties at full license power. A certes of thirty- '

,  ; two start-wp tests were sempleted at warious power levels, seecluded wit.h the ,

ene hundred hour full power deseastration l which was temp 1sted as December 12, 1969, ct 11:00 p.m. i

! Initial criticality wea achieved with the head off the reactor vessel at 2:17 p.m.

on May 3, 1969. With the complettee of low power testing, the insta11atten of hot vibretten testing sensors, and the instal-l latte of moisture separator and stem dryer, the reacter vassal heed was installed j om June 19, 1%9. One quarter power was I. achieved on September 22, 1M93 ene half l pmser on September 26, 1969; three-quarter j power en November 19, 1969, and full power

, en December _7, 1969. The turbins generator l 3 was first synchresised to the traaemission l I system on Septeenber 23, 1969.

I I l During the period of ascension to full power several situations developed which required g shutdooms for eerrective- acties or fu:rther

, investigation end easign modification. la general and in chronological order, the felleving itaus were of major concern.

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-1. Investigation of stainlass steel piping and miscelleseous valms as reported in Amendment No. 53 to the FD$AR..

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l 2 I.eactor haildies roe rrepairs aseesesty

' to achieve satisfactory operation of the

.. Amergency Standby Cas Treatzesat System.

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IFf87EE CE.EEK (Colff'D) 3. Standby See Treatment Systan* */ *- .

modifications as reported in W Mo. 52 and No. 53 to the Fus&R.. p,q:2 v,

4. Internal inspestien of three meAm staan line isolation valves - M043 3803A and NB038 S. Removal and reinstallaties of the recirculsttom pump mochemical osals.
6. Difficulty in restarting the re-circulation pumps wat experienced when the reactor was et oprating prese=re.
7. Replacement- of c.11 sixteen sir.iach safety valves.
8. "D" recireeletten pump tripped and would not restart. N pump was dis-assembled and shipped of f-site fee repair.
  • L During the entire start-up program, operatiemal dif ficulties were e7perien ed with the teacter Cleanup Systas, pressure redtseing valve problems persisted md the system experienced two entages u the direct-result of tube f ailures la the soaregemers-
tive beat encharger.

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10. Several problems developed wit.h the star l up of the turbine. Meet socable were these l related to the air ejector system asid the j immer and af ter eendenser dratos. The draiu system as installed did not work and a tem- '

perary draim systam was tastalled (the permanent drain system was scheduled for

f. completion in 1970). Problems were owperi-j- anced with the tuning-up of the mechanteal pressure regulater and an electric pressure

.reguister failure acestred as reported by letter of sevenber 3, 1969. N moisture separater and robester drata tank-flash task system required many adjestmeate and drais valve modifiestions to pinee it ta soltable' eervice.  ;- .

11. "D" recirculation pump was seinstalled

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MstER CREEK (Courr'D) 12. All fewr auto-depressorise N +/ -

riectromatic relief valves were pseved for sorrecties of main and pilat webue .

eest leakage. ChP4 1 1

13. Raacter operatar licensing ====t=ations !

were sempleted as September 19, 1M 9.

14. Castrel red drive internal filter plugging was experiemeed, reaultih6 La slow seren time. while at is11 remeter presouro (report of October 14, IM9).

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15. Be.1 diesel generator engine was re-

! placed with a new engiae eue to failure '

{ of the original engir e as ceM try water .

leakaga into No. 19 eylinder.

f 16. Main stems isolation valve testing l undar hot pressurised conditions (reports of December 24, 1969, and March 20,1970),

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, lharing the period of this report, the fleet I- Operations Leview Committee Fald a total of 40 eneecinas. The General office Review u.rd t . t.t.t .,.,gh, as...

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Form. A10.)lO gflev. 9-53) AICM 0240 9 v. e. novs ewant pain tino or net: t ot e o . m. o v r

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