Similar Documents at Perry |
---|
Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in Pnpp to Ceico ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at Pnpp & Use of Table IWB-3514 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20211H6791997-09-18018 September 1997 Safety Evaluation Authorizing Licensees Request for Alternative from Augmented Insp of Reactor Pressure Vessel Circumferential Weld in Plant,Unit 1 ML20211A5881997-09-11011 September 1997 Safety Evaluation Supporting Evaluation of First 10-yr Interval ISI Program Plan Requests for Relief PT-004,PT-005 & PT-006 for Plant,Unit 1 ML20217K9061997-08-12012 August 1997 Safety Evaluation Accepting Plant First 10-yr Interval ISI Program Plan Relief Request PT-007 ML20141L9131997-05-27027 May 1997 Safety Evaluation Accepting Relief Requests for First 10-yr Interval Inservice Insp Program Plan for Plant,Unit 1 ML20147H4211997-04-0101 April 1997 Safety Evaluation Accepting Changes to USAR Sections,Which Continue to Satisfy Criteria of App B of 10CFR50 ML20134D1061997-01-27027 January 1997 Safety Evaluation on Revised EALs for Plant.Proposed EALs Changes Are Consistent W/Guidance in NUMARC/NESP-007,with One Exception,& Meets Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 ML20058M6761993-09-29029 September 1993 Safety Evaluation Accepting Rev 10 to Plant Emergency Plan for NRC Review Under 10CFR50.54(q) ML20246F6481989-08-23023 August 1989 Safety Evaluation Accepting Proposed Turbine Sys Maint Program ML20246Q0291989-07-14014 July 1989 Safety Evaluation Re Updated Safety Analysis Rept Appendix 1B,license Commitment Revs ML20244D6351989-06-0707 June 1989 Safety Evaluation Supporting Licensee Response to Generic Ltr 83-28,Item 4.5.3 Re Reactor Trip Sys Reliability NUREG-0133, Safety Evaluation Accepting Licensee Rev 3 to ODCM for Plant Through Temporary Change 4.Rev Meets Criteria of NUREG-0133 & Other Guidance. Guidance1989-06-0505 June 1989 Safety Evaluation Accepting Licensee Rev 3 to ODCM for Plant Through Temporary Change 4.Rev Meets Criteria of NUREG-0133 & Other Guidance. Guidance ML20246Q0771989-05-0909 May 1989 Safety Evaluation Supporting Proposed Mod to Delete K74B & K74D Relays from Electrical Control Circuitry of MSIV to Resolve Spurious Opening of MSIV on Loss of Reactor Protection Sys Bus a or B ML20248G2921989-03-30030 March 1989 Safety Evaluation Accepting Util 840406 Response to Generic Ltr 83-28,Item 4.5.2, Reactor Trip Sys Reliability On-Line Testing ML20236E0141989-03-15015 March 1989 Safety Evaluation Supporting Util Implementation of 10CFR50.62 ATWS Rule ML20196D4311988-12-0606 December 1988 Safety Evaluation Documenting NRC Review of Licensee Response to Generic Ltr 83-28.Evaluation Concludes That Licensee Adequately Meets Provisions of Part 1 of Item 2.2 to Generic Ltr 83-28 ML20213A5661987-04-20020 April 1987 Safety Evaluation Supporting Amend 4 to License NPF-58 ML20205Q9771987-04-0101 April 1987 Safety Evaluation Supporting Amend 3 to License NPF-58 ML20203N6981986-10-10010 October 1986 Sser Supporting Util Request for Relief from Preservice Insp Program Requirements ML20203N6951986-10-10010 October 1986 Safety Evaluation Supporting Request for Relief from ASME Code Exam Requirements in Preservice Insp Program ML20202G4321986-07-0808 July 1986 SER Approving Tdi Diesel Generator Owners Group Program to Validate & Upgrade Design & Mfg Quality of Tdi Diesel Generators for Nuclear Emergency Standby Svc ML20198C3951985-11-0505 November 1985 Safety Evaluation Re Reliability of Tdi Standby Emergency Diesel Generators for Application at Domestic Nuclear Plants.Diesel Generators Will Provide Reliable Standby Source of Onsite Power,W/Listed License Conditions ML20138N7461985-10-28028 October 1985 SER Supporting Reliability of Tdi Standby Emergency Diesel Generators.Viewgraphs & Final Draft Tech Specs Encl 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20212J2011999-09-30030 September 1999 Safety Evaluation Supporting Transfer of Dl Ownership Interest in Pnpp to Ceico PY-CEI-NRR-2437, Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2429, Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pnpp,Unit 1.With PY-CEI-NRR-2424, Monthly Operating Rept for July 1999 for Perry Npp.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Perry Npp.With ML20210J3851999-07-28028 July 1999 Pnpp - Unit 1 ISI Summary Rept Results for Outage 7 (1999) First Period,Second Interval PY-CEI-NRR-2416, Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Perry Nuclear Power Plant,Unit 1.With ML20196A1951999-06-17017 June 1999 Instrument Drift Analysis ML20207G2741999-06-0707 June 1999 Safety Evaluation Concluding That Firstenergy Flaw Evaluation Meets Rules of ASME Code & That IGSCC & Thermal Fatigue Crack Growth Need Not Be Considered in Application PY-CEI-NRR-2409, Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2393, Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored1999-05-12012 May 1999 Special Rept Update:On 990327 Refueling Outage 7 Began & Troubleshooting Efforts Began.Troubleshooting of Affected Calbe Confirmed Fault in Drywell Section of Cable.Determined That Installation of Newer Technology Should Be Explored ML20206G6451999-05-0303 May 1999 Safety Evaluation Authorizing Requests for Relief IR-032 to IR-035 & IR-037 to IR-040 Re Implementation of Subsections IWE & Iwl of ASME Section XI for Containment Insp PY-CEI-NRR-2399, Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Perry Nuclear Power Plant,Unit 1.With ML20206E2261999-04-29029 April 1999 Safety Evaluation Concluding That Proposed Alternatives Will Result in Acceptable Level of Quality & Safety.Authorizes Use of Code Case N-504 for Weld Overlay Repair of FW Nozzle Weld at Pnpp & Use of Table IWB-3514 ML20206D7911999-04-23023 April 1999 Rev 6 to PDB-F0001, COLR for Pnpp Unit 1 Cycle 8,Reload 7 ML20205P4371999-04-15015 April 1999 Safety Evaluation Concluding That Licensee Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking or Thermal Binding ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20206D8461999-03-31031 March 1999 Rev 1 to J11-03371SRLR, Supplemental Reload Licensing Rept for Pnpp,Unit 1 Reload 7 Cycle 8 PY-CEI-NRR-2389, Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Perry Nuclear Power Plant,Unit 1.With ML20205G4221999-03-31031 March 1999 Safety Evaluation Accepting Second 10-yr Interval IST Program Releif Requests for Plant,Unit 1 ML20205D3101999-03-26026 March 1999 Safety Evaluation Supporting Amend 103 to License NPF-58 ML20205C3761999-03-26026 March 1999 Safety Evaluation Supporting Request for Proposed Exemption to 10CFR50,app a GDC 19 PY-CEI-NRR-2369, Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 9902271999-03-0303 March 1999 Special Rept:On 990127,PAMI Was Declared Inoperable.Caused by Low Resistance Reading Existing in Circuit That Goes to Drywell.Troubleshooting of Affected Cable Will Commence During RFO on 990227 PY-CEI-NRR-2372, Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With1999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Perry Nuclear Power Plant,Unit 1.With ML20203A5961999-02-0202 February 1999 Safety Evaluation Accepting Licensee Proposed Revs to Responsibilities of Plant Operations Review Committee as Described in Chapter 17.2 of USAR ML20203A5211999-01-27027 January 1999 Safety Evaluation Accepting Licensee Calculations Showing That Adequate NPSH Will Be Available for HPCS Pumps ML20198R8921999-01-0707 January 1999 SER Accepting Licensee Proposed Amend to TSs to Delete Reference to NRC Policy Re Plant Staff Working Hours & Require Administrative Controls to Limit Working Hours to Be Acceptable ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl PY-CEI-NRR-2356, Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Perry Nuclear Power Plant,Unit 1.With ML20198J0031998-12-22022 December 1998 SER Accepting Licensee Response to GL 92-08,ampacity Derating Issues for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2346, Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Perry Nuclear Power Plant,Unit 1.With ML20195F6891998-11-0505 November 1998 Safety Evaluation Accepting Proposed Reduction in Commitment in Quality Assurance Program to Remove Radiological Assessor Position PY-CEI-NRR-2335, Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2329, Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Perry Nuclear Power Plant,Unit 1.With ML20153B8221998-09-16016 September 1998 Safety Evaluation Accepting Changes to USAR Section 13.4.3, 17.2.1.3.2.2,17.2.1.3.2.2.3 & App 1A PY-CEI-NRR-2323, Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Perry Nuclear Power Plant,Unit 1.With PY-CEI-NRR-2313, Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 11998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2306, Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 11998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Perry Nuclear Power Plant,Unit 1 ML20249A1891998-06-11011 June 1998 SER on Moderate Energy Line Pipe Break Criteria for Perry Nuclear Power Plant,Unit 1 & Requests Addl Info to Demonstrate That Plant & FSAR in Compliance W/Staff Position & GDC as Discussed in SER PY-CEI-NRR-2289, Monthly Operating Rept for May 1998 for Perry,Unit 11998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Perry,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted PY-CEI-NRR-2282, Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 11998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D2051998-04-20020 April 1998 SER Authorizing Licensee to Use Code Case N-524 Until Such Time as Code Case Included in Future Rev of RG 1.147 PY-CEI-NRR-2277, Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 11998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Perry Nuclear Power Plant,Unit 1 ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216G3901998-03-11011 March 1998 SER on Proposed Merger Between Duquesne Light Co & Allegheny Power Sys,Inc ML20216J1401998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Perry Nuclear Power Plant,Unit 1 PY-CEI-NRR-2258, Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 11998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Perry Nuclear Power Plant,Unit 1 1999-09-30
[Table view] |
Text
~
./ 'o
~g UNITED STATES 8 o NUCLEAR REGULATORY COMMISSION h : WASHINGTON D. C. 205S5
%...../
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT NO. 3 TO FACILITY OPERATING LICENSE NO. NPF-58 CLEVELAND ELECTRIC ILLUMINATING COMPANY, ET AL PERRY NUCLEAR POWER PLANT, UNIT NO. 1 DOCKET NO. 50-440 I.0 INTRODUCTION By letter dated March 4,1987, as supplemented on March 19, 1987, Cleveland Electric Illuminating Company, Duquesne Light Company, Ohio Edison Company, PennsylvaniaPowerCompany,andToledoEdisonCompany,(thelicensees) requested an amendment to Facility Operating License No NPF-58 for the Perry Nuclear Power Plant, Unit No. 1. The proposed amendment would change the maximum isolation time allowed by the Technical Specifications from 50 seconds to 20 seconds for operation of the Reactor Core Isolation Cooling (RCIC) system inboard containment isolation valve (IE51-F063). This change was requested in relation to a planned conversion of this normally-closed valve, which is presently operated by a direct-current (DC) motor operator, to be normally-open with a more reliable alternating-current (AC) motor operator. The amendment would also delete from the Technical Specifications the load represented by the DC motor operator on the valve and the identification of the motor control center through which DC power is supplied to the motor operator. The replacement AC supply will be from another motor control center which is presently identified in the Technical Specifications.
2.0 EVALUATION
~
The purpose of the RCIC system is to provide reactor coolant makeup when the reactor pressure vessel is isolated but still at high pressure. The F063 valve serves as the inboard isolation valve in the line which provides steam to operate the RCIC turbine. This valve was installed with a DC powered operator to assure that the RCIC system can operate independent of any normal or emergency AC power and the valve is kept normally closed to !
provide maximum assurance of containment isolation in the event of a break
{
in the RCIC steam line outside containment. j CEI is proposing to modify the present arrangement because operability tests have shown that the DC motor operator is unreliable and attempts to correct this problem have been unsuccessful. Changing the power source for the motor operator to AC would facilitate replacement of the motor operator with another component which is already qualified for service inside the drywell. The power supply will be Class 1E. The addition of the valve motor operator to the Division 2 AC system would have only a minor impact I on system loading.
g40gg M o P ,
1
~
?
l l
l The second change is that the valve will now be normally open; this is l necessary to meet the design requirement that RCIC be operable independent of AC power. The isolation function (which need not be independent of AC ;
power) will be provided automatically upon receipt of a signal indicating a break in the RCIC steam line, i The F053 valve is designed to close in less than 20 seconds after receipt of an isolation signal. . The licensee has reported that the dose consequences for a break in the RCIC line with a 20-second isolation valve closure time are bounded by the existing steam line break analysis. Since the RCIC stean line flow area is about a factor of 20 smaller than the main steam line flow area and the RCIC isolation valve closure time is only a factor of 4 larger than the MSIV closure time, the staff agrees that the dose consequences are bounded. The licensee has also stated that safety equipment in rooms where reactor coolant could be released under accident conditions is qualified for the environment resulting from a break with isolation in 20 seconds.
The staff questioned CEI as to the reliability of the F063 valve under flow conditions expected during a break in the RCIC steam line. The licensee indicated that the valve is designed to operate against the maximum calculated system pressure. However, the valve has not actually been tested under flow conditions which could occur in the event of a line break. As a consequence, the licensee has committed to further evaluate the proposed design configuration, as well as alternative configurations, to determine the most desirable desion. The evaluation will take into
~
account both system availability and isolation capability. CEI bas committed to provide the results of the evaluation to the staff by December 31, 1987.
By October 31, 1987 CEI will provide to the staff a summary of the alternative configurations being considered. Prior to startup following the first refueling outage, CEI will implement the appropriate modifications,-
if required by the staff.
The staff considers the licensees' commitments sufficient to address the concern regarding isolation valve operability. We also note that this issue is currently being pursued by the staff as Generic Issue 87:
" Failure of HPCI Steam Line Without Isolation." Operation until the first refueling outage is considered acceptable since the Perry Plant equipment layout is such that it is unlikely that more than one emergency core cooling (ECC) subsystem could be affected by a break in the RCIC steam line. Different ECC subsystems are in different equipment rooms separated by physical barriers so that environmental disturbances (such as pipe rupture) in one system will not affect the remaining subsystems. Any one water injection subsystem of the ECCS has sufficient capacity for main-taining the core covered after a RCIC steam line break. Therefore, significant fuel failures would not be expected for this event.
1 I
].3 t
3.0 EXIGENT CIRCUMSTANCES
Due to several instances in which the RCIC system inboard containment isolation valve had failed to open during tests, CEI informed the NRC, in a letter dated February 24, 1987, of its-intent to make physical changes to the motor operator on the valve. In order to complete Startup Test Condition 1 prior to making such changes, CEI requested and was granted interim relief for a period of 30 days from the requirement that this normally-closed valve be operable (letter from Robert H. Bernero, NRC, to Murray R. Edelman, CEI, February 24,1987).
Subsequently, CEI decided to replace the existing DC motor operator on i .the valve.with an AC motor operator and to modify the position of the valve to normally open. These modifications involve changes in the
! Technical Specifications, which were requested by the licensees by a letter on March 4, 1987. Since the changes are necessary to allow operation of the plant beyond March 26, 1987, there was insufficient time to process this amendment in the normal manner, which allows 30 days for public comment following publication of a notice of the proposed action in the Federal Recister. However, there was sufficient time for a two-week comment period. Therefore, CEI requested that this amendment be processed under exigent circumstances, in accordance with 10 CFR 50.91(a)(6).
The staff has reviewed the circumstances associated with the licensees' request and agrees that the amendment is necessary for continuation of startup testing and that failure to act upon the request in a timely manner would prevent resumption of plant operation. The staff concluded that this situation could not have been avoided and, therefore, valid c exigent circumstances exist, as defined by 10 CFR 50.91(a)(6).
3.1 FINAL NO SIGNIFICANT HAZARDS CONSIDFRATION DETERMINATION The Comission has provided standards for determining whether a
, significant hazards consideration exists as stated in:10 CFR 50.92. A proposed amendment to an operating license for a facility involves no significant hazards considerations if operation of the facility in
- accordance with a proposed amendment would not: (1) involve a j' significant increase in the probability or consequences 'of an accident previously evaluated; or (2) create the possibility of a new or
- different kind of accident from any accident previously evaluated; or j
(3) involve a significant reduction in a margin of safety.
ihe licensee has provided an analysis of its proposed amendment request
. in relation to the above standards and has concluded that it involves no
- significant hazards considerations. The Connission also has made a final i
detemination that the amendment request involves no significant hazards considerations, based on the above standards and the following considerations:
l l
l The-proposed change does not involve a significant increase in the probability or consequences of an accident previously analyzed because the change from a DC motor operator to an AC motor operator and the decrease in the operating time requirement from 50 seconds to 20 seconds will serve to increase rather than decrease the availability of the RCIC system and the operation of the RCIC s / stem with the valve normally open, but able to close within 20 seconds, is within the bounds of the existing main steam line break analysis. For environmental qualification, the licensees have performed an analysis which demonstrates that line isolation within 20 seconds will not jeopardize equipment required for safe shutdown r in the environmental zones (pressure, temperature, humidity) related to the ,
postulated pipe break. i The proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated because the RCIC system reliability will be increased, the RCIC system operation will remain within the bounds of existing safety analyses, and the basic operation of ,
the RCIC system will not change. Furthermore, the change from DC to AC e operation will not significantly affect either the AC or DC power systems, as the AC power has more than sufficient capacity to supply the increased load of the valve operation and the load on the DC power system will decrease.
The proposed change does not involve a significant reduction in a margin of safety because the basic operation of the RCIC system is not changed, the isolation valve will maintain all of its present isolation signals, and it will be capable of operating against the maximum calculated system pressure while satisfying all applicable General Design Criteria of Appendix A to 10 CFR Part 50. As indicated in the staff's evaluation (Section 2.0 above), the F063 valve has not actually been tested under flow conditions which could occur in the event of a RCIC steam line break downstream. However, it is unlikely that more than one ECC subsystem could be affected by a RCIC steam line break and any one of the ECC water injection subsystems has sufficient capacity for keeping the reactor core covered after such a break.
Accordingly, the amendment does not involve significant hazards considerations.
3.2 JTATECONSULTATION The staff consulted with the State of Ohio by telephone on March 26, 1987. There were no comments on this amendment.
4.0 ENVIRONMENTAL CONSIDERATION
l This amendment involves a change to a requirement with respect to the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20 and changes to the surveillance require-ments. The staff has determined that the amendment involve's' no significant
- O increase in the amounts, and no significant change in the types, of any effluents that may be released offsite and that there is no significant increase in individual or cumulative occupational radiation exposure.
The Commission previously issued a proposed finding that this amendment involves no significant hazards consideration and there has been no public comment on such finding. Accordingly, this amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pur-suant to 10 CFR 51.22(b), no environmental impact statement nor environ-mental assessment need be prepared in connection with the issuance of this amendment.
5.0 CONCLUSION
The staff has concluded, based on the considerations discussed above, that: (1) the amendment does not (a) significantly increase the probability or consequences of an accident previously evaluated, (b) create the possibility of a new or different kind of accident from any previously evaluated, or (c) significantly reduce a safety margin and, therefore, the amendment does not involve significant hazards consider-atians; (2) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner; and (3) such activities will be conducted in compliance with the Commission's regulations and the issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public.
Prinicipal Contributors:
T. Collins and P. Leech Dated: April 1, 1987 t