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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML20217F0941999-10-14014 October 1999 Application for Amends to Licenses DPR-39 & DPR-85,to Revise TS Sections 2.2 & 3.0/4.0 to Support Mod P000224 Which Will Install New Power Range Neutron Monitoring Sys & Incorporate long-term thermal-hydraulic Stability Solution Hardware ML20216J3341999-09-27027 September 1999 Supplements Application for Amends to Licenses NPF-39 & NPF-45,to Modify Appearance of TS Page 3/4 4-8 as Typo Was Identified in Section 3.4.3.1 of Ts.Corrected TS Page,Encl ML20212H5521999-09-27027 September 1999 Application for Amends to Licenses NPF-39 & NPF-85,revising TS to Clarify Several Administrative Requirements,Deleting Redundant Requirements & Correcting Typos ML20212F9521999-09-20020 September 1999 Application for Amend to License NFP-39,requesting Issuance of TS Change Request 98-08-0 Re Increase in Allowable as- Found Main Steam SRV Setpoint Tolerance.Util Had Originally Requested That Subject TS Change Be Deferred in ML20196F5471999-06-22022 June 1999 Application for Amends to Licenses NPF-39 & NPF-85,change Request 99-01-0,to Revise TS to Delete Surveillance Requirement 4.4.1.1.2 & Associated TS Administrative Controls Section 6.9.1.9.h ML20195G0421999-06-0707 June 1999 TS Change Request 98-09-0 for Licenses NPF-39 & NPF-85, Revising TS Section 3/4.4.3, RCS Leakage,Leakage Detection Systems, by Clarifying Action Statement Re Inoperative Reactor Coolant Leakage Detection Systems ML20195E7521999-06-0707 June 1999 TS Change Request 91-08-01 to License NPF-39,reflecting Permanently Deactivated Instrument Reference Leg Isolation Valve HV-61-102 in TS Table 3.6.3-1, Primary Containment Isolation Valves & Associated Notations ML20195B8361999-05-26026 May 1999 TS Change Request 99-02-0 for Licenses NPF-39 & NPF-85, Revising TS Section 4.1.3.5.b by Removing & Relocating Control Rod Scram Accumulators Alarm Instrumentation to UFSAR & Revising TS Section 3.1.3.5 ML20207L6561999-03-11011 March 1999 TS Change Request 98-07-2 for License NPF-85,revising MCPR Safety Limit Contained in TS Section 2.1, Safety Limits. Proprietary & non-proprietary Info Re Cycle Specific SLMCPR for Lgs,Unit 2 Cycle 6,encl.Proprietary Info Withheld ML20199G1651999-01-12012 January 1999 TS Change Request 98-08-0 to Licenses NPF-39 & NPF-85, Proposing Rev to TS Section 3/4.4.2 & TS Bases Sections B 3/4.4.2,B 3/4.5.1 & B 3/4.5.2.Supporting TSs & Proprietary & non-proprietary Trs,Encl.Proprietary Info Withheld ML20199A6861999-01-0404 January 1999 TS Change Request 97-01-01 to Licenses NPF-39 & NPF-85, Revising Administrative Section on Controlled Access to High Radiation Areas & Rept Dates for Listed Repts ML20155H6311998-10-30030 October 1998 Application for Amends to Licenses NPF-39 & NPF-85, Respectively,Revising TS Surveillance Requirements 4.8.4.3.b.1,4.8.4.3.b.2 & 4.8.4.3.b.3 in Order to Reflect Relay Setpoint Calculation Methodology ML20154Q8781998-10-15015 October 1998 TS Change Request 97-04-0 to Licenses NPF-39 to NPF-85, Adding New TS Section & TS Bases Section to Incorporate Special Test Exception to Allow Rc Temp Greater than 200 F During IST & Hydrostatic Testing ML20151Z4541998-09-14014 September 1998 TS Change Request 98-04-2 to License NPF-85,revising TS Table 4.4.6.1.3-1 Re Withdrawal Schedule for Reactor Pressure Vessel Matl Surveillance Program Capsules.Ge Rept GE-NE-B1100786,encl ML20151V0731998-09-0404 September 1998 TS Change Request 96-23-0 to Licenses NPF-39 & NPF-85, Revising TS Pages to Ensure Fidelity Between TS Pages & 970324 Submittal ML20236L5151998-07-0202 July 1998 Supplemental Application for Amend to Licenses NPF-39 & NPF-85,consisting of TS Change Request 96-06-0,modifying Appearance of Unit 1,FOL Page 8 ML20202G7591998-02-0909 February 1998 Application for Amend to License NPF-39,revising TS Section 2.1, Safety Limits, to Revise Minimum Critical Power Ratio Safety Limit.Proprietary Supporting Info Withheld (Ref 10CFR2.790) ML20199G7701998-01-27027 January 1998 Application for Amends to Licenses NPF-39 & NPF-89,removing Maximum Isolation Time for HPCI Turbine Exhaust Containment Isolation Valve HV-055-1(2)F072 from Ts.Change Request 98-01-0 & marked-up TS Encl ML20198M7551998-01-12012 January 1998 TS Change Request 97-02-1 to License NPF-39,revising TS Table 4.4.6.1.3-1 to Change Withdrawal Schedule for First Capsule to Be Withdrawn from 10 Effective Full Power Yrs to 15 Efpy.Ge Rept GE-NE-B1100786-01,Rev 1 Encl ML20212D1761997-10-24024 October 1997 Application for Amend to License NPF-39,revising TS Section 3/4.1.3.6,to Exempt Control Rod 50-27 from Coupling Test for Remainder of Cycle 7,provided Certain Conditions Are Met ML20216H0931997-09-0808 September 1997 Application for Amends to Licenses NPF-39 & NPF-85, Supplementing Changes Request 96-06-0 by Adding Three Addl TS Pages Containing Typo Errors Discovered Since 970225 Submittal ML20210T9141997-09-0202 September 1997 TS Change Request 96-20-0 to Licenses NPF-39 & NPF-85, Revising TS Section 4.0.5 & Bases Sections B 4.0.5 & B 3/4.4.8,re SRs Associated W/Isi & Inservice Testing of ASME Code Class 1,2 & 3 Components ML20137X7931997-04-0909 April 1997 TS Change Request 96-24-0 to Licenses NPF-39 & NPF-85, Deleting Requirement to Correct Specific Gravity Values Based on Electrolyte Battery State of Charge ML20137G6611997-03-24024 March 1997 Application for Amends to Licenses NPF-39 & NPF-85,deleting Drywell & Suppression Chamber Purge Sys Operational Time Limit & Adding SR to Ensure Purge Sys Large Supply & Exhaust Valves Are Closed as Required ML20135D0861997-02-25025 February 1997 Application for Amends to Licenses NPF-39 & NPF-85, Reflecting Name Change from PA Electric Co to PECO Energy Co ML20135F0911996-12-0606 December 1996 Application for Amend to License NPF-85,revising TS 2.1 to Change Minimum Critical Power Ratio Safety Limit ML20135A3841996-11-25025 November 1996 Application for Amends to Licenses NPF-39 & NPF-85,revising TS SR 4.8.1.1.2.e.2 & Supporting TS Bases Section 3/4.8,to Clarify Requirements Associated W/Single Load Rejection Testing of EDGs ML20128N7551996-09-27027 September 1996 Application for Amends to Licenses NPF-39 & NPF-85, Requesting Rev to Increase Reactor Enclosure Secondary Containment Maximum Inleakage Rate ML20116L2551996-08-0808 August 1996 Application for Amends to Licenses NPF-39 & NPF-85,revising TS Sections 3/4.3.1,3/4.3.2,3/4.3.3 & Associated TS Bases Sections 3/4.3.1 & 3/4.3.2 to Eliminate Selected Response Time Testing Requirements ML20116H6161996-08-0505 August 1996 Application for Amend to License NPF-85,revising TS Section 2.1, Safety Limits, to Revise Min Critical Power Ratio Safety Limit ML20116E5981996-08-0101 August 1996 Application for Amend to License NPF-85,revising TS Section 3/4.4.4.6 to Reflect Addition of Two Hydroset Curves Effective for 6.5 & 8.5 Effective Full Power Years,To Existing Pressure-Temp Operating Limit for LGS Unit 2 ML20115A9071996-06-28028 June 1996 Application for Amend to Licenses NPF-39 & NPF-85 to Perform Containment leakage-rate Testing Per 10CFR50,App J, Primary Reactor Containment Leakage Testing for Water-Cooled Power Reactors, Option B ML20117H2441996-05-20020 May 1996 TS Change Request 96-12-0 to Licenses NPF-39 & NPF-85, Revising TS Sections 3/4.4.9.2,3/4.9.11.1,3/4.9.11.2 & Associated TS Bases 3/4.4.9 & 3/4.9.11 to More Clearly Describe,Rhr Sys Shutdown Cooling Mode of Operation ML20117D7451996-05-0303 May 1996 Application for Amends to Licenses NPF-39 & NPF-85,revising TS SRs to Change Surveillance Test Frequency for Performing Flow Testing of SGTS & RERS from Monthly to Quarterly ML20107M5061996-04-25025 April 1996 TS Change Request 95-08-0 to Licenses NPF-39 & NPF-85, Relocating TS 3/4.7.7 Re Traversing in-core Probe LCO ML20101L9111996-03-29029 March 1996 Application for Amends to Licenses NPF-39 & NPF-85, Respectively,Revising TS SR 4.5.1.d.2.b to Delete Requirement to Perform Functional Testing of ADS Valves as Part of start-up Testing Activities ML20095K4801995-12-22022 December 1995 Application for Amend to Licenses NPF-39 & NPF-85,increasing Drywell & Suppression Chamber Purge Sys Operating Time Limit from 90 H Each 365 Days to 180 H Each 365 Days ML20092J3941995-09-18018 September 1995 TS Change Request 95-01-0 to Licenses NPF-39 & NPF-85, Revising TS Table 4.3.1.1-1, RPS Instrumentation SRs to Reflect Change in Calibr Frequency for LPRM Signal from Every 1,000 EFPH to Every 2,000 Megawatt Days Per Std Ton ML20092J3181995-09-14014 September 1995 Application for Amends to Licenses NPF-39 & NPF-85,revising TS to Remove Secondary Containment Isolation Valve Tables ML20087C9451995-08-0101 August 1995 TS Change Request 95-12-0 Revising TS Section 3/4.9.1, to Provide Alternate Actions to Allow Continuation of Core Alterations in Event Certain RMCS & Refueling Interlocks Are Inoperable ML20086S5981995-07-28028 July 1995 Application for Amends to Licenses NPF-39 & NPF-85,revising TS Table 4.3.1.1-1,to Reflect Changes to Surveillance Test Frequency Requirements for Various RPS Instrumentation ML20086U4821995-07-28028 July 1995 TS Change Request 94-28-0 to Licenses NPF-39 & NPF-85, Revising TS SR & Deleting Specific Requirements to Perform Surveillances Prior to Beginning or Resuming Core Alterations or CR Withdrawal Assoc W/Refueling Activities ML20086U4361995-07-28028 July 1995 TS Change Request 95-09-0 to Licenses NPF-39 & NPF-8, Revising Ts,By Deleting Operability & SR Involving Secondary Containment Diffrential Pressure Instrumentation ML20086T6061995-07-28028 July 1995 TS Change Request 95-13-0 of License NPF-39 & NPF-85, Requesting Change to Ts,To Eliminate TS Requirement to Perform 10CFR50,App J,Type C,Hydrostatic Testing on Certain Valves ML20086A1631995-06-23023 June 1995 Application for Amend to License NPF-85,consisting of Change Request 95-07-2,extending AOT to Allow Adequate Time to Install Isolation Valves & cross-ties on ESW & RHRSW Sys to Facilitate Future Insps or Maint ML20085M8811995-06-20020 June 1995 Application for Amend to Licenses NPF-39 & NPF-85,consisting of Change Request 95-06,requesting one-time Schedular Exemption from 10CFR50,App J, Primary Containment Leakage Testing for Water-Cooled Power Reactors ML20085M9171995-06-19019 June 1995 Application for Amend to License NPF-39,consisting of Change Request 95-03,revising TS Section 2.1, Safety Limits, to Change MCPR Safety Limit,Due to Use of GE13 Fuel Product Line ML20084Q9241995-06-0505 June 1995 Application for Amends to Licenses NPF-39 & NPF-85, Consisting of TS Change Request 94-49-0,revising TS Section 3/4.1.5, SLCS to Remove Min Flow Rate Requirement for SLCS Pumps ML20083R0031995-05-19019 May 1995 Application for Amends to Licenses NPF-39 & NPF-85, Consisting of Change Request 95-02,revising TS Table 3.3.3-3, ECCS Response Times to Reflect Value of 60 Seconds for HPCI Sys Response Time Instead of 30 Seconds ML20082J4001995-04-0606 April 1995 Application for Amends to Licenses NPF-39 & NPF-85, Consisting of TS Change Requests 94-51 Delete Independent Tech Review Section from TS, 94-52 Delete Nrb Review Section from TS, 94-53 Delete Nrb Audit Section from Ts 1999-09-27
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML20217F0941999-10-14014 October 1999 Application for Amends to Licenses DPR-39 & DPR-85,to Revise TS Sections 2.2 & 3.0/4.0 to Support Mod P000224 Which Will Install New Power Range Neutron Monitoring Sys & Incorporate long-term thermal-hydraulic Stability Solution Hardware ML20216J3341999-09-27027 September 1999 Supplements Application for Amends to Licenses NPF-39 & NPF-45,to Modify Appearance of TS Page 3/4 4-8 as Typo Was Identified in Section 3.4.3.1 of Ts.Corrected TS Page,Encl ML20212H5521999-09-27027 September 1999 Application for Amends to Licenses NPF-39 & NPF-85,revising TS to Clarify Several Administrative Requirements,Deleting Redundant Requirements & Correcting Typos ML20212F9521999-09-20020 September 1999 Application for Amend to License NFP-39,requesting Issuance of TS Change Request 98-08-0 Re Increase in Allowable as- Found Main Steam SRV Setpoint Tolerance.Util Had Originally Requested That Subject TS Change Be Deferred in ML20196F5471999-06-22022 June 1999 Application for Amends to Licenses NPF-39 & NPF-85,change Request 99-01-0,to Revise TS to Delete Surveillance Requirement 4.4.1.1.2 & Associated TS Administrative Controls Section 6.9.1.9.h ML20195E7521999-06-0707 June 1999 TS Change Request 91-08-01 to License NPF-39,reflecting Permanently Deactivated Instrument Reference Leg Isolation Valve HV-61-102 in TS Table 3.6.3-1, Primary Containment Isolation Valves & Associated Notations ML20195G0421999-06-0707 June 1999 TS Change Request 98-09-0 for Licenses NPF-39 & NPF-85, Revising TS Section 3/4.4.3, RCS Leakage,Leakage Detection Systems, by Clarifying Action Statement Re Inoperative Reactor Coolant Leakage Detection Systems ML20195B8361999-05-26026 May 1999 TS Change Request 99-02-0 for Licenses NPF-39 & NPF-85, Revising TS Section 4.1.3.5.b by Removing & Relocating Control Rod Scram Accumulators Alarm Instrumentation to UFSAR & Revising TS Section 3.1.3.5 ML20207L6561999-03-11011 March 1999 TS Change Request 98-07-2 for License NPF-85,revising MCPR Safety Limit Contained in TS Section 2.1, Safety Limits. Proprietary & non-proprietary Info Re Cycle Specific SLMCPR for Lgs,Unit 2 Cycle 6,encl.Proprietary Info Withheld ML20199G1651999-01-12012 January 1999 TS Change Request 98-08-0 to Licenses NPF-39 & NPF-85, Proposing Rev to TS Section 3/4.4.2 & TS Bases Sections B 3/4.4.2,B 3/4.5.1 & B 3/4.5.2.Supporting TSs & Proprietary & non-proprietary Trs,Encl.Proprietary Info Withheld ML20199A6861999-01-0404 January 1999 TS Change Request 97-01-01 to Licenses NPF-39 & NPF-85, Revising Administrative Section on Controlled Access to High Radiation Areas & Rept Dates for Listed Repts ML20155H6311998-10-30030 October 1998 Application for Amends to Licenses NPF-39 & NPF-85, Respectively,Revising TS Surveillance Requirements 4.8.4.3.b.1,4.8.4.3.b.2 & 4.8.4.3.b.3 in Order to Reflect Relay Setpoint Calculation Methodology ML20154Q8781998-10-15015 October 1998 TS Change Request 97-04-0 to Licenses NPF-39 to NPF-85, Adding New TS Section & TS Bases Section to Incorporate Special Test Exception to Allow Rc Temp Greater than 200 F During IST & Hydrostatic Testing ML20151Z4541998-09-14014 September 1998 TS Change Request 98-04-2 to License NPF-85,revising TS Table 4.4.6.1.3-1 Re Withdrawal Schedule for Reactor Pressure Vessel Matl Surveillance Program Capsules.Ge Rept GE-NE-B1100786,encl ML20151V0731998-09-0404 September 1998 TS Change Request 96-23-0 to Licenses NPF-39 & NPF-85, Revising TS Pages to Ensure Fidelity Between TS Pages & 970324 Submittal ML20236L5151998-07-0202 July 1998 Supplemental Application for Amend to Licenses NPF-39 & NPF-85,consisting of TS Change Request 96-06-0,modifying Appearance of Unit 1,FOL Page 8 ML20247M6891998-05-14014 May 1998 Amend 128 to License NPF-39,documenting NRC Staff Approval of Implementation of Plant Mod to Support Installation of Replacement Suction Strainers for ECCS at Plant,Unit 1 ML20217Q5001998-05-0404 May 1998 Amend 127 to License NPF-39,revising Minimal Critical Power Ratio Safety Limits for Operation Cycle 8 ML20217M0731998-03-31031 March 1998 Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively, Revising LGS Units 1 & 2 TS Section 4.0.5 & Bases Sections B 3/4.4.8 Re Surveillance Requirements Associated W/Isi & IST ML20202G7591998-02-0909 February 1998 Application for Amend to License NPF-39,revising TS Section 2.1, Safety Limits, to Revise Minimum Critical Power Ratio Safety Limit.Proprietary Supporting Info Withheld (Ref 10CFR2.790) ML20199G7701998-01-27027 January 1998 Application for Amends to Licenses NPF-39 & NPF-89,removing Maximum Isolation Time for HPCI Turbine Exhaust Containment Isolation Valve HV-055-1(2)F072 from Ts.Change Request 98-01-0 & marked-up TS Encl ML20198M7551998-01-12012 January 1998 TS Change Request 97-02-1 to License NPF-39,revising TS Table 4.4.6.1.3-1 to Change Withdrawal Schedule for First Capsule to Be Withdrawn from 10 Effective Full Power Yrs to 15 Efpy.Ge Rept GE-NE-B1100786-01,Rev 1 Encl ML20212D1761997-10-24024 October 1997 Application for Amend to License NPF-39,revising TS Section 3/4.1.3.6,to Exempt Control Rod 50-27 from Coupling Test for Remainder of Cycle 7,provided Certain Conditions Are Met ML20216H0931997-09-0808 September 1997 Application for Amends to Licenses NPF-39 & NPF-85, Supplementing Changes Request 96-06-0 by Adding Three Addl TS Pages Containing Typo Errors Discovered Since 970225 Submittal ML20210T9141997-09-0202 September 1997 TS Change Request 96-20-0 to Licenses NPF-39 & NPF-85, Revising TS Section 4.0.5 & Bases Sections B 4.0.5 & B 3/4.4.8,re SRs Associated W/Isi & Inservice Testing of ASME Code Class 1,2 & 3 Components ML20137X7931997-04-0909 April 1997 TS Change Request 96-24-0 to Licenses NPF-39 & NPF-85, Deleting Requirement to Correct Specific Gravity Values Based on Electrolyte Battery State of Charge ML20137G6611997-03-24024 March 1997 Application for Amends to Licenses NPF-39 & NPF-85,deleting Drywell & Suppression Chamber Purge Sys Operational Time Limit & Adding SR to Ensure Purge Sys Large Supply & Exhaust Valves Are Closed as Required ML20135D0861997-02-25025 February 1997 Application for Amends to Licenses NPF-39 & NPF-85, Reflecting Name Change from PA Electric Co to PECO Energy Co ML20135F0911996-12-0606 December 1996 Application for Amend to License NPF-85,revising TS 2.1 to Change Minimum Critical Power Ratio Safety Limit ML20135A3841996-11-25025 November 1996 Application for Amends to Licenses NPF-39 & NPF-85,revising TS SR 4.8.1.1.2.e.2 & Supporting TS Bases Section 3/4.8,to Clarify Requirements Associated W/Single Load Rejection Testing of EDGs ML20128N7551996-09-27027 September 1996 Application for Amends to Licenses NPF-39 & NPF-85, Requesting Rev to Increase Reactor Enclosure Secondary Containment Maximum Inleakage Rate ML20116L2551996-08-0808 August 1996 Application for Amends to Licenses NPF-39 & NPF-85,revising TS Sections 3/4.3.1,3/4.3.2,3/4.3.3 & Associated TS Bases Sections 3/4.3.1 & 3/4.3.2 to Eliminate Selected Response Time Testing Requirements ML20116H6161996-08-0505 August 1996 Application for Amend to License NPF-85,revising TS Section 2.1, Safety Limits, to Revise Min Critical Power Ratio Safety Limit ML20116E5981996-08-0101 August 1996 Application for Amend to License NPF-85,revising TS Section 3/4.4.4.6 to Reflect Addition of Two Hydroset Curves Effective for 6.5 & 8.5 Effective Full Power Years,To Existing Pressure-Temp Operating Limit for LGS Unit 2 ML20115A9071996-06-28028 June 1996 Application for Amend to Licenses NPF-39 & NPF-85 to Perform Containment leakage-rate Testing Per 10CFR50,App J, Primary Reactor Containment Leakage Testing for Water-Cooled Power Reactors, Option B ML20117H2441996-05-20020 May 1996 TS Change Request 96-12-0 to Licenses NPF-39 & NPF-85, Revising TS Sections 3/4.4.9.2,3/4.9.11.1,3/4.9.11.2 & Associated TS Bases 3/4.4.9 & 3/4.9.11 to More Clearly Describe,Rhr Sys Shutdown Cooling Mode of Operation ML20117D7451996-05-0303 May 1996 Application for Amends to Licenses NPF-39 & NPF-85,revising TS SRs to Change Surveillance Test Frequency for Performing Flow Testing of SGTS & RERS from Monthly to Quarterly ML20107M5061996-04-25025 April 1996 TS Change Request 95-08-0 to Licenses NPF-39 & NPF-85, Relocating TS 3/4.7.7 Re Traversing in-core Probe LCO ML20101L9111996-03-29029 March 1996 Application for Amends to Licenses NPF-39 & NPF-85, Respectively,Revising TS SR 4.5.1.d.2.b to Delete Requirement to Perform Functional Testing of ADS Valves as Part of start-up Testing Activities ML20095K4801995-12-22022 December 1995 Application for Amend to Licenses NPF-39 & NPF-85,increasing Drywell & Suppression Chamber Purge Sys Operating Time Limit from 90 H Each 365 Days to 180 H Each 365 Days ML20092J3941995-09-18018 September 1995 TS Change Request 95-01-0 to Licenses NPF-39 & NPF-85, Revising TS Table 4.3.1.1-1, RPS Instrumentation SRs to Reflect Change in Calibr Frequency for LPRM Signal from Every 1,000 EFPH to Every 2,000 Megawatt Days Per Std Ton ML20092J3181995-09-14014 September 1995 Application for Amends to Licenses NPF-39 & NPF-85,revising TS to Remove Secondary Containment Isolation Valve Tables ML20087C9451995-08-0101 August 1995 TS Change Request 95-12-0 Revising TS Section 3/4.9.1, to Provide Alternate Actions to Allow Continuation of Core Alterations in Event Certain RMCS & Refueling Interlocks Are Inoperable ML20086S5981995-07-28028 July 1995 Application for Amends to Licenses NPF-39 & NPF-85,revising TS Table 4.3.1.1-1,to Reflect Changes to Surveillance Test Frequency Requirements for Various RPS Instrumentation ML20086U4821995-07-28028 July 1995 TS Change Request 94-28-0 to Licenses NPF-39 & NPF-85, Revising TS SR & Deleting Specific Requirements to Perform Surveillances Prior to Beginning or Resuming Core Alterations or CR Withdrawal Assoc W/Refueling Activities ML20086U4361995-07-28028 July 1995 TS Change Request 95-09-0 to Licenses NPF-39 & NPF-8, Revising Ts,By Deleting Operability & SR Involving Secondary Containment Diffrential Pressure Instrumentation ML20086T6061995-07-28028 July 1995 TS Change Request 95-13-0 of License NPF-39 & NPF-85, Requesting Change to Ts,To Eliminate TS Requirement to Perform 10CFR50,App J,Type C,Hydrostatic Testing on Certain Valves ML20086A1631995-06-23023 June 1995 Application for Amend to License NPF-85,consisting of Change Request 95-07-2,extending AOT to Allow Adequate Time to Install Isolation Valves & cross-ties on ESW & RHRSW Sys to Facilitate Future Insps or Maint ML20085M8811995-06-20020 June 1995 Application for Amend to Licenses NPF-39 & NPF-85,consisting of Change Request 95-06,requesting one-time Schedular Exemption from 10CFR50,App J, Primary Containment Leakage Testing for Water-Cooled Power Reactors ML20085M9171995-06-19019 June 1995 Application for Amend to License NPF-39,consisting of Change Request 95-03,revising TS Section 2.1, Safety Limits, to Change MCPR Safety Limit,Due to Use of GE13 Fuel Product Line 1999-09-27
[Table view] |
Text
Station support De;artmtnt 10 CFR 50.90 v
"c= e~ c ~ ,
PECO ENERGY Nuclear Group Headquarters 965 Chesterbrook Boulevard Wayne, PA 19087-5691 December 22,1995 Docket Nos. 50-352 50-353 Ucense Nos. NPF-39 NPF-85 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
Subject:
Umerick Generating Station, Units 1 and 2 Technical Specifications Change Request No.95-184 Increase Purge System Operational Time Umits Gentlemen:
PECO Energy Company (PECO) is submitting Technical Specifications (TS) Change Request ,
No.95-184, in accordance with 10 CFR 50.90, requesting a change to TS (i.e., Appendix A) of i operating Ucense Nos. NPF-39 and NPF-85 for Umerick Generating Station (LGS), Units 1 and 2.
J The proposed changes wbI revise LGS TS 3.6.1.8 *Drywell and Suppression Chamber Purge System," increasing the Drywell and Suppression Chamber Purge System operating time limit from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 365 days to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days.
4 A similar TS amendment was approved by the NRC on October 16,1995 for Public Service ;
Electric and Gas Company's Hope Creek Generating Station which increased the purge
. operating limit from 120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> to 500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> per 365 days. ;
i information supporting this TS Change Request is contained in Attachment 1 to this letter. The i proposed changes to the LGS, Units 1 and 2, TS pages are contained in Attachment 2. The TS change information is being submitted under affirmation, and the required affidavit is enclosed.
- We request that if approved, the TS Change be issued by June 21,1996, and become effective within 30 days of issuance. j If you have any questions, please do not hesitate to contact us.
Very truly yours,
- G. A. Hunger, ., j Director-Ucensing Enclosure, Attachments cc: T. T. Martin, Administrator, Region I, USNRC (w/ enclosure, attachments)
N. S. Perry, USNRC Senior Resident inspector, LGS (w/ enclosure, attachments)
R. R. Janati, PA Bureau of Radiation Protection (w/ enclosure, attachments)
gggb 9512290040 951222 PDR ADOCK 05000352 .
g4 P PDR l g
a COMMONWEALTH OF PENNSYLVANIA :
- ss.
COUNTY OF CHESTER :
D. B. Fetters, being first duly swom, deposes and says: That he is Vice President of PECO Energy Company, the Applicant herein; that he has read the enclosed Technical Specifications Change Request No. 95-18-0
" Increase Purge System Operational Time Umits," for Umerick Generating Station, Unit 1 and Unit 2, Facility Operating Ucense Nos. NPF-39 and NPF-85, and knows the contents thereof; and that the statements and matters set forth therein are true and correct to the best of his knowledge, information and belief.
t
,m s .
Vice President Subscribed and swom to before me thi day ofMurde1995.
[
Nota Public
'~-
N0'A.J ki sed Notary Public i Mary 1.cu SMN I Tredyttm Twp Chester C
' "y Commi Mn BP"5' M -
r' Ygnty _,
. . ~ .
ATTACHMENT 1 UMERICK GENERATING STATION UNITS 1 AND 2 Docket Nos.
50-352 50-353 Ucense Nos.
NPF-39 NPF-85
" increase Purge System Operational Time Limits' information Supporting Changes - 4 pages 1
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Page 1 of 4 DISCUSSION AND DESCRIPTION OF THE PROPOSED CHANGES PECO Energy Company (PECO Energy) is requesting Technical Specifications (TS) changes which wHI revise LGS TS 3.6.1.8 'Drywell and Suppression Chamber Purge System," increasing the Drywell and f
, Suppression Chamber Purge System operating time limit from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 365 days to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days.
The Limerick Generating Station (LGS) TS and Updated Final Safety Analysis Report (UFSAR) l commitments currently limit the operating time of the Drywell and Suppression Chamber Purge System j to 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 365 days during Operational Conditions 1,2, and 3. This operating restriction was )
placed on the use of the vent and purge valves since in the Limerick design several exceptions were ;
j taken to the Standard Review Plan 6.2.4 " Containment Isolation System" and Branch Technical Position CSB 64 " Containment Purging During Normal Plant Operations." The intent of the restriction is to i reduce the probabHity of, and minimize the consequences of, equipment damage resulting from a Loss j Of Coolant Accident (LOCA) during the time that the large purge and vent valves are open.
! This evaluation assesses revising the Drywell and Suppression Chamber Purge System operating limit
! from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 365 days to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days. During the 1995 operational year the LGS 4
units experienced planned and unplanned outages which required the use of the Drywell and Suppression Chamber Purge Systems. As an example, the Unit 1 purge system was operated a total of 85.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The added 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> wHi provide additional operational flexibility and obviate the need for a future request for enforcement discretion if similar circumstances were to occur and the current limit was reached.
j SAFETY ASSESSMENT Technical Specification 3.6.1.8 for the Drywell and Suppression Chamber Purge System limits the operation of this system to 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 365 days for Operational Conditions 1,2, and 3. This limit is 1 proposed to be changed from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days. The Bases for this Technical Specification states that this limit is imposed to protect the Integrity of the Standby Gas Treatment i System (SGTS) futers. Analysis Indicates that should a LOCA occur while this pathway is being utHlzed, the design pressure of the duct-work and the design differential pressure of the SGTS filters may be exceeded. Imposing the 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> operational limit reduces the likelihood that a LOCA wHl occur during the time that the vent and purge valves are open. Although this operation limit has been imposed, an analysis (UFSAR Section 9.4.5.1.2.2) was perforrnsd to determine the consequences of a LOCA during
. high volume purging operations. This analysis concluded that faRure of the operating SGTS filter bank is of little significance due to the limited benefit derived from SGTS for accident sequences important to plant risk and that the backup futer bank would be operable. It is noted that the Offsite Dose Calculation
. Manual (ODCM) paragraph 3.3.6 requires that both SGTS trains be operable prior to purging through the SGTS. When the purge system is in use during Operational Conditions 1,2 and 3 only one SGTS train i shall be used to prevent damage to both trains should a LOCA occur. System operating procedures for venting and purging require that the backup SGTS filter train be isolated (reference system procedures j S57.1.A 'Inerting Primary Containment", S57.5.A 'De-Inerting and Purging Primary Containment", and j S57.5.B "De-inerting and Purging the Drywell Only"), thus assuring the availability of SGTS should a i LOCA occur as postulated in the above scenario. Even if faRure of the backup SGTS train occurs (postulated single active faRure), the analysis also showed that total faRure of SGTS during a LOCA would not result in significant releases.
The operational limit was required since in the Limerick design several exceptions to Standard Review a
Plan 6.2.4 and Branch Technical Position (BTP) CSB 6-4 were taken. The high volume purge exceptions are discussed in paragraph 6.2.4.3 of the LGS Safety Evaluation Report (SER), NUREG 0991, and are as i follows:
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l Page 2 of 4 i 1) The use of the high volume purge lines, which are larger than the 8-inch line size specified in
- BTP CSB 6-4, during startup, power operation, and hot shutdown (i.e., larger lines create the potential for larger releases).
- ' 2) Contrary to BTP CSB 6 4, Position B.S.b, if a LOCA occurs whle the purge system containment isolation valves are open, it is possible that safety-related duct-work and/or the Standby Gas l Treatment System futers could be damaged by the pressure surge preceding valve closure l
and/or the moisture content of the released gases Duct faRure could result in additional equipment fagures in the reactor enclosure due to duct impact, impingement, and/or the resulting environmental conditions.
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- The consequences of a LOCA occurring whue the high volume purge system containment isolation l
valves are open have been evaluated and previously found to be acceptable by the NRC based on the
- following. The radiological consequences have been evaluated as a means of justifying the line sizes.
1 Using assumptions in BTP CSB 6-4, the resulting dose was determined to be well below 10CFR100
! guideline values (reference UFSAR Section 9.4.5.1.2.2 and SER Section 6.2.4.3). Additional analysis also concluded that falure of the SGTS is of little significance because of the limited benefit derived from the
' SGTS for beyond design basis severe accident sequences related to plant risk. It was further determined that the environmental qualification of equipment is sufficient to ensure operability under the predicted environmental conditions if duct-work does rupture, and, the potential does not exist for
' impact or impingent related damage to essential equipment from duct ruptures.
l UFSAR Section 9.4.5.1.2.2 contains the operating time limits for high volume purging. The UFSAR also
' contains the evaluated consequences of a LOCA should the vent and purge valves be open. The conclusions of the analysis are as follows:
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l 1. The containment isolation valves would close rapidly (less than 6 seconds after receipt of an 4 isolation signal) and would terminate the release. Isolation wNl be complete long before any fuel damage or significant offsite exposure would occur.
- 2. FaHure of the operating SGTS filter bank as a result of over-pressurization or moisture is of little significance since falure of SGTS during a LOCA does not contribute to any significant releases.
Additionally, the backup filter bank would be operational.
i Based on the above analysis and the subject operational limit, the NRC concluded in the SER that the
! Impact on plant risks resulting from a LOCA while purging and the potential for falure of the SGTS i
contribute little to the likelihood of an uncontrolled radioactive release. Increasing the operationallimit i for the Drywell and Suppression Chamber Purge system from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> to 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> each 365 days increases the risk to containment integrity following a design basis accident; however, this increase in
, risk was evaluated under a Level 2 Probablistic Safety Assessment (PSA) analysis and has been determined to be acceptable since it is well within the bounds of the EPRI PSA Applications Guideline for
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permanent changes. Although these changes involve an acceptable Increase in risk, they will not alter
- or impact the previous LOCA analyses.
This activity does not affect the ability of the Drywell and Suppression Chamber Purge isolation valves to l function in response to a LOCA but does increase the probabuity that these valves wHl be open during l the initiation of a LOCA. The probablity that one of the two SGTS filter trains wRl be damaged as a 3 consequence of high volume purging wHI increase as a result; therefore, the following information
- supporting a Finding of No Significant Hazards Consideration was prepared.
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- Infourh Sonnortina a Findina of No Sionificant Hm=ds Consideratinn 1
We have concluded that the proposed changes to the Umerick Generating Station, Unit 1 and Unit 2, Technical Specifications, which wul revise the drywell and suppression chamber purge system operating limit from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 366 days to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 366 days, do not involve a Significant Hazards j Consideration. In support of this determination, an evaluation of each of the three (3) standards set forth in 10 CFR 50.92 la provided below.
1, The ornanand Technical Soecificatians chanoes do not involve a sianificant increase in the j ornhahuity or conseauences of an accident oreviousiv evaluated.
These TS changes do not increase the probabulty of occurrence of an accident previously evaluated in the SAR. This activity involves changing the allowable operating limit for the Drywell and Suppression Chamber Purge System from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> each 366 days to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days. This change 4
increases the probabuity that this system will be in service should a LOCA occur, but does not increase j the probabNity that a LOCA wul occur.
Increasing the operating limit for the Drywell and Suppression Chamber Purge System from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days does not increase the consequences of a LOCA as previously evaluated in the SAR. These proposed TS changes increase the probablity of a LOCA occurring during the time the i Drywell and Suppression Chamber Purge System is in operation, and therefore, increase the probabuity
- of the fauure of the operating SGTS futer bank. However, the risk to containment integrity was previously evaluated and found to be acceptable (UFSAR Section 9.4.5.1.2.2 and WASH - 1400 " Reactor
- Safety Study").
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, Increasing the duration that the vent / purge line isolation valves may be open does not increase the
- probabuity that these valves will not perform as designed (i.e., close upon receipt of an isolation signal) in response to a LOCA. However, the changes wNI increase the likelihood that the vent and purge j valves wHl be called on to close. As discussed in UFSAR Section 6.2.4.2, the containment purge valves i have undergone extensive testing and analyses to demnnstrate the operabuity of these valvos following a LOCA.
in addition to the existing Safety Analysis Report (SAR) evaluations, a Level 2 PSA Analysis (containment failure) was performed to determine the additional risk associated with changing the operating limit from 90 to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days. The PSA evaluation conservatively assumed a 200 hour0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> vent / purge duration per a 365 day period. The figure of merit evaluated is the large early release frequency (LERF) which represents the likelihood of containment faHure following core damage that could significantly l affect the public (e.g., release of a large amount of radioactive material early enough in the accident that evacuation of the public has not occurred). The 200 hour0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> vent / purge duration increased the LERF approximately 3% from the base value of 2.57E-8 for all PSA initiators. This analysis concluded that the l increase in risk of containment falure is well within the bounds of the EPRI PSA Applications Guideline
! for permanent changes. The same relativo increase applies to the large Design Basis Accident LOCA LERF.
These changes do not directly or indirectly degrade the performance of any other safety systems (assumed to function in the accklent analysis) below their design basis. The potential for other equipment faHures in the reactor enclosure due to duct-work impact, impingement, and the resulting
. environmental conditions was evaluated. It was concluded that the environmental qualifications for the LGS equipment are sufficient to ensure operablity under the predicted environmental conditions, and there is no impact or impingement - related damage to essential equipment. Although the probabuity of
! occurrence of a malfunction of equipment important to safety is increased, the existirg SAR analysis and Level 2 PSA Analysis demonstrate the increased risk and radiological consequences are not significant.
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- 2. The orocosed TS chanaes do not create the ooanthulty of a new or different kind of accident from any accident oreviousiv evalugtg1 This activity does not change the function of the Drywell and Suppression Chamber Purge System, the containment isolation system, or SGTS as previously evaluated in the SAR. Changing the duration of operation of the vent and purge system does not create an accident initiator not considered in the SAR.
Therefore, the possibuity of an accident of a different type is not created.
This activity does not create a failure mode not considered in the SAR. All possible equipment fauures that could occur as a result of a LOCA during high volume purging have previously been identified and evaluated in the SAR. Therefore, this activity does not create the possibuity of a different type of malfunction of equipment important to safety.
Therefore, the proposed TS changes wHi not create the possibility of a new or different type of accident from any accident previously evaluated.
- 3. The orooosed TS chanaes do not involve a slanificant reduction in a marain of safety.
The Bases of Technical Specification 3.6.1.8 states that the intent of the 90 hour0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> per 365 day operating limit for the Drywell and Suppression Chamber Purge System is to protect the integrity of the SGTS filters. As discussed above, the requirements specified in ODCM paragraph 3.3.6 assure the availability of the backup SGTS futer train during operation of the vent and purge system. Furthermore, as discussed above, revising the operating limit from 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br /> to 180 hours0.00208 days <br />0.05 hours <br />2.97619e-4 weeks <br />6.849e-5 months <br /> each 365 days does not involve a significant increase in risk. The margin of safety as defined in the Bases of Technical Specification 3.6.1.8 is maintained.
Therefore, the implementation of the proposed TS changes will not involve a significant reduction In a margin of safety.
Information Suncortina an Environmental Assessment An Environmental Assessment is not required for the Technical Specifications changes proposed by this Change Request because the requested changes to the Limerick Generating Station, Unit 1 and Unit 2, TS conform to the criteria for " actions eligible for categorical exclusion,' as specified in 10CFR51.22(c)(9). The requested changes will have no impact on the environment. The proposed TS changes do not involve a Significant Hazards Consideration as discussed in the preceding safety assessment section. The proposed changes do not involve a significant change in the types or significant increase in the amounts of any effluent that may be released offsite. In addition, the proposed TS changes do not involve a significant increase in Individual or cumulative occupational radiation exposure.
Conclusion The Plant Operations Review Committee and the Nuclear Review Board have reviewed these proposed changes to the Limerick Generating Station, Unit 1 and Unit 2, Technical Specifications, and have concluded that theyfig involve an unreviewed safety question; however, they do not involve a significant hazards consideration, and wHI not endanger the health and safety of the public.
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