ML19351F092

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LER 80-085/01T-0:on 801208,HPCI Steam Supply Outside IV Operator Motor Failed.Caused by Mechanical Failure of Torque Switch Assembly.Motor Rewound & Assembly Parts Replaced
ML19351F092
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 12/17/1980
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19351F091 List:
References
LER-80-085-01T, LER-80-85-1T, NUDOCS 8012290474
Download: ML19351F092 (1)


Text

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,,,,; 9 satisfy TS 3 7.0 and other systems were verified operable as required by TS 3.5.C.2.at

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A Prompt (24-hour) Recort was made to. satisfy IE Sulletin 80-17 paragraph 6.a. No l

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3 34 33 21 40 42 42 CAUSE OESCRIPDCN AND COAAECTIVE AC*!CNs @
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Mechanical failure of the torque switch assembly caused the motor to fall. Followingl i, ,,, ;

rewind of the motor and replacement of torque switch assembly parts, valve and HPCI 1 system were restored to operable status within four (4) days. -

No additiorial action (

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