|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20028G3801983-01-27027 January 1983 Uptated LER 82-010/03X-1 on 820212,following Reactor Trip, Element Assembly 19 Discovered Stuck at 8-inch Withdrawn Position.Cause Undetermined.Control Element Assembly & Associated Bundle Inspected ML20052J0421982-05-14014 May 1982 LER 82-018/03L-0:on 820417,control Element Assembly 21 Dropped Into Core After Electricians Inadvertently Disconnected Power,Resulting in Pressurizer Level Deviation Exceeding Tech Spec Limit.Caused by Personnel Error ML20003C6001981-03-0101 March 1981 Updated LER 81-002/03L-1:on 810108 & 0227,diesel Generator 12 Started Automatically.Generator Was Stopped & Start Failure Alarm Received.Caused by Insufficient Contact Wipe by Local Break Glass Start Switch.Actuator Fitting Removed ML20003A3881981-01-27027 January 1981 LER 80-066 Has Been Cancelled ML19345B8391980-11-26026 November 1980 LER 80-050/03L-0:on 801027,wide Range ex-core Nuclear Instrument Channel B Failed.Caused by Greater than or Equal to 15-volt Dc Power Supply Having Low Supply W/Ac Ripple. Power Supply Replaced ML19323C4191980-05-13013 May 1980 LER 80-024/03L-0:on 800417,during Containment Entry ,Leak in Middle Seal Instrument Line Flexible Hose Discovered.Cause Unknown.Failed Part Is Inside Containment Bldg & Is Still Radiologically Contaminated ML19209C8601979-10-0909 October 1979 LER 79-035/03L-0:on 790922,plant Computer Failed.Caused by Printed Circuit Board Failure Which Generated Rapid Access Data Storage Disc Stop Signal.Circuit Board Replaced ML19208A8031979-09-13013 September 1979 LER 79-034/03L-0:on 790813,during Routine Surveillance Test, Control Element Assembly Deviation Exceeded 7.5 Inches Required to Initiate Assembly Motion Inhibit.Caused by Circuit Failing,W/High Conduction Affecting Other Failures ML19225C2021979-07-20020 July 1979 LER 79-023/03L-0 on 790621:diesel Tripped Repeatedly on Low Lube Oil Pressure During Test.Caused by Isolation of Engine Oil Pressure Switch Following 790620 Preventive Maint Calibr.Preventive Maint Procedure Changed ML19246A5801979-06-25025 June 1979 LER 79-019/03L-0 on 790606:discovered That Number 11 Control Room Air Conditioning Unit Breaker Had Tripped.Caused by Windings of Compressor Motor Exceeding Resistance Acceptance Criteria.Compressor Replaced 1993-07-09
[Table view] Category:RO)
MONTHYEARML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20028G3801983-01-27027 January 1983 Uptated LER 82-010/03X-1 on 820212,following Reactor Trip, Element Assembly 19 Discovered Stuck at 8-inch Withdrawn Position.Cause Undetermined.Control Element Assembly & Associated Bundle Inspected ML20052J0421982-05-14014 May 1982 LER 82-018/03L-0:on 820417,control Element Assembly 21 Dropped Into Core After Electricians Inadvertently Disconnected Power,Resulting in Pressurizer Level Deviation Exceeding Tech Spec Limit.Caused by Personnel Error ML20003C6001981-03-0101 March 1981 Updated LER 81-002/03L-1:on 810108 & 0227,diesel Generator 12 Started Automatically.Generator Was Stopped & Start Failure Alarm Received.Caused by Insufficient Contact Wipe by Local Break Glass Start Switch.Actuator Fitting Removed ML20003A3881981-01-27027 January 1981 LER 80-066 Has Been Cancelled ML19345B8391980-11-26026 November 1980 LER 80-050/03L-0:on 801027,wide Range ex-core Nuclear Instrument Channel B Failed.Caused by Greater than or Equal to 15-volt Dc Power Supply Having Low Supply W/Ac Ripple. Power Supply Replaced ML19323C4191980-05-13013 May 1980 LER 80-024/03L-0:on 800417,during Containment Entry ,Leak in Middle Seal Instrument Line Flexible Hose Discovered.Cause Unknown.Failed Part Is Inside Containment Bldg & Is Still Radiologically Contaminated ML19209C8601979-10-0909 October 1979 LER 79-035/03L-0:on 790922,plant Computer Failed.Caused by Printed Circuit Board Failure Which Generated Rapid Access Data Storage Disc Stop Signal.Circuit Board Replaced ML19208A8031979-09-13013 September 1979 LER 79-034/03L-0:on 790813,during Routine Surveillance Test, Control Element Assembly Deviation Exceeded 7.5 Inches Required to Initiate Assembly Motion Inhibit.Caused by Circuit Failing,W/High Conduction Affecting Other Failures ML19225C2021979-07-20020 July 1979 LER 79-023/03L-0 on 790621:diesel Tripped Repeatedly on Low Lube Oil Pressure During Test.Caused by Isolation of Engine Oil Pressure Switch Following 790620 Preventive Maint Calibr.Preventive Maint Procedure Changed ML19246A5801979-06-25025 June 1979 LER 79-019/03L-0 on 790606:discovered That Number 11 Control Room Air Conditioning Unit Breaker Had Tripped.Caused by Windings of Compressor Motor Exceeding Resistance Acceptance Criteria.Compressor Replaced 1993-07-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000317/LER-1999-006, :on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With1999-10-22022 October 1999
- on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With
ML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With 05000317/LER-1998-011, :on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With1999-09-20020 September 1999
- on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With
ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20211J3531999-09-0101 September 1999 Safety Evaluation Supporting Amends 231 & 207 to Licenses DPR-53 & DPR-69,respectively ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-005, :on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With1999-08-23023 August 1999
- on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With
05000317/LER-1999-004, :on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With1999-08-23023 August 1999
- on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With
ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-003, :on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With1999-07-30030 July 1999
- on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With
ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-039, Part 21 Rept Re Defect of ABB 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of ABB 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified LD-99-035, Part 21 Rept Re ABB 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re ABB 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-002, :on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With1999-05-25025 May 1999
- on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With
ML20206U7031999-05-18018 May 1999 Rev 1 to Ran 97-031, Main CR Fire Analysis for IPEEE Section 4-1 ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on ABB CE ECCS Performance Evaluation Models ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20205J8331999-04-0707 April 1999 Safety Evaluation Concluding That Security Lighting,Portable Lighting & Helmet Lights,As Described by Licensee Satisfies Underlying Purpose of 10CFR50,App R,Section Iii.J.Grants Licensee Request for Exemption ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20204B5961999-03-17017 March 1999 Corrected Page 7 to SER for Amend 205 for License DPR-69. Staff Deleted Word Not on Line One of Page 7 ML20207L2991999-03-0808 March 1999 Safety Evaluation Supporting Amend 205 to License DPR-69 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons 05000317/LER-1997-010, :on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With1999-01-29029 January 1999
- on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With
ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed 05000317/LER-1998-009, :on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With1999-01-0808 January 1999
- on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With
ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20196J6771998-12-0808 December 1998 Safety Evaluation Supporting Amends 229 & 204 to FOLs DPR-53 & DPR-69,respectively ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative 05000317/LER-1998-008, :on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With1998-11-11011 November 1998
- on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With
ML20195D4271998-11-0505 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-69 ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With 1999-09-30
[Table view] |
Text
{{#Wiki_filter:r. .. . -3
# .1, .
~
s B AL.TIMORE .
GAS AND-ELECTRIC
{ i f7 CHARLES CENTER e P.O. BOX 1475 e BALTIMORE, MARYLAND 21203 1475
[. :'
CALVERT. Cliff 8 NUCLEAR POWER PLANT DEPARTilENT CALVERT CLFFS NUCLEAR POWER PLANT ,
LUSS7. MARYAND 30657 .t G March 6, 1990 i
'U. S. Nuclear Regulatory Commission Docket;No. 50 318 ,
Document Control Desk License No. DPR 69
~ Washington, D. C. 20555-
Dear Sirs:
The attached LER 89-12, Revision 1,'is being sent to you as required under 10 ij- .CFR 50.73 guidelines. This LER~was erroneously issed as LER 89-22, Revision O.
Also, please note that Unit 1 LER numbers 89 21 and 89-22 (Doc. No. 50-317) were not used.
4 Should you have any questions regarding' this report, we would be pleased to discuss them with you.
EVery truly yours, f
~
% ^
f R. I. Denton- ,
j Manager CDS/1r I
'ec: William T. Russell Director, Office of Management Information and Program Control Messrs: G. C. Creel C. H. Cruse R. P. Heibel J. R. Lemons L. B. Russell
{{
0 M
n h I
9003140377 9'00306 g
.PDR ADOCK 05000318
+-
g
- s PDC- _
E' e' NRCF5,Jatt U.S. NUCLEl% LEiULiTORY COMMIS8 SON LPPROVED OMS NO 2190 1104 3
LICENSEE EVENT REPORT (LER) '""'88'*
F ActLITY hAME 114 DOCEE T NUh00ER (21 PAGE (3)
Calvert Cliffs, Unit 2 o l5 j o lo lol31; 8 i jopj g Core Alterations Performed With Only One of Two Containment Vent Valves cl o s'e d . Violating Technical Soccifications E VENT DATE
- LE R NUhetE R 181 REPORT DATE (7) OTHER F ACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR "g$ 'L n E*[w*e"j MONTH DAY YEAR #acsLity Naves DOCEE Y NUM0E Rist Cnivert Cliffs. Unit 1 o l5 ] o j o l 0 l3 l 3 l 7
~ ~
1l 2 2l7 89 8l 9 d1l2 0l1 0l3 0 l6 9l0 0 1 5l0l0:0 i I l TH18 REPORT 18 $UDMITTED PURSUANT TO THE flkOUIREMENTS OF 10 CFR $. (Cnece one e, mese e, the ,odrowmpf H1)
OPE R ATING h40DE (S) $ M 402(bl 90 73WGHet 73h bl.
M 406M 20 406tell1Hil 80.38tsH11 80.72ielGilvi 73.7 het j H01 0l O0 i 20 40si.HiHiin so.3 i.H2i
.0.73i.n2Hvhi
_ gHEgg,,, 4.;,,.c,4 20 406teH1 Held X SOMielGHQ 60MWH2HvmHA) M A) 20 406Lmit1Hm! 50.73teH2Het to.734eH2HvihH81 to 40steH1Hol no.734sH2ils4H 50.73telt2Hal LICENSEE CONT ACT FOR THIS LER H2)
NAME TE LEPHONE NUMBER -
AHE A CODE C. D. Sly - Licensing Engineer 3 l 011 216l0 l -l 4 l81518 COMPLETE ONE LINE FOR E ACH COMPONENT F ALLURE DESCRISED IN TH18 REPORT (131 CAUSE SYSTEM COMPONENT MQ C.
HEPOR,TAgE . \l CAUSE system COMPONENT f "8 TO NPR E
l l l l l l l' l l l l l l l l 1 I I I I I l l l l 1 1 1 SUPPLEMENT AL flE*CRT E MPECTED (14l MONTH DAY VEAR SUOM15$10N J VE& (If , e. compiere fM9ECTIO SusseissION DA Til No l l l A. T R ACT u ,,~, M ,,oo . . . ,.. . ., ,,n ,, ,y. .<, ,,,..,,u. , . , H . ,
ABSTRACT On December 27, 1989, at 1415 hours, a Technical Specification (TS) violation was discovered to have existed at Calvert Cliffs Unit 2. The violation was the result of performing core alterations and/or movement of irradiated fuel within containment ,
without assuring that both containment vent isolation valves were closed in accordance I with TS 3/4.9.14.
The immediate cause of the event was a procedural deficiency. One of the containment vont valves was erroneously deleted from the STP which satisfied TS 4.9.14. The root cause was an error in a review to assure that the STP satisfied the TS limiting conditions for containment penetrations during core alternations or movement of irradiated fuel wititin containment. The error resulted from a failure to recognize that a double valve isolation is required for the containment vent penetration in MODE
- 6. The error resulted in the deletion of one of the redundant valves from the MODE 6 STP to verify containment integrity.
4 The STP's for both units were revised to include the deleted valves. The valves will be flagged referencing the Basis section of the Technical Specifications. The Surveil-lance Test Program instruction has been revised to reduce occurrence of such events.
l*f,c'a=
y *
.s ..
uciuses aveur nanont <teni rixr couriuuari:n 7 .',0.7, r , r P
- -- m .......
-+ ... . .
Calvert Clif fs, l' nit 2 ,
via= ' imp : - "';*g 818181818 l3 l tl 8 m_..,__ 81 9. -. 011l 2 -
oli ol2 or o l6
'I. DESCRIPTION OF EVENTS On December 27, 1989, at 1415 hours, a Technical Specification (TS) violation was discovered to have had existed at Calvert Cliffs Unit-2. The violation was the result of performing core alterations and/or movement of irradiated fuel within containment without assuring that both containment vent isolation valves ,
were closed in accordance with TS 3/4.9.14. The event was discovered during a-concentrated effort to identify discrepancies between TS's and associated Surveillance Test Procedures (STP's). At the time the event was discovered.
Unit-1 was in cold shutdown with the reactor coolant system at 105 F and 10 psig and Unit 2 was defueled.
Calvert Cliffs TS 3,9,14 requires that during core alterations or movement of r irradiated fuel within the containment, the containment vent - isolation valves shall be closed. There are two containment vent isolation valves, MOV-6900, (inside containment) and MOV-6901 (outside containment). TS 4.9.14 requires that the containment vent isolation valves be determined to be closed within 72 hours prior to the start of, and at least once per 7 days during, core alterations or movement of irradiated fuel within the containment.
Surveillance Test Procedures 0-55A 1 and -2 are titled, " Containment Integrity Verification (Mode 6)". These procedures were originally created to satisfy the requirements of TS 3/4.9.4, " Refueling Operations, Containment Penetrations".
TS 3.9.4 requires that during core alterations or movement of irradiated fuel i- within the containment that each penetration providing direct access from l
containment to outside shall be either;
- 1. Closed by an isolation valve, blind flange, or manual valve, or
- 2. Be capable of being closed by an operable automatic containment purge valve.
TS 4,9,4 requires verification of the above within 72 hours prior to the start o f ,- and at least once per 7 days during, core alterations or movement of irradiated fuel inside containment, 1
( Due to the similarity between TS 3/4.9.4 and 3/4,9.14 and their surveillance requirements, they are both included in STP 0-55A-1 and 2.~ The major difference between the two is that TS 3/4.9.14 requires a double isolation of the containment vent containment penetration during refueling operations while TS 3/4,9,4 requires only a single isolation of all other containment penetrations.
l TS 3/4.9,4 is part of the original Calvert Cliffs Technical Specifications. TS 3/4.9,14 was added to Unit-1 and -2 TS's as part of amendment 88 and 75, respectively. These TS amendments became effective on November 17, 1983 and June 6, 1984 for Units 1 and 2, respectively. Both Units had appropriate changes made to STP 0-55A to include both MOV 6900 and 6901.
l' i ;.g .c m ... ,
UCENSEE EVENT REPORT (LER) TEXT CONTINUATION .o oo
. - o,
- . ~ . ... . .
Calvert Clif f s, Unit '2
"'1*a m,, ,
0 [5 l0 l0 l0 l3 l 118 8l 9 -
o l 1l 2 -
0l1 o l, joF nlg During the first quarter of 1987, a review of all penetrations that could provide a direct flow path from inside to outside containment was conducted. The intent of this review was to provide increased confidence that a direct path could not be inadvertently created through a penetration that could be overlooked during core alterations. A - set of acceptance criteria was established. One of these acceptance criteria was to identify all penetrations that could provide a direct flow path from inside to outside containment and assure that all such penetrationo were isolated by at least one valve, blank flange, or other approved barrier.
The penetration review determined that penetration 48A, the containment vent outlet, provided a direct path to the plant vent system (outside containment).
It was therefore concluded that the MOV-6900 should be maintained shut. It was ,
not recognized that TS 3/4,9,14 required both MOV 6900 and 6901 to be maintained closed in MODE 6. STP 0 55A 2 was revised to reflect the findings, of the review. STP 0-55A-2, revision 11, dated April 10, 1987 deleted Unit-2 ,
MOV-6901 based on the above noted review and STP 0 55A-1, revision 13, dated March 1, 1989 deleted Unit-1 MOV-6901.
After the deletion of MOV-6901 from STP 0 55A-1 and -2, each STP was performed several times. STP 0 55A 1 was performed twice, but not for core alteration purposes. Thus, no violation of TS 3/4.9.14 actually occurred for Unit-1. STP 0-55A-2 on the other hand, was performed several times for the purposes of allowing core alterations during Unit-2 outages between March and July 1987 and between March 1989 and present. Thus, several violations of Unit-2 TS 3/4.9.14 did actually occur.
II. CAUSE OF EVENT The cause of this event was procedural deficiency. The procedures, STP 0-55A 1 and 2, did not contain both containmont vent isolation valves MOV-6900 and 6901.
The root cause of the event was an error in the previously discussed 1987 review of penetrations that could provide a direct path from inside to outside
- containment. The review was done to assure that the single isolation conditions of TS 3/4.9.4 were satisfied for all containment penetrations, but did not I recognize the required double isolation of the containment vent isolation valves.
l This led to the deletion of the redundant containment isolation vent valve MOV-6901 from STP 0-55A-2 on April 10, 1987 and from STP 0-55A-1 on March 1, 1989.
l I
l l
l l
l l
;.g.m m. .
Nag pyan m
. **". W 8. seVCLt'2 f.40WL*.70A 7 Consasimi0se UCENSEE EVENT REPORT (LER) TEXT CCNTINUATl3N maovio e o me.o.
nmes sse P4SILify es4AW 06 DOCEST NunSSA m tem e,Waie0A tes pageg3 Calvert Cliffs, Unit 2 *
" D M a" O'Oi! +
m__,, 818 l' l 0 l 813 l 118 81 9 -
011l 2 -
Oli ol 4 0F 016 III. ANALYSIS OF EVENT ,
The event is considered reportable under 10 CFR 50.73(a)(2)(1)(B) because core alterations were performed for Unit 2 during outages in 1987 and 1989 without verifying that both containment vent isolation valves were closed in accordance with TS 3/4.9.14. There was no such violation of the TS for Unit-1 because no core alterations or movement of irradiated fuel were performed during the period that MOV-6901 was removed from STP 0 55A 1.
TS 3/4.9.14 was added to Unit 1 and -2 TS's by amendments 88 and 75, respectively. The valves were formally designated as hydrogen purge outlet valves. The TS amendments proposed that the hydrogen purge outlet valves be ;
re-designated as containment vent isolation valves, and be required to close automatically in less than 20 seconds as verified by periodic testing.
In Modes 5 and 6, the TS amendment proposed the addition of the TS 3.9.14.
This new TS required both containment vent isolation valves remain closed during core alternations or movement of irradiated fuel within containment. The basis for this requirement is that the closure restrictions on these valves are sufficient to restrict radioactive material release from a fuel element rupture based upon the lack of - containment pressurization potential while in the refueling mode.
TS 3.9.4 addresses the required status of all other containment penetrations in modes 5 and 6. The TS requires a single isolation of all applicable containment penetrations by an isolation valve, blind flange, or manual valve.
The basis for this requirement is that the closure restrictions are sufficient to restrict radioactive material release from a fuel element rupture based upon the lack of containment pressurization potential while in the refueling mode.
l' It is concluded that no adverse safety consequences resulted from this event. At all times during core alterations and movements of irradiated fuel within containment the TS surveillance requirement was satisfied for MOV 6900. Thus, single isolation of this particular containment penetration was maintained. The single closed isolation valve would have effectively prevented the release of l radioactive material from a fuel element rupture in the refueling mode. Why TS 3/4.9.14 requires double isolation of a containment penetration and TS 3/4.9.4 requires only single isolation of similar penetrations is unknown.
The total duration of MOV-6901 being deleted from STP 0-55A-2 was from April 10, j 1987 to November 2, 1989, a total of two and one-half years. There were no components or systems which were inoperable and/or out of service which contributed to this event. No plant systems or component failures resulted from
'this event.
I zapaw a.. !
c
5 gg pg,g, g
**- , U8,HuCL&it $_atutat0AY C0hses ea0s,
' ~
UCENSEE EVENT REPORT (LER) TEXT CONTINUATION <*ncvio o= o se-cio.
an,nesssue unsurv name m ****"""'****
Lea muusen ie eau m CaIvert Cliffs, Unit 2- " "D'Ea"
'l'%'O' .
vert,, . . . , _ % , O I' l' l' l 813 l 1l 8 8 l 9 -
0l1l2 -
0l1 0l5 0F 0 l6 IV, CORRECTIVE ACTIONS
- 1. ' Effective November 2, 1989, STP 0-55A-1 and 2 were revised to include MOV-6901.
- 2. MOV 6900 and 6901 will be flagged in STP O-55A-1 and 2 referencing it to the Basis section of-the Technical Specifications.
- 3. The Surveillance Test . Program instruction has been revised to reduce occurrence of events such as the deletion of MOV-6901 from 0-55A-1.and 2.
Changes include the addition of Functional Surveillance Test Coordinators (FSTCs) who are responsible for coordinating the preparation of STPs and revisions to STPs. The FSTCs provide focused, discipline-specific control of surveillance test content, review and scheduling.
V. ADDITIONAL INFORMATION There have been several previous reportable events caused by inadequate, incomplete , - or lack of procedures at Calvert Cliffs. However, no previous similar reportable events have occurred at Calvert Cliffs involving inadvertent deletion of TS requirements from STP's, j Identification of Components Referred to in this LER I Component IEEE803 IEEE805 EIIS Funct. System ID l
l (1) MOV-6900 VTV BB 1
(1) 2-MOV-6901 VTV BB 1
F l
;.g. .. u... .
L
v '-_._
s, *'
p{ . TABLE 1-
.g .g a:
- .f
~
fg ' j HISTORY OF IMPLEMENTATION OF TS 3/4. 9.14 VIA STP 0-55A-1 AND 2.
.l
-g I i l
j.
5 REEVEL STP 0-55A- 'l 3
'N 3 1- 3/4.9.14 STP 0-55A 'FIRST REFUEL MOV-6901'- OUTAGE CHANGE TO -
' UNIT TS AMEND REVISION- OUTAGE AFTER' DELETIO AFTER RETURN Z NO' DATE/NO -DATE/REV. AMENDMENT DATE/REV. DELETION MOV-6900 '"
O
- I -
i 1. 88 -4/23/84 10/9/83 Rev. 13 11/2/89 .p o to NONE . Change No. $ g 11/17/83 Rev. 10 12/9/83 3/1/89 0-89-168 [. ". 'e-g-
-! E 9 '
m
- 2. 75 4/23/84 4/21/84 Rev. 1 3/14/87 11/2/89 (
to to Change No. 3-6/6/84 --Rev. 9 7/1/84 4/10/87 7/2/87 0-89-168 ."-
3 3/18/89.. , 5~
~
to i eresent 4 jL.
I i
3 o o
2 1 "$ -
a E C -
m , p.
~
A b 6 l e.-
o *
,g CC 2 !!
c 5
= c e
E 't o E!
~ s. .- h.
II E5 i o 65 5 7o .8 3
. ~E
'o I s-;
E k ^
- o .. = ,l s .g l, - A + > ~ ,
- , ,~I,. y
< en -t r- , , t . . , , l.-n.,w+ -- , ee ,-w. -er, ,a ,n, a n . .e w ,s -.}}