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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3271994-10-0303 October 1994 LER 94-020-00:on 940901,discovered That Elapsed Time Meters Installed in Essential CR HVAC & SGTS Due to Defective Procedures at Time of Installation.Crefs & SGTS Declared inoperable.W/941003 Ltr ML20029E5871994-05-13013 May 1994 LER 94-007-00:on 940413,HPCI Sys Declared Inoperable.Caused by Lack of Sufficient Restraint on Tubing.Corrective Action: Tubing Placed Back on Fitting & Clamp Was Retensioned.W/ 940513 Ltr ML20029C7211994-04-22022 April 1994 LER 92-020-00:on 920130,containment Level Instruments Were Removed & re-installed Without Being Declared Inoperable. Caused by Personnel Failure to Follow Procedures.Operators retrained.W/940422 Ltr ML20046B4881993-07-30030 July 1993 LER 93-028-00:on 930630,two Potentially Valves Were Inoperable Due to Inadequate Design of Valve Operators by Manufacturer.Modified Valve operators.W/930730 Ltr ML20046A3001993-07-21021 July 1993 LER 93-010-01:on 930331 & 0621,RPS Bus B Deenergized Due to Defective Under Frequency (Uf) Trip Unit Resulting in Unplanned Actuations of Several Esfs.Action Initiated to Permanently Remove Uf feature.W/930721 Ltr ML20045H6011993-07-13013 July 1993 LER 93-025-00:on 930618,determined That Hydrogen/Oxygen Monitoring Sys May Not Effectively Perform post-accident Monitoring Functions.Caused by Insufficient Slope in Lines.Filters Removed & Pump Internals Upgraded ML20045H6051993-07-13013 July 1993 LER 93-026-00:on 930618,discovered That Hydrostatic Tests of Essential Portions of Svc Water & Reactor Equipment Cooling Sys Not Performed Once Per 10 Year ISI Interval. Inclusion of Essential Sys Portion Being Reevaluated ML20045H6071993-07-13013 July 1993 LER 93-027-00:on 930308,standby Gas Treatment Sys Unable to Establish & Maintain Reactor Bldg Pressure + or - 0.25 Inches Water Gauge Under Calm Wind Conditions.Evaluation of Secondary Containment Operability in Progress ML20045E9861993-06-28028 June 1993 LER 93-023-00:on 930528,fuel Assemblies Loaded Into Reactor Core Without Control Rods Fully Inserted,In Violation of TS 3.10.A.2.Caused by Need to Reposition Fuel Support Piece. Training Will Be revised.W/930628 Ltr ML20045E6561993-06-28028 June 1993 LER 93-024-00:on 930527,discovered That Testing of Four Reactor Vessel Low Water Level RPS Sensors Not Completed as Scheduled.Caused by Personnel Error.Stroke Testing Suspended & Surveillance Testing completed.W/930628 Ltr ML20045B4701993-06-11011 June 1993 LER 93-021-00:on 930611,determined That RB Ventilation Exhaust Inboard Isolation Valve HV-AOV-261AV Inoperable & Open Due to Personnel Error.Subj Valve Manually Closed. Proposed Change to TS Will Be submitted.W/930611 Ltr ML20045A5431993-06-0505 June 1993 LER 93-020-00:on 930507,determined That H2/O2 Sys Not Leak Tested to Verify Primary Containment Integrity During Testing of Sys.Caused by Failure to Have Administrative Controls in Place.Pressure Testing conducted.W/930605 Ltr ML20045A4331993-06-0101 June 1993 LER 93-SO1-00:on 930429,discoverd That Individual Had Tested Positive for Drugs at Another Facility on 930226.Employer Had Not Previously Been Notified.Approved Contractor Access Authorization Program suspended.W/930601 Ltr ML20045A4611993-06-0101 June 1993 LER 93-019-00:on 930501,nonconservative Testing Methodology Discovered During LLRT Due to Nonconservative Interpretation of Info Supplied by Valve Mfg.Testing Conducted for Valves Not Previously tested.W/930601 Ltr ML20044G8011993-05-28028 May 1993 LER 93-017-00:on 930428,discovered That Hourly Fire Watch Patrol for RB Per TS Had Not Been Performed.Caused by Personnel Error.Review of Fire Watch Patrol Implementation Process Will Be conducted.W/930528 Ltr ML20044E6301993-05-20020 May 1993 LER 93-015-00:on 930420,design Discrepancy in HPCI Sys Identified.Caused by Design Deficiency in Original Design. Mods Will Be Made to Startup from Current Refueling Outage to Correct Design discrepancy.W/930520 Ltr ML20044D8211993-05-17017 May 1993 LER 93-014-00:on 930316,small through-wall Leak Developed on High Pressure Side of SW Throttle Valve.Caused by Inadequate Valve Design.Frequency of Visual Insp of Valve Internals Will Be Increased to Once Per cycle.W/930517 Ltr ML20044D6511993-05-15015 May 1993 LER 93-013-00:on 930415,determined That as-found Setpoint for Seven SRVs Not within TS Limit.Caused by Lift Setpoint Discrepancies of Srvs.Review of Setpoint Data Will Be performed.W/930515 Ltr ML20044D5341993-05-14014 May 1993 LER 93-012-00:on 930414,violation of Primary Containment Integrity Occurred.Caused by Personnel Error.Procedure Change Being Made to Eliminate Test Return Line Venting When Primary Containment Integrity required.W/930514 Ltr ML20044D2041993-05-12012 May 1993 LER 93-011-00:on 930308,max Differential Pressure Between Reactor Bldg & External Environ of -0.22-inches Water Gauge Exceeded TS Required Min.Caused by Lack of Loop Seal on Rupture Seal Drain Line.Seals replaced.W/930512 Ltr ML20024G7421991-04-23023 April 1991 LER 91-002-00:on 910324,RWCU Occurred Due to High Sys Temp During Plant Cooldown.Caused by Failed Temp Indication & Potential Equipment Failure.Failed Thermocouple & Temp Switch Replaced & calibr.W/910423 Ltr ML20043D2311990-05-30030 May 1990 LER 90-005-00:on 900430,reactor Protection Sys B Motor Generator Set Output Breaker Tripped.Caused by Equipment Malfunction & Preventive Maint Program Deficiency.Sys Restored to Pretrip Operational state.W/900530 Ltr ML20042G9411990-05-10010 May 1990 LER 90-004-00:on 900413,ESF Group Isolations & Diesel Generator Starts Occurred Due to Equipment Malfunction & Personnel Error.Equipment Repaired,Manual Disconnect Operating Location Labeled & Personnel trained.W/900510 Ltr ML20011F1321990-02-23023 February 1990 LER 90-001-00:on 900124,outboard Steam Supply Line Isolation Valve Unexpectedly Closed During Surveillance Testing,Causing Isolation of HPCI Sys.Caused by Procedural Inadequacy.Test Procedure Will Be upgraded.W/900223 Ltr ML20005E3331989-12-26026 December 1989 LER 89-026-00:on 891125,reactor Scram Occurred Due to Closure of Outboard Msivs.Caused by post-filter Media Ignition by Hot Air or Particles from Dryer.Air Dryer B Disassembled & inspected.W/891226 Ltr ML19332F1191989-12-0707 December 1989 LER 88-016-02:on 880517,pipe Stress Analyses Revealed That Resultant Stresses for Five Piping Segments/Components Exceed Plant Design Basis.Caused by Support Design Problems. Long-term Corrective Program implemented.W/891207 Ltr ML19325E2201989-10-27027 October 1989 LER 89-025-00:on 890928,main Turbine Trip Occurred,Followed Immediately by Reactor Scram.Caused by Spurious Actuation of Level Switch Due to Equipment Vibration.Plant Stabilized & Temporary Instruction Re Pump Shifting issued.W/891027 Ltr ML20024C3571983-06-28028 June 1983 LER 83-008/03L-0:on 830530,HFA Relay 9-17-16A K6B Contacts Failed to Open.Cause Not Determined.Relay Coil Replaced. Systematic Replacement of All Relays within 4-yr Period planned.w/830628 Ltr ML20028F0921983-01-20020 January 1983 LER 82-025/03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified ML20028F0781983-01-20020 January 1983 LER 82-024/03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced ML20028B4671982-11-22022 November 1982 LER 82-022/03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified ML20028B4661982-11-19019 November 1982 LER 82-021/03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement ML20052G5321982-05-0606 May 1982 LER 82-008/03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair ML20052B4041982-04-22022 April 1982 LER 82-007/03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modified ML20052A3561982-04-21021 April 1982 LER 82-006/03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established ML20050B2101982-03-19019 March 1982 LER 82-005/03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position ML20041F8271982-03-0505 March 1982 LER 82-004/03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised ML20041C4151982-02-18018 February 1982 LER 81-003/03L-1:on 810223,valve RHR-MO-26B Motor Current Increased & Remained High When Valve Reached Closed Position.Valve Motor Breaker Manually Tripped & Valve Declared Inoperable.Caused by Failure of Brake Coil ML20041C3881982-02-17017 February 1982 LER 82-003/03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily ML20041C3741982-02-17017 February 1982 LER 82-002/03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced ML20041C3871982-02-17017 February 1982 LER 82-001/03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed ML20040D3491982-01-20020 January 1982 LER 81-026/03L-0:on 811223,switches NBI-LIS-01A & NBI-LIS- 101B Found Set at Level Lower That Tech Spec Limits.Caused by Setpoint Drift.Switches Returned to Correct Setpoints. Instrument Drift to Be Closely Monitored ML20040D9261982-01-0505 January 1982 LER 81-025/04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded ML20038C5321981-12-0303 December 1981 LER 81-024/03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced ML20010G0961981-08-25025 August 1981 LER 81-020/03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule ML20010F9881981-08-25025 August 1981 LER 81-019/03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced ML20010G2661981-08-25025 August 1981 LER 81-021/03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced ML20010A1391981-07-22022 July 1981 LER 81-018/03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset ML20010A1671981-07-13013 July 1981 LER 81-017/03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed ML20010A5391981-07-0909 July 1981 LER 81-016/03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient 1994-05-13
[Table view] Category:RO)
MONTHYEARML20024J3271994-10-0303 October 1994 LER 94-020-00:on 940901,discovered That Elapsed Time Meters Installed in Essential CR HVAC & SGTS Due to Defective Procedures at Time of Installation.Crefs & SGTS Declared inoperable.W/941003 Ltr ML20029E5871994-05-13013 May 1994 LER 94-007-00:on 940413,HPCI Sys Declared Inoperable.Caused by Lack of Sufficient Restraint on Tubing.Corrective Action: Tubing Placed Back on Fitting & Clamp Was Retensioned.W/ 940513 Ltr ML20029C7211994-04-22022 April 1994 LER 92-020-00:on 920130,containment Level Instruments Were Removed & re-installed Without Being Declared Inoperable. Caused by Personnel Failure to Follow Procedures.Operators retrained.W/940422 Ltr ML20046B4881993-07-30030 July 1993 LER 93-028-00:on 930630,two Potentially Valves Were Inoperable Due to Inadequate Design of Valve Operators by Manufacturer.Modified Valve operators.W/930730 Ltr ML20046A3001993-07-21021 July 1993 LER 93-010-01:on 930331 & 0621,RPS Bus B Deenergized Due to Defective Under Frequency (Uf) Trip Unit Resulting in Unplanned Actuations of Several Esfs.Action Initiated to Permanently Remove Uf feature.W/930721 Ltr ML20045H6011993-07-13013 July 1993 LER 93-025-00:on 930618,determined That Hydrogen/Oxygen Monitoring Sys May Not Effectively Perform post-accident Monitoring Functions.Caused by Insufficient Slope in Lines.Filters Removed & Pump Internals Upgraded ML20045H6051993-07-13013 July 1993 LER 93-026-00:on 930618,discovered That Hydrostatic Tests of Essential Portions of Svc Water & Reactor Equipment Cooling Sys Not Performed Once Per 10 Year ISI Interval. Inclusion of Essential Sys Portion Being Reevaluated ML20045H6071993-07-13013 July 1993 LER 93-027-00:on 930308,standby Gas Treatment Sys Unable to Establish & Maintain Reactor Bldg Pressure + or - 0.25 Inches Water Gauge Under Calm Wind Conditions.Evaluation of Secondary Containment Operability in Progress ML20045E9861993-06-28028 June 1993 LER 93-023-00:on 930528,fuel Assemblies Loaded Into Reactor Core Without Control Rods Fully Inserted,In Violation of TS 3.10.A.2.Caused by Need to Reposition Fuel Support Piece. Training Will Be revised.W/930628 Ltr ML20045E6561993-06-28028 June 1993 LER 93-024-00:on 930527,discovered That Testing of Four Reactor Vessel Low Water Level RPS Sensors Not Completed as Scheduled.Caused by Personnel Error.Stroke Testing Suspended & Surveillance Testing completed.W/930628 Ltr ML20045B4701993-06-11011 June 1993 LER 93-021-00:on 930611,determined That RB Ventilation Exhaust Inboard Isolation Valve HV-AOV-261AV Inoperable & Open Due to Personnel Error.Subj Valve Manually Closed. Proposed Change to TS Will Be submitted.W/930611 Ltr ML20045A5431993-06-0505 June 1993 LER 93-020-00:on 930507,determined That H2/O2 Sys Not Leak Tested to Verify Primary Containment Integrity During Testing of Sys.Caused by Failure to Have Administrative Controls in Place.Pressure Testing conducted.W/930605 Ltr ML20045A4331993-06-0101 June 1993 LER 93-SO1-00:on 930429,discoverd That Individual Had Tested Positive for Drugs at Another Facility on 930226.Employer Had Not Previously Been Notified.Approved Contractor Access Authorization Program suspended.W/930601 Ltr ML20045A4611993-06-0101 June 1993 LER 93-019-00:on 930501,nonconservative Testing Methodology Discovered During LLRT Due to Nonconservative Interpretation of Info Supplied by Valve Mfg.Testing Conducted for Valves Not Previously tested.W/930601 Ltr ML20044G8011993-05-28028 May 1993 LER 93-017-00:on 930428,discovered That Hourly Fire Watch Patrol for RB Per TS Had Not Been Performed.Caused by Personnel Error.Review of Fire Watch Patrol Implementation Process Will Be conducted.W/930528 Ltr ML20044E6301993-05-20020 May 1993 LER 93-015-00:on 930420,design Discrepancy in HPCI Sys Identified.Caused by Design Deficiency in Original Design. Mods Will Be Made to Startup from Current Refueling Outage to Correct Design discrepancy.W/930520 Ltr ML20044D8211993-05-17017 May 1993 LER 93-014-00:on 930316,small through-wall Leak Developed on High Pressure Side of SW Throttle Valve.Caused by Inadequate Valve Design.Frequency of Visual Insp of Valve Internals Will Be Increased to Once Per cycle.W/930517 Ltr ML20044D6511993-05-15015 May 1993 LER 93-013-00:on 930415,determined That as-found Setpoint for Seven SRVs Not within TS Limit.Caused by Lift Setpoint Discrepancies of Srvs.Review of Setpoint Data Will Be performed.W/930515 Ltr ML20044D5341993-05-14014 May 1993 LER 93-012-00:on 930414,violation of Primary Containment Integrity Occurred.Caused by Personnel Error.Procedure Change Being Made to Eliminate Test Return Line Venting When Primary Containment Integrity required.W/930514 Ltr ML20044D2041993-05-12012 May 1993 LER 93-011-00:on 930308,max Differential Pressure Between Reactor Bldg & External Environ of -0.22-inches Water Gauge Exceeded TS Required Min.Caused by Lack of Loop Seal on Rupture Seal Drain Line.Seals replaced.W/930512 Ltr ML20024G7421991-04-23023 April 1991 LER 91-002-00:on 910324,RWCU Occurred Due to High Sys Temp During Plant Cooldown.Caused by Failed Temp Indication & Potential Equipment Failure.Failed Thermocouple & Temp Switch Replaced & calibr.W/910423 Ltr ML20043D2311990-05-30030 May 1990 LER 90-005-00:on 900430,reactor Protection Sys B Motor Generator Set Output Breaker Tripped.Caused by Equipment Malfunction & Preventive Maint Program Deficiency.Sys Restored to Pretrip Operational state.W/900530 Ltr ML20042G9411990-05-10010 May 1990 LER 90-004-00:on 900413,ESF Group Isolations & Diesel Generator Starts Occurred Due to Equipment Malfunction & Personnel Error.Equipment Repaired,Manual Disconnect Operating Location Labeled & Personnel trained.W/900510 Ltr ML20011F1321990-02-23023 February 1990 LER 90-001-00:on 900124,outboard Steam Supply Line Isolation Valve Unexpectedly Closed During Surveillance Testing,Causing Isolation of HPCI Sys.Caused by Procedural Inadequacy.Test Procedure Will Be upgraded.W/900223 Ltr ML20005E3331989-12-26026 December 1989 LER 89-026-00:on 891125,reactor Scram Occurred Due to Closure of Outboard Msivs.Caused by post-filter Media Ignition by Hot Air or Particles from Dryer.Air Dryer B Disassembled & inspected.W/891226 Ltr ML19332F1191989-12-0707 December 1989 LER 88-016-02:on 880517,pipe Stress Analyses Revealed That Resultant Stresses for Five Piping Segments/Components Exceed Plant Design Basis.Caused by Support Design Problems. Long-term Corrective Program implemented.W/891207 Ltr ML19325E2201989-10-27027 October 1989 LER 89-025-00:on 890928,main Turbine Trip Occurred,Followed Immediately by Reactor Scram.Caused by Spurious Actuation of Level Switch Due to Equipment Vibration.Plant Stabilized & Temporary Instruction Re Pump Shifting issued.W/891027 Ltr ML20024C3571983-06-28028 June 1983 LER 83-008/03L-0:on 830530,HFA Relay 9-17-16A K6B Contacts Failed to Open.Cause Not Determined.Relay Coil Replaced. Systematic Replacement of All Relays within 4-yr Period planned.w/830628 Ltr ML20028F0921983-01-20020 January 1983 LER 82-025/03L-0:on 821222,coil of Reactor Protection Relay 915-5AK8C Overheated.Relay Did Not Fail.Cause Undetermined. Relay Replaced & Proper Operation Verified ML20028F0781983-01-20020 January 1983 LER 82-024/03L-0:on 821221,pressure Switch RHR-PS-120A Setpoint Found Outside Range Specified in Tech Specs.Caused by Failed Diaphragm.Pressure Switch Adjusted & Subsequent Testing Showed Nonrepeatable Trip Point.Switch Replaced ML20028B4671982-11-22022 November 1982 LER 82-022/03L-0:on 821025,RHR Time Delay Relay 10A-K45A Failed to Operate within Required Time Limits.Caused by Setpoint Being Set Too Conservatively.Relay Readjusted & Correct Operation Verified ML20028B4661982-11-19019 November 1982 LER 82-021/03L-0:on 821023,relay 917-16A-K44B Failed to Open Contacts When de-energized.Cause Not Determined.Relay Replaced & Correct Operation Verified.Monitoring Program Implemented to Determine Need for Generic Replacement ML20052G5321982-05-0606 May 1982 LER 82-008/03L-0:on 820415,during Diagnostic Testing of Mechanical Snubbers,Model PSA-10 SN/544 Snubber Exceeded Specified Acceleration Rate.Caused by Improper Installation of Clutch Spring.Snubber Sent to Manufactures for Repair ML20052B4041982-04-22022 April 1982 LER 82-007/03L-0:on 820324,differential Pressure Between Drywell & Suppression Chamber Reduced Below Tech Spec Limits During RHR Test Mode Operation.Caused by Nitrogen Flow from Drywell to Suppression Chamber.Return Piping to Be Modified ML20052A3561982-04-21021 April 1982 LER 82-006/03L-0:on 820322,while Inerting Drywell,Ductwork Between Primary Containment & Reactor Bldg Ventilation Found Failed in Several Places,Preventing Oxygen Concentration & Differential Pressure from Being Established ML20050B2101982-03-19019 March 1982 LER 82-005/03L-0:on 820221,MSIV-86A Found to Have Closing Time Faster than Tech Spec.Cause Unknown.Closing Time Adjusted & Control Valve Locked Into Required Position ML20041F8271982-03-0505 March 1982 LER 82-004/03L-0:on 820109,during Planned Power Reduction, Min Critical Power Ratio Was Below Operating Limit W/O Initiation of Corrective Actions Required by Tech Specs. Caused by Personnel Error.Procedures Will Be Revised ML20041C4151982-02-18018 February 1982 LER 81-003/03L-1:on 810223,valve RHR-MO-26B Motor Current Increased & Remained High When Valve Reached Closed Position.Valve Motor Breaker Manually Tripped & Valve Declared Inoperable.Caused by Failure of Brake Coil ML20041C3881982-02-17017 February 1982 LER 82-003/03L-0:on 820126,overload Alarm Condition Received While Closing Valve RHR-MO-26B,caused by Motor Brake Coil Failing to Release.New Motor & Brake Installed & Tested Satisfactorily ML20041C3741982-02-17017 February 1982 LER 82-002/03L-0:on 820121,during Routine Surveillance Testing NBI-LIS-101A Found to Trip at Lower than Tech Spec Limits.Caused by Barton Model 288 Switch Actuating at Random Positions.Switch Replaced ML20041C3871982-02-17017 February 1982 LER 82-001/03L-0:on 820122,reactor Vessel Level Switch NBI-LIS-72C Failed to Trip at Tech Spec Setpoint.Caused by Misalignment of Switch Mechanism.New Switch Calibr & Installed ML20040D3491982-01-20020 January 1982 LER 81-026/03L-0:on 811223,switches NBI-LIS-01A & NBI-LIS- 101B Found Set at Level Lower That Tech Spec Limits.Caused by Setpoint Drift.Switches Returned to Correct Setpoints. Instrument Drift to Be Closely Monitored ML20040D9261982-01-0505 January 1982 LER 81-025/04T-0:on 811224,during Full Power,Discharge Was Made from Floor Drain Sample Tank W/O Adequate Sampling & Analysis of Batch.Caused by Personnel Error.Liquid Discharge Procedures Being Revised.Personnel Reprimanded ML20038C5321981-12-0303 December 1981 LER 81-024/03L-0:on 811106,safety Relief Valve 71-D Failed to Close After Test.Caused by Failure of Solenoid Plunger to Drop Out When Solenoid de-energized.Solenoid Replaced ML20010G0961981-08-25025 August 1981 LER 81-020/03L-0: on 810728, During Procedure Returning Diesel Generator 1 to Svc After Flexible Fuel Line Leak, Control Air Line Fitting Failed Causing Generator to Shut Down. Caused by Broken Air Line Due to Crimped Ferrule ML20010F9881981-08-25025 August 1981 LER 81-019/03L-0:on 810728,during Surveillance to Prove Operability of Diesel Generator 1,fuel Supply Hose Developed Leak.Caused by Excessive Localized Flexure & Vibration. Hose Replaced ML20010G2661981-08-25025 August 1981 LER 81-021/03L-0:on 810728,during Performance of Surveillance Procedure on Diesel Generator 2,injection Line Failed.Caused by Metal Fatigue & Vibration.Component Replaced ML20010A1391981-07-22022 July 1981 LER 81-018/03L-0:on 810625,pressure Switch NBI-PS-52A Found W/Trip Point Less Conservative than Tech Spec.Apparently Caused by Setpoint Drift.Switch Readjusted.Setpoints for Switches Reset ML20010A1671981-07-13013 July 1981 LER 81-017/03L-0:on 810613,reactor Core Isolation Cooling Sys Steam Supply Valve RCIC-MOV-M016 Failed to Open.Caused by Improperly Wired Motor Operator Circuit.Jumper Installed ML20010A5391981-07-0909 July 1981 LER 81-016/03L-0:on 810610,core Thermal Power Calculation Performed by Process Computer Found Incorrect Due to Incorrect Feedwater Flow Value in Computer.Caused by Personnel Error in Changing Conversion Coefficient 1994-05-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212K9781999-09-30030 September 1999 Safety Evaluation Accepting USI A-46 Implementation Program ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217G7461999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Cooper Nuclear Station ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212C5001999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cooper Nuclear Station ML20211D6491999-08-25025 August 1999 Part 21 Rept Re Nonconformance within LCR-25 safety-related Lead Acid Battery Cells Manufactured by C&D.Analysis of Cells Completed.Analysis of Positive Grid Matl Shows Nonconforming Levels of Calcium within Positive Grid Alloy ML20210R0381999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Cooper Nuclear Station ML20210J2921999-07-29029 July 1999 Special Rept:On 990406,OG TS & Associated Charcoal Absorbers Were Removed from Svc.Caused by Scheduled Maint on Hpci. Evaluation of Offsite Effluent Release Dose Effects Was Performed to Ensure Plant Remained in Compliance ML20209H8281999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Cooper Nuclear Station ML20211A9981999-07-12012 July 1999 Draft,Probabilistic Safety Assessment, Risk Info Matrix, Risk Ranking of Systems by Importance Measure ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209E1061999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Cns.With ML20196B3851999-06-17017 June 1999 Summary Rept of Facility Changes,Test & Experiments,Per 10CFR50.59 for Period 970901-990331.Summary of Commitment Changes Made During Same Time Period Also Encl ML20195K2851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Cooper Nuclear Station.With ML20206P0481999-05-12012 May 1999 Safety Evaluation Concluding That NPP Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at CNS & Adequately Addressed Actions Requested in GL 96-05 ML20206J0811999-05-0404 May 1999 Rev 14 to CNS QA Program for Operation ML20206P9751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Cooper Nuclear Station ML20205Q0891999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Cooper Nuclear Station.With ML20204G8951999-03-15015 March 1999 CNS Inservice Insp Summary Rept Fall 1998 Refueling Outage (RFO-18) ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20204B3701999-03-11011 March 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Requests for Relief for RI-17,Rev 1 and RI-25,Rev 0.Request for Relief RI-13,Rev 2 Involving Snubber Testing & Is Being Evaluated in Separate Report ML20204C9751999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Cooper Nuclear Station ML20199E6751999-01-14014 January 1999 Monthly Operating Rept for Dec 1998 for Cooper Nuclear Station ML20195B9191998-12-31031 December 1998 1998 NPPD Annual Rept. with ML20196J9641998-12-0707 December 1998 Safety Evaluation Accepting Licensee Third 10-yr Interval Inservice Insp Plan Request for Relief RI-27,rev 1 ML20198D2471998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Cooper Nuclear Station.With ML20196A2861998-11-23023 November 1998 SER Re Core Spray Piping Weld for Cooper Nuclear Station. Staff Concluded That Operation During Cycle 19 Acceptable with Indication re-examined During RFO 18 ML20196A5241998-11-23023 November 1998 Safety Evaluation Accepting Proposed Alternative to Use UT Techniques Qualified to Objectives of App Viil as Implemented by PDI Program in Performing RPV Shell Weld & Shell to Flange Weld Examinations ML20196A5061998-11-23023 November 1998 Safety Evaluation Re Flaw Indication Found in Main Steam Nozzle to Shell Weld NVE-BD-N3A at Cns.Plant Can Be Safely Operated for at Least One Fuel Cycle with Indication in as-is Condition ML20196C4241998-11-20020 November 1998 Rev 1 to Cooper Nuclear Station COLR Cycle 19 ML20195H1761998-11-17017 November 1998 SER Authorizing Proposed Alternative in Relief Requests RV-06,RV-07,RV-09,RV-11,RV-12 & RV-15 Pursuant to 10CFR50.55a(a)(3)(ii).RV-08 Granted Pursuant to 10CFR50.55a(f)(6)(i) & RV-13 Acceptable Under OM-10 ML20195F8601998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Cooper Nuclear Station.With ML20155D9961998-10-31031 October 1998 Rev 0 to GE-NE-B13-01980-24, Fracture Mechanics Evaluation on Observed Indication at N3A Steam Outlet Nozzle to Shell Weld at Cooper Nuclear Station ML20154Q5661998-10-0505 October 1998 Rev 0 to CNS COLR Cycle 19 ML20154L5381998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Cooper Nuclear Station.With ML20151Z6141998-09-16016 September 1998 SER Accepting Util Responses to NRC Bulletin 95-002 for Cooper Nuclear Station ML20154F7931998-08-31031 August 1998 Rev 0 to J11-03354-10, Supplemental Reload Licensing Rept for CNS Reload 18,Cycle 19 ML20153B1101998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Cooper Nuclear Station ML20237E7771998-08-20020 August 1998 Revised COLR Cycle 18 for Cooper Nuclear Station ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C0591998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Cooper Nuclear Station ML20236R9131998-07-20020 July 1998 SER Accepting Rev 13 to Quality Assurance Program for Operation Policy Document for Plant ML20236P2971998-07-0707 July 1998 Rev 2 to NPPD CNS Strategy for Achieving Engineering Excellence ML20236R0931998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Cooper Nuclear Station ML20249A7701998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Cooper Nuclear Station ML20247G6131998-05-13013 May 1998 Part 21 Rept Re Defect Contained in Automatic Switch Co, Solenoid Valves,Purchased Under Purchase Order (Po) 970161. Caused by Presence of Brass Strands.Replaced Defective Valves ML20247G0951998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Cooper Nuclear Station ML20237B6861998-04-24024 April 1998 Vols I & II to CNS 1998 Biennial Emergency Exercise Scenario, Scheduled for 980609 ML20217A1531998-04-16016 April 1998 Closure to Interim Part 21 Rept Submitted to NRC on 970929. New Date Established for Completion of Level I & 2 Setpoint Project Committed to in .Final Approval of Setpoint Calculations Will Be Completed by 980531 ML20216G5331998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Cooper Nuclear Station 1999-09-30
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NRC FOAM 366 U. S. NUCLE AR REGUL AToRY CoMMISSloN (7 77)
LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLEASE PRINT oR TYPE ALL REQUIRED INFoRMATioN)
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o i 8 9 lN l ELICENSEE l C lCODE P l Rl 141l@l 15 0l 0l- l 0 [ LICENSE 0 l 0 NUMBER 0 l-l 0l 0 0l@l4 25 26 l1 lLICENSE1 l 1TYPE l 1JGl@l$7 CAT l
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CON'T O i 3[nN 60lL @ 0 15 l0DOCK l0 0 2l9l8 68@l1 69 0l 1 2] 7l 9]@ l i i lREPORT EVENT DATE 74 75 0 l 91 7 l 980l@
DATE I 8 61 ET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h O 2 puring normal operation, a routine tour of the plant indicated a through-wall crack l o 3 pf a weld in the REC supply to the south critical loop, upstream of the supply o 4 lLsolation valve. This portion is isolatable from the critical loop. The redundant ;
o s fEC loop and Service Water supply were available to supply this critical loop. If ;
O s phe weld failed completely, it would be detectable. Reference LER Report No. 78-27 g O 7 ffor an event of similar nature. This event presented no adverse consequences from l 0 s [the standpoint of public health and safety. 80 I
7 8 9 F' STEM CAUSE CAUSE COMP VALVE CODE CODE SUSCODE COMPONENT CODE SU8 CODE SU8 CODE O '3 l S I B lh [E_jh lu X lh XlX X Xl XlX l h (X_j h (Z_j h i a 9 io n i3 m is 2o SEQUE N TI AL OCCUR RE NCE REFORT REVISION EVENT YE AR REPORT NO. CODE TYPE NO.
LER O a gu ,RO a; I7191 1-1 1012 9l d l0 l3 l Ll l-l (0_J
_ 21 22 23 24 26 21 N M 36 31 J2 TAK N A T ON ON PL NT ET HOURS 22 $8 IT FO 8. SL,,PPLI MANUFACTURER l X j@l34C l@
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42 lg lAlg 43 J l0 3 5lg 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i O IThe component involved is a weld. The failure is a through-wall crack which has sur-l l1 Iil Ifaced as a oinhole leak of undeterminable cause. A soft patch has been applied and I
, , Ithe weld evaluated acceptable for continued service. During the next shutdown of m l sufficient duration, the weld will be replaced. An evaluation of a similar failure l i i 4 Iwhich was not reportable, will dedermine the cause. Update report will be submitted.]
7 8 9 80 ST S POWER OTHER ST A TUS ISCO RY DISCOVERY OESCRIPTION i b d h l Ol o 6lhl NA l [_Ajhl Operator Observation l A TIVITY CONTENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE F
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I 4 3 10 68 69 80 5 NAVE OF PREPARER PHONE-
P COOPER NUCLEAR STATION P.O. Box 98, BRoWNvlLLE, NEBR A5KA 68321 Nebraska Public Power Distr =ct i TEtEPeoNe <402> .2s.3.i >
CNSS790554 November 5, 1979 Mr. K. V. Seyfrit U.S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region IV 611 Ryan Plaza Suite 1000 Arlington, Texas 76011
Dear Sir:
This report is submitted in accordance with Section 6.7.2.B.2 of the Technical Specifications for Cooper Nuclear Station and discusses a reportable occurrence that was discovered on October 8, 1979. A li-censee event report form is also enclosed.
Report No.: 50-298-79-28 Report Date: November 5, 1979 Occurrence Date: October 8, 1979 Facility: Cooper Nuclear Station Brownville, Nebraska 68321 Identification of Occurrence:
A condition which lead to operation in a degraded mode permitted by a limiting condition for operation established in Section 3.19.B of the Technical Specifications.
Conditions Prior to Occurrence:
The reactor was at a steady state power level of approximately 9}%
of rated thermal power.
Description 'f Occurrence:
Unile laspecting the cable spreading room it was noted that a four inch diameter pipe sleeve in the fire wall between the cable spreading room and the cable expansion room was not properly sealed.
Designation of Apparent Cause of Occurrence:
Inadequate control of installe. tion of fire seals during a microwave communications system installation in December 1978.
1398 185
Mr. K. V. Seyfrit November 5, 1979 Page 2.
Analysis of Occurrence:
The four inch sleeve, located in the wall between the cable spread-ing room and the cable expansion room, carries two 1 inch conduits through it. One conduit contains control cable for reactor re-circulation motor generator set ventilation flow indication. The other conduit contains cable for microwave communication. The space inside the four inch sleeve and outside of the two one inch conduits was not adequately sealed. The possibility of a fire starting in this area is minimal because no combustible material was present. The cable spreading room is equipped with an auto-matic sprinkler system which could extinguish a fire if one started.
The possibility of a fire spreading through the unsealed sleeve was remote because the sleeve contained no combustible material. This occurrence presented no adverse effect to public health and safety.
Corrective Action:
The four inch sleeve was immediately sealed and an adequate fire barrier established. All remaining sleeves in this area were inspected and verified to be properly sealed. The Technical Spec-ifications also require that the penetrations in the cable spread-ing room be inspected every 18 months. This event was discussed with the appropriate personnel.
Sincerely, L. C. Lessor Station Superintendent Cooper Nuclear Station LCL:cg irtach.
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N AC FDRM 366 U. S. NUCLEAR REGULATORY COMMISSION (7 77)
UCENSEE EVENT REPORT CONTROL 8 LOCK: l l I l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI i e 7
O i 8 9 INlElC PlR 1 l@l O i O!- I O l 0 l 0 l 0 l - l 0 l 01 0 l@l4 LICENSEE CODE 14 15 LICENSE NUM8ER 25 26 1LICENSE Il l1l1l@l TYPE J0 l
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REPORT OATE EVENT DESCRIPTICN AND PROB ABLE CONSEQUENCES h O 2 During inspection of cable spreading room it was noted that one 4 inch pipn sleevo I o 3 fin the wall between cable spreadine room and cable evnnnaion room una noe ann 1pa i o 4 T.S. 3.19.B. The possibility of a fire in this aren is minimal because no combus- 1 IOI5I Itible material was present. Cable spreadine room is eauipped with an automatic l O 6 l cnrink1 pr evneon. Nn si gni fi e nn e ncenvranco e n nte nlano Thic ovone hnd nn offoce l 0 7 lunon nublic health nnd unfaty_ This avane is nne renprieive. I O a l 7 8 3 00 SYSTEM CAUSE CAUSE COMP. VALVE CODE CUDE SU8 CODE COMPONENT CODE SU8 CODE SUSCODE 7
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_ 21 22 23 24 26 27 28 29 30 31 31 4CT:ON FUTURE EFFECT SHUTOOWN ATTACHMENT NPRD-4 PRIVE COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 26 SygMITTED FORM bu8. SUPPLIER MANUFACTURER LsJ@Liij@ W@ IZ l@ 0101010 L N_J @ l I@ I43Z l@ Zl9 9 l 91@
33 34 3b 36 37 40 41 42 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l Four inch sleeve in the wall has apparently been unsealed since December 1978.
Ii li l l The sleeve was immediately sealed. All other sleeves in this area were also in-
, , spected and verified to be properly sealed. The incident was discussed with ap-i 3 l propriate personnel, i A i . I
? 8 ') 80 F ActLt TV METHOD OF STATUS , POWER OTHE R $TA TUS DISCOV E R Y DISCOV ERY DESCRIPTION 32 i 5 lE@ l0 9l5l@l NA l W @l Shift Supervisor Observation l A flVITY CONTENT RELEASED OF RE L C ASE AMOUNT OF ACTIVf fY LOCATION OF RELE ASE 1 6 [,,_gj @ @l NA l l NA l 7 d ') 10 ii 44 45 80 PE RSONNE L F MPOSURES NtM8f R TYPE D E SCRIP TION i NA 7
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7 n <> 10 68 69 80 5 NAVE OF PREP ARER Ladislav F. Bednar PHONE.
402-825-3811 2