ML19275A142

From kanterella
Revision as of 17:27, 1 February 2020 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-015/03X-1 on 790525:breaker 1AS Failed to Close Automatically After Reactor Scrammed.Caused by Improper Operations of Switch 52 in Breaker 1AN.Breaker 1FA Failed to Trip.Caused by Misaligned Trip Coil & Armature
ML19275A142
Person / Time
Site: Cooper Entergy icon.png
Issue date: 08/01/1979
From: Bednar L
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19275A141 List:
References
LER-79-015-03X, LER-79-15-3X, NUDOCS 7908310444
Download: ML19275A142 (1)


Text

_ . _ _ _ . _ . _ _ ._ ._ . _ _ _ _ _

NRC FQflM 366' U.S. NUCLEAR REGULATORY COMMISSION (7pl UPDATE REPORT PREVIOUS _RE_P_0ET_DATE__ JUNE 23, 1979

", LWCW3tt CV CW I M tt'U M I (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

CONTROL BLOCK:

1 l l l l l lh 6

o 1 lNlE l C l P l R l 141 l@l 15 0 l 0 l - l 0 lLICENSE l 0 l - l 0 0 l 025l@l264 l 1LICENSE 0 l 0NUM.iER l 1 TYPE 1 1l@l JO l

57 CAT 58 I@

7 8 9 LICENSEE CODE CCN'T 0 1 5ouRC I60L l@LOi s l 0DOCKETl 0 lNUMBER 0 l 2 i 9 l 868 @l69 01512 5 7 I8 74@ l0 EVENTI DATE 75 0l . 01ATE 7l ol@

l AlREPORT 80 7 8 61 .

EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 lAf ter reactor scrammed on APRM Hi upscale, breaker lAS failed to close automaticallv. I m lThe breaker was then closed by its control switch. Breaker lAS ties 4160V bus lA to l o 4 Ithe startup transformer when the generator trips. Breaker 1FA failed to trip automatic-l o s lally and when its control switch was operated to TRIP. This breaker is one of two brea l-10 is I lakers connected in series which ties 4160V bus IF to bus 1A.This occurrence presented l 0 7 ln0 adverse Consequences to public health and safety. Redundant systems were available. I o 8 preaker IFA failure to trip is repetitive (79-8) . 80 I

7 8 9 SYSTEM CAUSE CAUSE COMP. VALV E CODE CODE SUSCODE COMPONENT CODE SUBCODE SUSCODE 7

o 9 8

l El Dl@ W@ W@ l Cl Kl Tl B RlKl@

9 10 11 12 13 18 19 E @ W@ 20 SEQUENTIAL OCCURRENCE REPORT REVISION EVENTYEAR REPORT NO. CODE TYPE NO.

LE R. RO h RE yu l 7l 9 21 22

[_j 23 l ol 1l Sl 24 26 d

27

[0]3 28 29 lX 30

(---J 31 l ll 32 K N AC ON ONP NT MET HOURS SB i FOR B. SLPP IER MANLF CTURER lEl@lZl@

33 34 35 Zl@ l36Zl@ l 0l 0l 0 0l40 l Nj@

37 41 42 l@ J@ lGl0l8l0l@

43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o l Breaker lAS apparently failed to close because of improper operation of switch 52 in 1

["i"TTl breaker 1AN. GE has been requested to evaluate. Switch < ontacts were cleaned ed :estell

, 2 l satisfactorily. Breaker 1FA failed to trip because misalignment of the trip co'1 and I i 3 l the trip armature. Breakers are GE Magna Blasr Type AMH 4.76-250. l i 4 I l

SO 7 8 9 .

ST * % POWE R OTHER STATUS Dis O RY DISCOVERY DESCRIPTION y l Gl@ l010 l0 l@l NA l lAl@l Operator Observation l ACTIVITY CO TENT RELEASEO OF MELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE NA 7

1 6 tl 9

@l ZI 10 11 NA 44 l l 45 80 l

PERSONNEL EXPOSURES NUMBE R TYPE OESCRIPTION i 7 1010101@l Zl@l NA l 8

' PER$cNNd%u'4ES NuMeEa DESCRIPTION @ / O 3;z . ,9 l i NA l 7

4 8 9 10101 Ol@l12 11 80 LOSS OF OR OAMAGE TO FACILITY h TYPE D E SC RIP TION  %/

2 NA l 7

1 8 9 l ZI@l10 2 ')

,SSe '@ % PT,0~ @ 79083leN

" " c ' ""

QJ l NA l 68 69 ll llllllll l1]:I

30. %

F is '3 to ehr PHCNE:

402-825-3811 NAME OF PAEPARER