IR 05000387/2009004

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UNITED NUCLEAR REGULATORY REGION 475 ALLENDALE KING OF PRUSSIA, PA November 13, 2009 EA-09-248 Mr. TimothySenior Vice President and Chief Nuclear Officer PPL Susquehanna, LLC 769 Salem Boulevard, NUCSB3 Berwick, PA 18603 SUSQUEHANNA STEAM ELECTRIC STATION -NRC INTEGRATED INSPECTION REPORT 05000387/2009004 AND 05000388/2009004

Dear Mr. Rausch:

On SeptElmber 30, 2009, the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your Susquehanna Steam Electric Station Units 1 and 2. The enclosed integrated inspection report presents the inspection results, which were discussed with you and other members of your staff during a preliminary exit meeting on October 9, 2009. This inspection examined activities completed under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, two examples of an apparent violation (A V) were identified, involving PPL Susquehanna, LLC (PPL) failing to ensure that individual license holders, on shift in the capacity of senior reactor operators (SROs), met the medical prereqUisites required for holding a license prior to performing the duties of a licensed operator as required by 10 CFR 55.3. In one occasion in August 2009, an SRO failed a medical examination which identified a disqualifying condition, in that, the examination identified that the SRO's vision did not meet the health requirements stated in ANSI/ANS 3.4-1983, Section 5.4.5, "Eyes." However, he performed the function of an SRO during three watches with a license that was not appropriately conditioned to require that corrective lenses be worn. In the second occasion, a different SRO performed licensed operator duties 52 times between April 1, 2009, and July 22, 2009, after the deadline for his biennial medical examination had passed. The medical examination may have identified an issue with the SRO's medical condition and general health that would have disqualified him from being authorized by a license. This app,arent violation is being considered for escalated enforcement action in accordance with the NRC Enforcement Policy. The current Enforcement Policy is included on the NRC's Web site at (http://www.nre.gov/about-nrciregulatorv/enforcementienforce-pol.html).Upon discovery, PPL removed both individuals from watchstanding duties pending follow-up medical evaluations and, in the August 2009 example involving the SRO who failed his vision examination resulting in a disqualifying condition, PPL requested a conditional NRC license to address the disqualifying medical condition. For the July 2009 example, the SRO passed his biennial medical examination when administered. Both issues have been entered into PPL's corrective action program. See Section 1 R11 of the attached report for additional details. In addition, since you identified the violation, and based on our understanding of your corrective actions, a civil penalty may not be warranted in accordance with Section VI.C.2 of the Enforcement Policy. The NRC believes we have enough information to make a final decision on the matter. Before the NRC makes its enforcement decision, we provided you an opportunity to either: (1) respond to the apparent violation addressed in this inspection report within 30 days of the date of this letter or, (2) request a predecisional enforcement conference. On November 9, 2009, I contacted Mr. Jeff Helsel, Susquehanna Plant Manager, and members of your staff and informed them of this opportunity. On November 10, 2009, Michael Crowthers, Susquehanna Regulatory Assurance Manager, informed my staff that you elected to provide a written response. Your written response should be clearly marked as a "Response to an Apparent Violation in Inspection Report 0500038"712009004 AND 05000388/2009004; EA-09-248" and should include for each example of the AV: (1) the reason for the AV, or, if contested, the basis for disputing the AV; (2) the corrective steps that have been taken and the results achieved; (3) the corrective steps that will be taken to avoid further violations; and (4) the date when full compliance will be achieved. Your response may reference or include previously docketed correspondence, if the correspondence adequately addresses the required response. If an adequate response is not received within the time specified or an extension of time has not been granted by the NRC, the NRC will proceed with its enforcement decision. In addition, please be advised that the number of violations and characterization of the AV described in the enclosed inspection report may change as a result of further NRC review. You will be advised by separate correspondence of the results of our deliberations on this matter. In addition, this report documents two NRC-identified findings and one self-revealing finding of very low safety significance (Green). Two of these findings were determined to involve a violation of NRC requirements. Additionally, one licensee-identified violation, which was determined to be of very low safety significance, is listed in this report. However, because of the very low safety significance and because they are entered into your corrective action program (CAP), the NRC is treating these findings as non-cited violations (NCVs), consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator Region I; the Director, Office of Enforcement, United States NRC, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Susquehanna Steam Electric Station. In addition, if you disagree with the characterization of the cross cutting aspect of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at theSusquehanna Steam Electric Station. The information you provide will be considered in accordance with Inspection Manual Chapter 0305. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the !\IRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.qov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,IRA! David C. Lew, Director Division of Reactor Projects Docket Nos. 50-387; 50-388 License Nos. NPF-14, NPF-22

Enclosures:

Inspection Report 05000387/2009004 and 05000388/2009004

Attachment:

Supplemental Information cc w/encl: Distribution via ListServ T. 4 Susquehanna Steam Electric Station. The information you provide will be considered accordance with Inspection Manual Chapter In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,IRA! David C. Lew, Director Division of Reactor Projects Docket Nos. 50-387; 50-388 License Nos. NPF-14, NPF-22 Inspection Report 05000387/2009004 and 05000388/2009004

Attachment:

Supplemental Information cc Distribution via ListServ Distribution w/encl: (via E-mail) S. Collins, (R10RAMAIL Resource) M. Dapas, (R10RAMAIL Resource) D. Lew, (R1 DRPMAIL Resource) J. Clifford, (R1 DRPAMAIL Resource) P. Krohn, DRP D. Holody OE (R10RAMAIL Resource) R Fuhrmeister, DRP A. Rosebrook, DRP E. Torres, DRP J. Bream, DRP F. Jaxheimer, DRP, SRI P. Finney, DRP, RI S. Farrell, DRP, OA L. Trocine, RI OEDO RidsNrrPMPeachBottom Resource RidsNrrDorlLpl1-2 Resource ML093170375 SUNSI Review Complete: AAR (Reviewer's Initials) DOCUMENT NAME: G:\DRP\BRANCH4\lnspection Reports\Susquehanna\SQ 3rd Qtr 2009\SUS2009 _004 _g.doc After declaring this document "An Official Agency Record" it will be released to the Public. To receive a copy of this document. indicate in the box: "C":: Copy without attachment/enclosure "E";; Copy with attachmenUenciosure liN" No copy OFFICE RIIDRP I RI/DRP I R1/0E I R1/DRP I NAME ARosebrookl PKrohnl DHoiody/AED for DLew lOATE 11/12/09 11/12/09 11112109 11/12/09 OFFICIAL RECORD COPY Docket No: License No: Report No: Licensee: Facility: Location: Dates: Inspectors: Reviewed By: Approved By: U.S NUCLEAR REGULATORY COMMISSION REGION I 50-387, 50-388 NPF-14, NPF-22 05000387/2009004 and 05000388/2009004 PPL Susquehanna, LLC Susquehanna Steam Electric Station, Units 1 and 2 Berwick, Pennsylvania July 1, 2009 through September 30, 2009 F. Jaxheimer, Senior Resident Inspector P. Finney, Resident Inspector G. Meyer, Senior Reactor Inspector S. Chaudhary, Reactor Inspector J. Furia, Senior Health Physicist A. Rosebrook, Senior Project Engineer O. Masnyk-Bailey, Health Physicist S. Hammann, Health Physicist J. Nicholson, Health Physicist Paul G. Krohn, Chief Projects Branch 4 David C. Lew, Director Division of Reactor Projects Enclosure TABLE OF

SUMMARY OF FINDINGS

.........................................................................................................

REPORT DETAILS

.....................................................................................................................1. REA,CTOR SAFETy ...........................................................................................................1R04 Equipment Alignment ..............................................................................................1R05 Fire Protection .........................................................................................................1R06 Flood Protection Measures ......................................................................................1R07 Heat Sink Performance ...........................................................................................1R11 Licensed Operator Requalification Program .......................................................... 1R12 Maintenance Effectiveness .................................................................................... 1R13 Maintenance Risk Assessments and Emergent Work Control ............................... 1R 15 Operability Evaluations .......................................................................................... 1R 18 Plant Modifications ................................................................................................ 1R19 Post-Maintenance Testing .....................................................................................1R22 Surveillance Testing ..............................................................................................1EP6 Drill Evaluation

RADIATION SAFETY

.......................................................................................................20S1 Access Control to Radiologically Significant Areas ................................................ 20S2 ALARA Planning and Controls ...............................................................................20S3 Radiation Monitoring Instrumentation .................................................................... 4. OTHER ACTiViTIES .........................................................................................................40A1 Performance Indicator Verification .........................................................................40A2 Identification and Resolution of Problems .............................................................. 40A5 Other Activities ......................................................................................................40A6 Meetings, Including Exit. ........................................................................................40A7 Licensee-Identified Violations ................................................................................ ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

..................................................................................................

LIST OF ITEMS

OPENED, CLOSED, AND DiSCUSSED .......................................................

LIST OF DOCUMENTS REVIEWED

......................................................................................

LIST OF ACRONYMS

...... .................................................................................................... Enclosure
SUMMAR Y
OF [[]]
IR 05000387/2009004,05000388/2009004,07/01/2009 -09/30/2009; Susquehanna Steam Electric Station, Units 1 and 2; Fire Protection, Licensed Operator Requalification Program, Maintenance Effectiveness,
ALARA [[Planning and Controls. The report covered a 3-month period of inspection by resident inspectors and announced inspections by regional reactor inspectors. Two Green non-cited violations (NCVs), and one Green finding were identified. In addition, one apparent violation (AV) item being considered for escalated enforcement action in accordance with the]]
NRC Enforcement Policy. The current Enforcement Policy is included on the
NRC [['s Web site at (http://wvvw.nrc.gov/about-nrc!regulatory/enforcementlenforce-pol.html). The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SOP). Cross-cutting aspects associated with findings are determined using]]
IMC 0305, "Operating Reactor Assessment Program," dated August 2009. Findings for which the
SOP does not apply may be Green or be assigned a severity level after
NRC management review. The
NRC 's program for overseeing the safe operation of commercial nuclear power reactors is described in
NUREG -1649, "Reactor Oversight Process," Revision 4, dated December 2006. A.
NRC -Identified and Self-Revealing Findings Cornerstone: Mitigating Systems Green. The inspectors identified a Green
NCV [[of the Susquehanna, Unit 2 Operating License Condition 2.C.(3), Fire Protection for failure to administratively control combustible loading in an area on the 686' elevation of the control structure. As a result, a normally locked storage area was discovered to contain numerous combustibles without deSignated detection, suppression, or a pre-fire plan. This issue was placed in]]
PPL [['s corrective action program (CAP) and immediate corrective actions included the removal of some of the combustible materials and the assignment of hourly fire watches. The finding was more than minor because it was associated with the external factors attribute (fire) of the Mitigating Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically,]]
PPL [[did not ensure that plant procedures controlled the use and storage of combustible materials and that a combustible loading analysis was maintained for a locked storage area fire zone in the control structure. The inspectors assessed this finding in accordance with]]
IMC [[0609, Appendix F, "Fire Protection Significance Determination Process", and determined the finding to be of very low safety significance (Green) because the fire barrier between the safety-related equipment in the lower relay room and this storage area was being properly maintained and found in good physical condition. The finding was determined to have a cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because]]
PPL did not implement a
CAP with a low threshold for identifying issues P.1(a). Specifically, PPL had reasonable opportunities to identify the combustible loading issue on multiple occasions during access of the storage room. (Section 'I R05) Enclosure
AV... [[]]
PPL identified two examples of an apparent violation (AV), involving
PPL Susquehanna,
LLC (PPL) failing to ensure that individual license holders, on shift in the capacity of senior reactor operators (SROs), met the medical prerequisites required for holding a license prior to performing the duties of a licensed operator as required by
10 CFR 55.3. In one occasion in August 2009, an
SRO failed a medical examination which identified a disqualifying condition, in that, the examination identified that the
SRO 's vision did not meet the health requirements stated in
ANSI /ANS 3.4-1983, Section 5.4.5, "Eyes." However, he performed the function of an
SRO during three watches with a license that was not appropriately conditioned to require that corrective lenses be worn. In the second occasion, a different
SRO performed licensed operator duties 52 times between April 1, 2009, and July 22, 2009, after the deadline for his biennial medical examination had passed. The medical examination may have identified an issue with the
SRO 's medical condition and general health that would have disqualified him from being authorized by a license. Upon discovery,
PPL removed both individuals from watchstanding duties pending follow-up medical evaluations and, in the case involving the
SRO whose failed medical examination resulted in a disqualifying condition,
PPL requested a conditional
NRC license to address the disqualifying medical condition. Both issues have been entered into
PPL [['s corrective action program. Each example was evaluated independently using the traditional enforcement process bf:lcause the failure to determine an operator's medical condition and general health has the potential to impact or impede the regulatory process. Specifically, medical certification and conditional licensing are used by the]]
NRC to ensure health conditions wi" not adversely affect operator duties or performance. The finding was determined to have a cross-cutting aspect in the area of Problem Identification and Resolution, Operating Experience, because
PPL did not systematically collect, evaluate, and communicate relevant external operating experience P.2(a). Specifically,
PPL failed to evaluate
NRC Information Notice 2004-20 for medical examination issue applicability in accordance with their operating experience review program as evidenced by the
2008 SL -
IV [[]]
NCV (
NRC [[]]
IR 50-387 & 50-388 2008302-01), for an initial licensed operator application submitted to the
NRC with a disqualifying medical condition, as well as these two events in July and August of 2009. (Section 1 R11.2) Green. The inspectors identified a Green
NCV of 10
CFR Part 50, Appendix B, Criterion
XVI , "Corrective Action," in that
PPL [[did not implement timely corrective actions to preclude repetition of a significant condition adverse to quality. Specifically, actions taken to address causes of the Unit 1 high pressure coolant injection (HPCI) stop valve failure to close in 2006 did not prevent the same]]
HPCI stop valve from failing to close on August 18, 2009. In both cases, the stop valve failure to close rendered this single train
HPCI system inoperable as it was unable to meet the 30 second injection response time as described in the design basis. Corrective maintenance was performed on the valve and the issue was entered into
PPL 's
CAP. [[The finding is more than minor because it adversely affected the performance attribute of the Mitigating Systems cornerstone objective, to ensure the availability, reliability, and capability of equipment that respond to initiating events to prevent undesirable consequences. Specifically, a full closed stop valve indication resets the]]
HPCI ramp generator via a lower limit switch. Without this reset, the governor is unprepared to restart the turbine from an idle state during a designed basis event. The inspectors assessed this finding in accordance with

IMC 0609, Attachment 4, "Phase 1 Initial Screening and Characterization of Findings" and determined the finding to be of very low Enclosure

safety significance because it did not result in an actual loss of safety function for greater than the Technical Specification allowed outage time. The finding was determined to have a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because

PPL [[did not take appropriate corrective actions to address safety issues in a timely manner, commensurate with their safety significance and complexity [P .1 (d)]. Specifically,]]
PPL did not appropriately implement corrective actions following the 2006 failure of the
HPCI stop valve. (Section 1 R12) Cornerstone: Occupational Radiation Safety Green. A self-revealing, Green finding was identified that involved inadequate work planning relative to the in-vessel visual inspection! inservice inspection (l
WIIISI ) of the reactor vessel that resulted in additional unplanned collective exposure contrary to low-as-is-reasonably-achievable (ALARA) controls. Specifically, the utilization of inexperienced workers to perform the various tasks involved in the
IWI l
ISI activity resulted in the additional collective exposure to perform this routine task. This finding was entered into
PPL [['s Correction Action Program for resolution. This finding is more than minor because it resulted in unplanned, unintended collective exposure that was greater than 50 percent above the intended collective exposure and greater than 5 person-rem. Additionally, the performance deficiency adversely affected the radiation protection cornerstone objective. The inspectors assessed the finding in accordance with]]
IMC 0609, Appendix C, "Occupational Radiation Safety Significance Determination Process," and determined that the finding was of very low safety significance (Green) because the finding was due to
ALARA [[work control planning and the 3-year rolling average collective exposure at Susquehanna was less than 240 person-rem (107 person-rem for 2005-2007). This finding was determined to have a cross-cutting aspect in the area of Human Performance, Resources, because]]
PPL [[did not utilize sufficiently qualified personnel to assure occupational radiation safety requirements were met H.2{b). Specifically,]]
PPL 's use of inexperienced contract workers resulted in additional collective exposure that could have been avoided. (Section 20S2) B. Licensee Identified Violations A violation of very low safety significance. which was identified by
PPL. has been reviewed by the inspectors. Corrective actions taken or planned by
PPL have been entered into

PPL's CAP. This violation and corrective action tracking numbers are listed in Section 40A7 of this report. Enclosure

.1

REPORT Summary of Plant Status Susquehanna Steam Electric Station (
SSES [[) Unit 1 began the inspection period at the authorized licensed power level of 94.4 percent rated thermal power (RTP). On September 4, 2009, Unit 1 was reduced to 70 percent over 26 hours in support of a control rod sequence exchangEl and pattern adjustment. Unit 1 remained at 94.4 percent]]
RTP for the remainder of the inspection period.
SSES Unit 2 began the inspection period at the authorized licensed power level of 94.4 percent
RTP. On September 12,2009, Unit 2 was reduced to 58 percent over 26 hours in support of a control rod sequence exchange and pattern adjustment. Unit 2 remained at 94.4 percent
RTP for the remainder of the inspection period. Note: The licensed
RTP for both units is 3952 megawatts thermal. The Extended Power Uprate (
EPU ) License Amendment for
SSES was approved in January 30,2008, and was implemented for both units in accordance with the issued license conditions. For the current inspection period, the authorized power level for both units is 94.4 percent of the
EPU licensed power limit.
REACTO R
SAFETY (RHR) components and instrumentation with focus on behavior during pressurization and venting; Plant discharge line (blow down) and river water make-up system parameters and lineup during investigation of groundwater issue described by]]
CR 1167146; and "An and "En emergency diesel generators (
EDG s) when "En
EDG substituted for "8"

EDG. b. Findings No findings of significance were identified. Enclosure

.2 Complete Walkdown (71111.04S -1 Sample) a. Inspection Scope The inspectors performed a detailed review of the alignment and condition of the station nitrogen system and the Unit 2 containment instrument gas system. The inspectors reviewed operating procedures, checkoff lists, and system piping and instrumentation drawings. Walkdowns of accessible portions of the systems were performed to verify components were in their correct positions and to assess the material condition of systems and components. The inspectors evaluated ongoing maintenance and outstanding Condition Reports (CR) associated with both systems to determine the effect on system health and reliability. The inspectors verified proper system alignment and looked at system operating parameters. Documents reviewed are listed in the Attachment. The walkdown included the following system and its interconnection: Unit 2, Nitrogen and Primary Containment Instrument Gas. b Findings No findings of significance were identified. 1 Fire Protection (71111.050 -5 Samples) Fire Protection -Tours a. Inspection Scope The inspectors reviewed

PPL 's fire protection program to evaluate the specified fire protection deSign features, fire area boundaries, and combustible loading requirements for selected areas. The inspectors walked down those areas to assess
PPL 's control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures to assess
PPL [['s fire protection program in those areas. Documents reviewed are listed in the Attachment. The inspected areas included: Unit 1, battery rooms, fire zones 0-28 B-1 (11) and 0-28 I thru N; Unit 1, containment access area (1-401); Security control center, fire zone 0-83,]]
FP -013-360; Control structure charcoal filter area and operations storage area on elevation 687',
FP -013-135; and Central access control area and chemistry laboratory, elevation 676', 134. b. Findings Introduction: The inspectors identified that

PPL was not administratively controlling combustible loading in an area on the 686' elevation of the control structure as specifically required by the Susquehanna Fire Protection Program and specifically described as a provision of the Fire Protection Program Report (FPPR). This finding Enclosure

was determined to be of very low safety significance (Green) and an

NCV of the
SSES Unit 2 Operating License Condition
2.C [[(3), Fire Protection. Description: During a fire walkdown inspection in the control structure, the resident inspectors identified that an operations department space, a normally locked storage area on 686' elevation, contained numerous combustibles. Most items stored in the area were found on open shelves or stacked on the floor. The accumulation of combustibles included (but was not limited to) wood, plastic, cardboard boxes, old paper records, rubber drain hoses, radio equipment, refueling support furniture, and labeling supplies. Inspectors immediately asked operations staff if this room was part of any fire pre-plan (fire fighting guideline/procedure). The room was not incorporated in any of the site fire pre-plans and inspectors did not locate any combustible storage permits. When inspectors could not verify the area was being controlled by the design control process as a combustible storage area and could not verify that]]
PPL was procedurally controlling the use and storage of combustible materials in this area, the issue was brought to
PPL management's attention.
PPL [[took immediate action to dispatch the fire protection engineer (FPE) and field unit supervisor to the area. An hourly fire watch was started for the area and some of the combustibles were promptly removed from the room. The operations shift manager determined that the area was overcrowded with materials that were no longer needed. Longer term correction actions are planned and the issue is tracked by]]
CR [[1179995. As part of the evaluation of this performance issue, inspectors also completed additional walkdowns and drawing reviews which revealed that the operations department storage area was actually located directly below the following rooms on the 698' elevation of the control structure: the computer maintenance room, the uninterrupted power supply computer room, Corridor C-200, and the Unit-2 lower relay room. Inspectors reviewed drawings, the]]
FPPR and held a discussion with the site
FPE [[, to verify that there was no automatic detection, no automatic suppression, and no fire pre-plan for this storage area. Analysis: The inspectors determined that this finding was more than minor because it was associated with the external factors attribute (fire) of the mitigating systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (Le., core damage). Specifically,]]
PPL [[did not ensure that fire combustible storage was procedurally controlled in the control structure. Fire combustibles accumulated in an area directly b,elow the Unit 2 relay room and three other separated rooms. This storage area did not have any fire suppression or detection capability. The inspectors assessed this finding in accordance with]]
IMC 0609, Appendix F, "Fire Protection Significance Determination Process." This finding was determined to be of very low safety significance (Green) in Phase 1 of the
SDP [[because it was assigned a low degradation rating. A low degradation rating was assigned because the fire barrier between the safety-related equipment in the lower relay room and this storage area was being properly maintained and found in good physical condition. The finding was determined have a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because]]
PPL did not implement a

CAP with a low threshold for identifying issues [P.1 (a)]. Specifically, PPL Enclosure

had reasonable opportunities to identify the combustible loading issue on multiple occasions during access of the storage room. Enforcement: The Susquehanna Unit 2 Operating License Condition

2.C. (3), requires that
PPL implement and maintain in effect all provisions of the Fire Protection Program as described in the
FPPR. [[]]
FPPR [[section 1.4 requires that plant procedures control the use and storage of combustible materials and section 6.0 also requires that the combustible loading analysis was maintained through the design control process. Contrary to these requirements, prior to September]]
2009 PPL [[did not procedurally control the use and storage of combustible materials on the 686' elevation of the control structure and did not evaluate changes to combustible storage in this area through the control process. Because the finding is of very low safety significance and has been entered into]]
PPL 's
CAP (
CR 1179995), this violation is being treated as a Cited Violation (NCV), consistent with Section
VI.A of the
NRC pump house and spray pond vault inspections]]
VA 006,
VA 007,
VA 011, and
VA [[012. b. Findings No findings of significance were identified. 1 Heat Sink Performance (71111.07T -3 Samples) Triennial Heat Sink a. Inspection Scope Based on safety significance and prior inspection history, the inspectors selected the following heat exchangers to evaluate]]
PPL 's means (inspection, cleaning, maintenance, and performance monitoring) of ensuring adequate heat sink performance. Unit 1 A

RHR heat exchanger; Enclosure

'A' Emergency diesel generator heat 1) Intercooler heat 2) Jacket water cooler; 3) Lubricating oil 'E' Emergency diesel generator heat 1) Intercooler heat 2) Jacket water cooler; 3) Lubricating oil The inspectors assessed the external condition of the above heat exchangers in the field, reviewed the eddy current, surveillance test and inspection results, and reviewed the applicable system health reports since the last inspection to confirm that results were acceptable and that design basis assumptions for flow rate, plugged tube percentage, and heat transfer capability had been met. The inspectors discussed piping corrosion, and heat exchanger practices, including the specifications and procedures for heat exchanger maintenance, and consistency with the Generic Letter 89-13 requirements with cognizant, system engineers, and chemistry personnel. The inspectors reviewed applicable corrective action program documents to confirm that identified problems and d,egraded conditions had been resolved properly. In addition to the inspections of heat exchangers in the

RHR and
EDG sediment depth. The review included discussions with the]]
RHR service water system engineer, a walk-down of the spray pond and pump house, and discussions with cl1emistry personnel and the emergency service water (
ESW basin (service water heat sink) were reviewed to verify that potential bio-fouling mechanisms were being addressed, including on-going treatment and monitoring as specified in the chemistry manual. The inspectors noted that the]]
SSES results were aided by the ability to chemically control their ultimate heat sink, the extensive use of stainless steel

AL-6XN in tubing, and the experience of involved engineering, testing, and chemistry personnel. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified. Enclosure

.1 1Licensed Operator Requalification Program (71111.11 Q -2 Sample) Resident Inspector Quarterly Review a. Inspection Scope On August 10, 2009, the inspectors observed as-found licensed operator simulator performance. The inspectors compared their observations to Technical Specifications (TSs), emergency plan implementation, and the use of system operating procedures. Tlhe inspectors also evaluated

PPL [['s critique of the operators' performance to identify discrepancies and deficiencies in operator training. Documents reviewed are listed in the Attachment. The following training was observed: Anticipated transient without scram, reactor pressure vessel power and level control, and event declaration. b. Findings No findings of significance were identified . . 2 Licensed Operator Medical Review (1 sample) a.. Inspection Scope The inspectors reviewed two instances in July 2009 and August 2009 where]]
PPL had identified issues with the medical qualification records for two separate Senior Reactor Operators. The inspectors reviewed the medical certification forms, reviewed the
PPL 's formal correspondence with the
NRC upon discovery of the issue to ensure timeliness requirements were met,
PPL conditional license request submittal and reviewed
PPL 's corrective actions. b. Findings Introduction: The licensee identified two examples of an
AV of 10
CFR 55.3, Licensed Requirements, for two cases in which
PPL [[licensed operators failed to have valid medical examinations consistent with their position. Specifically, one licensed operator performed duties with an expired biennial medical examination while another licensed operator performed duties with a failed visual examination. In both cases, operators performed the function of a senior reactor operator without meeting the medical for requalification specified in 10]]
CFR 55.21,
10 CFR 55.23 and 10
CFR 55.33. As such both operators were not qualified while being assigned to and performing licensed duties as required by
10 CFR 55.3. Discussion: During July and August 2009, two instances were identified where

SSES licensed operators failed to meet the medical requirements to maintain their license, and these operators subsequently performed licensed operator duties. ,!;,vent 1: On October 13, 2008, a senior reactor operator (SRO) self-identified a medical issue that resulted in his disqualification, a medical restriction entered into a corporate database and an automatic update of TMX, (the site's training and qualification database) was completed from the corporate source. The operator subsequently Enclosure

completed a medical follow-up and was reinstated on December 12, 2008. While the corporate database entry could have been deleted upon reinstatement, manual corrections to

TMX were made. When the restriction was manually updated with a December 12, 2008 date,
TMX automatically and incorrectly changed the medical examination due date to October 31, 2010, to reflect a biennial requirement from the date of the
SRO 's self-identified medical issue. In 2004, the
NRC issued
NUREG -1021, Revision 9, which clarified the periodicity of medical examinations. Appendix F of the
NUREG defines biennial as 730 days and allows for an extension to include the remaining days in the anniversary month. For example, the subject
SRO had a biennial medical examination due on March 9, 2009, exactly two years from the previous examination but the permitted extension carried the due date to March 31,2009. During a medical record review on July 22, 2009,
PPL discovered that the
SRO had not received a biennial licensed medical examination by March 31, 2009. The
SRO qualifications for the individual were immediately revoked and a physical was scheduled for July 24, 2009. The operator passed the physical examination and was subsequently reinstated on July 30,2009. Upon review, it was determined that the
SRO stood a total of 52 watches in a
TS licensed position without a certifying medical examination as outlined in
ANSI /
ANS -3.4-1983, "Medical Certification and Monitoring of Personnel Requiring Operator Licenses for Nuclear Power Plants." Upon discovery,
PPL placed this issue in their corrective action program under
CR 1166686. Event 2: On August 18, 2009, a
PPL health services specialist determined that an shift
SRO did not pass the corrected or uncorrected visual examination which had been performed during the previous week. Upon discovery, the
SRO was disqualified for the licensed position and the operator was removed from standing watch.
PPL operations staff promptly initiated Condition Report 1173182, which described the non-compliance and established corrective actions to implement measures to mitigate the recurrence of similar conditions.
PPL also implemented actions to request a conditional license for this
SRO adding a condition to the operator's license requiring corrective lenses be worn. It was determined that the licensed operator performed licensed duties during three scheduled work shifts which included assuming the role of the refueling
SRO during fuel moves for a dry fuel storage campaign. This
SRO performed licensed duties even though he had not met the medical condition and general health prescribed for licensed operators at the facility as outlined on
NRC Form 396 and required by 10
CFR 55.21. Information Notice (IN) 2004-20, "Recent Issues Associated with
NRC Medical Requirements for Licensed Operators," states, "Given the importance of the operators' role in maintaining reactor safety, the
NRC [[staff becomes concerned whenever inspection results, facility audits, and other indicators suggest that facility medical programs may not be receiving sufficient management oversight to ensure that the fitness of licensed operators is being maintained at the required level." Despite the fact that]]
PPL entered

IN 2004-20 into their corrective action program for operating experience evaluation (CRs 625137 and 622658), that evaluation did not occur. Enclosure

Analysis: Event 1: The inspectors determined that

PPL [['s failure to ensure that the licensed operator received a biennial medical examination was a performance deficiency. This finding was evaluated using the traditional enforcement process because the failure to determine an operator's medical condition and general health has the potential to impact or impede the regulatory process. Specifically, there was potential for license termination or the issuance of a conditional license to accommodate the medical problems. This operator performed licensed duties during 52 scheduled work shifts as an]]
SRO. Tile
NRC [[notes that the operator was actually qualified the entire time (his follow-up medical examination results were satisfactory), he had not developed any condition that required a license condition and there was no actual impact to his requalification; the fact that the]]
SRO was never the only
SRO being credited to met minimum
TS manning requirement; and the fact that the
SRO 's job performance was satisfactory during the period of the expired physical examination, and these factors will be considered prior to a final severity level determination. Event 2: The inspectors determined that
PPL [['s failure to ensure that the licensed operator received the required vision examination and passed the required visual before assuming licensed reactor operator duties was a performance deficiency. This finding was evaluated using the traditional enforcement process because the failure to determine an operator's medical condition and general health has the potential to impact or impede the regulatory process. Specifically, there was a potential for license termination or the issuance of a conditional license to accommodate for medical problems. This operator perform licensed duties during three scheduled work shifts, which included assuming the role of the refueling]]
SRO during fuel moves for the ongoing dry fuel storage campaign, but he did so with a disqualifying condition that would have required his license to be amended. The
NRC notes that the Fuel Handling
SRO position is a procedurally required position which was performed by a qualified individual; the
SRO had an actual disqualifying medical condition which required an amended license; and the
SRO [['s job performance was satisfactory during three watches he stood with this identified condition, and these factors will be considered prior to a final severity level determination. Each of the two events would be considered violations of the same regulatory standard (10]]
CFR 55.3) and share a common root cause of programmatic issues within
PPL 's licensed operator medical reviews. The finding was determined to have a cross-cutting aspect in the area of Problem Identification and Resolution, Operating Experience, because
PPL did not systematically collect, evaluate, and communicate relevant external operating experience P.2(a). Specifically,
PPL failed to properly evaluate
IN 2004-20 for medical examination issue applicability in accordance with their operating experience review program as evidenced by the
2008 SL -
IV [[]]
NCV (
NRC [[]]
IR 50-387 & 50-388 2008302-01), for an initial licensed operator application submitted to the

NRC with a disqualifying medical condition, as well as these two events in July and August of 2009. Enclosure

Enforcement: Event 1:

10 CFR 55.21 requires, in part, that "a licensee shall have a medical examination by a physician every two years. The physician shall determine that the applicant or licensee meets the requirements of 10
CFR 55.33(a)(1).
10 CFR 55.33(a)(1) states, in part, that the applicants medical condition and general health will not adversely affect the performance of assigned job duties or cause operational errors endangering public health and safety. 10
CFR 55.3 states that, "A person must be authorized by a license issued by the Commission to perform the function of an operator or a senior operator as defined in this part". Contrary to the above, between April 1, 2009, and July 22, 2009,
PPL failed to ensure that the individual licensee, an
SRO , while on shift, was authorized by a license to perform the function of an
SRO , after he failed to have the required two-year medical examination. Specifically, the
SRO performed licensed operator duties 52 times between April 1, 2009, and July 22, 2009, after the deadline for his medical examination had passed. The medical examination may have identified an issue with the
SRO 's medical condition and general health that would have disqualified him from being authorized by a license. Event 2: 10
CFR 55.21 requires, in part, that a licensee shall have a medical examination by a physician every two years. The physician shall determine that the applicant or licensee meets the requirements of
10 CFR [[55.33{a)(1). 10]]
CFR [[55.33(a){1) states, in part, that the applicant's medical condition and general health will not adversely affect the performance of assigned job duties or cause operational errors endangering public health and safety.]]
10 CFR 55.33(b) states, in part, if an applicant's general medical condition does not meet the minimum standards under 10
CFR 55.33(a)(1) the Commission may approve the application and include conditions in the license to accommodate the medical defect.
10 CFR 55.23(b) states in part, when the certification requests a conditional license based on medical evidence, the medical evidence must be submitted to the Commission and the Commission then makes a determination in accordance with 10
CFR 55.33.
10 CFR 55.3 states that a person must be authorized by a license issued by the Commission to perform the function of an operator or a senior operator as defined in this part. Contrary to the above, between August 10,2009, and August 18, 2009,
PPL failed to ensure that the individual licensee, an
SRO , while on-shift, was authorized by a license to perform the function of an
SRO , after he failed a medical examination which identified a disqualifying condition. Specifically, a medical examination conducted on August 10, 2009, identified that the
SRO 's vision did not meet the health requirements stated in
ANSI /ANS 3.4-1983, Section 5.4.5, "Eyes." However, he performed the function of an
SRO [[during three watches with a license that was not appropriately conditioned to that corrective lenses be worn. Each example was evaluated independently using the traditional enforcement process because the failure to determine an operator's medical condition and general health has the potential to impact or impede the regulatory process. Specifically, medical certification and conditional licensing are used by the]]

NRC to ensure health conditions Enclosure

will not adversely affect operator duties or performance. (AV 05000387; 02, Violation of

10CFR 55.3, Senior Reactor Operators Performing Licensed Duties While Not Qualified Due to Medical Examination Issues) Maintenance Effectiveness (71111.120 -3 Samples) a. Inspection Scope Tile inspectors evaluated
PPL 's work practices and follow-up corrective actions for selected structures, systems and components (SSC) issues to assess the effectiveness of
PPL 's maintenance activities. The inspectors reviewed the performance history of those
SSC s and assessed
PPL 's extent of condition determinations for these issues with potential common cause or generic implications to evaluate the adequacy of
PPL 's corrective actions. The inspectors reviewed
PPL 's problem identification and resolution actions for these issues to evaluate whether
PPL had appropriately monitored. evaluated. and dispositioned the issues in accordance with
PPL procedures and the requirements of 10
CFR 50.65, "Requirements for Monitoring the Effectiveness of Maintenance." In addition, the inspectors reviewed selected
SSC classification, performance criteria and goals, and
PPL 's corrective actions that were taken or planned. to verify whether the actions were reasonable and appropriate. Documents reviewed are listed in the Attachment. The following issues were reviewed: Unit 1,
HPCI turbine stop valve failure and previous corrective actions for inadequate preventative maintenance; Multiple failures of
EDG air start system relief valves which caused "A"
EDG unavailability; and Station blackout (
SBO ) diesel generator (DG) unavailability due to radiator coolant leakage. b. Findings Introduction: The inspectors identified a Green
NCV of 10
CFR Part 50, Appendix
B. Criterion
XVI. "Corrective Action," in that,
PPL did not implement timely corrective actions to preclude repetition of a significant condition adverse to quality. Specifically, the actions taken to address the causes of the Unit 1
HPCI stop valve failure to close in 2006 did not prevent the same Unit
1 HPCI [[stop valve from failing to close on August 18, 2009. In both cases, the failure of the stop valve to close rendered this single train high pressure injection system inoperable as it was unable to meet the 30 second injection response time as described in the design basis. Discussion: On August 18, 2009, the Unit 1]]
HPCI stop valve (FV-15612) indicated dual position after performance of the weekly lubricating oil functional check.
FV [[-15612 did not go full closed as expected and was verified to be approximately one inch from full closed. Operations cycled the valve with maintenance personnel present in the field and found that the valve did not operate smoothly when closing. Based on previous history with]]
FV -15612, engineering recommended that the
HPCI system be declared inoperable. Unit 1
HPC r was declared inoperable and the
FV 15612 valve was disassembled and repaired. The failure of
FV -15612 Significantly impacts
HC pr operation because the
HPCI ramp generator resets to idle when the lower limit switch opens (at the full closed indication on Enclosure
FV -15612). Thus,
FV -15612's closure is necessary to prepare the governor to restart the turbine and if
FV -15612 does not fully close, the generator can not reset, and the governor would demand full open when the turbine restarts. This condition greatly increases the probability of an overspeed trip upon turbine start. Historical data from the original
HPCI speed control design reveals that it would be expected to have at least 1 or 2 overspeed trips before the
HPCI governor would be able to control turbine speed. In this condition the
HPCI 30 second design basis response time would not be met. (Ref:
TS 3.5.1.13). Therefore,
HPCI [[was not able to perform its safety function with design limits and was inoperable. In addition, this degraded component also challenges the system protective features {overspeed trip function} which reduces the reliability of the system to function. The safety system remained unavailable for several days as extensive effort was required to repair the component for this type of degradation. Inspectors witnessed some of the maintenance work and observed that there were many physical similarities to the conditions found when this valve was disassembled and repaired following the failure to close in August of 2006. One documented cause for the]]
2006 FV -15612 failure was an observed seal area that is periodically wetted by
HPCI operation and a material which is susceptible to general corrosion and requires periodic replacement to maintain proper operation. In 2006,
PPL [[took the action to replace the rod bushing. However, there were no actions to address the cause and reduce moisture exposure, change or evaluate materials to reduce the susceptibility to corrosion, and no actions to increase component monitoring for moisture or corrosion. The second documented apparent cause for the 2006]]
FV -15612 failure was inadequate preventive maintenance (PM). An administrative error had caused this component to go past the
PM expiration date.
PPL performed the inspections as part of the 2006 repair and recalculated a new due date for the
PM task.
PPL did not change the 10 year interval for maintenance and inspection and did not increase the
PM frequency for this component to more appropriately address this identified apparent cause (inadequate
PM ). The inspectors determined that the limited corrective actions taken following the apparent cause evaluation in 2006 contained in
CR 806988 were a primary contributor to the repeat failure of the
FV -15612 in 2009. In both cases, valve
FV [[15612 failed in the same manner and would not travel to the full closed position. In both cases, the actuator stem to bushing interface was very tight and required the use of pullers and/or hammers during actuator disassembly. For both failures the most likely cause was due to increased friction between the actuator shaft and the rod bushing as a result of corrosion. The inspectors also identified that the corrective action report]]
CR 806988 did not have an effectiveness review plan. The
CR stated that given the long duration of the
PM interval, it would be unreasonable to hold an effectiveness review open for several years. The inspectors reviewed
PPL 's cause evaluation for the August 2009 valve failure, as documented in
CR 1172997. This evaluation described how the leakage through the seat of the Unit
1 HPCI Steam Admission Valve (

HV-155F001) was a contributing cause to the 2009 component failure. The HV-155F001 had chronic through seat leakage for the last decade. Inspectors concluded that this leakage and moisture source was also a contributing factor from 2006, and that more aggressive action to fix the seat leakage which contributed to the corrosive environment would have reduced the probability and/or frequency of the experienced component failure. Enclosure

Analysis: The finding is more than minor because it adversely affected the equipment pE:lrformance attribute of the Mitigating Systems cornerstone objective, to ensure the availability, reliability and capability of equipment that respond to initiating events to prevent undesirable consequences. Specifically, with

FV -15612 unable to fully close, the
HPCI 30 second design basis response time would not be met. Not only did this dE3graded component make the
HPCI [[system inoperable; it also challenged the system protective features (overspeed trip function) which reduced the reliability of the system to function. In addition, the repairs necessary to restore the system required extensive effort and resulted in several days of unplanned unavailability for a single train safety system. The inspectors assessed this finding in accordance with]]
IMC 0609 Attachment 4, "Phase 1 -Initial Screening and Characterization of Findings" and determined the finding to be of very low safety significance (Green) because it did not result in an actual loss of safety function for greater than the
TS [[allowed outage time. The finding was not potentially risk Significant due to seismic, flood, or severe weather initiating events. This finding was determined to have a cross-cutting aspect in the area of Problem Identification and Resolution, Corrective Action Program, because]]
PPL [[did not take appropriate corrective actions to address safety issues in a timely manner, commensurate with their safety Significance and complexity [P.1 (d)]. Specifically,]]
PPL did not take appropriate corrective actions for a significant condition adverse to quality from the 2006 failure of the
HPCI stop valve to prevent the 2009 failure of the same valve. Enforcement:
10 CFR Part 50, Appendix B, Criterion
XVI , "Corrective Action," requires, in-part, for significant conditions adverse to quality, measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition. Contrary to the above,
PPL did appropriately identify several causes but corrective actions following the 2006 valve failure did not prevent repetition of the same
HPCI [[stop valve failure on August 18, 2009. In both cases, the failure of the stop valve to close rendered this single train high pressure injection system inoperable as it was unable to meet the 30 second injection response time as described in the design basis. In 2009 this particular failure also caused several days of unplanned unavailability due to the extensive effort to repair the component. Because the finding is of very low safety significance and has been entered into]]
PPL 's
CAP (CR 710737), this violation is being treated as a Non-Cited Violation (NCV), consistent with Section
VI.A of the
NRC Enforcement Policy. (NCV 05000387/2009004-03, Inadequate Corrective Actions Result in a Repeat Failure of Unit
1 HPCI Turbine Stop Valve). 1 R 13 Maintenance Risk Assessments and Emergent Work Control (71111.13 7 Samples) a. Inspection Scope The inspectors reviewed the assessment and management of selected maintenance activities to evaluate the effectiveness of
PPL 's risk management for planned and emergent work. The inspectors compared the risk assessments and risk management actions to the requirements of
10 CFR Part 50.65(a)(4) and the recommendations of

NUMARC 93-01, Section 11, "Assessment of Risk Resulting from Performance of Maintenance Activities." The inspectors evaluated the selected activities to determine Enclosure

whether risk assessments were performed when specified and appropriate risk management actions were identified. The inspectors reviewed scheduled and emergent work activities with licensed operators and work-coordination personnel to evaluate whether risk management action threshold levels were correctly identified. In addition, the inspectors compared the assessed risk configuration to the actual plant conditions and any in-progress evolutions or external events to evaluate whether the assessment was accurate, complete, and appropriate for the emergent work activities. The inspectors performed control room and field walkdowns to evaluate whether the compensatory measures identified by the risk assessments were appropriately performed. Documents reviewed are listed in the Attachment. The selected maintenance activities included: Unit 1, 2-4

GPM leak on
RWCU filter demineralizer outlet isolation valve emergent work control; Unit 1, Yellow Risk during corrective maintenance on
SBO [[]]
DG concurrent with Unit
1 HPCI stop valve and "B"
EDG jacket water heater failures on August 21; Units 1 and 2, 2A residual heat removal service water (RHRSW) pump inoperable due to loose electrical junction box supports concurrent with Unit
1 RHRSW subsystem inoperable for scheduled maintenance; dual unit 72 hour shutdown limiting condition for operation (
LCO ); Orange equipment out-of-service risk for both Unit 1 and Unit 2 during "A"
EDG outage and emergent "E"
EDG inoperability,
CR 1165553; Replace recirculation/standby gas treatment system (
SGTS ) damper actuator; dual unit 4 hour shutdown
LCO ; Emergent wiring repairs on
ESS transformer
OX 203 in 72 hour
LCO [[; and T20 startup transformer (T20) high voltage bushing replacement and Bus 20 clean and inspect. b. Findings No findings of significance were identified. 1 Operability Evaluations (71111.15 -7 Samples) a. Inspection Scope The inspectors reviewed operability determinations that were selected based on risk insights, to assess the adequacy of the evaluations, the use and control of compensatory measures, and compliance with]]
TS s. In addition, the inspectors reviewed the selected operability determinations to evaluate whether the determinations were performed in accordance with
NDAP -QA-0703, "Operability Assessments." The inspectors used the
TS s, Technical Requirements Manual, Final Safety Analysis Report (
FSAR ), and associated DeSign Basis Documents as references during these reviews. Documents reviewed are listed in the Attachment. The issues reviewed included: Unit 1,
RHR Oivision I, gas entrainment issue; Unit 1, repeat failure of 1 B

RHRSW pump 1ST; Unit 2, '0' main steam line radiation monitor on multiple alarms and work orders; Enclosure

.1 Unit 2,

HPCI operators disabled auxiliary oil pump during surveillance restoration steps on May 16, 2009; Common cause analysis after "C"
EDG [[trip on overspeed; <IE"]]
EDG with failed turbocharger overspeed speed trip circuit,
OFR 1166085; and "0"
EDG ,
ESW piping clamp support on floor,
CR [[1181216. b. Findings No findings of significance were identified 1 Plant Modifications (71111.18 -2 Samples) T,emporary Plant Modifications (1 Sample) a. Inspection Scope The inspectors reviewed a temporary plant modification to determine whether the change adversely affected system or support system availability, or adversely affected a function important to plant safety. The inspectors reviewed the associated system design bases, including the]]
FSAR ,
TS [[s, and assessed the adequacy of the safety determination screening and evaluation. The inspectors also assessed configuration control of the change by reviewing selected drawings and procedures to verify whether appropriate updates had been made. The inspectors compared the actual installation to the temporary modification documents to determine whether the implemented change was consistent with the approved documents. The inspectors reviewed selected post-installation test results to determine whether the actual impact of the change had been adequately demonstrated by the test. Documents reviewed are listed in the Attachment. The following modification and document was included in the review: Unit 1, Temporary Engineering Change 1136133, bypass gas discharge temperature trip on 1 K206B. b. Fr:ndings No findings of significance were identified . . Permanent Plant Modifications (1 Sample) a. Inspection Scope The inspectors reviewed a permanent plant modification to determine whether the change adversely affected system or support system availability, or adversely affected a function important to plant safety. The inspectors reviewed the associated system design bases, including the]]

FSAR, TSs, and assessed the adequacy of the safety determination screening and evaluation. The inspectors also assessed configuration control of the change by reviewing selected drawings and procedures to verify whether appropriate updates had been made. The inspectors compared the actual installation to the permanent modification documents to determine whether the implemented change was consistent with the approved documents. The inspectors reviewed selected Enclosure

post-installation test results to verify whether the actual impact of the change had been adequately demonstrated by the test. Documents reviewed are listed in the Attachment. The following modification and document was included in the review: Engineering Work Request 1086364, T20 H1 bushing replacement. b. Findings No findings of significance were identified. Post-Maintenance Testing (71111.19-6 Samples) a. Inspection Scope The inspectors observed portions of post-maintenance test (PMT) activities in the field to determine whether the tests were performed in accordance with the approved procedures. The inspectors assessed the test adequacy by comparing the test methodology to the scope of maintenance work performed. In addition, the inspectors evaluated acceptance criteria to determine whether the test demonstrated that components satisfied the applicable design and licensing bases and

TS requirements. The inspectors reviewed the recorded test data to determine whether the acceptance criteria were satisfied. Documents reviewed are listed in the Attachment. The
PMT activities reviewed included: Unit 1,
HPCI [[]]
PMT valve exercising,]]
HV 152F0005A and F015A after breaker swaps; Unit 2, reactor core isolation cooling (
RCIC ) pump and flow testing and overspeed trip test following resolution of turbine trip tappet nut alignment,
CR 1146099; Unit 2,
PMT of
PSV [[251 F087 after maintenance to eliminate emergency core cooling system keepfill leakage past valve; and T20 high bushing replacement, tap charger inspection and bus 20 cleaning and inspection. b. Findings No findings of significance were identified. 1 Surveillance Testing (71111.22 -4 Routine Surveillance and 1 1]]

ST Samples) a. Inspection Scope The inspectors observed portions of selected surveillance test activities in the control room and in the field and reviewed test data results. The inspectors compared the test results to the established acceptance criteria and the applicable TS or Technical Requirements Manual operability and surveillance requirements to evaluate whether the systems were capable of performing their intended safety functions. Documents Enclosure

reviewed are listed in the Attachment. The observed or reviewed surveillance tests included: Unit 1, quarterly functional test of reactor vessel water level channels LlS-B21-IN031A, 3B, C, D,

SI -180-203; Unit 2, 1
ST testing of
RCIC pump flow indication from remote shutdown panel; "A"
SGTS filter and absorber leak tests; "D"
EDG full load rejection test,
SE -024-D01; and Monthly operation of
SGTS train "A",
SO [[-070-001. b. Findings No findings of significance were identified. 1 Drill Evaluation (71114.06 -1 Sample) a. Inspection Scope Tlhe inspectors reviewed the combined functional drill scenario (2009 Gold Team Emergency Drill) that was conducted on August 25, 2009, and observed selected portions of the drill in the simulator control room and technical support center. The inspection focused on]]
PPL [['s ability to properly conduct emergency action level classification, notification, and protective action recommendation activities and on the evaluators' ability to identify observed weaknesses and/or deficiencies within these areas. Ten performance indicator (]]
PI ) opportunities were included in the scenario. The inspectors attended the evaluators' post-drill critique and compared identified weaknesses and deficiencies including missed
PI opportunities against those identified by
PPL to determine whether
PPL was properly identifying weaknesses and failures in tbese areas. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified.
RADIAT ION
SAFETY Cornerstone: Occupational Radiation Safety (
OS ) Access Control to Radiologically Significant Areas (71121.01 6 Samples) a. Inspection Scope The inspectors reviewed and assessed the adequacy of
PPL 's internal dose assessment for any actual internal exposure greater than 50 mrem committed effective dose equivalent. The inspectors examined

PPL's physical and programmatic controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools. Enclosure

For high radiation work areas with significant dose rate gradients (factor of 5 or more), the inspectors reviewed the application of dosimetry to effectively monitor exposure to pE!rSOnnel. The inspectors discussed with the radiation protection manager high dose rate-high radiation area, and very high radiation area controls and procedures. The inspectors focused on any procedural changes since the last inspection. The inspectors verified that any changes to

PPL [['s procedures did not substantially reduce the effectiveness and level of worker protection. The inspectors discussed with health physics supervisors the controls in place for special areas that have the potential to become very high radiation areas during certain plant operations. The inspectors determined that these plant operations required communication beforehand with the health physics group, so as to allow corresponding timely actions to properly post and control the radiation hazards. The inspectors verified adequate posting and locking of entrances to high dose rate-high radiation areas, and very high radiation areas. The inspectors evaluated]]
PPL 's performance against the requirements contained in
10 CFR 20 and Plant Technical Specification 5.7. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified. 20S2
ALARA Planning and Controls (71121.02 -3 Samples) a. Inspection Scope The inspectors obtained from
PPL a list of work activities ranked by actual/estimated exposure that are in progress or that have been completed during the last outage and select the 2 work activities of highest exposure significance (in-vesse
IISIII VVI and
EPU alternate decay heat removal modification). The inspectors reviewed
PPL [['s method for adjusting exposure estimates, or re-planning work, when unexpected changes in scope or emergent work are encountered. The inspectors evaluated whether adjustments to estimated exposure (intended dose) were based on sound radiation protection and]]
ALARA principles or just adjusted to account for failures to control the work. The inspectors evaluated

PPL's performance against the requirements contained in 10 CFR 20.1101. Documents reviewed are listed in the Attachment. Enclosure

b. Findings Introduction: A self-revealing Green finding was identified due to a deficiency in the area of maintaining occupational radiation exposures

ALARA. Work performance involving the
IWI /ISI during the Unit 2 14th Refuel and Inspection Outage was less than adequate resulting in collective exposure for the work to expand from 5.00 person-rem to 11.04 person-rem. Description: The
IWI /
ISI dose overrun was primarily due to the utilization of inexperienced contract workers to perform the task. The contractor selected by
PPL utilized workers for major
IWIIIS . Actual hours to perform these tasks with the inexperienced workers were over 5000 hours0.0579 days <br />1.389 hours <br />0.00827 weeks <br />0.0019 months <br />. The original exposure estimate was 5.00 person-rem. When compared to the actual work activity exposure of 11.04 person-rem, the results were 120 percent greater than the exposure estimate. Analysis: Inadequate work planning that resulted in significant unplanned collective exposure was a performance deficiency which was reasonably within]]
PPL [['s ability to foresee and correct and which should have been prevented. Specifically, the original exposure estimate was 5.00 person-rem. When compared to the actual work activity exposure of 11.04 person-rem, the results were 120 percent greater than the exposure estimate. The finding is more than minor because the issue involved actual collective exposure greater than 5 person-rem that was greater than 50 percent above the estimated or intended exposure and the dose overrun was due to activities within]]
PPL [['s control. This issue is similar to the greater than minor examples provided in Appendix E of Manual Chapter 0612. Further, the performance deficiency is associated with the radiation safety cornerstone attribute of the program (ALARA planning) and adversely affected the cornerstone objective to ensure adequate protection of worker health and safety from exposure to radiation. The finding was evaluated in accordance with]]
IMC 0609, Appendix C, "Occupational Radiation Safety Significance Determination Process." The inspectors determined that the finding was of very low safety significance (Green) because: (1) it involved an
ALARA planning issue, and (2) the 3-year rolling average collective dose history was less than 240 person-rem (107 person-rem annual exposure for 2005-2007). This finding was entered into
PPL 's
CAP (CR 1140623 and 1137835). This finding was determined to have a cross-cutting aspect in the area of Human Performance, Resources, because
PPL did not utilize sufficiently qualified personnel to assure occupational radiation safety requirements were met H.2(b). Specifically,

PPL's use of inexperienced contract workers resulted in additional collective exposure that could have been avoided. Enclosure

Enforcement: Enforcement action does not apply because the performance deficiency did not involve a violation of regulatory requirement. The

ALARA rule contained in 1(I
CFR 20.1101 (b) Statements of Consideration indicates that compliance with the
ALARA [[requirement will be judged on whether the licensee has incorporated measures to track and, if necessary, to reduce exposures and not whether exposures and doses represent an absolute minimum or whether the licensee has used all possible methods to reduce exposures. The overall exposure performance of the nuclear power plant is used to determine compliance with the]]
ALARA rule. Since
SSES is below the year-rolling-average of 240 person-rem and
PPL has an established
ALARA program to reduce exposure consistent with the statements of consideration for 10
CFR [[20.1101, no violation of regulatory requirements [10]]
CFR [[20.11 01 (b)] is considered. Because this finding does not involve a violation of regulatory requirements and has very low safety significance, it is identified as (]]
FIN [[05000388/2009004-04, Failure to Maintain Occupational Radiation Exposure as Low as Reasonably Achievable during the Unit 2 Refueling Outage) 20S3 Radiation Monitoring Instrumentation (71121.03 -1 Sample) a. Inspection Scope The inspectors verified the calibration, operability, and alarm setpoints of several types of instruments and equipment. Verification methods included: review of calibration documentation and observation of]]
PPL [['s source check or calibrator exposed readings. The inspectors reviewed the detector measurement geometry, calibration method and appropriate selection of calibration sources to closely represent the actual measurement conditions in the plant. The inspectors observed electronic and radiation calibration of these. The inspectors reviewed the alarm set point determinations and observed in-field source checks. The inspectors determined what actions were taken when, during calibration or source checks, an instrument was found significantly out of calibration (>50 percent). The inspectors determined the possible consequences of instrument use since last successful calibration or source check. The inspectors determined if the out of calibration result was entered into the]]
CAP. During an on-site visit, the inspectors reviewed calibration data, quality assurance (QA) data and National Voluntary Laboratory Accreditation Program audits and intercomparison test data for
PPL 's personnel dosimetry laboratory located in Allentown. The inspectors evaluated
PPL 's performance against the requirements contained in
10 CFR 20.1501,10

CFR 20.1703 and 10 CFR 20.1704. Documents reviewed are listed in the Attachment. b. Findings No findings of significance were identified. Enclosure

.1

OTHER [[]]
ACTIVI TIES Performance Indicator Verification (71151 -8 Samples) Injtiating Events Inspection Scope The inspectors reviewed
PPL 's
PI data for the period of August 2008 through August 2009 to verify whether the
PI data was accurate and complete. The inspectors examined selected samples of
PI data,
PI data summary reports, and plant records. The inspectors compared the
PI data against the guidance contained in Nuclear Energy Institute 99-02, "Regulatory Assessment Performance Indicator Guideline." Documents reviewed are listed in the Attachment. The following
PI s were included in this review: Units 1 and 2 unplanned scrams per 7000 critical hours (
IE 01); Units 1 and 2 unplanned power changes per 7000 critical hours (IE03); Units 1 and 2 unplanned scrams with complications (IE04); Common Occupational Exposure Control Effectiveness (OR01); and Common
RETS /
ODCM [[Radiological Effluents (PR01) No findings of significance were Identification and Resolution of Problems (71152 -1 Sample) Review of Items Entered into the Corrective Action Program Inspection Scope As specified by Inspection Procedure 71152, Problem Identification and Resolution, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed screening of all items entered into]]
PPL 's
CAP. This was accomplished by reviewing the description of each new action requesUcondition report and attending daily management meetings. No findings of significance were identified . Annual Sample: Review of
PPL 's Progress in Implementing Corrective Actions to Address General Work Environment and Potential Chilling Effect Concerns Inspection Scope The inspectors performed a detailed review of
PPL 's corrective actions associated with the Root Cause Analysis (RCA) conducted in response to the
NRC 's Potential Chilling Effect (

PCE) letter of January 28, 2009 and the associated action plan. The inspectors reviewed the RCA, the general work environment action plan, Employees Concern Enclosure

Program (ECP),

QA documents, and selected reference
RCA documents. The inspectors also reviewed the corrective action schedules and reviewed completed corrective actions such as revised procedures, training material, and records. The inspectors also conducted interviews with site
ECP and
QA [[personnel, and several focus groups consisting of workers and supervisors from the Security, Work Management, Health Physics, and Operations Departments. These interviews were performed in order to assess how the staff viewed the effectiveness of the corrective actions to date in addressing the general work environment. The inspectors also assessed]]
PPL 's longer term action plan items by verifying action item entries in the
CAP as well as through interviews of responsible personnel. b. Findings and Observations No findings of significance were identified. Background: On January 28, 2009, the
NRC issued a
PCE letter advising
PPL of concerns related to the safety conscious work environment (
SCWE ) at
SSES and requested
PPL provide: (1) a description of
PPL 's current action plans to address existing
SCWE concerns to preclude a chilled work environment at
SSES ; (2)
PPL plans for further evaluating the health of the
SCWE at
SSES ; and (3) the metrics
PPL intended to monitor to determine the effectiveness of their actions and ensure a
SCWE at
SSES (
ML 090280115). Also, on January 28, 2009, the
NRC issued
SSES -NRC Integrated Inspection Report 05000387/2008005 and 05000388/2008005 (ML090230434) which described the
SCWE concerns at
PPL and provided additional background.
PPL completed their formal
RCA of the work environment issues in May 2009. The
NRC 's review of that
RCA is documented in
NRC Integrated Inspection Report 05000387/2009003 and 05000388/2009003 (
ML 092230158). Root Cause Analysis Corrective Actions The inspectors determined that the corrective actions developed by the
RCA [[team to address the root cause and causal factors were being appropriately scheduled and that the actions were being completed in accordance with that schedule. The time frame for completion of these scheduled actions was also determined to be appropriate. Any changes to the schedule required a review by the Management Review Committee and approval by senior management. Corrective actions completed to date included the roll out of the]]
RCA through formal site presentations and small group discussions, the establishment of two methods for workers to raise an anonymous concern (Safety Hotline and anonymous generated
CR [[s), developing training materials and case studies related to work environment issues and conducting this training with all first line supervisors and positions above, and revising several procedures. The training was well received by plant personnel and the new anonymous concern processes was being utilized by plant personnel. In addition, several organizational changes were made including the arrival of the new e]]
NO in July 2009, the establishment of a plant manager position, restructuring to have
QA ,

ECP, and Regulatory Affairs directly reporting to the CNO, and the selection of several new personnel for key management positions. The inspectors observed that these changes were well communicated to the site and generally have been well Enclosure

received. Most personnel interviewed felt the organizational changes were appropriate and the personnel selected were a good fit for their new positions. These changes have allowed progress to be made in re-establishing trust between the workers and upper management and improving the general work environment. Employee Concerns Program Another corrective action from the

RCA was to evaluate and make changes to the
ECP. A strong
ECP is a pillar of a successful safety culture. However, in the past at
SSES , the
ECP was not seen by many plant employees as a viable and effective program. During the third quarter 2009,
PPL restructured the
ECP program by eliminating the Ombudsman position and hiring an additional
ECP representative who was full time on-site at
SSES. The inspectors interviewed
ECP representatives and discussed the
ECP program re-organizations with each of the focus groups. The inspectors concluded that
PPL did a good job communicating the changes in the
ECP program to the site. All groups interviewed knew who the new
ECP representative was and were aware that the Ombudsman position had been eliminated. Most had a positive impression and an inherent level of trust for the new on-site
ECP representative selected. In addition, corrective actions were completed changing the organizational reporting requirements, taking the
ECP program out to the line organization and making it a direct report to the
CNO. However, additional organizational changes in the
ECP Oversight Team remain to ensure that the
ECP process is viewed by the workforce as a viable alternative for issues. See
NRC [[Integrated Inspection Report 05000387/2009003 and 05000388/2009003 (ML092230158) for further details on this concern. Challenges: The inspectors identified two upcoming challenges which have the potential to impact the general work environment. The first challenge will be the implementation of the]]
NRC Fatigue Rule (10
CFR [[26 Subpart I) which went into effect October 1,2009. The inspectors observed that the plant had done a good job communicating the new rule, and had done a good job working with the departments most heavily impacted (Operations and Security); however, several workers and supervisors interviewed expressed uncertainty as to how the rule will be implemented and what will be the true impact.]]
PPL [[acknowledged it was slow in engaging the bargaining unit regarding potential shift rotation adjustments in the Health Physics Department, which was a concern to the mc:ijority of the Health Physics personnel interviewed. In a similar note, the upcoming collective bargaining unit negotiations have the potential to impact the general work environment. Assessment During the 3rd quarter of 2009,]]
PPL made reasonable process in implementing their action plan and
RCA corrective actions to address the general work environment at
SSES. Based on interviews with a sample population of site employees, the actions to date have been well received and are making a positive impact on the general work environment at
SSES. Overall, the workers stated they were cautiously optimistic that changes were being implemented; however, they acknowledged that significant work remained to be done and several Significant challenges still need to be addressed. The

NRC plans to continue monitoring PPL's progress in this area. Enclosure

.1 40A5 Other Activities Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. b. Findings No findings of Significance were identified . . 2 Independent Spent Fuel Storage Installation (60855 and 60855.1) a. Inspection Scope The inspectors observed selected activities associated with loading of a dry cask canister to ensure that

TS s were met and equipment operated properly. The inspectors reviewed documents and records associated with the operation of the
SSES [[independent spent fuel storage installation (ISFSI), including training records for personnel involved with loading of a dry cask canister. A list of the documents reviewed is provided in the Supplemental Information section. The inspectors met with reactor engineering personnel to review the fuel selection process and associated documentation. The inspectors discussed how the cask loading computer program is created for each cask loading. The video recording of the fuel bundles placed into the canister was reviewed to ensure that each bundle was placed into the proper location. The inspectors observed work activities on the refuel floor associated with the fuel selection, loading of fuel into the cask, vacuum drying, welding, and moving of the loaded canister to the truck bay. b. Findings No findings of significance were identified. However, the inspectors did identify an issue regarding compliance with procedure]]
MT -
GM -014, "Rigging and Lifting Equipment Inspection." This procedure references
ASME [[code 830.9-2003, "Slings." Both documents require that slings are to be inspected annually. While the licensee also performs an inspection of each sling prior to use in accordance with the same procedure, the pre-job inspection does not meet the annual inspection requirement. Inspectors noted that when synthetic slings used in dry cask storage are inspected by]]
PPL they receive an August 5th due date sticker for the following year, regardless of when they are inspected in the current year. This presented a potential for a sling to exceed its annual inspection based on the annotated date.
PPL entered this issue into their corrective action program under

CR 1173698, "SSES Rigging Committee review of procedural guidance." The licensee's extent of condition review did not identify any slings used in safety related activities which had actually exceeded the annual inspection criteria. As a result, this issue was determined to be of minor significance and a violation of minor significance that is not subject to enforcement action in accordance with the NRC's Enforcement Policy. However, for assessment purposes, this issue does Enclosure

.3 illustrate a weakness in

PPL 's Corrective Action Program because it did not identify a non compliance with a regulatory requirement. Operation of an
ISFSI at Operating Plants (60855) a. Inspection Scope The inspectors verified by direct observation and independent evaluation that
PPL had performed loading activities at the
ISFSI in a safe manner and in compliance with applicable procedures. This included observing the loading of one canister of spent fuel into the
ISFSI on August 10, 2009. The inspectors verified by direct observation that radiation dose and contamination levels were within prescribed limits after a dry cask storage system container had been installed at the
ISFSI. b. Findings No findings of significance were identified. 40A6 Meetings, Including Exit On August 14, 2009, the health physics inspector presented inspection results to Mr.
C. [[Gannon and other members of his staff, who acknowledged the findings. The inspector confirmed that proprietary information was not provided or examined during the inspection. On August 21,2009, the health physics inspectors presented inspection results to Mr. C. Gannon and other members of his staff, who acknowledged the findings. The inspectors confirmed that proprietary information was not provided or examined during the inspection. On October 9,2009, the resident inspectors presented their findings to Mr. T. Rausch, and other members of his staff, who acknowledged the findings. The inspectors confirmed that proprietary information was not provided or examined during the inspection. 40A7 Licensee-Identified Violations The following violation of very low safety significance (Green) was identified by]]
PPL and is a violation of
NRC requirements which meets the criteria of Section
VI of the
NRC Enforcement Policy,
NUREG -1600, for being dispositioned as an
NCV On 25 August 2009, while performing pre-start checks to place Unit 2
RHR in suppression pool cooling, a field operator identified the
ESW cooling water valves 211193 and 211194 to be unlocked and closed. These valves are required to be locked open to assure supply of cooling to a Unit 2
RHR room cooler and 2C
RHR pump motor oil cooler. This was an identified violation of
TS 5.4.1, and a violation of those procedures that must be implemented for operation of the unit and for the performance of maintenance as delineated in Regulatory Guide 1.33. Contrary to
NDAP -

QA-0302, "System Status and Enclosure

Equipment Control,"

PPL did not use a proceduralized method to maintain status control of these valves and contrary to
NDAP -QA-502, "Work Control Process," these valves were not returned to the original design configuration following maintenance.
PPL determined that the status control of these valves was most likely lost during the post-modification testing performed in late April 2009. Upon discovery, the valves were promptly aligned to provide cooling flow and the performance issue was captured in
CR 1174837. Using a Phase
III risk evaluation model, the region staff determined this finding to be of very low safety significance (Green).
AITACH MENT:
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION Enclosure
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]
CONTAC T Licensee Personnel
N. D'Angelo, Manager, Station Engineering R. Doty, Radiation Protection Manager T Iliadis,
GM -Nuclear Operations
S. Ingram, Dosimetry Supervisor R. Kessler, Health Physicist -
ALARA [[]]
A. Klopp, Heat Exchanger Program Engineer D. Leimbach, Eddy Current Level
III , In-service Inspection
R. Pagodin,
GM -Nuclear Engineering
G. Ruppert,
GM -Work Management
S. Davis, Fire Protection Program Engineer
LIST [[]]
OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
AND [[]]
DISCUS SED Opened 05000387; 388/200900402 Violation of
10CFR [[55.3, Senior Reactor Operators Performing Licensed Duties While Not Qualified Due to Medical Examination Issues (1 R11.2) Opened/Closed 05000388/200900401 Failure to Implement and Maintain the Fire Protection Program with Respect to the Use and Storage of Combustibles in the Control Structure (1 R05) 05000387/200900403 Inadequate Corrective Actions Result in a Repeat Failure of Unit 1]]
HPCI Turbine Stop Valve (1R12) 05000388/200900404 Failure to Maintain Occupational Radiation Exposure As Low As Reasonably Achievable during the Unit 2 Refueling Outage (20S2) Attachment
BASELI [[]]
NE [[]]
INSPEC [[]]
TION [[]]
PROCED [[]]
URE [[]]
PERFOR [[]]
MED [[]]
LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]
ED (Not Referenced in the Report) Section 1 R04: Equipment Alignment Condition 1168300, 1175048, 1176331,
OP -225-001, Containment Instrument Gas System. Revision
CL [[-225-0012, Unit 2 Containment Instrument Gas Mechanical, Revision M-2126, Unit 2 Containment Instrument Gas Sheets 1 and 2, Revision 33 and M-157, Unit 1 Containment Atmosphere Control, Revision 47 M-134, A-D Diesel Auxiliaries Fuel Oil, Lube Oil. Air Intake and Exhaust and Jacket Water Cooling System. Revision 45 Engineering Work Request:]]
EWR 1168578 Other: Chemistry Analysis and Sample Results Attached to
CR 1167146 Drainage Contour Map, Potentiometric Surface Contours Overburden Monitoring Wells August/September 2008 Section 1 R05: Fire Protection Condition Reports: 1172702 Procedures:
FP -113-113, Containment Access Area (1-401, 1-404, 1-405) Fire Zones 1-4A-N, S, W, Elevation 719'-0", Revision 6

FP-013-168, Equipment and Battery Rooms Unit 1 West Side (C-605, 606, 600,601,607) Fire Zones 0-28B-11, 0-28K, 0-28L, 0-281, Elevation 771'-0", Revision 5 FP-013-169, Equipment and Battery Rooms Unit 1 East Side (C-604, 602, 603, 608) Fire Zones 0-28B1, 0-28M, 0-28N, 0-28J, Elevation 771'-0", Revision 4 Attachment

Section 1 R06: Flood Protection Measures Condition Reports: 1121942,1171337,1172365,and606589 Work Order: 606837 Section 1 R07: Heat Exchanger Performance Condition Reports and Action Requests: 1003096,915409,984635,1136415,1153052, 1178867, 1095358, 1109759, 1172704,892305, 1095358,1109759,1162322,1084289, 1162414, 1108376, and 1044430 Procedures: H-1001, Heat exchanger tube cleaning, Revision 5 H-1004, Heat exchanger inspection and condition assessment, Revision 6 H-1005, Eddy Current Examination Services, Revision

6 NDAP -
QA -0504, Heat Exchanger Program, Revision
4 TP -149-079,
RHR Heat Exchanger Performance Test, Revision1
ER -
AA -340,
GL 89-13 Program Implementing Procedure, Revision 4
ER -AA-340-1001,
GL 89-13 Program Implementation Instructional Guide, Revision 6
ER -AA-5400, Buried Pipe and Raw Water Corrosion Program Guide, Revision
1 ER -
AA -5400-1001, Raw Water Corrosion Program Guide, Revision
0 ER -
AA -5400-1002, Buried Piping Examination Guide, Revision 1 Limerick
GL 89-13 Program Basis Document, Revision 0
CY -LG-120-828, Clam Control Activities, Revision
5 CY -
LG -120-1102, Outside Chemistry/NPDES related Sampling and analysis schedule, R:evision
18 CY -
LG -120-1117, Spray Pond Chemistry Guide, Revision
2 ST -2-011-390-0,
ESW /Diesel Generator Heat Transfer Test, Revision 4 M-011-001,
LGS Preventive Maintenance Procedure for Diesel Generator Heat Exchanger Cleaning and Examination, Revision12 Standing work order R0920468-01,
EDG heat exchangers Drawings Drawing # M-109/E106214, Service Water System, Revision 50, Drawing # M-111/E106216, Emergency Service Water System, Revision 48 Drawing # M-112/E106217,
RHR Service Water System, Revision 47 Drawing # M-120/E106225, Diesel Oil Transfer System, Revision 32
SIM -M-12, Emergency Service Water!
RHR s Area, Revision 14 8031-E-'1046, Cathodic Protection Plan -]]
PCMU ,
RHR &

ESW Piping, Units 1 & 2, Revision 14 Unit 2 RHR Heat Exchanger Assembly & Cross Section Drawings, April 1972 Attachment

Work Orders: 796290, 796291,2E205A,889724,888029,OE505A1&2, 1078542,808322,OE505E1&2, 889732,889516,OE506A, 1111425, 1067871,OE506E,916733,889717,OE507A, 1111426, 1067872,OE507E,941280,889240 Miscellaneous Documents Regulatory Guide 1.27, Ultimate Heat Sink for Nuclear Power Plants, dated January Generic Letter 89-13 and Supplement 1, Service Water System Problems Safety-Related Equipment, Dated July

1989 PPL responses to
GL 89-13, dated Feb. 23,1990, through Feb. 12, 1997, et al Spray Pond Inspection Report, November 13, 2007 Zebra Mussel & Asiatic Clam Survey, November 6,
2007 ECT Test Report for Heat Exchanger 2A-E205, March 2005
WO R0966553, Clean and eddy current test 2A-E205, performed May 19,
2005 IC -C-11-02021, Testing of Cathodic Protection System, performed September 4, 2007
RT -1-012-390-0,
RHR Heat Exchanger Heat Transfer Performance Computation Test, performed Feb. 15, 2005
RT -2-011-251-0,
ESW Loop A Flow Balance, Rev. 15, performed April 26, 2008
RT -6-012-390-2, 2A-E205 Heat Exchanger Heat Transfer Test, performed Feb. 9,
2005 RT -6-109-001-0, Cathodic Protection Monthly Inspection, performed September 4, 2007
ST -1-012-901-0, Spray Pond Structural Inspection, performed September 5,2002, August 10, 2003, August 10, 2005, and July 27,2007
ST -6-011-231-0, A Loop
ESW Pump, Valve, and Flow Test, performed May 9,2008, and August 8,
2008 ST -6-012-232-0, A Loop
RHRSW Pump, Valve, and Flow Test, performed May 16, 2008, elnd August 7,2008 Structural Integrity Associates, Inc., Limerick
ESW /
RHRSW Pre-Outage Support, May 7,2008 Nuclear Event Report
NC -07-044, Essential Service Water Piping Degradation, Rev. 0 & 1 Operational Event Review -Degradation of Essential Service Water Piping, January 15, 2008 Technical Evaluation -Cumulative Leakage from the
ESW System (CR 714581-02) Technical Evaluation
EDG Permissible Fouling Factors as a Function of
ESW Flow and Plugged Tubes (IR 691841) Apparent Cause Evaluation -Internal Corrosion of
RHRSW System Piping (
CR 731389) Apparent Cause Evaluation -Increased Frequency of
ESW Throttle Valve Silting (11/14/05) Apparent Cause Evaluation -Diesel Heat Exchanger
GL 89-13 Heat Transfer Test Performed Too Soon After Cleaning (CR 174574)
RHRSW Pipe Minimum Wall Thickness Action Plan (
IR 693495-32) 1 D-G501,
EDG Heat Exchanger Inspection Report, June 23, 2008 2D-G501,
EDG Heat Exchanger Inspection Report, December 10,2007
LG 96-02349-000, Undersized Lube Oil Cooler
LG 01-0'1096-000,
LGS Unit 1 & 2
GL 98-13 Program Recommendation -Heat Exchanger Cleaning
LG 01-00968-000, Final Report on
DG Heat Exchanger Performance Tests
GL 89-13 Calculation
LM -0225, Performance Curve for
EDG Heat Exchanger for
GL 89-13 Engineering Analysis
LEAM -0007, Emergency Diesel Heat Exchanger Performance Tests
GL 89-13, September 10, 2001. Evaluation of 0-22
EDG Heat Exchanger Performance Test of August 26, 2003 Evaluation of 0-22

EDG Heat Exchanger Performance Test of July 24,2004 Attachment

Evaluation of lube oil cooler fouling factor increases in winter, October 1, Commitment Change Evaluation

ECR [[]]
LG 96-02349, Undersized Lube Oil
ECR [[]]
LG 01-01096,
GL 98-13 Program Recommendation Heat Exchanger
ECR [[]]
LG 01-00968, Final Report on
DG Heat Exchanger Performance Tests
GL [[]]
ECR [[]]
LG 04-00433, Licensing Basis of
RHRSW Summary of
RHRSW /
ESW Valve Pit Other: Station Health Reports for
RHR and
EDG Systems: 2009, 1st period -Jan 1 -May 2008, 151 period -Jan 1 -Apr. 2nd period -May 1-Aug. 3rd period -Sept 1 -Dec. 2007, 1sl period -Jan 1 -Apr 2ndperiod -May 1 Aug 3rd period Sept 1-Dec Eddy Current Testing Final Reports 1E205B** 1B
RHR Hx, 2E205A -1A
RHR Hx,
OE 505 -Ai, A2, E1, E2,
OE 505,
OE 506 A, E,
OE 526 E,
OE 507 A, E
ESSW Spray Pond Dive Inspection Report Ecology
III , Inc. report dated 3 August 2009
SO -054-A03, Quarterly
ESW flow verification -Loop A, February 23, 2005 and November 24, 2004
SO -054-803, Quarterly
ESW flow verification -Loop B, February 16, 2005 and November 17, 2004
TP -054-076,
ESW flow balance, September 24, 2004 Chemistry Matrix Ch-054-001 (
ESW ), Revision 23, March 05, 2008 Design Calculations
CALC [[]]
EC -CHEM-1018, Justification for the Assurance of Adequate Heat Removal Capabilities, Revision
5 CALC [[]]
EC -054-0537,
ESW System Heat Load and Flow Rate Requirements for Updated Power Conditions, Revision 5
CALC -049-1001,
RHR Heat Exchanger Performance at 8000 gpm
RHR Flow, Revision 5 Section 1R11: Operator Re-qualification Program Condition Report: 1159194,1173155,1173182,622658,625137,389555,1166686 Procedures:
ON -164-002, Loss of Reactor Recirculation Flow, Revision 28
ON -178-002, Core Flux Oscillations, Revision 14 Attachment
ON -100-101,
SCRAM ,
SCRAM Imminent, Revision
EO -000-113, Level/Power Control, Revision
EO -000-102,
RPV Control, Revision
NDAP -
QA -0725, Operating Experience Review Program, Revision Other:
OP 002-09-06-01, Simulator Scenario, Revision 0 Section 11R12: Maintenance Effectiveness Condition Report: 1172458,1173175,1173454,1173859,1174337 Procedure:
ES -002-001, Supplying
125 VDC Loads with Portable Diesel Generator, Revision 12 Work Orders: 1172466,1172530 Section 1R13: Maintenance Risk Assessments and Emergent Work Control Condition 1162039,1172088,1171760,1171814, 1171764,and
MT -GE-030,
ITT Damper Hydramotor Model
NH 91
NH 93 Overhaul, Revision
OI -AD-029, Emergency Load Control, Revision
MT -
GE -030,
ITT Damper Hydramotor Model
NH 91 and
NH 93 Overhaul, Revision E-102, Sheet 17,
ESS Transformer 101R201 Isolating Relay Control, Revision 13 E-102, Sheet 17 Circuit Breaker
DA 10406 Control, Revision 11 M-144, Sheet 2, Reactor Water Clean-Up, Revision 11 M-144, Sheet 1, Reactor Water Clean-Up, Revision 41 E6-8, sheet 1,
ESS Trans
EX 201 and
OX 203, Revision
8 VC -175, Heating, Ventilation and Air-Conditioning Control Diagram
SBGT System, Revision 31 M-145, Sheet 1, Clean-up Filter Demineralizer, Revision 21 Work Order: 1162052 and 828214 Other: Attachment
2009 RFM Daily Status Report August 3-4,2009 -Cask 53 Section 1 R15: Operability Evaluations Condition Reports: 1159448,1159214,1159461,478425,794697,478350, 1160418, 1160653, 1112465, 1147886,1145418,1152053,1152076,1161825, 1162050, 1172110, and
FSAR [[]]
TRO J-412, Sheet 6,
RHR [[]]
SW Pump Discharge Pressure, Revision M-134, Sheet 3, A -D Diesel Auxiliaries Starting Air System, Revision Work Engineering Work
EWR 10M 183-2,
KSV Diesel Generator Instruction Manual, Revision Section 1 R18: Permanent Plant Modifications Condition 1179204,1179788,1179777,1178870,1136097, 1136107, 1136188,
FSAR 9.4.2.2,9.2.12.3, Table
TRO 3.8.6 and

LA-1K206B-001, 1K206B Reactor Building Chiller B Safety Indicator Panel, Revision M310-245, Sheet 2, Chiller 1K206B, Revision Work Attachment

Engineering Work Request:

EWR 1086364
TEC 1136133, Bypass Gas Discharge Temperature Trip on -IK206B Other: 10M 694, Type
SL Core Form Substation Transformer Type
UTT -B Load Tap Changer Spare Startup Transformer, Revision 2 Section '1 R19: Post-Maintenance Testing Condition Reports: 1079703" 1161553, 1174414, 1174403, 1177692, 1177906, 1183410 Procedures:
SO -151-014, Core Spray System Cold Shutdown Valve Exercising, September 28,2009, Revision 16
SO -151-A04, Quarterly Core Spray Valve Exercising Division I, September 28,2009, Revision
9 SO -152-006, High Pressure Coolant Injection Comprehensive Flow Verification, Revision 8
SO -158-001, "Weekly Manual Scram Control Switch Functional Check," Revision
12 OP -003-003, Startup Bus 20 (
OA [[104)fr20 Outage and restoration, Revision 1 Drawing 9220248, Connection Diagram Hydraulic Control Unit, Revision 3 10505411, Box and Cables Hydraulic Control Unit, Revision 3 105D5634, Connection Diagram Hydraulic Control Unit, Revision 2 922D234, Assembly Electrical box, Revision 3 E-157, Sheet 3, Trip Signals to hydraulic control unit Unit 1, Revision 7 Sheet 12, Elementary Diagram Reactor Protection System, Revision 13 Work Orders: 1046829., 1177693, 1012176 Engineering Work Reguest:]]
EC 1100766, Generic
ECO 480V MCC Bucket Replacement Section'1R22: Surveillance Testing Condition Reports: 10419999,1159516, 1159518,1159520,1176579,917309,1041999, 1176718,1176719 Procedures: Attachment
SE -070-A09, "A"
SGTS [[]]
HEPA Filter and Charcoal Adsorber in-Place Leak Test, Revision 5
MT -GM-076, Operations of the Aerosol Detector and Aerosol Generator for Testing
HEPA Filters, Revision 3
MT -GM-077, Operation of the Halide Detector and Halide Generator for Testing Charcoal Filters, Revision
4 SI -250-312, 24 Month calibration of
RCIC System Pump Flow Channel
FT -E51-2N003 Remote Shutdown
SE -150-004,
RCIC Functional Test at 1C2014, January 21,2008, Revision
SE -100-008,
RCIC Functional test at Remote Shutdown Panel, Revision
SE -200-008,
RCIC Functional test at Remote Shutdown Panel, January 21, 2009, Revision
SE -100-011,
HV 143F023B, Functional Test at 1C2014, March 5, 2008, Revision Work Orders: 875249,1130776 Drawing:
VC -175, Sheet 3,
HVAC Control Diagram
RB [[]]
SGTS , Revision 31 E-201, Sheet 9,
SGTS Dampers
HD -0755A &B, Revision 17 E-154, Sheet 3,
RCIC Outboard Steam Line Isolation Valve Unit 1, Revision 18 E-154, Sheet 22,
RCIC Outboard Steam Line Isolation Valve Unit 2, Revision 5 E-149, Sheet 6, Remote Shutdown Panel 2C201, transfer Switches Unit 2, Revision 9 Section 1
EP 6 Drill Evaluation Condition
EP -
TP -001,
EAL Classification Levels, Revision August 25,2009 Drill Results Section 20S1: Access Control to Radiologically Significant Areas Condition 1168353; 1167515; 1167427; 1162310; and Section 20S2:

ALARA Planning and Controls Condition 1155780; 1153396; and Section 20S3: Radiation Monitoring Instrumentation Attachment

Quality Assurance Internal Audit Reports: 665555; 819260; and

1093653 NIST [[]]
NVLAP On-Site Assessment Report, March 13,2009 Personnel Dosimetry Performance Testing Quarterly Report, 4th Quarter 2007 Section 40A1: Performance Indicator Verification
NDAP -
QA [[-0737, Reactor Oversight Process Performance Indicators, Revision Operator Logs, Unit 1 and Unit Section 40A2: Identification and Resolution of Problems Condition Reports: 1159518, 1159523, 1160653, 1161370, 1161398, 1162307, 1168487, 1168500, 1172365, 1173445,1173454,1174011,1174052,1174964,1175030, 1175048, 1175140, 1175332, 1175332, 1176331,1176959,1177165,1177499,1177965,1178870, 1179656, 1179995, 1027040,1044490,1073866,1114121,1128499, 1147908, 1148761,1148762,1148765, 1148790,1148824,1148828,1148834,1148851, 1148852, 1148853, 1148854, 1148859, 1148862,1148879,1148884,1148887,1148891, 1148895, 1148900,1157872,1158039, 1162998,.1173604,1173611,1173614, 1173619,1173697, 1181243 Engineering Work Request: 1161370 Procedures:]]
NDAP -00-0109, "Employee Concerns Program", Revision 13
NDAP -QA-0702, "Action Request and Condition Report Process", Revision
23 NRC Letter-
EA -09-003, Work environment Issues at
SSES -
PCE , dated January 28,
2009 PPL Lettt:3r
PLA -6486,
SSES [[]]
NRC Request to Address Work Environment Issues at
SSES , dated February 27, 2009
PPL Letter
PLA -6489
SSES [[]]
NRC Request to Address Work Environment Issues at
SSES , dated March 13,
2009 PPL Letter
PLA -6528
SSES [[]]
PPL Susquehanna
LLC Work Environment Improvement Plan, dated June 23, 2009
SSES Organization chart dated 9/10/2009
SS [[]]

ES Concerns Hotline flyer Attachment

Safety Conscious Work Environment Trending Survey November 2008, Revision 0 General Work Environment-PCE Power Point Presentation, dated June 15, 2009 Communication Plan for Work Environment Root Cause Analysis report, dated June 3,

2009 USNRC Allegation Website allegation data from January 2005 -August 2009
SSES Organizational Effectiveness Oversight Panel, Employee Focus Group Meeting May 5-7, 2009 summary report
SSES [[Focus (Internal Communications newsletter) dated July 16, 2009; July 21,2009; July 29, 2009; July 31, 2009:;August 7, 2009 (2); August 14, 2009, August 17,2009, August 20, 2009, August 24,2009, August 26,2009, August 31,2009; September 1,2009, September 4, 2009; September 11, 2009; September 14, 2009 (2); September 15, 2009; September 22, 2009; and September 23, 2009]]
SSES Grapevine dated August 28, 2009; September 2, 2009; and September 8,
SSES Work Environment Performance Indicators for July 2009 and August Proposed Draft General Work Environment Performance Indicator data September 23,
PPL Performance Planning and Review Process-Personnel Goals and Observation sheet dated April 21, Nuclear culture review survey provided to Operations Department on 8/19/09 and evaluation of the data Memorandum of Agreement between
PPL and
IBEW Local 1600 dated may 9,2002
SSES [[]]
RCA rollout Presentation and feedback forms Section 40A5: Other Condition Reports:
1173698 ISFSI related Condition Reports since July 12, 2006 Procedures:
ME -ORF-023, Dry Fuel Storage
61 BT Dry Shielded Canister, Revision 14
MT -EO-045, Guidance and Use of
NUHOMS Automated Welding System for Welding Operation, Revision 1
ME -ORF*,179, Dry Fuel Storage EqUipment List and Reference Information, Revision
8 NDAP -
QA -0658, Dry Fuel Storage Program, Revision
6 IVIE -
ORF -152, Dry Fuel Storage Response to Crane/RigginglTransfer Equipment, Malfunction and Certificate of Compliance Technical Specification Requirements, Revision
2 MT -
EO -058, E1000 Series Vacuum Drying System Operation, Revision
8 ME -
ORF *,150, Dry Fuel Storage Dry Shielded Canister Unloading, Revision
1 RE -081-43, Selection and Monitoring of Fuel for Dry Storage, Revision 5
ON -089-001, Dry Fuel Storage Temperature Anomaly, Revision
6 MT -199-001, Reactor Building Crane Operating Procedure, Revision 18
MT -199-002, Reactor Building Crane Main & Auxiliary Hoist Limit Switch Testing, Revision
6 MT -
GM -014, Rigging and Lifting Equipment Inspection, Revision 16 Work Orders:
ERPM 937419, Inspect 1H213 Crane for Proper Operation

ERPM 1065158, 1H213 Perform 4 year Weld Inspections, completed May 30,2009 Attachment

Other:

2008 PPL [[]]
SSES [[]]
LLC Dry Fuel Storage Project Completion Review Self 2009 Dry Fuel Storage Readiness Annual Synthetic Round Sling Inspection 72.48 Screens,
SO 00041,
SO 00035,
SO 00038,
SO 00033,
SO 00035,
SO 00028,
SO 00027,
SO 00024,
SO 00000022,
SO 00016,
SO 00015,
SO Final safety Analysis Report (
FSAR ), November 9, Decay Heat Calculation,
EC -Fuel-1185, Revision
FACCTA S for
DSC #53, July 31,2009, Revision
ISFSI Temperature Monitoring System Software Requirement Specification, July 2, Revision Annual Preventative Maintenance Plan for Unit 1 Reactor Building Crane,
WO completed December 5,
SSES Area Survey Map,
ISFSI Facility, dated: January 28, 2008; April 22, 2008; 25, 2008; October 24, 2008; January 22, 2009; April 25, 2009; May 1,
LIST [[]]
OF [[]]
ACRONY MS
ADAMS Agencywide Document and Access Management System
ALARA As Low As Is Reasonably Achievable
AV Apparent Violation
CAP Corrective Action Program
CFR Code of Federal Regulations
CR Condition Report
DG Diesel Generator
ECP Employee Concerns Program
EDG Emergency Diesel Generator
EPU Extended Power Uprate
ESW Emergency Service Water
FIN Finding
FPE Fire Protection Engineer
FPPR Fire Protection Program Report
FSAR [[[]]
SSES [[] Final Safety Analysis Report]]
HPCI High Pressure Coolant Injection
HV High Voltage
IN Information Notice
IMC Inspection Manual Chapter
ISFSI Independent Spent Fuel Storage Installation l
SI Inservice Inspection
IWIIIS I In Vessel Visual I nspectionll nservice Inspection
LCO Limiting Condition for Operation
NCV Non-Cited Violation
NDAP Nuclear Department Administrative Procedure
NRC Nuclear Regulatory Commission
PARS Publicly Available Records
PCE Potential Chilling Effect
PI [[[NRC] Performance Indicator PM Preventive Maintenance Attachment]]
PMT [[]]
PPL [[]]
QA [[]]
RCA [[]]
RCIC [[]]
RHR [[]]
RHR [[]]
SW [[]]
RTP [[]]
SBO [[]]
SCWE [[]]
SOP [[]]
SG [[]]
TS [[]]
SRO [[]]
SSC [[]]
SSES [[]]
TS T20 Post-Maintenance Test
PPL Susquehanna,
LLC Standby Gas Treatment System Senior Reactor Operator Structures, Systems and Components Susquehanna Steam Electric Station Technical Specifications T20 Startup Transformer Attachment]]