ML19331E018

From kanterella
Revision as of 16:54, 31 January 2020 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 80-032/03L-0:on 800725,during Performance of Surveillance Procedure 6.2.2.2.1,isolation of HPCI Steam Line Occurred.Cause Not Fully Determined.Probable Cause Due to Transient in Common Sensing Line
ML19331E018
Person / Time
Site: Cooper Entergy icon.png
Issue date: 08/22/1980
From: Lawrence L
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19331E016 List:
References
LER-80-032-03L, LER-80-32-3L, NUDOCS 8009050203
Download: ML19331E018 (1)


Text

.NRdFORM 366 U. S. NUCLE AR REGULATORY COMMISSION 31-fU ')lh LICENSEE EVENT REPORT CONTROL 8 LOCK: l l l l l l  ! (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 10 lil8 l3 N l E 7

l C l P l Rl141l@l LICENSEE CODE IS Ol 0l- l 0 LICENSE l0 l 0NUMdERl 0 l - l 0 l 0 l 25O l@l426 l1 l1 il l 1 l@l$7 CAT LICENSE TYPE 40 l

b8 l@

CON'T I0liI 3[,c" "' l L @l015 l0 l0 l0 l2 l 9 l 8 @l 0 l 7 l 2 l Sl 8l OMl0 l 8 l 2 l 2 l 8 l 0 l@

7 8 60 61 COCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCLS h I o 12 I Durine nerformance of surveillance procedurp 6_2_2_2_1_ AD A th e a r Teval hneefnnr1/ I I o i 31 Calibration Test, a HPCI isolation occurred at about the same time as NB,I-LIS-83A I 10141 kas returtud to service. The isolation was immediatelv repet and HPCI van nonrnhia_ l 10 I S I All remainine ECCS Systems were onerable. This event hnd nn efface nn niihlic han1*h I I o 16 I lana anforv. l 10171 l l 10181! l 7 8 9 00 SYSTEu CAUSE CAUSE COMP. VA LV E CODE CODE SUSCODE COVPONENT CODE SU8 CODE SUSCODE R lS l Fl @ IX l@ l C l @ lI l N l S l T l R I U l@ (_Sj @ [_Z_j @

1 8 9 to 11 12 13 18 19 20

,_ SEQUE N TI AL OCCURRENCE REPORT REVISION tg g 90 EVENT YEAR REPORT No. CODE TYPE NO.

@ aj ,T r 18101 1-1 10 13121 L<J 10I31 Itl L-J 10 1

_ 21 22 23 24 26 27 N 29 30 31 J2 TAKE ACTO ON PLANT M T HOURS SS IT D FOR b B. SLPPL1 R VAN FACT ER kJJ l@Lz_J@ J4 LzJ@

35 Iz l@ 101010101 31 Ltd@ l l@ IN l@ l44Y l 0 l 11 Ol@

36 40 43 42 4J 47 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS Iilol The cause of the occurrence may have been caused bv a transient in the common sens- 1 I i 1 i 1 Ang line introduced by opening the isolation valve prior to the pressurizine val' e -

i I i 1 a 1 pr by opening the pressurizing valve to quicklv. A definira enuso fnr ehfe n c e t t v- l Li_L1,J Irence enu1d nne ha aacominaa- 1 I i 131 l I 7 8 80

'S'TWIs' POWER OTsER STATUS @ S'S$vSRv' oiSCOvERY oESCRiPTiON @

l i I 5 I [_E_j@ l ]l 0 l 0 l@l NA l lAl@l Operator Observation l A Tivt TY CO TENT RELE ASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE R [Z_j @ [ Z_j @ l NA l l NA l 7 8 9 to 11 44 45 80 PERSONML FXPOSURES NUVBER TYPE DESCRIPTION lil7ll0l0l0l@lZl@l NA l

PERsONu'L ,~wLS Nu mER oESCRiPTiON@

li l I lo lo in l@l n we m __. - I

$ IN OH O 1AG TO FACILI TY Ld2J r n n l2_J@lto n I 80 1.:. Ut LittP f H)N

  • ITT gl (z_[@l
  1. '> 10 NA l l1Illll1ll ! ll}

68 69 80 T.

NAVE OF PREPARER L. I. Lawrence PHONE:

402-825-3811 8009050 @ 3