ML20003B285

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LER 81-003/03L-0:on 810106,during Routine Insp While in Cold Shutdown,Main Steam Line Snubber 413019 Found W/No Visible Fluid Level.Caused by Plastic Fluid Reservoir Damaged by Overheating During Outage.Defective Snubber Replaced
ML20003B285
Person / Time
Site: Millstone Dominion icon.png
Issue date: 01/30/1981
From: Tresetar J
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003B279 List:
References
LER-81-003-03L, LER-81-3-3L, NUDOCS 8102100598
Download: ML20003B285 (1)


Text

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REPORT DATi;

? 8 60 81 DOCK ET NUMB ER 68 EVENT DATE EVENT DESCRIPTION AND PROBABt.E CONSEQUENCES h 10 l 2 l l During a routine inspection, main steam line snubber 413019 was found with nn vicihlo l 10121 I fluid level . At the time of the disenverv tha n12n+ m2e in a enla ehnt%wn cnnai+4cn 1 10141 I The snubber is an ITT Grinnell, FIG. 200, 4 inch bore by 5 inch stenka unit I l0 lsI I Similiar LER's 77-47, 79-28, 80-12 l I

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l 110 l l The plastic fluid reservoir deformed due tn nvorhaatinn when insulating nads wara l I, li I I installed over a portion of the snubber after relocation of the hancer and snnhhpr l

,,,,,i during a recent outage. The defective snubber was replaced. An inspection was cer- 1 I i i s ! I formed verifvino additinnal hanner wnrie hae nne r=need eimiliar neenren,ee_ l l

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