05000336/LER-1981-003-03, /03L-0:on 810106,during Routine Insp While in Cold Shutdown,Main Steam Line Snubber 413019 Found W/No Visible Fluid Level.Caused by Plastic Fluid Reservoir Damaged by Overheating During Outage.Defective Snubber Replaced

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/03L-0:on 810106,during Routine Insp While in Cold Shutdown,Main Steam Line Snubber 413019 Found W/No Visible Fluid Level.Caused by Plastic Fluid Reservoir Damaged by Overheating During Outage.Defective Snubber Replaced
ML20003B285
Person / Time
Site: Millstone Dominion icon.png
Issue date: 01/30/1981
From: Tresetar J
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20003B279 List:
References
LER-81-003-03L, LER-81-3-3L, NUDOCS 8102100598
Download: ML20003B285 (1)


LER-1981-003, /03L-0:on 810106,during Routine Insp While in Cold Shutdown,Main Steam Line Snubber 413019 Found W/No Visible Fluid Level.Caused by Plastic Fluid Reservoir Damaged by Overheating During Outage.Defective Snubber Replaced
Event date:
Report date:
3361981003R03 - NRC Website

text

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8 60 81 DOCK ET NUMB ER 68 69 EVENT DATE 74 75 REPORT DATi; 80 EVENT DESCRIPTION AND PROBABt.E CONSEQUENCES h 10 l 2 l l During a routine inspection, main steam line snubber 413019 was found with nn vicihlo l

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10121 I fluid level. At the time of the disenverv tha n12n+ m2e 10141 I The snubber is an ITT Grinnell, FIG. 200, 4 inch bore by 5 inch stenka unit I

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