02-24-2017 | On December 28, 2016, at 2119 hours0.0245 days <br />0.589 hours <br />0.0035 weeks <br />8.062795e-4 months <br /> (EST), standby liquid control ( SLC) subsystem A was declared inoperable in accordance with the surveillance instruction for performance of a routine surveillance test. At 2229 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.481345e-4 months <br />, control room operators received an out-of-service alarm for SLC discharge valve B. With both subsystems inoperable, the SLC system was in a condition that required reporting under 10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.72(b)(3)(v)(D). At 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br />, the surveillance was completed and subsystem A was declared operable.
The cause for subsystem B inoperability was an indicated loss of continuity to one of the two firing circuits in the discharge valve due to a loose connection between a pin and jack on the connector. This was not a safety system functional failure since continuity was interrupted to only one of the two redundant firing circuits for discharge valve B and if an initiation signal was sent to the valve, it would have operated as designed and supported chemical injection to the vessel. The risk of this event is considered small in accordance with the regulatory guidance. The power supply cable was replaced and post maintenance testing was completed satisfactorily. The preventative maintenance task will be revised to include a step to inspect connection pins and jacks when changing the firing assembly. Additionally, the cable on the discharge valve for SLC subsystem A will be replaced and sent to FirstEnergy BETA Laboratory for analysis when the valve is replaced during the next refueling outage.
The analysis will be used to determine if a new preventative maintenance task is necessary for periodic replacement of these cables. |
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Category:Letter
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[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000440/LER-2024-003, Technical Specification Required Shutdown Due to Increase in RCS Unidentified Leakage2024-07-15015 July 2024 Technical Specification Required Shutdown Due to Increase in RCS Unidentified Leakage 05000440/LER-2024-002, Reactor Water Clean Up Leak Detection Loss of Safety Function2024-06-27027 June 2024 Reactor Water Clean Up Leak Detection Loss of Safety Function 05000440/LER-2024-001, Operation of the Residual Heat Removal Loops B and C Alternate Keep Fill Configuration Was Prohibited by Technical Specifications and Resulted in an Unanalyzed Condition2024-06-20020 June 2024 Operation of the Residual Heat Removal Loops B and C Alternate Keep Fill Configuration Was Prohibited by Technical Specifications and Resulted in an Unanalyzed Condition 05000440/LER-2023-003, Plant Trip During Reactor Protection System Power Transfer2023-09-28028 September 2023 Plant Trip During Reactor Protection System Power Transfer 05000440/LER-2023-002, Main Steam Line Leakage Exceeded Technical Specification Limit2023-04-26026 April 2023 Main Steam Line Leakage Exceeded Technical Specification Limit 05000440/LER-2023-001, Manual ECCS Actuation Following Automatic Reactor Trip2023-02-22022 February 2023 Manual ECCS Actuation Following Automatic Reactor Trip 05000440/LER-1922-002, Steam Bypass Valve Demand Limited on the B Train Due to a Degraded Signal in the Max Combined Flow Limit Circuit2022-12-0505 December 2022 Steam Bypass Valve Demand Limited on the B Train Due to a Degraded Signal in the Max Combined Flow Limit Circuit 05000440/LER-2022-001, Low Pressure Core Spray Inoperable Due to Loss of Minimum Flow Valve2022-08-17017 August 2022 Low Pressure Core Spray Inoperable Due to Loss of Minimum Flow Valve 05000440/LER-2017-0062017-12-0101 December 2017 Loss of Safety Function due to the Inoperability of Both Trains of Motor Control Center Ventilation, LER 17-006-00 for Perry Nuclear Power Plant Regarding Loss of Safety Function due to the Inoperability of Both Trains of Motor Control Center Ventilation 05000440/LER-2017-0042017-10-0404 October 2017 Loss of Safety Function for High Pressure Core Spray Suppression Pool Level Instrumentation, LER 17-004-00 for Perry re Loss of Safety Function for High Pressure Core Spray Suppression Pool Level Instrumentation 05000440/LER-2017-0052017-10-0404 October 2017 Controller Malfunction results in Momentary Degradation of Secondary Containment Pressure, LER 17-005-00 for Perry Nuclear Power Plant Regarding Controller Malfunction Results in Momentary Degradation of Secondary Containment Pressure 05000440/LER-2017-0022017-06-27027 June 2017 Loss of Safety Function Due to Main Turbine Bypass Valve Opening, LER 17-002-00 for Perry Nuclear Power Plant Regarding Loss of Safety Function Due to Main Turbine Bypass Valve Opening 05000440/LER-2017-0032017-06-26026 June 2017 Annulus Exhaust Gas Treatment System Loss of Safety Function, LER 17-003-00 for Perry Nuclear Power Plant Regarding Annulus Exhaust Gas Treatment System Loss of Safety Function 05000440/LER-2016-0042017-02-24024 February 2017 Loss of Safety Function Due to Two Inoperable Standby Liquid Control Subsystems, LER 16-004-00 for Perry Regarding Loss of Safety Function Due to Two Inoperable Standby Liquid Control Subsystems L-16-365, LER 16-01-001 for Perry, Unit 1, Regarding Pressure Boundary Leakage, Level 8 Automatic SCRAM, and APRM Loss of Safety Function2016-12-21021 December 2016 LER 16-01-001 for Perry, Unit 1, Regarding Pressure Boundary Leakage, Level 8 Automatic SCRAM, and APRM Loss of Safety Function L-16-366, LER 16-03-001 for Perry Nuclear Power Plant Loss of Safety Related Electrical Bus Results in a Loss of Shutdown Cooling2016-12-21021 December 2016 LER 16-03-001 for Perry Nuclear Power Plant Loss of Safety Related Electrical Bus Results in a Loss of Shutdown Cooling ML16138A3342016-05-17017 May 2016 ASP Analysis - Reject Perry Nuclear Power Plant, Unit 1 (440-2014-005) ML16138A3362016-05-17017 May 2016 ASP Analysis - Reject Perry Nuclear Power Plant, Unit 1 (440-2014-004) 05000440/LER-2016-0032016-04-0808 April 2016 Loss of Safety Related Electrical Bus Results in a Loss of Shutdown Cooling, LER 16-003-00 for Perry Regarding Loss of Safety Related Electrical Bus Results in a Loss of Shutdown Cooling 05000440/LER-2016-0022016-04-0808 April 2016 Manual Reactor SCRAM Due to Spurious Opening of Safety Relief Valves, LER 16-002-00 for Perry Regarding Manual Reactor SCRAM Due to Spurious Opening of Safety Relief Valve 05000440/LER-2016-0012016-03-23023 March 2016 Pressure Boundary Leakage, Level 8 Automatic SCRAM, and APRM Loss of Safety Function, LER 16-001-00 for Perry Nuclear Power Plant Regarding Drywell Leakage, Level 8 Automatic SCRAM and APRM Loss of Safety Function L-13-194, LER 13-S02-01 for Perry, Unit 1 Regarding Security Weapon Left Unattended2013-06-25025 June 2013 LER 13-S02-01 for Perry, Unit 1 Regarding Security Weapon Left Unattended L-13-143, LER 13-S02-00, for Perry Nuclear Power Plant, Unit 1, Regarding Security Weapon Left Unattended2013-04-30030 April 2013 LER 13-S02-00, for Perry Nuclear Power Plant, Unit 1, Regarding Security Weapon Left Unattended L-13-119, LER 13-S01-00 for Perry Nuclear Power Plant, Unit 1, Regarding Local Power Range Monitors Delivered to the Incorrect Address2013-03-15015 March 2013 LER 13-S01-00 for Perry Nuclear Power Plant, Unit 1, Regarding Local Power Range Monitors Delivered to the Incorrect Address L-12-114, LER 12-S02-00, for Perry Nuclear Power Plant, Unit 1, Regarding Potential Vulnerability in a Safeguards Security System2012-03-22022 March 2012 LER 12-S02-00, for Perry Nuclear Power Plant, Unit 1, Regarding Potential Vulnerability in a Safeguards Security System L-12-083, LER 12-S01-00, Latent Software Error Resulted in Improperly Authorized Visitor Access Into Protected Area2012-02-29029 February 2012 LER 12-S01-00, Latent Software Error Resulted in Improperly Authorized Visitor Access Into Protected Area L-08-052, LER 07-04-001 for Perry Nuclear Power Plant Re Automatic Reactor Protection System Actuation Due to Feedwater Control Power Supply Failure2008-02-15015 February 2008 LER 07-04-001 for Perry Nuclear Power Plant Re Automatic Reactor Protection System Actuation Due to Feedwater Control Power Supply Failure ML0533301242005-11-18018 November 2005 LER 05-03-00 for Perry Nuclear Power Plant Lack of Suction Flow Path Causes High Pressure Core Spray to Be Inoperable ML0509602632004-12-17017 December 2004 Final Precursor Analysis - Perry Grid Loop 2024-07-15
[Table view] |
used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
440 - 004 - 00 Perry Nuclear Power Plant 05000 - YEAR 2016 Energy Industry Identification System (EIIS) codes are identified in the text as [XX].
INTRODUCTION
On December 28, 2016, at 2229 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.481345e-4 months <br /> (EST), both standby liquid control (SLC) [BR] subsystems were declared inoperable due to performance of a surveillance test on subsystem A and the indicated loss of continuity to a firing circuit on the discharge valve for subsystem B.
With both subsystems having been declared inoperable, this was determined to be a reportable event under 10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.72(b)(3)(v)(D) for an event or condition that that could have prevented the fulfillment of the safety function of structures or systems that are needed to shut down the reactor and maintain it in a safe shutdown condition and mitigate the consequences of an accident. As such, an event notification was made to the NRC Operations Center and recorded under Event Number 52468.
This event is being reported in accordance with 10 CFR 50.73(a)(2)(v)(A) and 10 CFR 50.73(a)(2)(v)(D), which requires reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to shut down the reactor and maintain it in a safe shutdown condition and mitigate the consequences of an accident. This was not a safety system functional failure since discharge valve B would have operated as designed and supported chemical injection to the vessel.
DESCRIPTION OF EVENT
On December 28, 2016, at 2119 hours0.0245 days <br />0.589 hours <br />0.0035 weeks <br />8.062795e-4 months <br />, with the plant in mode 1 at 98 percent power, SLC subsystem A was declared inoperable for performance of a routine surveillance test. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.1.7, Action A was entered, which required restoring the single subsystem to operable status within 7 days.
On December 28, 2016, at 2229 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.481345e-4 months <br />, the control room received an out-of-service alarm for SLC subsystem B directly after pump A was started in accordance with the surveillance instruction. Control room operators verified this alarm to be due to an indicated loss of continuity to discharge valve B, as read on a control room indicator. At 2229 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.481345e-4 months <br />, SLC subsystem B was declared inoperable and TS LCO 3.1.7, Action B was entered, which required restoring one SLC subsystem to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. With both subsystems declared inoperable, the SLC system was in a condition that rendered it unable to fulfill its safety function.
On December 28, 2016, at 2257 hours0.0261 days <br />0.627 hours <br />0.00373 weeks <br />8.587885e-4 months <br />, pump A was stopped in accordance with the surveillance instruction and at 2302 hours0.0266 days <br />0.639 hours <br />0.00381 weeks <br />8.75911e-4 months <br />, the SLC B out-of-service alarm reset. Following performance of the surveillance test at 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br />, SLC subsystem A was declared operable and TS LCO 3.1.7, Action B was exited.
Troubleshooting determined that the cause for SLC subsystem B inoperability was an indicated loss of continuity to one of the two firing circuits in the discharge valve. On December 29, 2016, at 1708 hours0.0198 days <br />0.474 hours <br />0.00282 weeks <br />6.49894e-4 months <br />, SLC subsystem B was declared operable and TS LCO 3.1.7, Action A was exited after repairs were completed.
CAUSE OF EVENT
Continuity was interrupted by a high resistance in a connector to one of the two firing circuits for discharge valve B. This brought in the alarm as expected for this condition and also reduced the available firing circuits used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
440 - 004 - 00 Perry Nuclear Power Plant 05000 - YEAR 2016 from two to one. Since the other firing circuit was complete, discharge valve B would have operated as designed and supported chemical injection to the vessel if it received an initiation signal. However, Surveillance Requirement (SR) 3.1.7.4, which verifies continuity of the explosive charges, was not met and on December 28, 2016 from 2229 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.481345e-4 months <br /> to 2335 hours0.027 days <br />0.649 hours <br />0.00386 weeks <br />8.884675e-4 months <br />, with both systems declared inoperable, the system was administratively in a condition that rendered it unable to fulfill its safety function.
The event was isolated to a small section of the cable that connects the discharge valve to the 120 VAC power supply. The direct cause for the loss of continuity to one of the two firing circuits in discharge valve B was a loose connection between a pin and jack on the connector. The apparent cause of the event was the preventative maintenance (PM) scope did not have a step to inspect the condition of the pins and jack in this connection, which allowed the wear to go undetected until it was self-revealed via an equipment issue.
ANALYSIS OF EVENTS
The safety function of the SLC system is to mitigate the consequences in the event that not enough control rods can be inserted in the reactor core to accomplish shutdown and cool-down in the normal manner, and to provide a pH buffering solution for injection into the reactor vessel suppression pool following a design basis LOCA. The system is manually initiated from the control room and consists of a boron solution tank, two positive displacement pumps and two explosive valves (discharge valves), which are provided in parallel for redundancy, and associated piping and valves used to transfer borated water from the storage tank to the reactor pressure vessel. The system is not a backup scram system for the reactor, but an independent backup system for the control rod drive (CRD) [AA] system. At the time of the event, the CRD system was operable and available.
Each discharge valve uses explosive charges as their opening mechanisms, which are electrically operated.
Each explosive charge contains two independent firing circuits, also known as primers, and a small electrical current continuously tests for continuity. For continuity testing, the charges are in series, therefore a break in any part of the circuit would break continuity and provide an out-of-service alarm in the control room. When called upon to function (i.e., fire the explosive charge), power is directed to the two independent firing circuits in parallel, meaning the electrical path for firing of the explosive charge is different than the electrical path for testing continuity.
A probabilistic risk assessment (PRA) evaluation of this event notes that the function of the Standby Liquid Control System remained available since discharge valve B would have operated as designed and supported chemical injection to the vessel. On this basis there would be no impact to the PRA model, and therefore no corresponding change (delta) in core damage frequency (CDF) and no corresponding change (delta) in large early release frequency (LERF). The delta CDF and delta LERF values are well below the acceptable thresholds of 1.0E-06/year and 1.0E-07/year, respectively, as discussed in Regulatory Guide 1.174. The risk of this event is therefore considered small in accordance with the regulatory guidance.
With both subsystems having been declared inoperable, this was determined to be a reportable event under 10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.72(b)(3)(v)(D) for an event or condition that that could have prevented the fulfillment of the safety function of structures or systems that are needed to shut down the reactor and maintain it in a safe shutdown condition and mitigate the consequences of an accident. As such, an event notification was made to the NRC Operations Center and recorded under Event Number 52468.
used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
440 - 004 - 00 Perry Nuclear Power Plant 05000 - YEAR 2016 Although it was subsequently determined that SLC subsystem B would have functioned if called upon and thus the safety function would have been met, this event is being reported in accordance with 10 CFR 50.73(a)(2)(v)(A) and 10 CFR 50.73(a)(2)(v)(D), as follow-up to the 10 CFR 50.72(b)(3)(v)(A) and 10 CFR 50.72(b)(3)(v)(D) notification made under Event Number 52468.
CORRECTIVE ACTIONS
The power supply cable was replaced and post maintenance testing was completed satisfactorily. The preventative maintenance procedure will be revised to include a step to inspect connection pins and jacks when changing the firing assembly.
Additionally, the cable on the discharge valve for SLC subsystem A will be replaced and sent to FirstEnergy BETA Laboratory for analysis when the valve is replaced during the next refueling outage. The analysis will be used to determine if a new preventative maintenance task is necessary for periodic replacement of these cables.
PREVIOUS SIMILAR EVENTS
A review of LERs and the corrective action database for the past three years showed no similar events.
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05000440/LER-2016-001 | Pressure Boundary Leakage, Level 8 Automatic SCRAM, and APRM Loss of Safety Function LER 16-001-00 for Perry Nuclear Power Plant Regarding Drywell Leakage, Level 8 Automatic SCRAM and APRM Loss of Safety Function | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000440/LER-2016-002 | Manual Reactor SCRAM Due to Spurious Opening of Safety Relief Valves LER 16-002-00 for Perry Regarding Manual Reactor SCRAM Due to Spurious Opening of Safety Relief Valve | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2016-003 | Loss of Safety Related Electrical Bus Results in a Loss of Shutdown Cooling LER 16-003-00 for Perry Regarding Loss of Safety Related Electrical Bus Results in a Loss of Shutdown Cooling | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2016-004 | Loss of Safety Function Due to Two Inoperable Standby Liquid Control Subsystems LER 16-004-00 for Perry Regarding Loss of Safety Function Due to Two Inoperable Standby Liquid Control Subsystems | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident |
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