Similar Documents at Salem |
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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML18107A4991999-08-25025 August 1999 Application for Amends to Licenses DPR-70 & DPR-75,proposing to Authorize Licensee to Perform Single Cell Charging of Connected Cells in Operable Class 1E Batteries ML18107A5141999-08-25025 August 1999 Suppl to 971114 Application for Amends to Licenses DPR-70 & DPR-75,deleting Footnotes Added as one-time Changes & Proposing Change Identified Subsequent to 971114 Submittal That Corrects Error Issued in Amend 69 for Unit 2 ML18107A4631999-07-29029 July 1999 Application for Amends to Licenses DPR-70 & DPR-75,replacing Surveillance 4.6.1.1a with Appropriate NUREG-1431 Requirements ML18107A4581999-07-23023 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Change TS Surveillance Requirement 4.8.1.1.2 D 7 by Removing Restriction to Perform Test Every 18 Months During Shutdown ML18107A4221999-07-0202 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Relocate TS 3/4.3.4 Lco,Surveillance Requirements & Bases from TS to Ufsar,Iaw GL 95-10 ML18107A3771999-06-10010 June 1999 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.6.1, Containment Integrity, by Clarifying When Verification of Primary Containment Integrity May Be Performed by Administrative Means ML18107A3571999-06-0404 June 1999 Application for Amends to Licenses DPR-70,DPR-75 & NPF-57 Re Transfer of PSEG Ownership Interests & Licensed Operating Authorities to New,Affiliated Nuclear Generating Company, PSEG Nuclear Llc.Proprietary Encls Withheld ML18107A2081999-04-14014 April 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.9.12, Fhvas, to Ensure Consistency Between TS Requirements for Fhavs & Sys Design Basis,Per NUREG-1431. Page 4 of 4 in Attachment 2 of Incoming Submittal Omitted ML18106B1571999-03-31031 March 1999 Suppl to 990115 Application for Amend to License DPR-70, Allowing Plant Operation to Continue to Thirteenth Refueling Outage (1R13),currently Scheduled to Begin on 990918 ML18106B0621999-02-0808 February 1999 Application for Amends to Licenses DPR-70 & DPR-75, Respectively.Proposed Amend Modifies ECCS Subsystems Surveillance Requirement 4.5.3.2.b by Adding Option of Providing Necessary Isolation Function When Testing ML18106B0501999-02-0202 February 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising Max Permissible Enrichment of Stored New Fuel Described in TS Section 5.6.1.1.Rept Entitled, Criticality Analysis of Salem Units 1 & 2 Fresh Fuel Racks, Encl ML18106B0221999-01-15015 January 1999 Application for Amend to License DPR-70,proposing one-time Changes to Certain Unit 1 TS Surveillance Requirements for Fuel Cycle 13,currently Scheduled to Begin on 990918 ML18106A9161998-10-12012 October 1998 Application for Amend to License DPR-75,requesting one-time Changes to Certain Unit 2 TS SR for Fuel Cycle 10.Basis for Requested Changes,Analysis Supporting No Significant Hazards Determination & Marked Up TS Pages,Encl ML18106A8921998-09-29029 September 1998 Application for Amends to Licenses DPR-72 & DPR-75,modifying TS 3/4.9.4 to Permit Use of Equivalent Methods to Obtain Containment Closure During Refueling Operations for Containment Equipment Hatch ML18106A8761998-09-17017 September 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TSs 3/4.8.2.2,3/4.8.2.4 & 3/4.8.2.6 to Address Movement of Irradiated Fuel & Deleting LCO Re Requirement to Establish Containment Integrity ML18106A8351998-08-12012 August 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS for Containment Air Locks for Salem Units 1 & 2 ML18106A7911998-07-30030 July 1998 Application for Amends to Licenses DPR-70 & DPR-75,revising Acceptance Criteria for CR Emergency Air Conditioning Sys from Maintaining CR at 1/8-inch Positive Pressure W/Respect to Adjacent Areas to Following Phrase ML18106A4271998-03-26026 March 1998 Application for Amend to License DPR-70,changing Applicability Statement from Mode 3 to Modes 1 & 2 ML18106A4221998-03-26026 March 1998 Application for Amends to Licenses DPR-70 & DPR-75, Respectively,Incorporating Note at Bottom of Salem Unit 2 T3/4.8.2 Into Salem 1 TS & Adding Asterisks to Word Inverters. ML18106A2521998-01-0808 January 1998 Supplemental Application for Amends to Licenses DPR-70 & DPR-75,respectively Adding Asterisk to Word Operable in LCO & Associated Note at Bottom of Page ML18106A2111997-12-15015 December 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS to Adopt Option B of 10CFR50,App J,For Type B & C Testing & Modifying Existing TS Wording for Previous Adoption of Option B on Type a Testing ML18106A1941997-12-11011 December 1997 Application for Amend to License DPR-70,requesting one-time Exemption to Allow Containment Purging in Modes 3 & 4 ML18102B6771997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing TS Surveillance Requirements to Codify Existing Procedural Commitments for SW Accumulator Vessels ML18102B6731997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75, Correcting Editorial & Administrative Errors in Ts,Which Existed Since Initial Issuance ML18102B6611997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.8.1 Re EDG & Deleting SR 4.8.1.1.2.d.1,calling for Diesels to Be Subjected to Insp Based on Vendor Recommendations ML18102B6571997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Surveillance Requirement 4.6.2.1.b to Verify That on Recirculation Flow,Containment Spray Pumps Develop Differential Pressure of Greater than or Equal to 204 Psid ML18102B6371997-10-29029 October 1997 Application for Amend to License DPR-75,revising TS 3/4.4.6, Steam Generators, Making One Time Change to Unit 2 SG Insp Schedule to Require Next Insp within 24 Months of Mode 2 for Unit 2 Fuel Cycle 10 ML18102B6411997-10-29029 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.8.1.1.2.d.2 Proposed in Util 960925 Submittal Re EDG Testing ML18102B6471997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.7.7, Auxiliary Building Exhaust Air Filtration Sys & Bases ML18102B6441997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Containment Hydrogen Analyzer SRs of TS 4.6.4.1 ML18102B6291997-10-21021 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,extending Applicability of Power Range Neutron Flux TS Trip to Require Operability & Surveillance Testing in Mode 3,when Reactor Trip Sys Breakers in Closed Position ML18102B6181997-10-14014 October 1997 Application for Amend to License DPR-70,modifying Pressure Isolation Valve Lco,Lco Action Statement,Surveillance Requirement & Table 4.4-4 to Be Consistent W/Salem Unit 2 ML18102B6061997-10-0606 October 1997 Application for Amend to License DPR-70,changing TS for LCOs 3.1.3.1, Movable Control Assemblies & 3.1.3.2.1, Position Indication Sys. ML18102B5551997-08-27027 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing Revised TS Bases Pages for TS 3.7.3, CCW Sys, to State That CCW Pumps Required to Be Operable to Meet LCO ML18102B5281997-08-19019 August 1997 Application for Amend to License DPR-75,providing Addl Operational Flexibility to Allow Orderly Resumption of Startup & Preclude Unwarranted Power Transients at Plant Unit 2 ML18102B5321997-08-18018 August 1997 Application for Amend to License DPR-75,incorporating Plant Computer (P-250) Into TS Bases for Movable Control Assemblies ML18102B4871997-08-0101 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,rewording TS Section 4.2.1 to State That Util Will Adhere to Section 7 Incidental Take Statement Approved by Natl Marine Fisheries Svc ML18102B3041997-05-14014 May 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.7.6.1.d.1 to Indicate That Specified Acceptable Filter Dp Is to Be Measured Across Filter Housing & to Reflecting Filter Dp Acceptance Value of Greater than 2.70 Wg ML18102B2611997-05-0101 May 1997 Suppl Info to Util 970211 Application for Amends to Licenses DPR-70 & DPR-75,revising TS for Chilled Water Sys - Auxiliary Bldg Subsystem.Ref to Radiation Monitoring Signal Removed from Bases Section ML18102B2581997-05-0101 May 1997 Application for Amend to License DPR-75,revising TS Section 3/4.7.7 to Reflect Extended Allowed Outage Times & Creating New TS Section 3/4.7.11 to Address Importance of Switchgear & Penetration Area Ventilation Sys ML18102B0071997-04-30030 April 1997 Application for Amends to Licenses DPR-40,DPR-56,DPR-70 & DPR-75,requesting Consent of NRC for Indirect Transfer of Control of Interest in Plants That Will Occur Under Proposed Merger ML18102B2511997-04-28028 April 1997 Submits Suppl to 970131 & 0314 Applications for Amends to Licenses DPR-70 & DPR-75,revising TS on Pressurizer Power Operated Relief Valves.Suppl Issued to State That Conclusion of NSHC Remains Valid ML18102B0221997-04-25025 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Eliminating Flow Path from RHR Sys to RCS Hot Legs as Specified in LCO 3.5.2.c.2 ML18102A9791997-04-11011 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Increasing Cw Flow to 2550 Gpm for 31 Day Surveillance Fans Started & Operated in Low Speed ML18102A8951997-03-0404 March 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying ECCS Surveillance Test Acceptance Criteria for Centrifugal Charging & SI Pumps ML18102A8491997-02-11011 February 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Addition of New TS 3/4.7.10, Chilled Water Sys ML18102A8361997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.4.3 to Ensure That Automatic Capability of Power Operated Relief Valve to Relieve Pressure Is Maintained When Valves Are Isolated by Closure of Block Valves ML18102A8021997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Rev to TS Re Containment Systems Air Temp to Ensure Representative Average Air Temp Is Measured ML18102A7861997-01-23023 January 1997 Application for Amend to License DPR-75,revising TS Bases 3/4.3.3.1 Re Radiation Monitoring Instrumentation Channel 2R41 ML18102A7361997-01-0707 January 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Eighteen Month Surveillance Performed to Measure RCS Total Flow Rate to Account for Necessary Plant Conditions for Performing Test in Mode 1 & Current Extended Plant Outages 1999-08-25
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML18107A4991999-08-25025 August 1999 Application for Amends to Licenses DPR-70 & DPR-75,proposing to Authorize Licensee to Perform Single Cell Charging of Connected Cells in Operable Class 1E Batteries ML18107A5141999-08-25025 August 1999 Suppl to 971114 Application for Amends to Licenses DPR-70 & DPR-75,deleting Footnotes Added as one-time Changes & Proposing Change Identified Subsequent to 971114 Submittal That Corrects Error Issued in Amend 69 for Unit 2 ML18107A4631999-07-29029 July 1999 Application for Amends to Licenses DPR-70 & DPR-75,replacing Surveillance 4.6.1.1a with Appropriate NUREG-1431 Requirements ML18107A4581999-07-23023 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Change TS Surveillance Requirement 4.8.1.1.2 D 7 by Removing Restriction to Perform Test Every 18 Months During Shutdown ML18107A4221999-07-0202 July 1999 Application for Amends to Licenses DPR-70 & DPR-75 to Relocate TS 3/4.3.4 Lco,Surveillance Requirements & Bases from TS to Ufsar,Iaw GL 95-10 ML18107A3771999-06-10010 June 1999 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.6.1, Containment Integrity, by Clarifying When Verification of Primary Containment Integrity May Be Performed by Administrative Means ML18107A3571999-06-0404 June 1999 Application for Amends to Licenses DPR-70,DPR-75 & NPF-57 Re Transfer of PSEG Ownership Interests & Licensed Operating Authorities to New,Affiliated Nuclear Generating Company, PSEG Nuclear Llc.Proprietary Encls Withheld ML18107A2081999-04-14014 April 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.9.12, Fhvas, to Ensure Consistency Between TS Requirements for Fhavs & Sys Design Basis,Per NUREG-1431. Page 4 of 4 in Attachment 2 of Incoming Submittal Omitted ML18106B1571999-03-31031 March 1999 Suppl to 990115 Application for Amend to License DPR-70, Allowing Plant Operation to Continue to Thirteenth Refueling Outage (1R13),currently Scheduled to Begin on 990918 ML18106B0621999-02-0808 February 1999 Application for Amends to Licenses DPR-70 & DPR-75, Respectively.Proposed Amend Modifies ECCS Subsystems Surveillance Requirement 4.5.3.2.b by Adding Option of Providing Necessary Isolation Function When Testing ML18106B0501999-02-0202 February 1999 Application for Amends to Licenses DPR-70 & DPR-75,revising Max Permissible Enrichment of Stored New Fuel Described in TS Section 5.6.1.1.Rept Entitled, Criticality Analysis of Salem Units 1 & 2 Fresh Fuel Racks, Encl ML18106B0221999-01-15015 January 1999 Application for Amend to License DPR-70,proposing one-time Changes to Certain Unit 1 TS Surveillance Requirements for Fuel Cycle 13,currently Scheduled to Begin on 990918 ML18106A9161998-10-12012 October 1998 Application for Amend to License DPR-75,requesting one-time Changes to Certain Unit 2 TS SR for Fuel Cycle 10.Basis for Requested Changes,Analysis Supporting No Significant Hazards Determination & Marked Up TS Pages,Encl ML18106A8921998-09-29029 September 1998 Application for Amends to Licenses DPR-72 & DPR-75,modifying TS 3/4.9.4 to Permit Use of Equivalent Methods to Obtain Containment Closure During Refueling Operations for Containment Equipment Hatch ML18106A8761998-09-17017 September 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TSs 3/4.8.2.2,3/4.8.2.4 & 3/4.8.2.6 to Address Movement of Irradiated Fuel & Deleting LCO Re Requirement to Establish Containment Integrity ML18106A8351998-08-12012 August 1998 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS for Containment Air Locks for Salem Units 1 & 2 ML18106A7911998-07-30030 July 1998 Application for Amends to Licenses DPR-70 & DPR-75,revising Acceptance Criteria for CR Emergency Air Conditioning Sys from Maintaining CR at 1/8-inch Positive Pressure W/Respect to Adjacent Areas to Following Phrase ML18106A4271998-03-26026 March 1998 Application for Amend to License DPR-70,changing Applicability Statement from Mode 3 to Modes 1 & 2 ML18106A4221998-03-26026 March 1998 Application for Amends to Licenses DPR-70 & DPR-75, Respectively,Incorporating Note at Bottom of Salem Unit 2 T3/4.8.2 Into Salem 1 TS & Adding Asterisks to Word Inverters. ML18106A2521998-01-0808 January 1998 Supplemental Application for Amends to Licenses DPR-70 & DPR-75,respectively Adding Asterisk to Word Operable in LCO & Associated Note at Bottom of Page ML18106A2111997-12-15015 December 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS to Adopt Option B of 10CFR50,App J,For Type B & C Testing & Modifying Existing TS Wording for Previous Adoption of Option B on Type a Testing ML18106A1941997-12-11011 December 1997 Application for Amend to License DPR-70,requesting one-time Exemption to Allow Containment Purging in Modes 3 & 4 ML18102B6771997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing TS Surveillance Requirements to Codify Existing Procedural Commitments for SW Accumulator Vessels ML18102B6731997-11-14014 November 1997 Application for Amends to Licenses DPR-70 & DPR-75, Correcting Editorial & Administrative Errors in Ts,Which Existed Since Initial Issuance ML18102B6611997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.8.1 Re EDG & Deleting SR 4.8.1.1.2.d.1,calling for Diesels to Be Subjected to Insp Based on Vendor Recommendations ML18102B6571997-11-0404 November 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Surveillance Requirement 4.6.2.1.b to Verify That on Recirculation Flow,Containment Spray Pumps Develop Differential Pressure of Greater than or Equal to 204 Psid ML18102B6371997-10-29029 October 1997 Application for Amend to License DPR-75,revising TS 3/4.4.6, Steam Generators, Making One Time Change to Unit 2 SG Insp Schedule to Require Next Insp within 24 Months of Mode 2 for Unit 2 Fuel Cycle 10 ML18102B6411997-10-29029 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.8.1.1.2.d.2 Proposed in Util 960925 Submittal Re EDG Testing ML18102B6471997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying TS 3/4.7.7, Auxiliary Building Exhaust Air Filtration Sys & Bases ML18102B6441997-10-24024 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising Containment Hydrogen Analyzer SRs of TS 4.6.4.1 ML18102B6291997-10-21021 October 1997 Application for Amends to Licenses DPR-70 & DPR-75,extending Applicability of Power Range Neutron Flux TS Trip to Require Operability & Surveillance Testing in Mode 3,when Reactor Trip Sys Breakers in Closed Position ML18102B6181997-10-14014 October 1997 Application for Amend to License DPR-70,modifying Pressure Isolation Valve Lco,Lco Action Statement,Surveillance Requirement & Table 4.4-4 to Be Consistent W/Salem Unit 2 ML18102B6061997-10-0606 October 1997 Application for Amend to License DPR-70,changing TS for LCOs 3.1.3.1, Movable Control Assemblies & 3.1.3.2.1, Position Indication Sys. ML18102B5551997-08-27027 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,providing Revised TS Bases Pages for TS 3.7.3, CCW Sys, to State That CCW Pumps Required to Be Operable to Meet LCO ML18102B5281997-08-19019 August 1997 Application for Amend to License DPR-75,providing Addl Operational Flexibility to Allow Orderly Resumption of Startup & Preclude Unwarranted Power Transients at Plant Unit 2 ML18102B5321997-08-18018 August 1997 Application for Amend to License DPR-75,incorporating Plant Computer (P-250) Into TS Bases for Movable Control Assemblies ML18102B4871997-08-0101 August 1997 Application for Amends to Licenses DPR-70 & DPR-75,rewording TS Section 4.2.1 to State That Util Will Adhere to Section 7 Incidental Take Statement Approved by Natl Marine Fisheries Svc ML20148K0841997-06-0404 June 1997 Amends 194 & 177 to Licenses DPR-70 & DPR-75,respectively, Changing TSs 3.4.3 & 3.4.5, Relief Valves, to Ensure That Automatic Capability of PORVs to Relieve Pressure Is Maintained When Valves Are Isolated ML18102B3041997-05-14014 May 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising SR 4.7.6.1.d.1 to Indicate That Specified Acceptable Filter Dp Is to Be Measured Across Filter Housing & to Reflecting Filter Dp Acceptance Value of Greater than 2.70 Wg ML18102B2611997-05-0101 May 1997 Suppl Info to Util 970211 Application for Amends to Licenses DPR-70 & DPR-75,revising TS for Chilled Water Sys - Auxiliary Bldg Subsystem.Ref to Radiation Monitoring Signal Removed from Bases Section ML18102B2581997-05-0101 May 1997 Application for Amend to License DPR-75,revising TS Section 3/4.7.7 to Reflect Extended Allowed Outage Times & Creating New TS Section 3/4.7.11 to Address Importance of Switchgear & Penetration Area Ventilation Sys ML18102B0071997-04-30030 April 1997 Application for Amends to Licenses DPR-40,DPR-56,DPR-70 & DPR-75,requesting Consent of NRC for Indirect Transfer of Control of Interest in Plants That Will Occur Under Proposed Merger ML18102B2511997-04-28028 April 1997 Submits Suppl to 970131 & 0314 Applications for Amends to Licenses DPR-70 & DPR-75,revising TS on Pressurizer Power Operated Relief Valves.Suppl Issued to State That Conclusion of NSHC Remains Valid ML18102B0221997-04-25025 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Eliminating Flow Path from RHR Sys to RCS Hot Legs as Specified in LCO 3.5.2.c.2 ML18102A9791997-04-11011 April 1997 Application for Amends to Licenses DPR-70 & DPR-75, Increasing Cw Flow to 2550 Gpm for 31 Day Surveillance Fans Started & Operated in Low Speed ML18102A8951997-03-0404 March 1997 Application for Amends to Licenses DPR-70 & DPR-75,modifying ECCS Surveillance Test Acceptance Criteria for Centrifugal Charging & SI Pumps ML18102A8491997-02-11011 February 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Addition of New TS 3/4.7.10, Chilled Water Sys ML18102A8361997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75,revising TS 3/4.4.3 to Ensure That Automatic Capability of Power Operated Relief Valve to Relieve Pressure Is Maintained When Valves Are Isolated by Closure of Block Valves ML18102A8021997-01-31031 January 1997 Application for Amends to Licenses DPR-70 & DPR-75, Requesting Rev to TS Re Containment Systems Air Temp to Ensure Representative Average Air Temp Is Measured ML18102A7861997-01-23023 January 1997 Application for Amend to License DPR-75,revising TS Bases 3/4.3.3.1 Re Radiation Monitoring Instrumentation Channel 2R41 1999-08-25
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, ,~-I Public Service Electric and Gas Company Louis F. Storz Senior Vice President - Nuclear Operations Public Service Electric and Gas Comp~E p 28* ;99;36, Hancocks Bridge, NJ 08038 609-339-5700 LR-N95054 LCR 95-05 United States Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
LICENSE AMENDMENT APPLICATION REACTOR COOLANT SYSTEM - CHEMISTRY SALEM GENERATING STATION UNIT NOS. 1 and 2 FACILITY OPERATING LICENSE NOS. DPR-70 AND DPR-75 DOCKET NOS. 50-272 AND 50-311 This letter submits an application for amendment to Appendix A of Facility Operating Licenses DPR-70 and DPR-75 for Salem Generating Station Unit Nos. 1 and 2, respectively, and is being filed in accordance with 10CFR50. 90. Pursuant to the requirements of 10CFR50.91(b) (1), a copy of this request for amendment has been sent to the State of New Jersey.
The proposed Technical Specification revisions c::ontained herein represent changes
- to "Reactor Coolant System Chemistry" Specification 3/4.4.7 and Specification 3/4.4.8, (Salem Units 1 and Unit 2, respectively) . The proposed changes will remove these sections of the Technical Specifications and relocates the Bases to the Salem Updated Final Safety Analysis Report (UFSAR) and the Surveillance Requirements and Limiting Conditions for Operation (LCOs) to applicable plant procedures controlled by the 10CFR50.59 process. The Applicability will be changed from "At all times" to "Modes 1,2,3,4,5 and 6".
A description of the requested amendment, supporting information and analyses for the changes, and the basis for a no significant hazards consideration determination are provided in Attachment 1.
The Technical Specification pages affected and that would be removed by the proposed change are provided in Attachments 2 and 3, with pen and ink changes, for Salem Units 1 and 2, respectively.
The proposed changes have been evaluated in accordance with 10CFR50. 91 (a) (1), using the criteria in 10CFR50. 92 (c), and it has been determ1ned that this request involves no significant hazards considerations.
Printed on Recycled Paper 9510050020 950928 PDR ADOCK 05000272 f\(JD \ I I p PDR
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Document Control Desk SEP 2 8 1995 LR-N95054 In accordance with the guidance presented in the "Final Policy Statement on Technical Specifications Improvements for Nuclear Power Reactors" as published in the Federal Register (58 FR 39132),
the proposed changes have received a multidisciplinary review by responsible technical supervisory personnel, including onsite operations personnel.
Upon NRC approval of this proposed changes, PSE&G requests that the amendment be made effective on the date of issuance, but implemented within sixty days to provide sufficient time for associated administrative activities.
Should you have any questions regarding this request, please contact us.
Sincerely,
~;,(~
Affidavit Attachments (3)
Document Control Desk SEP 2 8 1995
. LR-N95054 C Mr. T. T. Martin, Administrator - Region I U. s. Nuclear Regulatory Commission 475 Allendale Road King of Prvssia, PA 19406 Mr. L. N. Olshan, Licensing Project Manager - Salem
- u. s. Nuclear Regulatory Commission One White Flint North Mail Stop 14E21 11555 Rockville Pike Rockville, MD 20852 Mr. c. s. Marschall (S09)
USNRC Senior Resident Inspector Mr. K. Tosch, Manager IV NJ Department of Environmental Protection Division of Environmental Quality Bureau of Nuclear Engineering CN 415 Trenton, NJ 08625
REF: LR-N95054 LCR 95-05 STATE OF NEW JERSEY )
)SS.
COUNTY OF SALEM )
L. F. Storz, being duly sworn according to law, deposes and says:
I am Senior Vice President - Nuclear Operations of Public Service Electric and Gas Company, and as such, I find the matters set forth in the above referenced letter, concerning the Salem Generating Station, Unit Nos. 1 and 2, are true to the best of my knowledge, information and belief.
Subscribed and Sworn to before me day o~pfu~ 1995 I
0 4~ 60];UIY'._ KIMBERLY JO BROWN NOTARY PUBLIC OF NEW JERSEY My Commission expires on My Commission Expires April 21, 19119
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ATTACHMENT 1 PROPOSED CHANGES TO TECHNICAL SPECIFICATIONS LICENSE AMENDMENT APPLICATION REACTOR COOLANT SYSTEM CHEMISTRY SALEM GENERATING STATION UNIT NOS. 1 AND 2 FACILITY OPERATING LICENSES DPR-70 AND DPR-75 LR-N95054 DOCKET NOS. 50-272 and 50-311 LCR 95-05 I. DESCRIPTION OF THE PROPOSED CHANGES The proposed changes relocate "Reactor Coolant System Chemistry" Technical Specification 3/4.4.7 (Salem Unit 1) and 3/4.4.8 (Salem Unit 2)and their associated Bases. It would remove these sections of the Technical Specifications and relocate the requirements to licensee documents controlled by the 10CFR50. 59 process. Additionally, the Applicability would be changed from "At all times" to "Modes 1,2,3,4,5 and 6 11
- II. REASONS FOR THE CHANGES The proposed changes to the Technical Specifications conform with the NRC's "Final Policy Statement on Technical Specifications Improvements for Nuclear Power Reactors", dated July 22, 1993 (58 FR 39132). During the development of NUREG-1431 "Standard Technical Specifications, Westinghouse Plants" the NRC issued a letter to the B&W Owners Group, T.E. Murley to w.s. Wilgus dated May 9, 1988, which identified in W-Table 2 "Westinghouse Standard Technical Specifications, LCOs Which May Be Relocated", the Reactor Coolant System Chemistry as a Limiting Condition for Operation (LCO) which may be relocated to other licensee-controlled documentation contingent upon NRC staff approval of the location of and controls over the relocated requirement.
Through this submittal, PSE&G is requesting implementation of the NRC' s recommendation regarding the relocation of the Reactor Coolant System Chemistry specification. The submittal will relocate the Bases to the Salem Generating station Unit Nos. 1 and 2 Updated Final Safety Analysis Report (UFSAR) and the Surveillance Requirements and LCOs to the applicable plant procedures. The Applicability will be changed from "At all times" to "Modes 1,2,3,4,5 and 6 11
- Removal of these specifications from the Technical Specifications is expected to produce an improvement in the safety of Salem Generating Station through a reduction in unnecessary plant transients and more efficient use of NRC and PSE&G resources. It would also reduce regulatory burden, Page 1 of 6
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ATTACHMENT 1
. REVISION OF SURVEILLANCE REQUIREMENTS FOR LCR 95-05 AREAS INSIDE CONTAINMENT since future changes to the Reactor Coolant System Chemistry functions would be conducted using the 10CFR50.59 process.
III. JUSTIFICATION FOR THE CHANGES The limitations on Reactor Coolant Chemistry ensure that corrosion of the Reactor Coolant System is minimized and that the potential for Reactor Coolant System leakage or failure due to stress corrosion is reduced. Maintaining the chloride, fluoride and dissolved oxygen chemistry within the limits specified in the Salem Generating Station Unit Nos. 1 and 2 UFSAR, Table 5. 2-28, "Reactor Coolant Water Chemistry Specifications", provides adequate corrosion protection to ensure the structural integrity of the Reactor Coolant System over the life of the plant. The associated effects of exceeding the chloride, fluoride and dissolved oxygen limits are time and temperature dependent. A review of the Reactor Coolant system Chemistry for chlorides, fluorides and dissolved oxygen for Salem Generating station Unit Nos. 1 and 2 for the past 5 years shows that the Action statement has not been entered while at normal power operation. During a Unit 2 shutdown in November 1991, while in Mode 3 and cooling down, the Reactor Coolant System chloride level was above Technical Specification limits for approximately 62 hours7.175926e-4 days <br />0.0172 hours <br />1.025132e-4 weeks <br />2.3591e-5 months <br />.
Moving all fuel to the Fuel Pool is a common outage activity.
This condition is commonly referred to as the "Mode Undefined." This Mode allows relief from certain equipment operability requirements in the Technical Specifications and permits draining the reactor vessel to facilitate outage work.
Performing water chemistry in accordance with the Technical Specifications in the Mode Undefined is an unnecessary task that does not provide commensurate safety benefit. When the Reactor Coolant System recirculation is removed from service and the reactor vessel is drained, samples are stagnant for lack of recirculation and represent coolant when the system was last in operation. The Bases for the Technical Specification is to minimize and reduce potential for Reactor Coolant System leakage or failure due to stress corrosion.
High stress and high temperature conditions which lead to stress corrosion, are absent in the Mode Undefined. After the reactor vessel is refilled and prior to fuel movement back to the reactor vessel, chlorides and fluorides are sampled to verify that Reactor Coolant System Chemistry is within limits.
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ATTACHMENT 1 LR-N95054
. REVISION OF SURVEILLANCE REQUIREMENTS FOR LCR 95-05 AREAS INSIDE CONTAINMENT Additionally, the plant procedure requirements will continue to provide adequate assurance that concentrations in excess of the limits will be detected in sufficient time to take corrective action.
With the conclusion of the Technical Specification Improvement Program, the NRC issued it's Final Policy Statement on Technical Specification Improvements for Nuclear Power Reactors (58 FR 39132). The NRC concluded that the purpose of the Technical Specifications is to impose those conditions or limitations upon reactor operation necessary to obviate the possibility of an abnormal situation or event giving rise to an immediate threat to the public heal th and safety. This was achieved by identifying those issues that are of controlling importance to safety and establishing on them certain limiting conditions for operation which cannot be changed without prior NRC approval.
This policy statement included a set of criteria which delineated those constraints on design and operation derived from the UFSAR and that belonged in the Technical Specifications in accordance with lOCFRS0.36. Specifically, these criteria are as follows:
Criterion 1 Installed instrumentation that is used to detect, and indicate in the control room, a significant abnormal degradation of the reactor coolant pressure boundary.
Licensee Determination Reactor Coolant System Chemistry is a chemical analysis of Reactor Coolant System water for chlorides, fluorides and dissolved oxygen. It is not installed chemistry analysis instrumentation that is used to detect, and indicate in the control room, a significant abnormal degradation of the reactor coolant pressure boundary.
Criterion 2 A process variable, design feature, or operating restriction that is an initial condition of a Design Basis Accident or Transient analysis that either assumes the failure of or' presents a challenge to the integrity of a fission product barrier.
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ATTACHMENT 1 e
. REVJ:SJ:ON OF SURVEJ:LLANCE REQUJ:REMENTS FOR LCR 95-05 AREAS INSIDE CONTAINMENT Licensee Determination A review of the appropriate Salem design bases documentation (i.e. , UFSAR) determined that Reactor Coolant System Chemistry is not a process variable, design feature, or operating restriction that is an initial condition of a Design Basis Accident or Transient analysis as discussed in the Accident Analysis Section of the UFSAR that either assumes the failure of or presents a challenge to the integrity of a fission product barrier.
Criterion 3 A structure, system, or component that is part of the primary success path and which functions or actuates to mitigate a Design Basis Accident or Transient that either assumes the failure of or presents a challenge to the integrity of a fission product barrier.
Licensee Determination A review of the appropriate Salem design bases documentation (i.e. UFSAR) determin.ed that Reactor Coolant System Chemistry is not a structure, system, or component that is part of the primary success path and which functions or actuates to mitigate a Design Basis Accident or Transient discussed in the Accident Analysis Section of the UFSAR that either assumes the failure of or presents a challenge to the integrity of a fission product barrier.
Criterion 4 A structure, system, or component which operating experience or probabilistic safety assessment has shown to be significant to public health and safety.
Licensee Determination A review of the Reactor Coolant System Chemistry for chlorides, fluorides and dissolved oxygen for Salem Generating Station Unit Nos. 1 and 2 for the past 5 years showed that the Action statement has never been entered while at normal power operation. During a Unit 2 shutdown in November 1991, while '
in Mode 3 and cooling down, the Reactor Coolant System chloride level was above Technical Specification limits for Page 4 of 6
ATTACHMENT 1 LR-N95054
. REVISION OF SURVEILLANCE REQUIREMENTS FOR LCR 95-05
.AREAS INSIDE CONTAINMENT approximately 62 hours7.175926e-4 days <br />0.0172 hours <br />1.025132e-4 weeks <br />2.3591e-5 months <br />. A review of the Probability Risk Assessment and the Individual Plant Examination for Salem Generating £tation showed that Reactor Coolant System Chemistry is not considered as a potential initiating event.
In summary, water chemistry, other than reactivity control, is not considered in the accident sequence evaluations.
Therefore, Reactor Coolant System Chemistry is not a structure, system, or component which operating experience or probabilistic safety assessment has shown to be significant to public health and safety.
In accordance with the NRC's criteria for determining those specifications which may be relocated to licensee-controlled documentation, PSE&G believes that this submittal for removing the Reactor Coolant system Chemistry specification from the Technical Specifications is justified. These changes will reduce regulatory burden while maintaining existing levels of plant safety.
IV. DETERMINATION OF NO SIGNIFICANT HAZARDS CONSIDERATION PSE&G has, pursuant to 10CFR50. 92, reviewed the proposed amendment to determine whether our request involves a significant hazards consideration. We have determined that operation of Salem Generating Station Unit 1 and Unit 2, in accordance with the proposed changes:
- 1. Will not involve a significant increase in the probability or consequences of an accident previously evaluated.
The proposed changes involve no hardware changes, no changes to the operation of any systems or components, and no changes to existing structures. Specifically, changing the Applicability from "At all times" to "Modes 1,2,3,4,5 and 6 11 by this submittal will not alter established chemistry for chlorides, fluorides and dissolved oxygen of the Reactor Coolant System. The relocation of this Surveillance Requirement/LCOs and Bases to plant procedures and the UFSAR respectively, will continue to ensure that the chemistry analysis of the Reactor Coolant System water is monitored and controlled. Changing the Applicability from "At all times" to "Modes 1, 2, 3, 4, 5 and 6" represent changes that do not affect plant safety and do not alter existing accident analyses.
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ATTACHMENT 1
- REVISION OF SURVEILLANCE REQUIREMENTS FOR LR-N95054 LCR 95-05 AREAS INSIDE CONTAINMENT
- 2. Will not create the possibility of a new or different kind of accident from any previously evaluated.
The proposed changes are procedural in nature concerning the location of the descriptive information and surveillance requirements for Reactor Coolant System Chemistry. Removing these specifications from the Technical Specifications and placing them in the UFSAR and plant procedures will not alter the maintenance of the Reactor Coolant System Chemistry or the ability to monitor its intended functions. Therefore, these changes will not create a new or unevaluated accident or operating condition.
- 3. Will not involve a significant reduction in a margin of safety.
The proposed changes relocate the Reactor Coolant System Chemistry Requirements/Leos from the Technical Specifications to the UFSAR and plant procedures in accordance with guidance provided by the NRC Final Policy Statement (58 FR 39132) regarding the improvement of Technical Specifications. The requirements that will reside in the UFSAR and plant procedures for the Reactor Coolant System Chemistry will ensure that the ability to determine chloride, fluoride and dissolved oxygen concentrations in the Reactor Coolant System is properly maintained and that the maintenance of the Reactor Coolant System Chemistry will be commensurate with its safety significance. Therefore, the proposed changes will not involve a significant reduction in any margins of safety.
V. CONCLUSIONS Based on the above, PSE&G has determined that the proposed change does not involve a significant hazards consideration.
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TECHNICAL SPECIFICATION PAGE WITH PEN AND INK CHANGES LICENSE AMENDMENT APPLICATION REACTOR COOLANT SYSTEM - CHEMISTRY SALEM GENERATING STATION UNIT 1 FACILITY OPERATING LICENSE DPR-70 LR-N95054 DOCKET NO. 50-272 LCR 95-05 The following Technical Specification for Facility Operating License No. DPR-70 is affected by this License Amendment Request:
Technical Specification Pages INDEX V, XII 3/4.4.7 3/4 4-17, 3/4 4-18, 3/4 4-19, B 3/4 4-4 INSERTS INSERT A 3/4.4.7 DELETED INSERT B 3/4.4.7 DELETED INSERT C PAGES 3/4 4-17 THROUGH 3/4 4-19 DELETED INSERT D 3/4 4-17 through 3/4 4-19 INSERT E 3/4.4.7 THIS SECTION DELETED
- TECHNICAL SPECIFICATION PAGE WITH PEN AND INK CHANGES LICENSE AMENDMENT APPLICATION REACTOR COOLANT SYSTEM - CHEMISTRY SALEM GENERATING STATION UNIT 2 FACILITY OPERATING LICENSE DPR-75 LR-N95054 DOCKET NO. 50-311 LCR 95-05 The following Technical Specification for Facility Operating License No. DPR-75 is affected by this License Amendment Request:
Technical Specification INDEX V, XII 3/4.4.8 3/4 4-20, 3/4 4-21, 3/4 4-22, B 3/4 4-5 INSERTS INSERT F 3/4.4.8 DELETED INSERT G 3/4.4.8 DELETED INSERT H PAGES 3/4 4-20 THROUGH 3/4 4-22 DELETED INSERT I 3/4 4-20 through 3/4 4-22 INSERT J 3/4.4.8 THIS SECTION DELETED