ML18219B522

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06/06/1978 Letter Licensee Event Report
ML18219B522
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 06/06/1978
From: Shaller D
American Electrtic Power System, Indiana Michigan Power Co, (Formerly Indiana & Michigan Power Co)
To: James Keppler
NRC/IE, NRC/RGN-III
References
LER 1978-031-03L
Download: ML18219B522 (6)


Text

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIBS>DISTRIBUTION FOR INCOMING MATERIAL'0-316 REC: KEPPLER J G ORG: SHALLER D V DOCDATE: 06/06/78 NRC IN 8.MI PWR DATE RCVD: 06/19/78 DOCTYPE: LETTER NOTARIZED:

NO COPIES RECEIVED

SUBJECT:

LTR 1 ENCL 1 FORWARDING LICENSEE EVENT REPT (RO 50-316/78-031>

ON 05/07/78 CONCERNING DURING NORMAL OPERATIONr TWENTY TWO EVENTS OCCURRED BETWEEN Tl IE DATES OF MAY 7 5 MAY 19'HERE ROD POSITION INDICATION DID NOT MEET THE PLUS-MINUS 12 STEP LIMIT OF TECH SPEC 3.1.3.2 PLANT NAME: COOK-UNIT 2 REVIEWER INITIAL: X JM DISTRIBUTOR INITIAL:~t" N DISTRIBUTION OF Tl-IIS MATERIAL IS AS FOLLOWS 4~4++<<<<<<<<+<<<+

4 NOTES: '1.SEND 3 COPIES OF ALL MATERIAL TO ISE, ED REEVES-1 CY ALL MATERIAL , COINCIDENT REPORTS (DISTRIBUTION CODE A002>, FOR ACTION: INTERNAL: EXTERNAL: BR F LWR82 BC~~W/4 ENCL REG FILE+/ENCL/Q ENCL I 5 C SYSTEMS BR++W/ENCL NOVAK/CHECK4+W/ENCL AD FOR ENG++W/ENCL HANAUER+4W/ENCL AD FOR OPER TECH>+W/ENCL ENGINEER(Ng gR+~W/ENCL KREGER/J.COLL INS4~+W/ENCL K SEYFRIT/IE+<W/ENCL LPDR S ST.JOSEPH MI++W/ENCL TIC4+W/ENCL NS IC++W/ENCL ACRS CAT B+~W/16 ENCL I~NRC PDI~%+W/ENCL MIPC<<W/3 ENCL EMERGENCY PLAN BR>~W/ENCL EEB44W/ENCL PLANT SYSTEMS BR>+W/EhlCL ,ADFQR PLANT SYSTEMS+<W/ENCL

REACTOR SAFETY BR<+W/ENCL
VOLLMER/BUNCH%<&W/ENCL POWER SYS BR+>W/ENCL Nllfl>"<<4g~<~DISTRIBUTION:

LTR 45 ENCL 45 SIZE: 1P~.i P+iP"WICI'"<<~<<~t e)<<~i%%%%%%%%-K%%%%8E<4"k4

%%889FCF%4F%%%%%%%%4%

Tl-IE END CONTROL NBR: 783.700017 I%%4%%%%%%%%%%8%%%%%%%%%00%%%%%%%>meriossn":" INDIANA&MICHIGAN PDNER CDMPANY DONALD C.COOK,'UCLEAR PLANT'.O.Box 458, Bridgman, Michigan'49106 June 6, 1978 41 g~'a og.)<~(gg Mr.J.G.Keppler, Regional Director Office of Inspection and Enforcement United States Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137

Dear Mr.Keppler:

Operating License DPR-74 Docket No.50-316 Pursuant to the requirements of the Appendix A Technical Specifications the following report is submitted:

RO 78-031/03L-O.

Sincerely, DE V.Shaller Plant Manager/bab cc: J.E.Dolan R.W.Jurgensen R.F.Kroeger R.Kilburn R.J.Vollen BPI K.R.Baker RO:III R.C.Callen MPSC P.W.Steketee, Esq.R.Walsh, Esq.G.Charnoff, Esq.G.Olson J.M.Hennigan PNSRC J.F.Stietzel Dir., IE (30 copies)Dir., MipC (3 copies)~~~,;go g$lsIIIIj'I'II g~gi+IIUii(JUil 09 iS>s 781700017 "f Q~h p t

~1, NRC FORM 366 U.S.NUCLEAR REGULATORY COMMISSION (7.77z 4-A LICENSEE EVENT REPORT CONTQOL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6 N I 0 C C 2 QE 0 0 0 0 0 0 0 0 0 0 0 QR 4 I I'1 1 Q4 89 LICENSEE CODE 14 15 I lICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T~o1 o~LQB 0 5 0 0 0 3 1 6Q70 5 0 7 7 8QB0 6 0 6 7 8 Qe DOCKET NUMBER 68 69 EVENT DATE~'74 IS REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES i&10~o2 DURING NORMAL OPERATION, TWENTY-TWO EVENTS OCCURRED BETWEEN THE DATES OF MAY 7 AND MAY 19, WHERE ROD POSITION INDICATION (RPI)DID NOT MEET THE+12"STEP LIMIT OF T.S~3~1~3~2~THE ATTACHED SUPPLEMENT DESCRIBES ALL THESE EVENTS~=AFTER THE EVENT ON 5 16 78 THE RPI FOR D 8 WAS DECLARED INOPERABLE.

THE ACTION REQUIREMENT OF B T.S.3.1.3.2a WAS FULFILLED.

PREVIOUS OCCURRENCES OF A SIMILAR NATURE INCLUDE RO 050/315-78-07 04 77-34 33 28 27 76-54 44 13 RO-050/316 78-22 08 07 o B (SEE ATTACHED SUPPLEMENT) 80 7 8 9 SYSTEM CAUSE CAUSE~OB Q11 fJ Q12 LI Q13'Q14~I Q15~Z Q16 7 8 9 IO 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LF RiRP EVENT YEAR REPORT NO, COQ.E TYPE NO.Q17 REPoRT LIIO Q~03 I Qr LOCI QL Q[JO 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.'OMPONENT TAKEN ACTION ON PLANT METHOD HOURS&22 SUBMITTED FORM SUB.SUPPLIER MANUFACTQBER.

~EQ16~ZQ16~ZQ26 gJ 0 0 0 Tl+YQ23~YQ24~NQ25 N 1" QR 33 34 35 36 37 40 41'2 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS&27~ID INVEST I GATION REVEAL'ED THAT MOST OF THESE EVENTS'INVOLVED MEASUR'ING THE AFFECTED DLII ROD'S SECONDARY COIL VOLTAGE TO VERIFY THAT THE ROD WAS AT THE PROPER POSITION.THE SIGNAL CONDITIONING MODULE WOULD THEN BE CALIBRATED AND PLACED BACK IN SERVICE RETURN 4 RETURNING TO WITHIN THE, 12 STEP T.S.LIMIT WITHOUT (SEE ATTACHED SUPPLEMENT) 8 9 FACILITY 3P METHOD OF E Q26~07 0 Q>>CII',~)PQ OPERATOR IIIITNYfAYfOIP"'

7 8 9 10 12 44 45 46 ACTIVITY CONTENT'ELEASED OF RELEASE AMOUNT OF ACTIVITY~LOCATION OF RELEASE Q EZ LI Q3'JQ34 NA NA 7 8 9 10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~39 7~OG 0 Q37 Z Q36 NA 7 8 9 11 12 13 PERSONNEL INJURIES 45 3 I N G R P I TO W I TH I N T H E+1 2 ST E P L I M I T.S E V E RA L 0 F T H E E V E N T S RE S U LT E D W I T H R P I 80 80 80 80 7 8 7 8 O 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION Z Q42 9 10 PUBLICITY ISSUED DESCRIPTION

~LmJQ44 9 10 NAME OF PREPARER NA NA Jack Rischlin 68 69 PHONE: 80 80 NRC USE ONLY ER ,BO o 0 L SUPPLEMENT TO EVENT DESCRIPTION OF LICENSEE EVENT REPORT 878-031/03L-0 THIS IS A LISTING OF EVENTS WHERE RPI DID NOT MEET THE 12 STEP LIMIT OF T.S.3.1.3.2.DATE TIME ROD POSITION INDICATION AFFECTED 5/7 5/8 5/8 5/9 5/9 5/10 5/10 5/10 5/10 5/10 5/12 5/14 5/14 5/15 5/15 5/15 5/15 5/16 5/16 5/16 5/19 5/19 2315 D-8,D-12, M-8, H-8 1210 C-9 1725 D-4, D-8, D-12, M-12'004 D-8 2213 D-4, D-8, D-12, M-8, H-4 0358 D-4, D-8, D-12, M-4, M-8, M-12, H-8 1148 D-8, H-8, D-12 1238 M-8, M-12, H-4 2115 D-12, H-8., 2318 D-8, M-4, H-8, H-12 0553 D-4, D-8, D-12, M-12 2015 H-8 2327 H-8 0355 D-8 0413 D-8 1658 D-8 2136 D-8 0040 D-8 0338 D-8 0748 , ,D-8 (D-8 RPI Determined inoperable) 0200 H-8 1611 H-8 TO CAUSE DESCRIPTION IVE ACTION.THE D-8 RPI PROBLEM WAS FOUND TO BE"CAUSED BY SUPPLEMENT ANY CORRECT A CONNECTOR ON THE REACTOR HEAD, THE PINS WERE RECESSED IN THE CONNECTOR CAUSING THE RPI TO FLUCTUATE AS SHORTS OCCURRED.