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 Entered dateSiteRegionReactor typeEvent descriptionTopic
ENS 4006314 August 2003 21:33:00PerryNRC Region 3GE-6

Automatic reactor scram due to a loss of offsite power. All rods fully inserted. Supplying power to vital buses via emergency diesel generators. All system operating properly. NRC Resident Inspector was notified of the event by the licensee.

  • * * UPDATE ON 08/15/03 @ 2007 BY STRACH TO GOULD * * *

The NOUE was terminated at 1952. Off site power was restored and the emergency diesels secured. Notified FEMA (Austin), Reg 3 RDO (Burgess) and EO (Richards)

ENS 401262 September 2003 16:43:00PerryNRC Region 3GE-6On August 1, 2003, at 2118 hours, the Perry Nuclear Power Plant experienced an actuation of several Division 2 Balance-of-Plant (BOP) inboard isolation valves. At the time of the event, the plant was in Mode 1 (Power Operation). The isolation closed one or more valves in each of the following Division 2 subsystems: Liquid Radwaste Sumps, Containment Vessel Chilled Water, Reactor Water Sampling, Drywell and Containment Radiation Monitoring, and Control Room Ventilation. The event is considered an invalid system actuation, and is reportable under 10 CFR 50.73(a)(2)(iv)(A). The isolation was not initiated in response to actual plant conditions or parameters, and was not a manual initiation. It meets the criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) as a general containment isolation signal affecting containment isolation valves in more than one system. Therefore, notification is being provided via 60-day optional phone call in accordance with 10 CFR 50.73(a)(1). All systems functioned as expected for a partial BOP (inboard) isolation. Repositioning of the valves did not present operational concerns; they were re-opened per restoration procedures. The BOP isolation was attributed to an electrical transient on 120 volt AC electrical bus EK-1-B1 as a result of a failed capacitor. The capacitor had been previously replaced during Refuel Outage 9. This event was documented in the Corrective Action Program. Remedial actions include replacement of the defective capacitor. The capacitor will be sent out for failure analysis. The licensee notified the NRC Resident Inspector.
ENS 4032617 November 2003 15:26:00PerryNRC Region 3GE-6

While aligning the Emergency Service Water (ESW) to the swale, the sluice gates were opened without the ESW being aligned to the swale. This condition made both Div 1&2 Diesel Generators and all ECCS systems inoperable. The probable cause of this event is that the wrong procedure was used in this evolution. Procedure SOI-P45/49 sec 7.3.1 "ESW Pumphouse Forebay Emergency Supply Initiation" was used instead of the correct procedure SOI-P45/49 section 7.3.3. "Alignment of ESW to Pumphouse Forebay Emergency Supply". The condition was discovered at 1215 and corrected at 1220 after section 7.3.1 was exited and section 7.3.3 was used to complete the lineup to the swale. The NRC Resident Inspector was notified.

  • * * RETRACTED AT 1457 ON 12/02/03 BY LAUSBERG TO ROTTON * * *

Further engineering analysis documented (that) the safety function of the Emergency Service Water (ESW) system was not lost while the system was inappropriately aligned. Also, plant design accounts for operator action to restore proper alignment and ensure continued functionality. Since the safety function of ESW was, and would continue to be maintained, the ECCS systems did not and would not lose the ability to perform their safety functions. Therefore, this condition is not reportable under 10CFR50.72(b)(3)(v)(B) and (D) as an event or condition that could have prevented fulfillment of a safety function and ENF 40326 is retracted. The licensee notified the NRC Resident Inspector. Notified R3DO Bruce Burgess.

ENS 4040422 December 2003 00:31:00PerryNRC Region 3GE-6On 12/21/03 at 2021, it was discovered that the temperature control valve for the Division 1 Emergency Closed Cooling system had two blown fuses. This results in the Division 1 Control Complex chiller becoming inoperable. Concurrent with this the Division 2 Control Complex chiller was inoperable for planned maintenance. With this configuration both trains of safety related ventilation have been declared inoperable. This results in a loss of safety function for AC and DC distribution systems. Additionally this results in all Emergency Core Cooling systems being inoperable. This is reportable under 10 CFR 50.72 (b) (3) (ii) (b) and (b) (3) (v) (a, b & d) for unanalyzed condition and loss of a single train safety system. The licensee notified the NRC Resident Inspector.Safe Shutdown
Unanalyzed Condition
ENS 4046923 January 2004 14:05:00PerryNRC Region 3GE-6On November 29, 2003, at 1526 hours, the Perry Nuclear Power Plant experienced an actuation of several Division 2 Balance-of-Plant (BOP) inboard isolation valves as a result of the loss of the normal power supply to the Reactor Protection System (RPS) B. At the time of the event, the plant was in mode 1(Power Operations) at about 100% power. The isolation closed one or more valves in each of the following Division 2 subsystems: Main Steam line drains, Fuel Pool Cooling and Cleanup, Liquid Radwaste Sumps, Containment Vessel Chilled WATER, Reactor Water Sampling, Drywell and Containment Radiation Monitoring, and Control Room Ventilation. Instrumentation that receives electrical power from RPS B also lost power. Division 1 components and valves were not affected. The event is considered an invalid system actuation, and is reportable under 10 CFR 50.73(a)(2)(iv)(A). The isolation was not initiated in response to actual plant conditions or parameters, and was not a manual initiation. It meets the criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) as a general containment isolation signal affecting containment isolation valves in more than one system. Therefore, notification is being provided via 60-day optional phone call in accordance with 10 CFR 50.73(a)(1). All systems functioned as expected for an inboard isolation. Repositioning of the valves did not present operational concerns; and the valves were re-opened per restoration procedures. The BOP isolation was attributed to the loss of power to RPS B as a result of a blown fuse. The blown fuse was the result of the failure of a GE CR105 contactor due to age related degradation (insulating varnish degradation resulting in a winding to winding short circuit). This event was documented in the corrective action program. Remedial actions included replacement of the failed fuse and the RPS A and B normal power supply contactors and the RPS A alternate power supply contactor. The RPS B alternate power supply contactor will also be replaced. The NRC Resident Inspector was notified of this event by the licensee.
ENS 4059819 March 2004 16:17:00PerryNRC Region 3GE-6This report is being made in accordance with 10CFR50.73 (a)(1), which states, in part, "in the case of an, invalid actuation reported under 10 CFR50.73(a)(2)(iv), other than actuation of the reactor protection system (RPS) when the reactor is critical, the licensee may, at its option, provide a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER." These invalid actuations are being reported under 10CFR50.73(a)(2)(iv)(A). On February 22, 2004, at 1016 hours, while operating at 100 percent power, the reactor protection system manual scram channel functional test was performed. When a division 1 manual scram pushbutton was depressed, in addition to the expected half scram, the reactor protection system (RPS) A motor-generator electrical protection assembly circuit breakers tripped open. Loss of power from the RPS A motor-generator caused the loss of electrical power to the RPS instrumentation. This resulted in the invalid actuation of the logic that is powered by RPS A. The actuations resulted in isolation signals that closed one or more valves in each of the following division 1 subsystems: main steam line drains, containment and drywell radiation monitors, reactor water cleanup, fuel pool cooling, suppression pool cleanup, containment and drywell radwaste sumps and containment chilled water. All systems and components responded as designed for the signals that resulted from the loss of RPS A buss. This is considered a partial actuation since only division 1 components were effected. Following restoration of power to the RIPS A buss, the actuation logic was reset, and the equipment/systems were returned to the status required by plant conditions. Discussion of the causes and corrective actions associated with this event are documented in the corrective action program in condition report 04-00901. The resident inspector has been notified.Half scram
ENS 4076721 May 2004 16:11:00PerryNRC Region 3GE-6Emergency Service Water "A" (ESW) Pump failure results in inoperability of all Div 1 ECCS systems. The plant entered the Limiting Condition for Operation for the ESW inoperability at 0150 on 05/21/04. The action times for Tech Spec 3.7.1 are as follows: restore ESW to operable status within 72 hours, if this cannot be accomplished be in Mode 3 (Hot Shutdown) in the following 12 hours and Mode 4 (Cold Shutdown) in 36 hours. Reactor power was reduced at 1600 to begin the shutdown process. Division 2 and 3 ECCS are fully operable. The NRC Resident Inspector was notified of this event by the licensee.
ENS 4077424 May 2004 17:12:00PerryNRC Region 3GE-6Emergency Service Water "A" (ESW ) Pump failure resulted in inoperability of all Div 1 ECCS systems at 0150 on 05/21/04 (See event notification 40767). A plant shutdown was initiated with mode 4 (cold shutdown) achieved at 0619 on 05/23/04. During the disassembly and inspection of ESW A pump, a failed coupling on the pump shaft was found to be the cause of the failure. An Operability Determination (OD) was requested on ESW B at 1330 on 05/24/04 since both pumps had the identical coupling design and the pumps had similar run times. At 1500, the Design Engineering Manager informed the control room that engineering could not return a completed OD within the allotted time that could justify continued ESW B operability. The control room Shift Manager than declared the ESW B pump inoperable. This results in a condition that could have prevented the fulfillment of a safety function, specifically the removal of residual heat. The licensee notified the NRC Resident Inspector.Operability Determination
ENS 4082116 June 2004 15:52:00PerryNRC Region 3GE-6

At 1400 hours on June 16, 2004, it was confirmed that the plant had operated in excess of its licensed maximum power limit of 3758 megawatts thermal by about two (2) megawatts thermal. The power limit was determined to have been exceeded due to a feedwater temperature RTD being replaced on May 24, 2004, without having installed a matching transmitter. This error caused a non-conservative input into the core power calculation resulting in a small error. The error allowed the power to be about two (2) megawatts above the limit while indicating that it was within requirements. This condition occurred during two periods on 06/14/04 and 06/15/04. On 06/14/04 the first occurrence lasted for approximately 7 hours. The second occurrence lasted for 16 hours commencing on 06/14/04 and terminating on 06/15/04. The licensee identified this condition on 06/15/04 @ 1130 and the condition was corrected on 06/15/04 @ 1315. This notification is being submitted in accordance with PNPP Operating License Condition 2.F, as a potential violation of the Maximum Power Level specified in PNPP Operating License The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM K Russell to W Gott at 1356 on 8/16/04 * * *

A 24 hour notification was made on June 16, 2004, in accordance with (Perry Nuclear Power Plant) PNPP Operating License Condition 2.F, a potential violation of the maximum power level specified in PNPP Operating License Condition 2.C(1). At the time of discovery, maximum licensed power level was determined to have been exceeded by about 2 megawatts thermal as a result of a feedwater resistance temperature detector (RTD) being replaced without installing a matching transmitter. The feedwater temperature provided by this RTD provides an input to the core power calculation and was initially determined to have caused an error in the calculation of about 3.1 megawatts. Subsequently, as-found calibration data was taken that determined the RTD loop error was smaller than initially calculated. The resultant error in thermal power was calculated to be 0.1 megawatts. Review of the power history using the recalculated thermal power error resulted in a determination that the maximum licensed power level was not exceeded. Since the maximum licensed power level was not exceeded, this notification retracts ENF 40821. This retraction was discussed with the Resident NRC Inspector. Notified R3DO (Clayton)

Time of Discovery
ENS 4088220 July 2004 04:04:00PerryNRC Region 3GE-6

At 0344 hrs. EDT, the licensee declared an Alert under Emergency Action Level HA.1. The initiating event was a pegged high off gas ventilation effluent radiation monitor and inability to obtain a confirmatory sample within 15 minutes. Only the gaseous channel failed high. The particulate and iodine channels remained reading normally. When plant chemistry technicians were able to obtain samples (an initial and back-up), they were negative with no activity greater than background detected. The plant management and operations team is currently evaluating their exit strategy for the Alert. The plant remains stable at 100% power, operating at normal operating parameters. The NRC entered monitoring mode at 0438 hrs. in response to this event. Notified DOC (Outlaw), DOE (Wyatt), USDA (Brzostek), EPA(NRC) (Baumgartner), and HHS (Phillips). The NRC Resident Inspector was notified and is present in the control room.

  • * * UPDATE FROM RALPH DAVIS TO JEFF ROTTON AT 0907 HRS ON 07/20/04 * * *

The licensee terminated the Alert at 0901 hrs. EDT. The basis for the termination was that samples taken at the site boundary were negative, samples taken locally at the skid indicated no activity, and the licensee determined that the radiation monitor equipment was faulted. The NRC Resident Inspector was notified by the licensee. The licensee notified the State of Ohio (Collins), Ashtabula County, OH, Geauga County, OH and Lake County, OH. The NRC exited monitoring mode at 0914 hrs. EDT. The NRC Operations Center notified DHS (Everett), FEMA (Biscoe), DOE (Smith), EPA(NRC) (Jones), USDA (Comeau), HHS (Molina), HQPAO (Brenner), DOC (Outlaw) and RIVDO (Farnholtz).

  • * * RETRACTION FROM MEADE TO CROUCH AT 1637 EDT ON 9/10/04 * * *

The following retraction was received from the licensee via facsimile: Update to Emergency Plan Alert Event Notification 40882 Retraction This is a follow-up notification to inform the NRC that Perry Nuclear Power Plant (PNPP) is retracting an Alert Emergency Declaration reported on July 20, 2004. Emergency Action Level HA.1, 'Any unplanned release of gaseous radioactivity to the environment that exceeds 200 times the ODCM (Offsite Dose Calculation Manual) Control limit for 15 minutes or greater', was entered based on an invalid reading due to a failed instrument. The Offgas Vent Pipe Gaseous Radiation Monitor had pegged offscale high. The post-accident high range Offgas Vent Pipe Gaseous Radiation Monitor, which monitors the same process stream, had started in response to the offscale reading and was indicating low, which did not correspond to the offscale readings. The radiation monitors for Offgas pre-treatment and post treatment process streams were both reading normally for the plant conditions. Other plant and process radiation monitors, post accident high range monitors, and area radiation monitors did not indicate increased radiation levels to support the off-scale Offgas Vent Pipe Gaseous Radiation Monitor. Aside from the one offscale radiation monitor, there were no corresponding indications that there was a release in progress. The Shift Manager took actions based on the offscale reading. In addition to the radiation monitor reading, the entry criteria for the Emergency Action Level (EAL) required entry into an Alert, unless gaseous effluent levels were verified by chemistry sample analysis methods to be less than the ODCM limits within 15 minutes. These results were not provided within 15 minutes, therefore the Shift Manager declared the Alert. Troubleshooting confirmed that the Offgas Vent Pipe Gas instrument reading was invalid. The Emergency Plan directs classification of events based on valid indications. At no time was there any unplanned release that would have required taking any emergency plan actions. Therefore, the entry criteria in the EAL were not met and the Alert emergency classification is being retracted. The licensee notified the NRC Resident Inspector of this retraction. Notified NRREO (Reis), R3DO (Hills) and IRD (Nieh).

ENS 4094913 August 2004 12:56:00PerryNRC Region 3GE-6A licensed employee was determined to be unfit for duty based on current requirements for unescorted access. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee HAS informed the NRC Resident Inspector.
ENS 410842 October 2004 15:22:00PerryNRC Region 3GE-6

A surveillance test was being performed on the Emergency Recirc vent System and all six dampers on both trains failed to stroke in the required Tech. Spec. times. Therefore, both trains of the Emergency Recirc Vent System were declared inoperable and the plant entered T.S. 3.0.3. The LCO action statement requires the plant to be in mode 2 in 7 hours and mode 3 in the following six hours and mode 4 in the following 24 hours. They are currently troubleshooting the problem. The NRC resident Inspector was notified HOO Note: see event 41085

  • * * UPDATE ON 10/02/04 AT 1940 EDT FROM FREDERICK SMITH TO GERRY WAIG * * *

Update to (Event) Notifications 41084 and 41085: At 1840 (EDT) on 10/02/04 it was determined that the apparent slow response times of the Control Room Emergency Recirculation (CRER) dampers was due to a malfunctioning relay in the initiation circuit, not due to failure of the dampers. The LCO actions associated with the CRER system were exited and the actions associated with the initiation instrument were entered. Therefore the plant is no longer required to shutdown per T.S. 3.0.3. The plant shutdown has been terminated. Plant power will be returned to 100%. The licensee has notified the NRC resident Inspector. Notified R3DO (Thomas Kozak).

  • * * RETRACTION FROM KEN MEADE TO BILL HUFFMAN ON 10/25/04 AT 1433 EDT * * *

At 1300 on 10/02/04, results of a surveillance indicated that dampers in both trains of the Control Room Emergency Recirculation System (CRERS) were slower than allowed by Technical Specifications (TS) requiring both trains of the CRERS to be declared inoperable. With both trains inoperable, Technical Specification 3.0.3 was entered which required a plant shutdown. The shutdown was commenced at 1500. This condition was reported as required in Event Notification 41085. Additionally, with both CRERS trains inoperable, this condition was determined to be reportable as a loss of safety function (accident mitigation) and was reported as required in Event Notification 41084. Subsequently, it was determined that the failure was the result of a defective time delay relay in the radiation monitor initiation circuit. Other inputs that would have caused the dampers to reposition in an accident were not impacted. The appropriate TS (3.3.7.1), for the radiation monitor, was entered and TS 3.0.3 was exited. The significant actions required by this TS were to restore the function within 7 days or place the system in emergency recirculation. It did not require entry into an action to shutdown. When this condition was identified, TS 3.0.3 was exited, the shutdown was terminated, and the plant was restored to full power. Since a TS required shutdown was not required, Event Notification 41085 is being retracted. The condition was also reported as a loss of safety function for the accident mitigation function of CRERS. The CRERS is automatically activated by a Loss of Coolant Accident (LOCA) signal or a Control Room Ventilation (CRV) high radiation signal. The LOCA instrumentation circuitry was not affected by the defective time delay relay and thus the damper stroke times were not impacted. The CRV airborne radiation monitor signal is considered a "diverse" signal to the LOCA signal. Since the LOCA signal would have properly initiated the CRERS and the CRV high radiation signal is redundant, there was no loss of safety function. Since there was no loss of safety function, Event Notification 41084 is being retracted. The licensee has notified the NRC Resident Inspector. NRC R3DO(Gardner) has been notified.

Stroke time
ENS 410852 October 2004 15:22:00PerryNRC Region 3GE-6

At 1500 hours the plant commenced reactor shutdown from 100% power for entering T.S. 3.0.3 due to both trains of the Emergency Recirc Vent System being declared inoperable. The reactor will be in mode 2 by 2000 hours, mode 3 by 0200 hours on 10/03 and mode 4 by 0200 hours on 10/04. If the problem is corrected, they will terminate the shutdown. The NRC Resident Inspector was notified. HOO Note: see event 41084

  • * * UPDATE ON 10/02/04 AT 1940 EDT FROM FREDERICK SMITH TO GERRY WAIG * * *

Update to (Event) Notifications 41084 and 41085: At 1840 (EDT) on 10/02/04 it was determined that the apparent slow response times of the Control Room Emergency Recirculation (CRER) dampers was due to a malfunctioning relay in the initiation circuit, not due to failure of the dampers. The LCO actions associated with the CRER system were exited and the actions associated with the initiation instrument were entered. Therefore the plant is no longer required to shutdown per T.S. 3.0.3. The plant shutdown has been terminated. Plant power will be returned to 100%. The licensee has notified the NRC resident Inspector. Notified R3DO (Thomas Kozak).

  • * * RETRACTION FROM KEN MEADE TO BILL HUFFMAN ON 10/25/04 AT 1433 EDT * * *

At 1300 on 10/02/04, results of a surveillance indicated that dampers in both trains of the Control Room Emergency Recirculation System (CRERS) were slower than allowed by Technical Specifications (TS) requiring both trains of the CRERS to be declared inoperable. With both trains inoperable, Technical Specification 3.0.3 was entered which required a plant shutdown. The shutdown was commenced at 1500. This condition was reported as required in Event Notification 41085. Additionally, with both CRERS trains inoperable, this condition was determined to be reportable as a loss of safety function (accident mitigation) and was reported as required in Event Notification 41084. Subsequently, it was determined that the failure was the result of a defective time delay relay in the radiation monitor initiation circuit. Other inputs that would have caused the dampers to reposition in an accident were not impacted. The appropriate TS (3.3.7.1), for the radiation monitor, was entered and TS 3.0.3 was exited. The significant actions required by this TS were to restore the function within 7 days or place the system in emergency recirculation. It did not require entry into an action to shutdown. When this condition was identified, TS 3.0.3 was exited, the shutdown was terminated, and the plant was restored to full power. Since a TS required shutdown was not required, Event Notification 41085 is being retracted. The licensee has notified the NRC Resident Inspector. NRC R3DO(Gardner) has been notified.

ENS 411734 November 2004 11:11:00PerryNRC Region 3GE-6

At 1054 EST on 11/04/04, the licensee declared an Unusual Event due to an acidic water spray in the Water Treatment Building affecting normal access. Licensee entered EAL MU-1, Toxic Gas detected within the Protected Area that impacts normal operations. There were two personnel in the building at the time of the leak, one Non-licensed operator and his supervisor. The Non-licensed operator was overcome by fumes and became nauseous and was taken to the onsite dispensary. The non-licensed operator was treated and taken to the local hospital. The supervisor did not seem to be affected, but he has been taken to the onsite dispensary for any necessary treatment. No unplanned release has occurred and no protective action recommendations are applicable at this time. The acidic water spray made contact with a 480 Vac panel in the building and has caused an electrical ground. Equipment in the building that may potentially affect plant operation if damaged are the clearwell pumps. The clearwell pumps supply seal water for the Main Circulating water pumps, and the non vital service water pumps. The licensee notified the NRC Resident Inspector and made all state and local government emergency management notifications.

  • * * Update on 11/04/04 at 1338 EST by Rick Wiles taken by MacKinnon * * *

Atmospheric conditions in the area have been confirmed to be normal. Slippery conditions and acid hazard still exist on the floor. Licensee is still in an Unusual Event. NRC Resident Inspector has been notified of this update. R3DO (S. Burgess) notified.

  • * * Update on 11/04/04 at 1512 EST by Rick Wiles taken by MacKinnon * * *

Unusual Event terminated at 1502 EST. Surrounding Counties and the State of Ohio were notified by the licensee that the Unusual Event was terminated. NRC Resident Inspector notified of the termination of the Unusual Event. R3DO (Sonia Burgess), NRR EO (Terry Reis), IRD (Dick Wessman), FEMA (Austin) and DHS (Lee) notified.

ENS 4119512 November 2004 15:20:00PerryNRC Region 3GE-6

The licensee had carbon dioxide release in the turbine lube oil bay affecting normal access. There was no unplanned radioactive release. There was no indication of a fire. There were no personnel injuries or equipment damage. At 1540 11/12/04, the NRC made the decision to remain in the Normal Mode. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM J BITONTI TO W GOTT AT 1556 ON 11/12/04 * * *

At 1540 Perry remains in an unusual event. The carbon dioxide release was not due to a fire. The licensee is ventilating the area to restore normal access. The fire department has been requested and is currently on site. There are no abnormal elevated radiation levels detected out the plant vents requiring consideration of offsite protective actions. Notified R3 (Lipa).

  • * * UPDATE AT 1651 ON 11/12/04 FROM J BITONTI TO M RIPLEY * * *

At 1636 EST the licensee secured from the Unusual Event. Normal access has been restored to the area and a fire watch established until the fire suppression system is restored to normal. The licensee notified the NRC Resident Inspector. Notified R3DO (Ring), IRD (Wessman), NRR (Reis), NSIR (Weber), DHS (Reed), and FEMA (Biscoe)

Fire Watch
ENS 4126917 December 2004 16:40:00PerryNRC Region 3GE-6

During the performance of the High Pressure Core Spray system (HPCS) quarterly pump and valve operability test, the waterleg pump discharge low pressure alarm was unable to be cleared. It was determined that the waterleg pump discharge check valve had failed to open to provide keepfill flow. The HPCS system had been declared (inoperable at 0818 for a planned surveillance activity. At 1109, the low pressure alarm came in as expected, but was not able to be cleared. Subsequent mechanical agitation of the waterleg pump discharge check valve caused the valve to open and the low pressure condition to clear. Tech Spec 3.5.1 is applicable. Entry time 0818 on 12/17/04. Action is to restore HPCS to Operable within 14 days. NRC Resident Inspector was notified.

  • * * UPDATE ON 01/05/05 @1211 BY KEN MEADE TO CHAUNCEY GOULD * * * RETRACTION

An 8 hour notification was made on December 17, 2004, in accordance with 10CFR50.72(b)(3)(v)(C) and 10CFR50.72(b)(3)(v)(D). The report was made due to a potential loss of the High Pressure Core Spray (HPCS) system safety function as a result of the loss of keep-fill pressure. The water-leg pump discharge check valve was determined to be the most likely cause of the loss of keep-fill pressure and was replaced. A preliminary investigation has determined that the water-leg pump discharge check valve had sufficient corrosion products (on the rising stem) to cause the valve disk to stick. With the check valve not able to fully open, the system low pressure alarm was activated. The lowest system pressure, about 24 psig, was determined to be just below the alarm setpoint of 27 psig. The alarm setpoint includes a 10 psig margin between receipt of the alarm and the pressure at which the piping would start to void. The pressure, 24 psig, was equivalent to the static head provided by the Condensate Storage Tank (CST) to the HPCS system. This alignment is the method used to maintain the system filled when the water-leg pump is unavailable. The 24 psig system pressure was adequate to maintain the system full. Since the system pressure was adequate and the HPCS system was maintained full, the safety function of the system was not adversely affected. Since the safety function was not affected, there is no reportable condition and Event Notification 41269 is retracted. The NRC Resident Inspector was notified.

ENS 4129024 December 2004 03:07:00PerryNRC Region 3GE-6At 2345 on 12/23/04 both reactor recirc pumps down shifted from fast to slow speed which resulted in reactor power reducing from 100% to 44%. At 2354 an automatic scram occurred from the activation of the Oscillation Power Range Monitor (OPRM) instrumentation. After the scram all safety systems responded as designed. Cause of the reactor recirc pump downshift is still under discovery. All rods fully inserted. No safety relief valves lifted during the transient. The licensee was in no major LCO at the time. Pressure control is via the steam bypass valves. The licensee has notified the NRC Resident Inspector.
ENS 413106 January 2005 04:01:00PerryNRC Region 3GE-6At approximately 0106 on 1-6-05, Reactor Recirculation Pumps A and B down-shifted from fast to slow speed which resulted in reactor power decreasing from 100% to approximately 46%. As operators started to reduce power using control rod insertion, Reactor Recirculation Pump A tripped to 'off.' At 0112 on 1-6-05, a manual reactor scram was inserted due to operating under undesirable power to flow conditions. At approximately 0119, the operators were unable to start the Motor Feedwater Pump, Reactor Core Isolation Cooling system was manually started. Level control was established using a Reactor Feed Pump Turbine and Reactor Core Isolation Cooling. The Main Steam Isolation Valves were closed to limit cooldown. Reactor level is being controlled with the Reactor Core Isolation Cooling System and safety relief valves are available for reactor pressure control. The cause of the Reactor Recirculation Pumps down-shifting and the subsequent trip of Reactor Recirculation Pump A is still under investigation. The cause of the Motor Feedwater Pump failure to start is likewise under investigation. All control rods fully inserted. The lowest reactor level reached was 154 inches above TAF. The electrical grid is stable and ESF systems remain available. Reactor pressure and level are being maintained by the Reactor Core Isolation Cooling system. The licensee notified the NRC Resident Inspector.
ENS 4134419 January 2005 05:54:00PerryNRC Region 3GE-6

The environmental temperature of the tornado missile enclosure for the Emergency Diesel Generators during an accident condition when all three testable rupture disks open is expected to exceed the limiting temperature for the structural concrete. A detailed analysis of the capability of the tornado missile enclosure concrete to meet that standard cited in the USAR section 3.8.3.3.7 has not been located. At 0237 on 19 January 2005, Division 1,2 & 3 Diesel Generators were declared inoperable. Actions of Technical Specification 3.8.2 were directed and compliance verified. NRC Resident Inspector was notified of this event by the licensee.

  • * * UPDATE ON 03/23/05 @ 1524 BY KEN MEADE TO CHAUNCEY GOULD * * * RETRACTION

The following information was provided by the licensee by fax: An 8-hour notification was made on January 19, 2005, in accordance with 10CFR50.72(b)(3)(ii)(B), for an unanalyzed condition and 10CFR50.72(b)(3)(v)(D), for the loss of the accident mitigation safety function. This report was made after declaring division 1, 2, and 3 diesel generators inoperable because the tornado missile enclosure concrete analysis demonstrating compliance with USAR section 3.8.3.3.7 could not be located. Compensatory measures were taken to protect the concrete and vent lines in the area while an analysis was performed. The required analysis was performed by a contract engineering firm. On March 23, 2005, the analysis was owner accepted with comments for incorporation into the final report. None of the comments affected the conclusion of the analysis. This analysis confirmed that the concrete enclosure, as originally designed, supported operability of the diesel generators and their support subsystems. Modifications are being implemented to improve the design margin of the safety related enclosure under accident conditions with the testable rupture disks open. These design modifications are improvements and were not required for past diesel generator operability. Since the operability of the diesel generators and their support subsystems were not affected, there was no unanalyzed condition that significantly degraded plant safety, nor was there a loss of safety function. Since there was no reportable condition, ENF 41344 is retracted. The NRC Resident Inspector was notified. Notified RDO (Kozak)

Unanalyzed Condition
Tornado Missile
ENS 4141717 February 2005 22:05:00PerryNRC Region 3GE-6The following information was provided by the licensee via facsimile: During testing of the Division 2 Diesel Generator Testable Rupture Disc (TRD), it was discovered that excessive force was needed to open its damper. The function of the TRD is to open to relieve exhaust pressure should the diesel generator's non-safety exhaust silencer become blocked. Upon inspection of the TRD, some deformation was noted on the TRD damper. Since the possibility that the condition might exist on the other two divisional diesel generators could not be ruled out, they were also declared inoperable and LCO 3.0.3 entered. An unanalyzed condition potentially exists because a change in engineering design potentially affected multiple trains. Since all three diesel generators are inoperable, a loss of off-site power would challenge safe shutdown capability, the ability to remove decay heat and accident mitigation. A plant shutdown required by Technical Specifications (LCO 3.0.3) was required due to declaring all 3 divisional diesel generators inoperable. LCO 3.0.3 was entered at 1730 hrs on 2/17/05. No power reduction was required as the Division 2 Diesel Generator was declared operable at 2011 after unlatching its Testable Rupture Disc (TRD) (and LCO 3.0.3 was exited). The resident NRC inspector was informed of the LCO 3.0.3 entry and exit (and this event notification). No other notifications of governmental agencies or the press are planned. At the time of the notification to NRC Headquarters, the Division 1 EDG TRD had been unlatched and declared operable. The Division 3 EDG TRD was expected to be unlatched within the next hour.Safe Shutdown
Unanalyzed Condition
ENS 415758 April 2005 05:32:00PerryNRC Region 3GE-6

The following information was provided by the licensee (licensee text in quotes): All three divisions of Emergency Diesel Generators were declared inoperable due to performing at risk design changes on the operable diesel. The design change was removed from the division one diesel and it was declared available at 2045 on 4/7/05. All three diesels remain inoperable. Perry 1 is currently shutdown in refueling mode 5 and no core alterations are in progress. The licensee will notify the NRC Resident Inspector.

  • * * RETRACTION FROM KEN MEADE TO PETE SNYDER AT 0852 EDT ON 4/24/05 * * *

Update to Event Notification (ENF 41575) Retraction: An 8-hour notification was made on April 7, 2005 under 10CFR50.72(b)(3)(v) for the loss of the safety function. The report was made due to declaring division 1 diesel generator inoperable at 2028 hours on April 7, 2005 with Division 2 and 3 inoperable for unrelated refuel outage activities. Division 1 diesel generator was declared inoperable as a result of performing an at-risk design change on the exhaust system, i.e., installing insulation blankets on the exhaust piping. The at-risk design change was removed from the division one diesel generator by 2045 hours on April 7, 2005. No other actions were taken during the course of events that would have otherwise rendered the Division 1 diesel generator inoperable. An evaluation was completed on April 8, 2005 confirming that the additional weight of the insulation on the exhaust piping had no impact on diesel generator operability. Division 1 diesel generator was subsequently declared operable at 0534 hours on April 9, 2005. Since there was no loss of safety function, there is no reportable condition. Since there was no reportable condition. ENF 41575 is retracted. The licensee has notified the NRC Resident Inspector. Headquarters Operations Officer notified R3DO (Hills).

Safe Shutdown
ENS 416572 May 2005 09:43:00PerryNRC Region 3GE-6

On 5/1/05 at 19:16, the plant entered MODE 2 and began a reactor startup. After withdrawing control rods, but prior to criticality, perturbations were noticed on reactor vessel level indications and control rod withdrawal was halted. At 22:32 control rods were inserted in reverse order to maintain the reactor subcritical. At that time, level instrumentation associated with the 'A' level reference leg was declared inoperable. All control rods were inserted at 23:02 in Mode 2. At 23:32 on 5/1/05 a 12 hour shutdown statement was entered due to the inoperable level instrumentation. Efforts were underway to troubleshoot and restore the level Instrumentation. On 5/2/05 at 06:11 the reactor mode switch was placed in shutdown - level instrumentation will not be restored within the time allowed by Technical Specifications. Instrument fill and vent procedures are being implemented at this time. The plant expects to enter Mode 2 later today. Technical specification 3.3.6.1 requires restoration within one hour, shutdown within 12 hours. This reference leg level affects both the wide and narrow range level instruments and feed into the Reactor Protective System, Emergency Core Cooling System Instrumentation, and Isolation Instrumentation systems. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 6/3/05 AT 12:02 FROM PERRY'S COMPLIANCE SUPERVISOR (KEN MEADE) TO ABRAMOVITZ * * *

Update to Event Notification (EN 41657) Retraction: A 4-hour notification was made on May 2, 2005, in accordance with 10CFR50.72(b)(2)(i), for a shutdown required by Technical Specifications. The report was made due to inserting all withdrawn control rods during a startup, prior to criticality, for Technical Specification 3.3.6.1 required actions. Technical Specification 3.3.6.1 was entered as a result of level perturbations determined to have been caused by reference leg keep-fill system operation when the reactor pressure vessel (RPV) was under vacuum conditions with minor component compression fitting leaks. Actions were taken to fix the minor leaks in the reference leg keep-fill panel. Additionally, the reference leg keep-fill system was removed from service until the RPV was pressurized. It was subsequently determined that since the reactor had not yet been taken critical, the reactor was in a shutdown condition. Per NUREG-1022, rev 2, section 3.2.1 'Plant Shutdown Required by Technical Specifications,' the 'initiation of any nuclear plant shutdown' does not include mode changes required by TS if initiated after the plant is already in a shutdown condition. Since the plant remained in a shutdown condition, this issue is not reportable. Since the condition is not reportable. EN 41657 is retracted. The licensee notified the NRC Resident Inspector. The R3DO (Burgess) has been notified.

ENS 416756 May 2005 16:46:00PerryNRC Region 3GE-6

Report - Loss of Safety Function On 5/5/06 at 1130 (EDT) it was discovered test equipment was left installed in the Reactor Water System instrumentation that rendered both system delta flow isolation instruments inoperable. The test equipment was removed and both instruments were declared operable at 1455. The system was in service at the time. The NRC Resident Inspector was notified.

  • * * RETRACTION FROM K. RUSSELL TO HOWIE CROUCH @ 1115 HRS. EDT ON 6/7/05 * * *

Update to Event Notification (ENF 41675) Retraction: An 8-hour notification was made on May 6, 2005, in accordance with 10CFR50.72(b)(3)(v), for the loss of the safety function for the control of radiation release. This report was made when it was discovered that test equipment (a pressure gauge) had been left attached to the Reactor Water Cleanup System (RWCU) differential flow isolation piping. The gauge was removed and the system aligned for proper operation. An engineering evaluation determined the temporary tubing and gauge would have maintained their structural integrity during a seismic event. Therefore, there was no impact on the piping for the leak detection capability of the RWCU differential flow isolation. Since there was no loss of function for the RWCU differential flaw isolation there was no loss of safety function for the control of radiation release. Because there is no loss of safety function, this condition is not reportable. Since the condition is not reportable, ENF 41675 is retracted. The licensee will be notifying the NRC Resident Inspector. Notified R3DO (Lara).

ENS 4207224 October 2005 12:41:00PerryNRC Region 3GE-6

This event is being reported as 10CFR50.72(b)(3)(ii)(B), an unanalyzed condition that significantly degrades plant safety. A postulated fire water system line break did not take into consideration the movement of a fire door boundary. Consequently, the break may affect safe shutdown of the plant. The door boundary was moved in May 1999. While assessing a calculation to update fire pump curves (CR 04-00422-04) it was found that the calculation does not appear to have been updated for the tornado depressurization event modifications (DCP 99-05014). Specifically, door DG-112 was moved to the control complex wall from the diesel generator wall. This door movement isolates the rattle space that was previously credited as a relief path for this internal flood. A full break is postulated for this line as the result of a safe shutdown earthquake. As the result of the postulated pipe break, both fire protection pumps are expected to auto start resulting in a break flow rate into the hallway of approximately 6,000 gpm. Standard Perry design practice is to assume a 30 minute duration for the pipe break flow isolation unless justified otherwise. The line in question was isolated at 2027 on 10/21/05. The valves are being maintained closed under administrative controls. The licensee notified the NRC Resident Inspector.

        • RETRACTION ON 10/28/05 AT 1748 EDT FROM H. KELLY TO P. SNYDER ****

An 8-hour notification was made on October 24, 2005 under 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades plant safety. The report was made due to a postulated break for a non-safety non-seismic fire water pipe that could possibly affect safe shutdown of the plant. An evaluation was completed on October 28, 2005. This evaluation confirmed that the current plant configuration is consistent with the design basis. The evaluation used for the original event notification assumed a full break of the involved piping. Perry design basis for this moderate energy system is a leakage crack. The postulated leakage from the crack in the piping remains within design basis and does not significantly degrade plant safety. Since Perry remains in compliance with design basis and there is no unanalyzed condition that significantly degrades plant safety, there is no reportable condition. Therefore, ENF 42072 is retracted. The licensee notified the NRC Resident Inspector. Notified R3DO (Lipa).

Safe Shutdown
Unanalyzed Condition
Safe Shutdown Earthquake
ENS 421164 November 2005 03:32:00PerryNRC Region 3GE-6

At 0200 on 11/03/05 a clearance was authorized that defeated the DW (Drywell) pressure high and Rx (Reactor) vessel low isolation features to valves in the Nuclear Closed Cooling System and Instrument Air Systems. The required T.S. (Technical Specification) actions after this discovery are that the plant should have been in Mode 3 at 1600 on 11/3/05. The clearance was removed and the circuit restored to operability at 0142 on 11/4/05. The time of discovery for the loss of safety function was 2345 on 11/3/05. The clearance was to perform pre-planned maintenance activities. The licensee plans on entering this incident into their corrective action program and will issue a Condition Report. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION ON 12/30/2005 AT 10:07 FROM KENNETH RUSSELL TO ABRAMOVITZ * * *

An 8-hour notification was made on November 3, 2005, in accordance with 10CFR50.72(b)(3)(v)(D), Accident Mitigation. This report was made when it was discovered that a clearance had unintentionally deenergized a portion of the containment isolation logic. This logic would have prevented a containment isolation valve for the nuclear closed cooling system and a containment isolation valve for the instrument air system from closing on a signal due to high drywell pressure or reactor vessel low level as designed. The condition was determined not to be a loss of containment (leakage) function since each containment penetration also has an inboard containment check valve which is leak tested and is credited for preventing leakage. The check valves in both penetrations were successfully tested to be in conformance with 10 CFR 50 Appendix J Option B criteria in March 2005. The containment isolation (instrumentation) function was also not lost. Only the logic for Group 2A outboard valves was deenergized. This was a small portion of the outboard logic and had no impact on the inboard logic. Since neither the containment function nor the containment isolation function was lost, there was no loss of safety function for an accident mitigation function and ENF 42116 Is retracted. As discussed in ENF 42116, a Technical Specification violation occurred and is reportable per 10CFR50.73(a)(2)(i)(B), as a condition prohibited by Technical Specifications." The licensee will be submitting a written LER for the 10CFR50.73(a)(2)(i)(B) event. The licensee notified the NRC Resident Inspector. Notified the R3DO (Hills).

Time of Discovery
ENS 4227218 January 2006 19:25:00PerryNRC Region 3GE-6This notification is being made pursuant to the Perry Nuclear Operating License section 2.C.6 (violation of the Fire Protection Program). Incorrect configuration of Division 1 remote shutdown panel wiring was identified during performance of surveillance testing. This incorrect configuration is associated with the Reactor Core Isolation Cooling motor operated exhaust valve. In the event of a fire in the control room, the motor operated exhaust valve would have the potential for spurious operation caused by fire induced shorts prior to isolation from the control room. Repairs and operator actions could have been taken to restore the valve. However, these repairs and operator actions are not currently identified in the Fire Protection Safe Shutdown analysis or associated operating procedures. Therefore, for this issue Perry does not comply with the Perry Fire Protection Program. Repairs have been completed and configuration has been restored. The licensee will notify the NRC Resident Inspector.Safe Shutdown
Fire Protection Program
ENS 4232910 February 2006 16:30:00PerryNRC Region 3GE-6At 1345, a notification was made to the Ohio EPA. This notification was based on 1) Any unanticipated bypass which exceeds any effluent limitation in the NPDES Permit and 2) Any discharge of water to the storm drains that is not covered by the following excerpt from the permit. The event itself was the pumping of rain water that had sulfuric acid (pH approximately 2.6) in it to a storm drain. Approximately 10 gallons of this mixture was pumped to the drain. The 10 gallons pumped contained approximately 1 milliliter of sulfuric acid. Sample taken at the storm drain out fall indicated normal pH value of 8.03. The licensee notified the NRC Resident Inspector.
ENS 4233011 February 2006 15:52:00PerryNRC Region 3GE-6

At 1506 EST, Operators heard a loud noise and discovered that a bearing in the Motor Control Switchgear in the Miscellaneous Equipment Area Return Fan "B" had failed. The Plant Fire Brigade responded and extinguished the fire. Offsite assistance was requested and did respond. No injuries were reported and all personnel have been accounted for. A reflash watch has been posted. The licensee will remain in the Alert awaiting completion of the ventilation transfer to the "A" train. The licensee notified state/local agencies and the NRC Resident Inspector.

  • * * UPDATE AT 1740 EST FROM KEN MEADE TO S. SANDIN * * *

At 1740 EST, the licensee terminated the Alert based on the fire being out and the plant stable. The licensee plans to issue a press release. Notified R3DO(Lanksbury), EO(Wermiel), IRD(Leach) and NRR ET(Dyer). Notified DHS SWO(Marianne), FEMA(Barden), DOE(DaSilva), HHS(Lt. Kleiman), USDA(Jimenez) and NRC-EPA(Crews).

ENS 424765 April 2006 15:05:00PerryNRC Region 3GE-6This notification is being made in accordance with 10CFR50.72(b)(2)(xi), i.e., notification of a government agency. FENOC provided a courtesy notification to state and local officials based on the detection of very low levels of tritium in the plant underdrain system. During routine quarterly sampling of the Perry plant's underdrain system on March 28, 2006, very low levels of tritium were detected in an underdrain system manhole. The plant's underdrain system directs water under the plant to the Emergency Service Water Pumphouse, where it is monitored and discharged. Samples taken off-site show no indications of detectable tritium. No reportable limits have been exceeded. The NRC Resident Inspector has been notified.
ENS 425524 May 2006 17:19:00PerryNRC Region 3GE-6The Perry Nuclear Power Plant (PNPP) Operating License requires that a report be made within 24 hours to the NRC operations center via the emergency notification system in the event that a violation of the PNPP Fire Protection Program occurs. On May 2, 2006, it was discovered that a specific set of Division 1 Emergency Diesel Generator (EDG) Control Room Control Switch contacts were not designed to isolate the Control Room from the local Division 1 EDG controls in the event of a control room fire. At 1430 on May 4, 2006 it was determined that this deficiency violated the PNPP fire protection program and could adversely affect plant shutdown in the case of a control room fire. A potential fire induced hot short in the diesel generator logic circuit(s), may result in a failure to start or a spurious trip of the Diesel Generator even if control is transferred to remote control. Although repairs and operator actions could have been taken to restore the Division 1 EDG if the Control Room fire caused a failure to start or a spurious trip of the Diesel Generator, these activities were not specifically identified in the Fire Protection safe shutdown analysis or associated operating procedures. The ability to achieve and maintain safe shutdown in the event of a fire in the Unit 1 Control Room could be adversely affected. Compensatory actions (procedure changes) have been completed to address this issue. A written report will follow in accordance with Technical Specification 5.6.6.a and Operating License Condition 2.F. The licensee discovered this discrepancy while researching a modification. This condition has existed since 1987. The licensee informed the NRC Resident Inspector.Hot Short
Safe Shutdown
Fire Protection Program
ENS 4265620 June 2006 16:54:00PerryNRC Region 3GE-6

Emergency plan unusual event entered due to a seismic event (LU-1). No equipment damage has been identified. The seismic event occurred at 1611hrs and tremors were felt in the Control Room. Unit 1 remained at full power and initial plant walkdown identified no safety equipment damage. Plant instrumentation indicated an acceleration of 0.005 Gs. Per U.S. Geological Survey website the quake was a 3.4 on the Richter scale and occurred NNW of the site. There is a small likelihood of after shocks. No radioactive releases have occurred.

  • * * UPDATE ON 06/20/06 AT 2019 EDT FROM JEFFREY D. ANDERSON TO M. RIPLEY * * *

Perry Plant has completed walkdowns from the Seismic Event that occurred at 1611. No Plant problems identified from walkdowns. Unusual Event has been terminated at 2000 on 6/20/06. The licensee notified the NRC Resident Inspector, State and local officials. Notified NRR (M. Case), IRD (Wilson), R3DO (O'Brien), DHS (Fite) and FEMA (Casto).

ENS 4267730 June 2006 17:55:00PerryNRC Region 3GE-6Notified by Security Shift Supervisor of a report by the Ashtabula County Sheriff that a 92 year old individual has been checked into the Ashtabula Clinic at 14:57 EDT, claiming to have an explosive device at his Kingsville home and at the Perry Power Plant. This is being considered as a non-credible security threat, based on his never having access to the site, ONI-P56-2 is not applicable, based on this report and assessment. Law enforcement officers are obtaining a warrant to access his home to investigate. The FBI and Lake County Sheriff's offices have been notified by the Security Shift Supervisor. This is an off site report from the Perry Plant to a government agency about the status of the Perry Plant. The Lake County Sheriff's office completed their search of individual's residence and found no bombs or related material. The licensee notified the NRC Resident Inspector.
ENS 426938 July 2006 09:22:00PerryNRC Region 3GE-6

On 6/29/06 at 1630 Neutralization Basin A was pumped to Lake Erie. On 7/7/06 the analysis of suspended solids for this discharge was completed with results outside of the daily limit. Results for the suspended solids for the basin discharge was 142 ppm with a limit of 100 ppm. State of Ohio EPA was notified for this non-compliance. This 4 hour notification is being made due to the notification to the State of Ohio EPA. Notification to the Ohio EPA was made at 0918 on 7/08/06. Specific. Reporting details required by Part 12.A are as follows: Discharge occurred- 6/29/06 at 16:30; Discovered 7/7/06 at 14:38 (analysis reported by First Energy Beta Drive Lab) Approximate amount 18,300 gallons; 7.94 Ph; 142 ppm Total Suspended Solids (backup sample 148 ppm) The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1007 EDT ON 7/11/06 FROM JIM CASE TO S. SANDIN * * *

This 4 hour notification is being made due to the additional notification to the State of Ohio EPA. This was follow-up information regarding event number 42693 ('Offsite Notification - exceeded limit for suspended solids in discharge'). On 7/10/06 final data analysis for NPDES Monthly Report was obtained and the 6/29/06 exceedance resulted in an exceedance in the monthly average of total suspended solids (TSS). Results for monthly average suspended solids were 44.2 ppm with a limit of 30 ppm. State of Ohio EPA was notified of this non-compliance at 0925 on 7/11/06. The licensee informed the NRC Resident Inspector. Notified R3DO (Steve Orth).

ENS 4285421 September 2006 20:13:00PerryNRC Region 3GE-6On September 14, 2006, the Plant Staff was notified by General Electric (GE) via a draft Safety Communication SC06-010 of a potential non-conservative setting of the OPRM Enabled Region Drive Flow Setpoint when the plant is in Single Reactor Recirculation Loop Operations. On September 21, 2006, at 1815 hours, based on available information, it was conservatively determined that all four OPRM channels were inoperable due to their current flow setpoint settings and uncertainties associated with OPRM enabling. The OPRM instrumentation provides inputs to the Reactor Protection System. The OPRM instrumentation is relied upon for providing a safe shutdown safety function when operating during an unstable power to flow condition. Operations personnel entered Technical Specification LCO 3.3.1.3 Action B.1 to initiate an alternate method to detect and suppress thermal hydraulic instability oscillations. This event is being reported as a condition that could have prevented the safety function of structures or systems required to shut down the reactor and maintain it in a safe shutdown condition. These actions and this report are based on preliminary information. Updates will be provided as necessary as additional information becomes available. The licensee notified the NRC Resident Inspector.Safe Shutdown
ENS 430213 December 2006 15:20:00PerryNRC Region 3GE-6

On December 3, 2006, at 0858 hours, control room operators received a Division 3 Emergency Diesel Generator (EDG) Carbon Dioxide (CO2) (Fire Protection) system initiation signal. The CO2 system for the Division 3 EDG room was out of service at the time and so no CO2 was released into the room. At 0905 hours, a first responder notified the control room operators that there was no indication of a fire in the Division 3 EDG room. A walkdown of the associated EDG room ventilation system confirmed the ventilation system tripped with the CO2 initiation signal locked in. At 0919 hours, the Division 3 EDG was declared inoperable and Technical Specification (TS) LCO 3.8.1 Condition B was entered. The required TS actions were implemented. The Division 3 EDG is available with restoration of the ventilation system using the CO2 Override switch. The CO2 initiation signal is currently locked in, and the Division 3 CO2 Fire Monitoring Panel, with associated equipment has been quarantined for further investigation. The Division 3 EDG provides emergency AC electrical power to the High Pressure Core Spray system. This event is being reported as a condition that could have prevented the safety function of structures or systems required to mitigate the consequences of an accident. The Resident Inspector has been notified.

* * * EVENT RETRACTED AT 1324 ON 12/14/06 FROM C. ELBERFELD TO P. SNYDER * * * 

The purpose of this call is to retract Event Number 43021. On December 3, 2006, at 1520 hours, a notification, Event Number 43021, was made to the NRC Operations Center by the Perry Nuclear Power Plant (PNPP) in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident. A spurious Carbon Dioxide (CO2) Fire Protection system initiation signal resulted in a tripped condition for the Division 3 Emergency Diesel Generator (EDG) room ventilation system. Operators declared the Division 3 EDG inoperable and took the appropriate Technical Specification actions. The Division 3 EDG provides emergency AC electrical power to the High Pressure Core Spray system. The High Pressure Core Spray system is a single train safety system. After further evaluation, it was determined that operators could promptly restore the ventilation system, with the CO2 initiation signal locked in, if the Division 3 EDG was needed, and that the safety function of the system could still be fulfilled during the time in question. Because the condition reported in Event Number 43021 would not have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident, the condition is not reportable, and this notification is retracted. The evaluation (i.e., Reportability Review) for this condition is documented in Condition Report 06-10843. The NRC Resident Inspector has been notified. Notified R3DO (Lara).

Time of Discovery
ENS 4304913 December 2006 05:49:00PerryNRC Region 3GE-6

A loss of instrument air caused a transient in feed system causing a lowering Hot Surge Tank Level. The Reactor was manually scrammed when Reactor Feed Booster Pumps were cavitating. Control Rod 42-55 did not insert on the initial scram. Control Rod 42-55 did insert when ARI was manually initiated. The loss of instrument air was the result of an air line rupture, and the licensee is steaming to the condenser while maintaining vessel level with feedwater. There was no ECCS injection, and the licensee is investigating the cause of the line rupture. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 0814 ON 12/13/2006 FROM MICHAEL BROGAN TO MARK ABRAMOVITZ * * *

This update is being made in accordance with 10CFR50.72(c)(2) to immediately report the results of ensuing evaluations or assessments of plant conditions, the effectiveness of response or protective measures taken, and information related to plant behavior that is not understood. On December 13, 2006, at 0549 hours, the Perry Nuclear Power Plant notified the NRC Operations Center (Event Number 43049) of a manual Reactor Protection System actuation associated with a loss of instrument air. In the initial report, it was stated that control rod 42-55 did not insert on the initial scram, but did insert when Alternate Rod Insertion was manually initiated. Subsequently, reactor engineering review of control rod performance during the event determined that the control rod scram time for control rod 4255 was satisfactory and that the problem was with the control rod indication. The plant remains stable at this time. Control rod indication has two channels. Control rod 42-55 displayed one fully inserted indication and one blinking green indication (i.e. not fully inserted). When the system was reset, all rods indicated fully inserted with a "00" position indication. The licensee notified the NRC Resident Inspector. Notified the R3DO (Lara).

ENS 432825 April 2007 21:22:00PerryNRC Region 3GE-6

At 2005, an injury occurred to a worker when the individual fell and injured his back. At 2122, the worker was attended by local Emergency Medical Personnel who transported the individual to our local Hospital. Due to his back injury his back will not be able to be completely monitored until arrival to the hospital. The individual is being classified as potentially contaminated. Radiation (Protection) personnel are accompanying the victim on the ambulance and to the local hospital emergency room to aid in radiological assessment. Due to our procedures we will be making notifications to the State Of Ohio and the local county Emergency Management Agencies of the incident. Due to the offsite notifications a 4 hour non-emergency call is required. The individual was a contractor onsite for outage support. The licensee notified the NRC Resident Inspector.

* * * UPDATE AT 2249 ON 4/5/07 FROM A. RABENOLD TO SNYDER * * * 

The contractor individual was found in the Containment Drywell 630 foot elevation. He fell off of scaffolding approximately 4-5 feet to the grating. When the medical personnel arrived at the scene they found him unconscious. He regained (consciousness) when medical personnel arrived at the scene. At 2218 (the licensee received a) report from Radiation Protection personnel that the individual was not contaminated. Notified R3DO (L. Kozak).

  • * * Update on 04/06/07 at 1130 EDT from M. Nemcek to MacKinnon * * *

The injured person was found not to have contamination on him but it was reported to Perry Nuclear Power plant that fixed contamination was found on his Protective Clothing (PC), Safety Belt and Tool Belt. Fixed contamination on the PC direct contact reading was between 100 to 150 cpm. Fixed direct on contact contamination on the Safety Belt & the Toll Belt was between 100 to 500 cpm. No contamination found in the ambulance or in the Hospital. NRC Resident Inspector was left a message of this information by the licensee. NRC R3DO (L. Kozak) notified.

Scaffolding
ENS 4336315 May 2007 01:53:00PerryNRC Region 3GE-6

An automatic reactor scram occurred due to lowering reactor water level. Digital feedwater tuning activities were in progress at the time of the scram. All systems functioned as designed. The reactor water level has been restored to normal level band. The plant is stable in Hot Shutdown. There were no ECCS injections. At the time of the scram, the feedwater pump was in manual control for feedwater tuning. When water level started going down quickly, the operator was not able to restore sufficient feedwater flow before the level 3 (water level low) actuation. All control rods fully inserted on the scram. No valves repositioned and no safety or relief valves lifted after the scram. Reactor water level is being maintained with the motor feed pump and decay heat is being removed to the main condenser. The plant is in the normal shutdown electrical lineup. Reactor pressure is 509 psi and stable. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM FREDERICK SMITH TO FANGIE JONES ON 05/17/07 AT 1301 * * *

This call is to clarify information provided in notification Event Number 43363 made by the Perry Nuclear Power Plant on May 15, 2007. The second paragraph, fourth sentence of the notification states: 'No valves repositioned and no safety or relief valves lifted after the scram.' The intent of the portion of the sentence 'No valves repositioned' was supposed to be in reference to the reporting requirement in 10 CFR 50.72(b)(3)(iv) to report any event or condition that results in valid actuation of general containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs).

The event on May 15, 2007, did not meet the 'containment isolation valves in more than one system / MSIVs criterion', however, subsequent review of the event identified that Residual Heat Removal 'B' Heat Exchanger Second Vent to Suppression Pool Containment Isolation Valve 1E12-F073B, closed, as designed, in response to the reactor coolant level 3 (water level low) condition that was present during the event. No additional reporting criteria have been identified and this update has been provided to clarify the earlier statement. The NRC Resident Inspector has been notified." Notified R3 RDO, (Ring), and NRR EO, (Ross Lee).

ENS 4345227 June 2007 15:17:00PerryNRC Region 3GE-6This event is being reported in accordance with 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A). This condition meets the criteria of 10 CFR 50.73(a)(2)(iv)(A) for any event or condition that results in manual or automatic actuation for any of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B). The specific requirements apply here to 'General containment isolation signals affecting containment isolation valves in more than one system.' During the performance of surveillance instruction 'Low Pressure Coolant Injection (LPCI) 'B' and 'C' Initiation and Loss of EH12 Response Time Test,' the following valves auto closed during the test activities: - 1G61-F0075 (Containment Equipment Drain Inboard Isolation), - 1G61-F0165 (Containment Floor Drain Inboard Isolation), - 1P11-F0090 (Containment Pools Drain Inboard Isolation), and - 1P50-F140 (Containment Vessel Chilled Water Inboard Return MOV Isolation) The signals are considered to be invalid as the signals were a result of test activities and not actual plant conditions. The valve logic to close the valves was momentarily satisfied due to the sequence of electrical power restoration during the test; however, the test did not address the valve movement and the valve actuations could not be considered to be preplanned. The system actuations were considered to be partial, and the valves functioned successfully as designed. The event was captured within the corrective action program under condition report (CR) 07-19866. The resident inspector was notified of this event notification.
ENS 4360327 August 2007 20:45:00PerryNRC Region 3GE-6At 1645 hours on 8/27/07 it was determined that a section of grating in the containment pool swell region was not properly restrained. During a postulated large break Loss of Coolant Accident, the grating could become dislodged and subsequently impact the ECCS suction strainer located in the suppression pool below the grating. An engineering review determined that the force of the impact could be larger than the impingement forces that had been previously evaluated. The forces were postulated to impact one of two concentric suction strainers. The resulting damage could cause either Residual Heat Removal B and C loops or High Pressure Core Spray (not both) to be inoperable. This condition was determined to meet the reporting requirements for 10 CFR 50.72(b)(3)(ii)(B), 'Any event or condition that results in: (B) The nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.' Since one of the strainers was for High Pressure Core Spray, a single train safety system, this event was also determined to meet the reporting criteria for 10 CFR 50.72(b)(3)(v)(D), 'Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of systems needed to (D) mitigate the consequences of an accident.' Technical Specification 3.5.1, ECCS - Operating, was entered and Required Actions taken within the specified completion time. The grating was subsequently restored to design configuration and the Technical Specification LCO was exited. Time of restoring grating to design was 1838 8/27/07, exited Tech Spec 3.5.1. Location of grating is in the Containment Building on the 599' elevation near the lower air lock. The section is a 3 X 7 foot piece of grating that is located on the level just above the suppression pool. We still are investigating when the grating hold down plates were removed, potentially removed during our recent recirc motor replacement in July 07. The grating hold down plates were discovered by an Operations Roving Operator during his tour on rounds. The licensee notified the NRC Resident Inspector.Unanalyzed Condition
Time of Discovery
ENS 4365320 September 2007 14:46:00PerryNRC Region 3GE-6

(The information below concerns a) September 19, 2007 NPDES Reportable Occurrence verbiage/Notification to the Ohio Environmental Protection Agency. This notification was made on September 20, 2007. Time of discharge is unknown. Cloudy water was discovered in 'Major Stream' diversion (also referred to as 'Red Mill Run') at approximately 1525 hours on September 19, 2007.

The amount of discharge is unknown. At the time of discovery, approximately 10 to 15 gallons of water, per minute, were observed discharging from the storm drain. On September 20, 2007, the observed discharge from the storm drain was approximately 1 to 2 gallons of water per minute. The pH of the stream was 11.2 standard units (SU) at 1650 hours on September 19, 2007 with white powdery deposition on the stream bed. At 1000 hours on September 20, 2007, a sample taken for pH indicated 8.48 SU. A number of small stressed fish were observed at time of discovery, along with approximately 5 to 10 small dead fish. No frogs, crayfish, or other local aquatic life forms were observed to have been negatively impacted. Initial analysis of the sediment from the stream bed indicated the main constituents were inorganic calcium & oxygen (possible materials include but not limited to calcium oxide, calcium carbonate, calcium hydroxide).

The source of the high pH and white sediment is unknown at this time and an investigation is in progress.

The affected area (has been inspected) and recommendations for clean-up remediation (provided). The recommendations are currently being evaluated.

This event is being reported in accordance with Appendix B to the Operating License (The Environmental Protection Plan) which requires reporting of any occurrence of an unusual or important event that indicates or could result in significant environmental impact causally related to plant operation (An example includes 'fish kills'). This event is also being reported in accordance with 10CFR50.72(b)(2)(xi). 'Any event or situation, related to the health and safety of the public or on-site personnel, or protection of the environment, for which a news release is planned or notification to other government agencies has been or will be made. Such an event may include an on-site facility or inadvertent release of radioactively contaminated materials'. The NRC Resident Inspector and applicable State authorities have been notified.

Time of Discovery
ENS 4380828 November 2007 08:39:00PerryNRC Region 3GE-6A reactor scram occurred at full power due to either a main turbine trip or loss of feedwater (cause is still under investigation). All rods fully inserted. RCIC started as expected but tripped shortly thereafter on a preliminary indication of low suction pressure. The Digital Feedwater System backup motor driven feedwater pump did not function as required and reactor water level decreased to level 2 ( 130 inches). High Pressure Core Spray (HPCS) started automatically at level 2 and restored water level. Currently reactor water level is at 188 inches and reactor pressure is at 927 PSI. Decay heat is being removed via the turbine bypass valves. No other significant equipment was out of service at the time of the scram. The scram had no impact on offsite or onsite power availability. The licensee attempted to restore RCIC a second time and experienced another trip. In addition, the licensee attempted to restore the digital feedwater and was unsuccessful. Feedwater continues to be supplied as needed via the HPCS while the licensee attempts to restore RCIC and Digital Feedwater System. The licensee notified the NRC Resident Inspector.
ENS 4386021 December 2007 12:31:00PerryNRC Region 3GE-6Annulus Exhaust Gas Treatment System (AEGTS) 'A' was removed from service (INOPERABLE) to obtain a charcoal sample. AECTS 'B' Train was the OPERABLE Train. At 0825 hours, the charcoal plenum for the 'A' train was opened to obtain a charcoal sample resulting in alarms for AECTS 'B' low flow and Annulus low differential pressure. Based on this indication AEGTS 'B' and secondary containment were INOPERABLE. AEGTS 'B' flow was restored to normal following closure of the charcoal plenum and annulus differential pressure was restored to normal at 0833 hours, restoring secondary containment. AEGTS 'B' was declared operable at 0845 hours. Early indication is that a discharge damper in the AEGTS 'A' train had not operated properly. This condition was determined to be reportable in accordance with 10 CFR 50.72(b)(3)(V)(C) and (D), as condition that could have prevented the safety function of structures or systems that are needed to: (C) Control the release of radioactive material; or (D) Mitigate the Consequences of an accident. The licensee notified the NRC Resident Inspector.
ENS 4411131 March 2008 19:18:00PerryNRC Region 3GE-6

At 1550 hours, a self identification call was made to the State of Ohio Environmental Protection Agency (EPA), offices in Columbus, Ohio to inform them of the recent discovery of non-compliance issues relating to the accumulation, storage, and shipment (i.e., 90 days to ship) of hazardous waste (reference 40 CFR 261, 'Identification and Listing of Hazardous Waste'). Guidance was requested from the state EPA for remediation and reporting of the condition. The Perry Nuclear Power Plant personnel were advised by the Ohio EPA to properly identify, package and ship the waste as soon as possible. The waste consists of three drums of floor grinding waste generated during the resurfacing of the Auxiliary Building floor in 2005, and approximately 100 bags of miscellaneous trash generated during disassembly of plant equipment in 2007. This issue was discovered during activities to prepare the waste for shipment off site. The waste will be shipped per the direction of the Ohio EPA and an out-of-cycle hazardous waste annual report will be made to the Ohio EPA. This report is being made in accordance with 10 CFR 50.72(b)(2)(xi) as an event or situation related to the protection of the environment for which a notification to another government agency has been made. The resident inspector has been notified. The hazardous material contains low level rad waste.

  • * * UPDATE FROM RICHARD O'CONNOR TO HOWIE CROUCH @ 1334 HRS EDT ON 6/03/08 * * *

On March 31, 2008, in accordance with 10 CFR 50.72(b)(2)(xi), notification was made for an event or situation related to the protection of the environment for which a notification to another government agency was made. This report was made when a self-identification call was made to the State of Ohio Environmental Protection Agency (EPA) offices in Columbus, Ohio, for the discovery of potential non-compliance issues with 40 CFR 261 requirements for the accumulation, storage, and shipment of hazardous waste. Based on further investigation using a Toxicity Characterization Leachate Procedure analysis of the waste, it was determined that the waste was, in fact, non-hazardous and could be shipped for off-site disposal. The requirements of 40 CFR 261 had been and continue to be met. The licensee has notified the NRC Resident Inspector and the State of Ohio. Notified R3DO ( Pelke).

ENS 4424528 May 2008 22:03:00PerryNRC Region 3GE-6On May 28, 2008, at 1730 hours, control room operators determined after testing, that the Emergency Service Water (ESW) Division 3 subsystem was inoperable due to a condition that will not allow the subsystem to maintain 'keep-fill' pressure in the event of a loss of offsite power. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.7.2 requires that the High Pressure Core Spray (HPCS) System (a single train safety system) be declared inoperable immediately when the ESW Division 3 Subsystem is inoperable. The plant immediately entered TS LCO 3.5.1 Condition B, HPCS System inoperable. TS LCO 3.5.1, Required Action B.1, verify by administrative means that the Reactor Core Isolation Cooling System is operable within one hour, was completed at 1730 hours. Required Action B.2 requires that the HPCS System be restored to operable status within 14 days. Maintenance/troubleshooting activities are in progress to determine the cause of the ESW Division 3 Subsystem condition. This event is being reported as a condition that could have prevented the safety function of structures or systems required to mitigate the consequences of an accident. The resident inspector has been notified.
ENS 4427910 June 2008 01:29:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant will be taking the ERDS out of service for scheduled maintenance. From approximately 0200 hours EDT, on June 10, 2008, until 2000 hours EDT, on June 10, 2008, personnel will be performing cleaning and inspection activities on the 120 VAC Emergency Response Information System (ERIS) Computer Power Center. During this planned preventive maintenance, the Integrated Computer System, the Safety Parameter Display System (SPDS), and the automatic mode calculation of the Computer Aided Dose assessment program (CADAP) will incur approximately two periods of unavailability of approximately two hours each. The unavailability periods are necessary to align a temporary power supply and reconnect the 120 VAC ERIS Computer Power Center upon completion of the activities. The dose assessment function will be maintained during the brief out of service time periods by manual input of data into CADAP and, if required, by manual calculation. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Plant Branch Exchange, the Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The ability to open and maintain on 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the two periods of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. A follow-up notification will be made when the activities are completed and the equipment is restored. The Resident Inspector has been notified.

  • * * UPDATE FROM DAVE O'DONNELL TO JOE O'HARA AT 1514 ON 6/10/08 * * *

ERDS is still in service and will not be restored to normal until tomorrow 6/11/08. The scheduled maintenance on the normal power supply today was delayed. Notified R3DO(Lipa)

  • * * UPDATE FROM DAVE O'DONNELL TO KARL DIEDERICH AT 1710 ON 6/11/08 * * *

ERDS was on a temporary power supply. ERDS restored to normal power supply at 1650. Notified R3DO (Louden).

ENS 4444026 August 2008 09:27:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant took the Plant Computer out of service for scheduled maintenance which will take ERDS out of service. From 0814 hours EDT, on August 26, 2008 for approximately 6 hours personnel will be performing disk maintenance activities on the Plant Computer. During this planned maintenance, the Safety Parameter Display System (SPDS) and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. The unavailability period is necessary to replace a disk drive. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Plant Branch Exchange, the Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. A follow-up notification will be made when the activities are completed and the equipment is restored. The resident inspector has been notified.

  • * * UPDATE PROVIDED AT 1425 EDT ON 08/26/08 FROM MIKE BROGAN TO JEFF ROTTON * * *

Computer maintenance is complete and the Plant Computer has been restored to service. SPDS, CADAP and ERDS are available. The licensee will notify the NRC Resident Inspector. Notified R3DO (Ring).

ENS 4461330 October 2008 05:10:00PerryNRC Region 3GE-6

This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii) as a condition that results in a major loss of emergency offsite communications capability. On October 30, 2008, at approximately 0020 hours EDT, 120 VAC non-essential electrical power was lost to the plant computer due to high temperature in the computer room (approximately 80 degrees F). This resulted in the Integrated Computer System (ICS), the Safety Parameter Display System (SPDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) being out of service. At 0028 hours, back-up computer room ventilation equipment was placed in service, and at 0040 hours, the electrical system high temperature shutdown was reset with the computer room temperature at 77 degrees F. At 0217 hours, the computer room high temperature alarm was reset with the room at 72 degrees F. The 120 VAC electrical power was restored to the plant computer room at approximately 0245 hours. The ICS, SPDS, and CADAP equipment functions are in process of restoration. Restoration is expected during dayshift hrs. on 10/30/08. A follow up to this notification will be made when ERDS is restored. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM DAVE O'DONNELL TO JOE O'HARA AT 1406 EDT ON 10/30/08 * * *

The ERDS system has been tested and restored to service. The NRC Resident Inspector has been notified. Notified R3DO(Kozak).

ENS 446222 November 2008 08:16:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant will be taking the Plant Computer out of service for scheduled maintenance which will take ERDS out of service. From 0830 hours EST, on November 2, 2008, for approximately 6 hours, personnel will be resetting computer time from EDT to EST and (will) troubleshoot the Plant Computer. During this planned maintenance, the Safety Parameter Display System (SPDS) and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) (will) be unavailable. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Plant Branch Exchange, the Off Premise Exchange, and various redundant infra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. A follow-up notification will be made when the activities are completed and the equipment is restored. The (NRC) Resident Inspector has been notified.

  • * * UPDATE FROM JIM CASE TO JOHN KNOKE AT 1530 EST ON 11/02/08 * * *

The Plant Computer was put back in operation at 1525 EST. Notified R3DO (Kozak)

ENS 4484310 February 2009 09:45:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant took the Plant Computer out of service for scheduled maintenance which took ERDS out of service. From 0810 hours EST on February 10, 2009 for approximately 6 hours, personnel will be performing maintenance activities on the Plant Computer. During this planned maintenance, the Safety Parameter Display System (SPDS) and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Private Branch Exchange, Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10CFR50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communication capability. A follow-up notification will be made when the maintenance activities are completed and the equipment is restored. The (NRC) Resident Inspector has been notified.

  • * * UPDATE AT 1250 EST ON 2/10/09 FROM STANLEY TO HUFFMAN * * *

At 1240 EST the licensee returned the plant computer to service. ERDS, CADAP, and SPDS have been restored to operable status. The licensee has notified the NRC Resident Inspector. R3DO (Burgess) has been informed.