ENS 40469
ENS Event | |
---|---|
20:26 Nov 29, 2003 | |
Title | Invalid System Actuation |
Event Description | On November 29, 2003, at 1526 hours0.0177 days <br />0.424 hours <br />0.00252 weeks <br />5.80643e-4 months <br />, the Perry Nuclear Power Plant experienced an actuation of several Division 2 Balance-of-Plant (BOP) inboard isolation valves as a result of the loss of the normal power supply to the Reactor Protection System (RPS) B. At the time of the event, the plant was in mode 1(Power Operations) at about 100% power. The isolation closed one or more valves in each of the following Division 2 subsystems: Main Steam line drains, Fuel Pool Cooling and Cleanup, Liquid Radwaste Sumps, Containment Vessel Chilled WATER, Reactor Water Sampling, Drywell and Containment Radiation Monitoring, and Control Room Ventilation. Instrumentation that receives electrical power from RPS B also lost power. Division 1 components and valves were not affected.
The event is considered an invalid system actuation, and is reportable under 10 CFR 50.73(a)(2)(iv)(A). The isolation was not initiated in response to actual plant conditions or parameters, and was not a manual initiation. It meets the criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) as a general containment isolation signal affecting containment isolation valves in more than one system. Therefore, notification is being provided via 60-day optional phone call in accordance with 10 CFR 50.73(a)(1). All systems functioned as expected for an inboard isolation. Repositioning of the valves did not present operational concerns; and the valves were re-opened per restoration procedures. The BOP isolation was attributed to the loss of power to RPS B as a result of a blown fuse. The blown fuse was the result of the failure of a GE CR105 contactor due to age related degradation (insulating varnish degradation resulting in a winding to winding short circuit). This event was documented in the corrective action program. Remedial actions included replacement of the failed fuse and the RPS A and B normal power supply contactors and the RPS A alternate power supply contactor. The RPS B alternate power supply contactor will also be replaced. The NRC Resident Inspector was notified of this event by the licensee. |
Where | |
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Perry Ohio (NRC Region 3) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1313.65 h54.735 days <br />7.819 weeks <br />1.799 months <br />) | |
Opened: | Ken Russell 14:05 Jan 23, 2004 |
NRC Officer: | John Mackinnon |
Last Updated: | Jan 23, 2004 |
40469 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 552632021-03-23T04:37:00023 March 2021 04:37:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Diesel Generator Initiation ENS 510842015-03-26T20:29:00026 March 2015 20:29:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Primary Containment and Drywell Isolation Valve Actuation ENS 504502014-07-26T17:13:00026 July 2014 17:13:00 10 CFR 50.73(a)(1), Submit an LER Electrical Transient Causes an Invalid System Actuation ENS 483192012-07-24T00:57:00024 July 2012 00:57:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuations ENS 434522007-05-03T05:58:0003 May 2007 05:58:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 405982004-02-22T15:16:00022 February 2004 15:16:00 10 CFR 50.73(a)(1), Submit an LER Partial Rps Actuation During Testing at Perry ENS 404692003-11-29T20:26:00029 November 2003 20:26:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 401262003-08-02T01:18:0002 August 2003 01:18:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Division 2 Balance-Of-Power Inboard Isolation Valves 2021-03-23T04:37:00 | |