ENS 41085
ENS Event | |
---|---|
19:00 Oct 2, 2004 | |
Title | Reactor Power Being Reduced Due to Entering Ts 3.0.3 Because of Inopeable Recirc Vent System |
Event Description | At 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> the plant commenced reactor shutdown from 100% power for entering T.S. 3.0.3 due to both trains of the Emergency Recirc Vent System being declared inoperable. The reactor will be in mode 2 by 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />, mode 3 by 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 10/03 and mode 4 by 0200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> on 10/04. If the problem is corrected, they will terminate the shutdown.
The NRC Resident Inspector was notified. HOO Note: see event 41084
Update to [Event] Notifications 41084 and 41085: At 1840 [EDT] on 10/02/04 it was determined that the apparent slow response times of the Control Room Emergency Recirculation [CRER] dampers was due to a malfunctioning relay in the initiation circuit, not due to failure of the dampers. The LCO actions associated with the CRER system were exited and the actions associated with the initiation instrument were entered. Therefore the plant is no longer required to shutdown per T.S. 3.0.3. The plant shutdown has been terminated. Plant power will be returned to 100%. The licensee has notified the NRC resident Inspector. Notified R3DO (Thomas Kozak).
At 1300 on 10/02/04, results of a surveillance indicated that dampers in both trains of the Control Room Emergency Recirculation System (CRERS) were slower than allowed by Technical Specifications (TS) requiring both trains of the CRERS to be declared inoperable. With both trains inoperable, Technical Specification 3.0.3 was entered which required a plant shutdown. The shutdown was commenced at 1500. This condition was reported as required in Event Notification 41085. Additionally, with both CRERS trains inoperable, this condition was determined to be reportable as a loss of safety function (accident mitigation) and was reported as required in Event Notification 41084. Subsequently, it was determined that the failure was the result of a defective time delay relay in the radiation monitor initiation circuit. Other inputs that would have caused the dampers to reposition in an accident were not impacted. The appropriate TS (3.3.7.1), for the radiation monitor, was entered and TS 3.0.3 was exited. The significant actions required by this TS were to restore the function within 7 days or place the system in emergency recirculation. It did not require entry into an action to shutdown. When this condition was identified, TS 3.0.3 was exited, the shutdown was terminated, and the plant was restored to full power. Since a TS required shutdown was not required, Event Notification 41085 is being retracted. The licensee has notified the NRC Resident Inspector. NRC R3DO(Gardner) has been notified. |
Where | |
---|---|
Perry Ohio (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-3.63 h-0.151 days <br />-0.0216 weeks <br />-0.00497 months <br />) | |
Opened: | Robert Kidder 15:22 Oct 2, 2004 |
NRC Officer: | Chauncey Gould |
Last Updated: | Oct 25, 2004 |
41085 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 41085\u003C/a\u003E - \u003Ca href=\"/Perry\" title=\"Perry\"\u003EPerry\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EReactor Power Being Reduced Due to Entering Ts 3.0.3 Because of Inopeable Recirc Vent System\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 41085 - Perry\n","link":"","lat":41.79572777777778,"lon":-81.145375,"icon":"/w/images/a/ad/FirstEnergy_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (83 %) |
WEEKMONTHYEARENS 571362024-05-23T08:00:00023 May 2024 08:00:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown ENS 530002017-10-04T06:50:0004 October 2017 06:50:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Perry Commenced Technical Specification Required Shutdown ENS 516792016-01-24T02:22:00024 January 2016 02:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Ts Required Shutdown Due to Unidentified Leakage in Drywell ENS 498042014-02-07T11:00:0007 February 2014 11:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Required by Technical Specifications Due to Containment Isolation Valve Over Leak Rate Limit ENS 491212013-06-16T04:00:00016 June 2013 04:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Shutdown Due to Small Reactor Coolant Leak on a Recirculation Flow Control Valve Vent Line ENS 473122011-10-02T05:00:0002 October 2011 05:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shutdown Required by Technical Specifications Due to Transformer Fault ENS 459182010-05-12T03:18:00012 May 2010 03:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Manual Reactor Scram Due to Loss of Control Rod Drive Charging Water Header Pumps ENS 454342009-10-15T16:25:00015 October 2009 16:25:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit Commenced Shutdown Due to Inoperable Division 2 Emergency Service Water System ENS 416572005-05-02T10:11:0002 May 2005 10:11:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown - Reactor Vessel Level Instrumentation ENS 410852004-10-02T19:00:0002 October 2004 19:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Reactor Power Being Reduced Due to Entering Ts 3.0.3 Because of Inopeable Recirc Vent System ENS 407672004-05-21T20:00:00021 May 2004 20:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown 2024-05-23T08:00:00 | |