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 Issue dateTitleTopic
05000000/LER-1950-237, Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis13 July 1976Updated LER 50-237/01L:on 760406,unacceptable Ultrasonic Indication Found on Isolation Condenser safe-end.Caused by Cracks in safe-ends.Cracked safe-end Removed & Sent to Bmcl for Metallographic Analysis
05000237/LER-1950-237, Updated LER 50-237/75-048:on 751007,through-wall Crack Found in Drywell/Torus Nitrogen Purge Line 1604-18.Addl Mods, Including Temp Controlled Isolation Valve Installation, Delayed Until Proposal Review10 June 1977Updated LER 50-237/75-048:on 751007,through-wall Crack Found in Drywell/Torus Nitrogen Purge Line 1604-18.Addl Mods, Including Temp Controlled Isolation Valve Installation, Delayed Until Proposal Review
05000237/LER-1976-053, Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates3 January 1977Updated LER 76-053/01T-1:on 760803,util Advised by GE That MAPLHGR Limits in Effect No Longer Considered Sufficiently Conservative at Low Core Flow Rates.Problem Thought to Be ECCS Models Used to Determine Rates
05000237/LER-1976-063, Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced3 March 1977Updated LER 76-063/03L-l:on 761003,stack Gas Sample Pump Flow Appeared Abnormally Low.Caused by Collection of Carbon Impeller Vane Products in Pump Cavity & Filter.Pump & Filter Replaced
05000237/LER-1976-066, Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced13 May 1977Updated LER 76-066/01T-1:on 761113,during Maint Outage,Hpci Injection Valve M02-23018 Found in Closed Position W/Valve Stem Severed.Caused by Mechanical Overstress of Stem.Stem Replaced
05000237/LER-1982-023, Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement23 July 1982Revised Deviation Rept for LER 82-023/03L-0:on 820623, Wrong Assumption Made for Drywell to Torus Differential Pressure.Caused by High Torus Pressure Transmitter 2-1673 Measurement
05000237/LER-1983-080, Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr20 December 1983Supplemental LER 83-080/03X-1:on 831124,offgas Log Rad Monitor 2-1705-A Delivered Offgas High Alarm & High Alarm Spiked & Drifted Downscale.Caused by Burned Out Resistor. Power Supply Installed & Monitor Calibr
05000237/LER-1983-084, Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr14 March 1984Updated LER 83-084/03X-1:on 831230,during Normal Operation, Primary Containment Oxygen Sample from Torus Alarmed on Low Level Sample Flow.Caused by Sample Line Moisture.Line Drained & Leads reconnected.W/840314 Ltr
05000254/LER-1976-002, Updated LER 76-002/03L Re Excessive Leakage from Double Gasketed Seal X-4.Initially Reported on 760202.Caused by Equipment Failure & Insufficient Compression.Hatch Bolts Tightened3 March 1976Updated LER 76-002/03L Re Excessive Leakage from Double Gasketed Seal X-4.Initially Reported on 760202.Caused by Equipment Failure & Insufficient Compression.Hatch Bolts Tightened
05000254/LER-1982-022, Supplemental LER 82-022/03L-1:on 820816,maint Outage for 1/2B Diesel Fire Pump Exceeded 7-day Limit.Cause Not Stated. Diesel Pump Wear Rings Replaced7 October 1982Supplemental LER 82-022/03L-1:on 820816,maint Outage for 1/2B Diesel Fire Pump Exceeded 7-day Limit.Cause Not Stated. Diesel Pump Wear Rings Replaced
05000254/LER-1984-018, :on 840922 & 24,reactor Bldg Fuel Pool Channel B Area Radiation Monitor 1705-16B Spiked High, Tripping Ventilation.Cause Unknown.Corrective Actions for Both Events Will Be Documented in Suppl to LER 84-01811 October 1984
on 840922 & 24,reactor Bldg Fuel Pool Channel B Area Radiation Monitor 1705-16B Spiked High, Tripping Ventilation.Cause Unknown.Corrective Actions for Both Events Will Be Documented in Suppl to LER 84-018
05000254/LER-1988-001, Sanitized Version of LER 88-001-00:on 880114,records Review Found Two Apparent Overexposures of Contractor Personnel During Fourth Quarter 1980.Caused by Inaccurate Secondary &/ or Primary Dosimetry.Dosimetry Sys Upgraded28 January 1988Sanitized Version of LER 88-001-00:on 880114,records Review Found Two Apparent Overexposures of Contractor Personnel During Fourth Quarter 1980.Caused by Inaccurate Secondary &/ or Primary Dosimetry.Dosimetry Sys Upgraded
05000254/LER-1990-01324 July 1990LER 90-013-00:on 900626,annunciators on Both Units & Reactor Recirculation Loop Sample Valve Closed.Caused by Actuation of Primary Containment Isolation Valve When Lightning Struck 345 Kv Line.Valve reopened.W/900724 Ltr
05000254/LER-1993-00811 August 1993LER 93-008-00:on 930709,reactor Bldg Ventilation Radiation Monitor Setpoints Set non-conservatively Four Times in Five Yrs.Caused by Instrument Maint Program Error. New Computer Program developed.W/930805 LtrOffsite Dose Calculation Manual
05000254/LER-1993-00913 August 1993LER 93-009-00:on 930714,SBGT Methyl Iodide Test Failed Due to Age of Charcoal Combined W/Stringent Test Criteria. Replaced Charcoal Absorber in Both Trains of Sbgt. W/930806 Ltr
05000254/LER-1993-01019 August 1993LER 93-010-00:on 930720,HPCI Declared Inoperable & HPCI Outage Rept Qcos 2300-2 Initiated Because IST Flow Rate Fell in IST Required Action Range Due to New Procedure. Surveillance Procedure Will Be revised.W/930819 Ltr
05000254/LER-1993-01118 August 1993LER 93-011-00:on 930721,discovered That 4kV Breaker 68 Feeding CS 1B Motor Pump Open & Discharged,Resulting in CS 1B Being Declared Inoperable.Wr Written to Investigate & repair.W/930813 Ltr
05000254/LER-1993-01224 August 1993LER 93-012-00:on 930726,light Socket Shorted Out When Operator Reset HPCI Logic Power.Caused by Short Circuit in Light Socket.Light Socket & Blown Fuses replaced.W/930824 LtrReactor Vessel Water Level
05000254/LER-1993-01327 August 1993LER 93-013-00:on 930729,identified Deviation from TS & Reg Guide 1.52 Requirements for Methyl Iodide Testing of Charcoal Sample Canisters.Caused by Failure to Implement Proper Canister Testing.Canisters Tested by Nucon
05000265/LER-1976-012, Updated LER 76-012/03L-1 Correcting Event Type,Category & Rept type.W/761001 Forwarding Ltr1 October 1976Updated LER 76-012/03L-1 Correcting Event Type,Category & Rept type.W/761001 Forwarding Ltr
05000265/LER-1982-018, Supplemental LER 82-018/03L-1:on 821006,emergency Diesel Generator Tripped on High Temp After Loading.Caused by Fouling of Diesel Generator Cooling Water Sys.Both HX Replaced1 December 1982Supplemental LER 82-018/03L-1:on 821006,emergency Diesel Generator Tripped on High Temp After Loading.Caused by Fouling of Diesel Generator Cooling Water Sys.Both HX Replaced
05000265/LER-1983-018, Revised LER 83-018/01T-1:on 831011,discovered 1-1/4 Inch long,20% through-wall Linear Indication in Weld 12S-S27. Caused by Intergranular Stress Corrosion Cracking.New Welds & Elbow Installed2 February 1984Revised LER 83-018/01T-1:on 831011,discovered 1-1/4 Inch long,20% through-wall Linear Indication in Weld 12S-S27. Caused by Intergranular Stress Corrosion Cracking.New Welds & Elbow InstalledHydrostatic
Liquid penetrant
05000265/LER-1983-020, Revised LER 83-020/01T-1:on 831028,weld 02B-S9,22-inch Pipe to Cap,Weld 02BS-S12,28-inch Elbow to Pipe & Weld 02BS-F14, 28-inch Pipe to Elbow Weld Had Circumferential Linear Indications9 December 1983Revised LER 83-020/01T-1:on 831028,weld 02B-S9,22-inch Pipe to Cap,Weld 02BS-S12,28-inch Elbow to Pipe & Weld 02BS-F14, 28-inch Pipe to Elbow Weld Had Circumferential Linear IndicationsWeld Overlay
05000265/LER-1983-021, Revised LER 83-021/01T-5:on 831028,ultrasonic Exams of Large Bore Stainless Steel Pipe Welds Identified 11 Welds W/Crack Indications.Caused by Intergranular Stress Corrosion Cracking.Weld Overlay Performed28 February 1984Revised LER 83-021/01T-5:on 831028,ultrasonic Exams of Large Bore Stainless Steel Pipe Welds Identified 11 Welds W/Crack Indications.Caused by Intergranular Stress Corrosion Cracking.Weld Overlay PerformedWeld Overlay
05000265/LER-1988-006, Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure4 June 1992Errata to LER 88-006-02:on 880404,station Notified That Eleven Flued Head Anchors Did Not Meet Design Requirements. Caused by Misinterpretation of Scope & Design Structures.Mod Initiated to Revise Structure
B130172, Safety Evaluation for Quad Cities Unit 1 Core Spray Line Repair31 January 1996Safety Evaluation for Quad Cities Unit 1 Core Spray Line RepairSafe Shutdown
Abnormal operational transient
Flow Induced Vibration
ML17174A10030 October 1979LER 79-055/03L-0:on 791004,following Pipe Hanger Repairs, Valve 2-1601-60 Failed to Close by Moving Control Switch, But Did Close When Versa Air Switching Valve Was Tapped. Caused by Malfunction of Versa Air Switching Valve
ML17174A10929 October 1979LER 79-054/03L-0:on 791004,portion of Drywell Ventilating Line 2-1605-10 Declared Inoperable Due to Degraded Pipe Supports.Caused by Insufficient Thread Engagement & Missing Nuts,Causing Hanger Supports to Become Loose.Nuts Replaced
ML17174A1111 November 1979LER 79-053/03L-0:on 791003,trip of Fuel Pool Area Radiation Monitor Resulted in Autostart of Standby Gas Treatment Sys & Isolation of Rx Bldg Vent Sys.Caused by Diaphram Drift to Setpoint Shift
ML17174A11431 October 1979LER 79-057/01T-0:on 791019,while in Shutdown,Three of 16 MSIV Scram Limit Switches Found W/Setpoints Greater than 10%.Caused by Not Performing Field Calibr on Switch Setpoints Set by Manufacturer.Limit Switches Readjusted
ML17174A11730 October 1979LER 79-027/03L-0:on 791003,half of Trip Sys Inoperable Due to Lifting of Flooding Magnetrol Switch Leads to Condenser Pit.Switch Leads Reattached.No Precise Cause Found
ML17174A12422 October 1979LER 79-033/03X-1:on 790428,while Performing Primary Containment Isolation Valve surveillance,2CTIP Machine Did Not Retract During Group 2 Isolation Test.Caused by Ball Valve Limit Switches Not Making Up When Ball Valve Opened
ML17187A80428 February 1994Containment Analysis of DBA-LOCA to Update Design Basis for Lpci/Ccs, for GENE-637-042-1193
ML17187A80531 January 1993Suppl 1 to GENE-770-26-1092, Long Term Containment Response to DBA-LOCA w/65 Fdegrees F Svc Water Temperature,80 Degrees F Initial Pool Temperature & Initiation of Containment Cooling at 1800 Seconds.Reactor Vessel Water Level
Fuel cladding
ML17192A51914 February 1980LER 80-002/03L-0:on 800122,while Performing LPCI Monthly surveillance,MO-3-1501-11B Valve Would Not Close. Reoccurrence on 800213.Investigation Revealed No Cause
ML17193A70830 November 1980SEP Review of NRC Safety Topic VI-7.A.3 Associated W/ Electrical,Instrumentation & Control Portions of ECCS Actuation Sys.Scram Discharge Volume
Fuel cladding
Coast down
ML17194A06331 May 1981Errata & Addenda Sheet 5,replacing Pages V/VI,3-1/3-2,4-10, 4-12,4-13 & 4-14 to LOCA Analysis Rept for Dresden Units 2 & 3 & Quad Cities 1 & 2 Nuclear Power Stations.
ML17194A06531 July 1981Errata & Addenda Sheet 6,replacing Pages V/VI,3-1,3-2,4-3 & 4-14,to LOCA Analysis Rept for Dresden Units 2 & 3 & Quad Cities 1 & 2 Nuclear Power Stations.
ML17194A37231 December 1981Control Room Habitability Study for Quad Cities 1 & 2, Final Rept
ML17195A95218 September 1985Safety Evaluation Approving Util plant-unique Analysis Rept on Pool Dynamic Loads
ML17195A95318 September 1985Safety Evaluation Approving Util Mods to Containments & Torus Attached Piping as Documented in COM-02-041-1 Through 7 Entitled, Technical Evaluation of Dresden Nuclear Power Station Units 2 & 3,Plant-Unique Analysis Rept.
ML17202G77631 December 1989Core Operating Limits Rept,Dresden Station Unit 2,Cycle 12,Rev 0.
ML17202L25931 May 1990Rev 1 to Core Operating Limits Rept,Dresden Station Unit 2, Cycle 12.Fuel cladding
ML17202L28829 June 1990II Upper Vessel Contract Variation Review.
ML17252A75330 November 1992Lpci/Containment Cooling Sys Evaluation.Reactor Vessel Water Level
Coatings
Turbine Missile
Flow Induced Vibration
ML17338B32720 September 1979LER 79-021/03L-0:on 790821,during Normal Operation,Offgas Monitor 3A Took Step Increase W/No Power Change & hi-hi Trip Light Was On.Caused by Faulty V1 Electrometer Tube,Which Was Replaced.Monitors Will Be Tested MonthlyPower change
ML17338B32817 September 1979LER 79-023/03L-0:on 790823,source Range Monitor Calibr Supplied Rod Block Trip at 1.03E5,exceeding Tech Specs Limit.Caused by Drift & Temp Dependency in Source Range Monitor.Defective Component Not Yet Identified
ML17340B41626 March 1980Updated LER 80-030/03X-1:on 791110,during Scram Testing in Refuel Mode,Substantial Loss of Position Indication Noted for Control Rod Driveline H-9.Caused by Improperly Seated Socket,Suggesting Faulty Electrical pin-socket Alignment
ML17340B41928 March 1980LER 80-011/03L-0:on 800305,while Conducting Steam Line Area Temp Switch Calibr Surveillance,Temp Switch TS 3-261-17B Tripped Above Tech Specs.Caused by Dirt Deposits on Switch Actuation Plunger.Switch Cleaned,Adjusted & Tested
ML17352B2501 October 1993LER 93-014-00:on 930902,discovered That IRM 11 & APRM Both in Bypassed Condition W/O Half Scram Being Inserted Due to Work Practices.Irm 11 Taken Out of Bypassed Condition & Individual Involved counselled.W/931001 LtrHalf scram