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05000285/FIN-2013008-222013Q2Fort CalhounFort Calhouns Station\'S Ability to Classify Components as SAFETY-RELATEDThe team found it difficult to determine how the licensee identified SSCs important to safety as required by 10 CFR Part 50, Appendix B, Criterion II. The team noted that several recent performance deficiencies have been identified by the NRC for not classifying SSCs as safety-related based on the safety function being performed. The team determined the licensees causal analysis to date for these issues was inadequate. Consequently, during the on-site inspection, the team questioned the classification of various SSCs which appear to meet the definition of safety-related, but have not been designated as such by the licensee. 10 CFR Part 50.2, Definitions defines safety-related SSCs as, ...those structures, systems, and components that are relied upon to remain functional during and following design basis events to assure: (1) the integrity of the reactor coolant pressure boundary; (2) the capability to shut down the reactor and maintain it in a safe shutdown condition; or (3) the capability to prevent or mitigate the consequences of accidents which could result in potential offsite exposures comparable to the applicable guideline exposures set forth in 10 CFR Part 50.34 (a)(1) or 10 CFR Part 50.100.11 of this chapter, as applicable. The team determined that the licensee may not have identified all the SSCs important to safety to ensure the controls of 10 CFR Part 50, Appendix B are applied. Additional review and follow up will be required to determine if this issue represents a performance deficiency or constitutes a violation of NRC requirements. This issue is identified as URI 05000285/2013008-22, Fort Calhoun Stations Ability to Classify Components as Safety-Related.
05000285/FIN-2013008-302013Q2Fort CalhounEvaluation of Change to Alternate Shutdown Cooling FlowpathThe team identified an unresolved item related to engineering change modifications that changed a procedure to include the replacement of automatic actions with manual actions. Specifically, the10 CFR 50.59 evaluation proposed a change to substitute automatic flow control of shutdown cooling flow and temperature with manual control using the low pressure safety injection loop injection valves alternate shutdown cooling flow control. During a review of Engineering Change Modification 54058, Procedure Change to Allow Closing of HCV-335 while on Alternate Shutdown Cooling, the team identified that the licensee changed a procedure to include the replacement of an automatic action with a manual action. Specifically, the engineering change proposed to close both shutdown cooling heat exchanger isolation valve HCV-335 and flow control valve FCV-326 while pinning open valve HCV-341 and manually throttling low pressure safety injection loop injection valves to maintain the desired RCS temperature and flow rate. The team questioned whether the licensee required prior NRC review and approval to make this change since flow control valve FCV-326 normally controls temperature and flow automatically as described in Section 9.3.4.3 of the USAR. The licensee entered this issue of concern into the CAP. Additional NRC review and follow up will be required to determine if this issue represents a performance deficiency associated with meeting the 10 CFR 50.59 requirement of more than a minimal increase in the likelihood of occurrence of a malfunction of a system, structure, or component important to safety previously evaluated in the USAR. This item is unresolved pending review of the licensees evaluation. This issue is identified as URI 05000285/2013008- 30, Evaluation of Change to Alternate Shutdown Cooling Flowpath.
05000285/FIN-2014002-052014Q1Fort CalhounUntimely Submittal of Required Licensee Event ReportsTwo examples of a cited Severity Level IV violation of 10 CFR 50.73, Immediate Notification Requirements for Operating Nuclear Power Reactors, were identified involving the failure to submit a required licensee event report (LER) within 60 days following discovery of an event requiring a report. In the first example, LER 2013-010-0 was submitted on July 2, 2013, seventy-nine days after the flow imbalance was observed by the licensees staff. In the second example, LER 2013-017-0 was submitted to the NRC on December 27, 2013, 62 days after the event date on the licensees reportability evaluation and sixty-six days after a condition report documented the reportable condition. The licensee initiated CR 2014-01358 on January 29, 2014 to document this repetitive violation. The violation was evaluated using Section 2.2.4 of the NRC Enforcement Policy, because the failure to submit a required LER may impact the ability of the NRC to perform its regulatory oversight function. As a result, this violation was evaluated using traditional enforcement. In accordance with Section 6.9(d)(9) of the NRC Enforcement Policy, this violation was determined to be a Severity Level IV violation. The inspetors determined that a cross-cutting aspect was not applicable to this performance deficiency because the failure to make a required report was strictly associated with a traditional enforcement violation.
05000285/FIN-2014009-012014Q3Fort CalhounFailure to Initiate Condition Reports for Gaps Identified in Resolving NRC Non-Cited ViolationsA non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instruction, Procedures, and Drawings, was identified involving the failure to follow procedures to initiate condition reports to enter conditions adverse to quality into the corrective action program. Specifically, the licensee failed to initiate condition reports in accordance with Procedure FCSG 24-1, Condition Report Initiation, Step 4.1.1.G, when deficiencies related to the stations corrective actions implemented for NRC violations were identified. The licensee entered this issue into its corrective action program as Condition Report 2014-09063 and initiated action to write condition reports for identified gaps related to previous NRC violations. This performance deficiency was more than minor, and therefore a finding, because if left uncorrected, it would have the potential to lead to a more significant safety concern. The team performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At- Power. Using IMC 0609 Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding was of very low safety significance (Green) because it did not involve a loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding, or severe weather initiating event. This finding has a cross-cutting aspect in the area of human performance because the licensee elected to use an informal system to resolve these issues rather than the corrective action program.
05000285/FIN-2014009-022014Q3Fort CalhounMultiple Examples of Failure to Evaluate Operability of Degraded or Non-Conforming ConditionMultiple examples of a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified involving the failure to follow Procedure OP-FC-108-115, Operability Determinations, Revision 0a. In each example, the team identified that the licensee failed to make an immediate determination of operability for a degraded or non-conforming condition or failed to make an immediate determination of operability based on a detailed examination of the deficiency. The licensee took immediate corrective actions to update the incomplete or inaccurate operability determinations and entered the collective failures to follow station operability procedures into their corrective action program as Condition Report 2014-09163. This performance deficiency was more than minor, and therefore a finding, because it affected the equipment performance attribute of the Mitigating Systems Cornerstone objective of ensuring the reliability of systems that respond to initiating events. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At- Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating system; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the area of human performance because the licensee failed to use decision-making practices that demonstrate that a proposed action is to be safe in order to proceed, rather than unsafe in order to stop. Specifically, the licensee made non-conservative decisions related to the impact of degraded or non-conforming conditions.
05000285/FIN-2014009-032014Q3Fort CalhounFailure to Adequately Perform an Operability Evaluation and a 50.59 EvaluationA non-cited violation of 10 CFR 50.59, Changes, Tests, and Experiments, and associated non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified involving the failure to evaluate and implement adequate compensatory measures for a degraded condition associated with raw water pump AC-10C. Specifically, the licensees operability determination established a compensatory measure to place pump AC-10C in pull-to-lock, contrary to the system single failure analysis design criteria described in the Updated Safety Analysis Report. The licensee entered this issue into its corrective action program as Condition Reports 2014-09104 and 2014-08515 and performed an operability evaluation and associated 10 CFR 50.59 evaluation that used an acceptable compensatory measure to pump water from affected manholes prior to affecting the degraded power feeder cable for raw water pump AC-10C. The NRC evaluated this performance deficiency as both a reactor oversight process finding and a traditional enforcement violation. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating system; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant for greater than 24 hours in accordance with the licensees maintenance rule program. This finding has a cross-cutting aspect in the area of problem identification and resolution with an aspect of evaluation because the licensee failed to ensure that resolutions address causes and extent of conditions commensurate with their safety significance (P.2). In addition, because this performance deficiency had the potential to impact the NRCs ability to perform its regulatory function in that the failure to obtain a license amendment for a change that could result in a malfunction of a structure, system or component with a different result than previously evaluated in the Updated Safety Analysis Report is in violation of 10 CFR 50.59(c)(2)(vi), the NRC also evaluated the violation using traditional enforcement. Since this violation is associated with a Green reactor oversight process violation, the traditional enforcement violation was determined to be a Severity Level IV violation, consistent with the example in paragraph 6.1.d(2) of the NRC Enforcement Policy.
05000285/FIN-2014009-042014Q3Fort CalhounFailure to Perform an Evaluation for a New Operator Manual Action to Refill Component Cooling Water System During Post- Accident ConditionsA non-cited violation of 10 CFR 50.59, Changes, Test, and Experiments, was identified involving the failure to evaluate if a change to the facility as described in the Updated Safety Analysis Report would require prior NRC review and approval. Specifically, the licensee failed to evaluate if a change implemented under Engineering Change 59252 that credited the non-safety related demineralized water system as a make-up source to the component cooling water system during post-accident conditions represented an adverse change to the Updated Safety Analysis Report described design function. The licensee entered this deficiency into its corrective action program for resolution as Condition Report 2014-09151 and established action items to update Engineering Change 59252. The NRC determined that the licensees failure to perform an evaluation prior to implementing a proposed change described in the Updated Safety Analysis Report was a violation of 10 CFR 50.59. Because this violation had the potential to impact the NRCs ability to perform its regulatory function, the NRC evaluated the violation using traditional enforcement. In accordance with Section 2.1.3.E.6 of the NRC Enforcement Manual, the NRC evaluated this finding using the significance determination process to assess its significance. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program. Therefore, in accordance with Section 6.1.d.2 of the NRC Enforcement Policy, this performance deficiency is characterized as a Severity Level IV violation. The team determined that a cross-cutting aspect was not applicable because the issue involving the failure to perform an adequate 10 CFR 50.59 evaluation was strictly associated with a traditional enforcement violation.
05000285/FIN-2014009-052014Q3Fort CalhounInadequate Design Inputs into Safety Injection Piping Stress CalculationA non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to implement appropriate design control measures associated with a safety-related pipe stress calculation. Specifically, several unverified and potentially non-conservative inputs were identified associated with Calculation FC07240 used to analyze stresses on a pipe reduction tee in the safety injection system. The licensee entered this issue into the corrective action program as Condition Report 2014-09098 and initiated action to update Calculation FC07240. This performance deficiency was more than minor, and therefore a finding, because it affected the design control attribute of the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of components that respond to initiating events. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating system; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) does not represent an actual loss of function of one or more nontechnical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the area of human performance in that the licensee failed to apply the appropriate rigor when evaluating the overstressed pipe union tee.
05000285/FIN-2014009-062014Q3Fort CalhounFailure to Maintain Design Control of Raw Water Strainer Control PanelA self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to maintain design control of the raw water strainer AC-12B control panel AI-348. Specifically, the licensee failed to adequately design control panel AI-348 to protect it from the effects of spraying and wetting as required by the plants licensing and design basis. The licensee entered this issue into its corrective action program as Condition Reports 2013-03301 and 2014-06974 and initiated action to encase control panel AI-348 to protect it against the effects of spraying and wetting. This performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, control panel AI-348 was not designed to prevent water intrusion that resulted in a loss of power to raw water strainer AC-12B. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding was of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program; and (5) did not involve the loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding or severe weather event. This finding has a crosscutting aspect in the area of problem identification and resolution associated with the organization thoroughly evaluating issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance.
05000285/FIN-2014009-072014Q3Fort CalhounFailure to Accurately Model Flow Path for External Flood MitigationA non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to accurately model cell level control of river water during external flooding events. Specifically, the licensee failed to account for losses due to the physical obstructions of trash racks for inflowing river water, the decreased withdrawal rate of the raw water pumps due to fouling across the traveling screens, and a bounding in leakage rate for the sluice gates when the river level is at maximum level of 1014 mean sea level and the intake cell levels are at minimum level of 9769 . The licensee entered this issue into its corrective action program as Condition Report 2014-09155, performed an operability determination, and initiated action to update station calculations related to intake cell level control. This performance deficiency was more than minor, and therefore a finding, because if left uncorrected, the finding would have the potential to lead to a more significant safety concern. Specifically, the failure to accurately model flow in and out of the cells could adversely affect the external flooding mitigation strategy beyond previously identified equipment capacities and operator actions. This finding was associated with the Mitigating Systems Cornerstone. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating system; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program; and (5) did not involve the loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding or severe weather event. This finding has a cross-cutting aspect in the area of problem identification and resolution, operating experience, in that the licensee failed to incorporate relevant internal operating experience related to previous NRC inspection into Calculation FC08081.
05000285/FIN-2014009-082014Q3Fort CalhounFailure to Report Loss of Environmental Qualification of Safety Related Limit Switches within Required Time LimitsA non-cited violation of 10 CFR 50.73(a)(1), Licensee Event Report System, was identified involving the failure to submit a required licensee event report. Specifically, the licensee failed to report within 60 days the discovery that NamcoTM Type EA 180 limit switches were not environmentally qualified as required due to inadequate maintenance procedures, a condition that resulted in operation prohibited by the plants technical specifications. The licensee restored compliance by submitting Licensee Event Report 05000285/2014-004 on June 20, 2014. The licensee entered this issue into its corrective action program as Condition Report 2014-08454. The NRC determined that the failure to submit a licensee event report within the time limits specified in regulations was a violation of 10 CFR 50.73. This violation was evaluated using Section 2.2.4 of the NRC Enforcement Policy, because the failure to submit a required licensee event report may impact the ability of the NRC to perform its regulatory oversight function. As a result, this violation was evaluated using traditional enforcement. In accordance with Section 6.9 of the NRC Enforcement Policy, this violation was determined to be a Severity Level IV, non-cited violation. The NRC determined that a cross-cutting aspect was not applicable because the issue was strictly associated with a traditional enforcement violation.
05000285/FIN-2014009-092014Q3Fort CalhounFailure to Incorporate Design Requirements for Switchgear Room CoolingA non-cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to translate applicable design requirements into the specifications for plant systems. Specifically, inadequate design control inputs were used for analyzing the ability of the vital switchgear room cooling system to perform its safety function under all conditions. The licensee entered this issue into its corrective action program as Condition Report 2014-08317 and initiated actions to analyze the ability of vital switchgear room cooling to meet its specified safety function. This performance deficiency was more than minor, and therefore a finding, because it affected the design control attribute of the Mitigating Systems Cornerstone, and it directly affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating system; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the evaluation component of the problem identification and resolution cross-cutting area because the licensee failed to thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the licensee failed to analyze and evaluate a 1998 loss of switchgear cooling event to ensure that its use as a design assumption bound the worst design basis event.
05000285/FIN-2014009-102014Q3Fort CalhounDeficient Evaluation of NRC Bulletin 88-04, Strong Pump Weak Pump Due to Failure to Consider the Effect of Auxiliary Feedwater Pumps Discharge Check Valves LeakageA cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to assure that applicable regulatory requirements and design bases were correctly translated into specifications, drawings, procedures, and instructions. Specifically, the licensee failed to properly evaluate NRC Bulletin 88-04, Potential Safety- Related Pump Loss, for strong pump weak pump interaction regarding auxiliary feedwater pumps FW-6 and FW-10. The evaluation failed to consider pump-to-pump interaction that may result due to pump discharge check valve leakage. In addition, the licensee failed to re-evaluate the condition after surveillance testing performed on November 28, 2010, and September 1, 2012, identified leakage past both pump discharge check valves. The licensee entered this issue into its corrective action program as Condition Report 2014-08381 and initiated actions to re-evaluate NRC Bulletin 88-04. This performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At- Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program. This finding has a cross-cutting aspect in the area of human performance because the licensee failed to demonstrate a conservative bias in decision making-practices. Specifically, the licensees determination that the event is not credible failed to consider documented check valve leakage in the auxiliary feedwater system.
05000285/FIN-2014009-112014Q3Fort CalhounFailure to Ensure Safe Operations at Design Basis Low River LevelA cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to ensure that the safety-related raw water pumps are available for safe plant operations down to the design basis low river level. Specifically, station analysis and abnormal operating procedures would not allow operation of the raw water pumps to the design basis low river water level. The licensee entered this issue into its corrective action program as Condition Report 2014-09159 which included actions to reevaluate the capability of the raw water pumps to operate at low river levels. This finding was more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At- Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program. This finding has a cross-cutting aspect in the area of human performance in that the licensee did not ensure that personnel, equipment, procedures and other resources are available and adequate to support nuclear safety. Specifically, the licensee deferred funding for a vendor analysis of the capabilities of the raw water pumps at the design low river level.
05000285/FIN-2014009-122014Q3Fort CalhounFailure to Maintain Effectiveness of an Emergency PlanA cited violation of 10 CFR 50.54(q)(2), Conditions of License, was identified involving the failure to maintain the effectiveness of the sites emergency plan. Specifically, the licensee established an Alert low river level emergency classification criteria that was below the raw water pumps minimum suction requirements, contrary to the standard emergency action level scheme. The licensee entered this issue into its corrective action program as Condition Report 2014-08757 which included actions to re-evaluate the capability of the raw water pumps to operate at low river levels. This finding was more than minor, and therefore a finding, because it was associated with the emergency response organization performance attribute of the Emergency Preparedness Cornerstone and affected the associated cornerstone objective to ensure that the licensee is capable of implementing adequate measures to protect the health and safety of the public in the event of a radiological emergency. Specifically, inaccurate emergency actions levels degrade the licensees ability to implement adequate measures to protect public health and safety. The finding was evaluated using the Emergency Preparedness Significance Determination Process, and was determined to be of very low safety significance (Green) because the finding was not a lost or degraded risk significant planning function. The planning standard function was not degraded because the emergency classifications would have been declared although potentially in a delayed manner. This finding has a cross-cutting aspect in the area of human performance in that the licensee did not ensure that personnel, equipment, procedures and other resources are available and adequate to support nuclear safety. Specifically, the licensee deferred funding for a vendor analysis of the capabilities of the raw water pumps at the design low river level.
05000285/FIN-2014009-132014Q3Fort CalhounFailure to Perform Evaluation for Design ChangeA cited violation of 10 CFR 50.59, Changes, Tests, and Experiments, was identified involving the failure to evaluate if a change to the facility as described in the Updated Safety Analysis Report would require prior NRC review and approval. Specifically, the licensee did not evaluate a change that would permanently substitute a manual action for an automatic action to add water and nitrogen gas to the component cooling water surge tank. The licensee entered this issue into its corrective action program as Condition Report 2014-09080 and initiated action to evaluate the change to the component cooling water system. The NRC determined that the licensees failure to perform an evaluation prior to implementing a proposed change described in the Updated Safety Analysis Report was a violation of 10 CFR 50.59. Because this performance deficiency had the potential to impact the NRCs ability to perform its regulatory function, the NRC evaluated the performance deficiency using traditional enforcement. In accordance with Section 2.1.3.E.6 of the NRC Enforcement Manual, the team evaluated this finding using the significance determination process to assess its significance. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program. Therefore, in accordance with Section 6.1.d.2 of the NRC Enforcement Policy this performance deficiency is being characterized as a Severity Level IV violation. The team determined that a cross-cutting aspect was not applicable to this finding because the issue was strictly associated with a traditional enforcement violation.
05000285/FIN-2014009-142014Q3Fort CalhounFailure to Account for Worst Case Diesel Frequency in Fuel Oil Consumption CalculaA cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, was identified involving the failure to account for design basis conditions in station calculations. Specifically, the licensee failed to account for worst-case electrical frequency when analyzing diesel fuel oil consumption and storage requirements. The licensee entered this issue into its corrective action program as Condition Report 2014-09157 and initiated action to update station calculations. This performance deficiency was more than minor, and therefore a finding, because it affected the design control attribute of the Mitigating Systems Cornerstone objective to ensure the availability, reliability, and capability of components that respond to initiating events. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding is of very low safety significance (Green) because: (1) the finding was not a deficiency affecting the design or qualification of a mitigating system; (2) the finding did not represent a loss of system and/or function; (3) the finding did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) the finding does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the area of problem identification and resolution in that the licensee failed to thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance.
05000285/FIN-2014009-152014Q3Fort CalhounFailure to Promptly Identify and Correct a Condition Adverse to QualityA non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified involving the failure to take corrective actions for a condition adverse to quality. Specifically, the licensee failed to take corrective actions to address multiple issues involving gas voiding of the component cooling water system. As immediate corrective action the licensee placed a maintenance hold on the component cooling water system until adequate fill and vent procedures were established. The licensee initiated corrective actions to analyze the effects of gas accumulation on the component cooling water system and entered this issue into the corrective action program as Condition Reports 2014-08892, 2014-09011 and 2014-09034. This performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that responds to initiating events to prevent undesirable consequences. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At- Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was of very low safety significance (Green) because the finding: (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program. This finding has a cross-cutting aspect in the area of human performance in that the licensee failed to operate the component cooling water system within design margins and failed to place special attention on minimizing longstanding equipment issues related to gas voiding in that system.
05000285/FIN-2014009-162014Q3Fort CalhounFailure to Correct Longstanding Software Classification IssuesA non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified involving the failure to take timely corrective actions to ensure the proper control and use of software products used in safety related applications. Specifically, the team identified multiple instances of uncontrolled software products in use at the licensees facility following identification of similar deficiencies in 2009 and 2011. The licensee entered this issue into their corrective action program as Condition Report 2014-09162 and initiated action to strengthen their software control program. The performance deficiency was more than minor, and therefore a finding, because if left uncorrected, it could lead to a more significant safety concern. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because: (1) the finding was not a deficiency affecting the design or qualification of a mitigating system; (2) the finding did not represent a loss of system and/or function; (3) the finding did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) the finding does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the area of human performance in that the licensee failed to provide training and ensure knowledge transfer to maintain a knowledgeable, technically competent workforce and instill nuclear safety values. Specifically, the apparent cause report for Condition Report 2009-04715 stated that a contributing cause was first and foremost (there is) a lack of knowledge associated with the procedural requirements for software control at FCS.
05000285/FIN-2014009-172014Q3Fort CalhounInadequate Corrective Actions to Properly Implement Applicable ASME OM Code RequirementsA non-cited violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was identified involving the failure to correct a condition adverse to quality associated with classification of check valves in the auxiliary feedwater system. Specifically, the licensee failed to update the in-service testing program to classify auxiliary feedwater discharge check valves as Category A/C valves and include required seat leakage testing. The licensee entered this issue into its corrective action program as Condition Report 2014-08452 and initiated actions to re-assess the current in-service testing methodology of check valves in the auxiliary feedwater system. This performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because: (1) the finding was not a deficiency affecting the design or qualification of a mitigating system; (2) the finding did not represent a loss of system and/or function; (3) the finding did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) the finding does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the area of problem identification and resolution because the licensee failed to thoroughly evaluate issues to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, the licensee failed to evaluate the function of discharge check valves FW-173 and FW-174 when developing the in-service testing program and addressing previous condition reports.
05000285/FIN-2014009-182014Q3Fort CalhounFailure to Complete Corrective Actions in a Timely MannerA non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified involving the failure to take timely corrective actions to address deficiencies in station calculations. Specifically, the licensee failed to update station calculations to incorporate actual test data for sluice gate leakage to ensure design basis flood levels do not adversely affect equipment important to safety. The licensee entered this issue into its corrective action program as Condition Report 2014-09156 and initiated actions to update station calculations. This finding was more than minor, and therefore a finding, because if left uncorrected, the finding would have the potential to lead to a more significant safety concern. Specifically, failure to complete accurate calculations that support engineering modifications for mitigating the consequences of an external flooding event could lead to unanalyzed conditions adversely affecting safety related systems or components. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because: (1) the finding was not a deficiency affecting the design or qualification of a mitigating system; (2) the finding did not represent a loss of system and/or function; (3) the finding did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program; and (5) did not involve the loss or degradation of equipment or function specifically designed to mitigate a seismic, flooding or severe weather event. This finding has a cross-cutting aspect in the area of human performance in that the licensee failed prioritize an update to Calculation FC08081 following completion of the May 2013 in-leakage test.
05000285/FIN-2014009-192014Q3Fort CalhounFailure to Maintain B.5.b Equipment in a State of Readiness to Support Mitigation StrategiesA non-cited violation of 10 CFR 50.54(hh)(2), Conditions of License, was identified involving the failure to maintain available equipment needed to implement mitigating strategies to maintain or restore core, containment, and spent fuel pool cooling capabilities following large fires or explosions. Specifically, the licensee failed to maintain available a flexible suction hose related to the reactor coolant system heat removal mitigating strategy. The licensee initiated Condition Report 2014-08876 to address this deficiency and initiated action to procure and replace the missing flexible suction hose. This performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). The NRC determined that this finding was of very low safety significance (Green) using NRC Manual Chapter IMC 0609, Appendix L, B.5.b Significance Determination Process, because it resulted in an unrecoverable unavailability of an individual mitigating strategy but did not result in multiple unavailable mitigating strategies such that reactor coolant system heat removal could not occur. This finding has a crosscutting aspect in the area of human performance in that the licensees inadequate B.5.b inventory procedure contributed to the lack of recognition that the degraded flexible suction hose was required to implement mitigating strategies.
05000285/FIN-2014009-202014Q3Fort CalhounFailure to Correct Conditions Adverse to Quality in the Diesel Generator Stating Air SystemA self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified involving the failure to take timely corrective actions to address service life related degradation of the emergency diesel generator starting air system. As a result, diesel generator 1 failed to roll during planned surveillance testing due to a degraded diesel starting air valve. The licensee replaced the faulty starting air valve and implemented corrective actions to develop preventative maintenance strategies for the starting air system. The licensee entered this issue into the corrective action program as Condition Report 2014-09424. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance Determination Process Phase 1 Initial Screening and Characterization of Findings , Exhibit 3, Mitigating Systems Screening Questions, dated May 9, 2014, the finding was of very low safety significance (Green) because the finding does not represent a loss of system safety function and the finding does not represent an actual loss of safety function of a single train for greater than its technical specification allowed outage time. This finding has a cross-cutting aspect in the area of human performance in that the licensee failed to recognize and plan for the possibility of latent issues, and inherent risk, even while expecting successful outcomes when determining the repair schedule for starting air valve SA-148.
05000285/FIN-2014009-212014Q3Fort CalhounFailure to Take Timely Corrective Actions for an Unsealed Raw Water System Control PanelA self-revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, was identified involving the failure to take corrective actions to address a design deficiency affecting the control panel for raw water strainer AC-12B. Consequently, the panel experienced a water intrusion event on August 3, 2014, resulting in an unplanned inoperability of the raw water system. Following identification of this issue, the licensee implemented corrective actions to seal conduits leading to control panel AI-348 to prevent future water intrusion. The licensee entered this issue into its corrective action program as Condition Report 2014-09572. This performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The NRC performed an initial screening of the finding in accordance with NRC Manual Chapter IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At- Power. Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, this finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating system; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of a single train for greater than its technical specification allowed outage time; and (4) does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours. This finding has a cross-cutting aspect in the area of problem identification and resolution in that the licensee failed to adequately review and provide timely responses to past operating experience that demonstrated that panel AI-348 was susceptible to water intrusion.
05000285/FIN-2014009-222014Q3Fort CalhounLicensee-Identified ViolationTitle 10 CFR Part 50, Appendix B, Criterion III, Design Control, requires, in part, that measures shall be established to assure that applicable regulatory requirements and the design basis for those structures, systems, and components are correctly translated into specifications, drawings, procedures, and instructions. Contrary to the above, from initial construction until January 13, 2013, the licensee failed to establish measures to assure that applicable regulatory requirements and the design basis were correctly translated into specifications, drawings, procedures, and instructions. Specifically, the licensee failed to control the design inputs to ensure that piping in the chemical and volume control system would perform acceptably during a seismic event. This finding is of very low safety significance (Green) because a chemical and volume control system piping failure event is enveloped by the small break loss of coolant accident as described in Updated Safety Analysis Report Section 14.5.5. This issue was entered into the licensees corrective action program as CR 2013-01796.
05000285/FIN-2014009-232014Q3Fort CalhounLicensee-Identified ViolationTitle 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to the above, on June 2, 2008, the licensee completed flow scan valve testing for the high pressure safety injection alternate header isolation valve (HCV-2987) that showed a much higher stem friction value than previously analyzed, but failed to promptly identify and correct the condition adverse to quality until CR 2012-01601 was initiated on February 29, 2012. This finding is of very low safety significance (Green) because valve HCV-2987s failure did not represent an actual loss of safety function of a single train for greater than the technical specification allowed outage time in that EOP/AOP Attachments, Revision 13, dated November 19, 2002, requires operators to also close downstream valves that would back up the closure function of valve HCV-2987. This issue was entered into the licensees corrective action program as CR 2012-01601.
05000285/FIN-2014009-242014Q3Fort CalhounLicensee-Identified ViolationTitle 10 CFR 50.73(a)(1) requires, in part, that licensees shall submit a licensee event report for any event of the type described in this paragraph within 60 days after the discovery of the event. Contrary to the above, on February 5, 2012, November 15, 2011, and February 19, 2013, the licensee failed to submit a licensee event report for an event meeting the requirements for reporting specified in 10 CFR 50.73. Specifically, the licensee submitted Licensee Event Reports 2012-013, 2012-015 and 2013-001 greater than 60 days following discovery of a reportable event. In accordance with Section 6.9 of the NRC Enforcement Policy, this violation was determined to be a Severity Level IV, non-cited violation. The licensee entered this issue into their corrective action program as CR 2014-02792.
05000285/FIN-2014009-252014Q3Fort CalhounLicensee-Identified ViolationTechnical Specification 5.8.1.a, requires, in part, that written procedures be established, implemented, and maintained as recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory Guide 1.33, Paragraph 9.a, requires that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, the licensee failed to establish procedures for maintenance that can affect the performance of safety related equipment as recommended in Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Specifically, prior to May 3, 2013, the licensees maintenance procedure for NamcoTM Type EA 180 limit switches did not specify the correct torque values for the switch top cover to maintain the components environmental qualifications. This finding was determined to be of very low safety significance because the affected limits switches only affected the radiological barrier provided for by the control room. This issue was entered into the licensees corrective action program as CR 2012-03651.
05000285/FIN-2015001-032015Q1Fort CalhounRequired In-Service Testing for Steam Generator Auxiliary Feedwater Inlet ValvesThe inspectors identified an unresolved item associated with required inservice testing (lSD for steam generator auxiliary feedwater (AFW) inlet valves. The licensee is updating a design analysis for these valves to establish a formal technical position with regard to the "active" safety functions that these valves serve. The inspectors will review the licensee's updated design analysis upon its completion to determine if the 1ST is being performed per the 1ST ASME OM Code. On December 22, 2014, the inspectors reviewed an operability determination following the licensee's discovery of a degraded condition related to a leak identified on AFW valve HCV-11 08A. The inspectors reviewed surveillance testing required by Technical Specification (TS) 3.9.3 which requires that the operability of HCV- 11 08A be confirmed in accordance with the licensee's 1ST program. The inspectors identified that these AFW valves had both open and close "active" safety functions per design basis document EA11-026, "CQE Valves w/Essential Accumulators". In addition, the valve is classified as a category "8" valve per their 1ST program. The licensee committed to ASME OM Code 1998 Edition w/1999 through 2000 addenda for their 1ST program. Applicable to this Code, an "active" safety function requires the valve to change position to accomplish its specific safety function. Category "8" valves with these "active" functions are required to be stroke time tested in the direction of valve repositioning. The inspectors discussed these requirements with the licensee and they subsequently identified that they were not performing ASME 1ST for HCV-1107A/8 and HCV-11 08AIB for the "active" close safety function of the valves. The licensee is performing a review of the "active" close safety function to determine whether the "active" safety function described in EA 11-026 is appropriate. The inspectors will review the licensee determination and assess whether the testing being performed on the steam generator AFW inlet valves meets the applicable ASME OM Code requirements. This issue will be tracked as unresolved item (URI) 05000285/2015001-03.
05000285/FIN-2015002-012015Q2Fort CalhounFailure to Include a Class 1 Component in the Reactor Vessel Pressure Boundary Integrity TestThe inspectors identified a non-cited violation of 10 CFR 50.55a(g)(4), involving the failure to adequately perform periodic reactor coolant system (RCS) integrity inspections as required by ASME Code Section XI. Specifically, Procedure OP-ST-RC-3007, Periodic Reactor Coolant System Integrity Test, required testing of all ASME Class 1 pressure boundary components of the reactor vessel pressure boundary but failed to include reactor vessel head vent line RC-2501R. As a result, the requirements of ASME Code Section XI were not met. This issue was entered into the licensees corrective action program as Condition Report 2015-05858. The inspectors concluded that the failure to include reactor vessel head vent line RC-2501R within the reactor vessel pressure boundary in the periodic RCS integrity inspection was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not result in exceeding the RCS leak rate for a small loss-of-coolant accident, and did not affect other systems used to mitigate a loss-of-coolant accident resulting in a total loss of their function. The inspectors determined that the finding had a conservative bias cross-cutting aspect in the area of human performance because the licensee failed to use decision making-practices that emphasized prudent choices over those that are simply allowable. (H.14
05000285/FIN-2015002-022015Q2Fort CalhounFailure to Perform a Valid 40-Month Inservice TestThe inspectors identified a non-cited violation of 10 CFR 50.55a(g)(4) for the failure to perform a valid 40-month inservice test of the spent fuel pool cooling system. Specifically, the licensee failed to identify an existing through-wall leak on discharge header vent valve AC-898 that invalidated the test. The licensee replaced vent valve AC-898 and repaired the affected weld in April 2015. This issue was entered into the licensees corrective action program as Condition Report 2015-05038. The failure to perform a valid 40-month inservice test of the spent fuel pool cooling system was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the design control attribute of the Barrier Integrity Cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not adversely affect decay heat removal capabilities from the spent fuel pool causing the pool temperature to exceed the maximum analyzed temperature limit specified in the site-specific licensing basis, did not result from fuel handling errors, dropped fuel assembly, dropped storage cask, or crane operations over the SFP that caused mechanical damage to fuel clad and a detectible release of radionuclides, did not result in a loss of spent fuel pool water inventory decreasing below the minimum analyzed level limit specified in the site-specific licensing basis, and did not affect the SFP neutron absorber, fuel bundle misplacement or soluble boron concentration. The inspectors determined that the finding had a conservative bias cross-cutting aspect in the area of human performance because individuals failed to use decision making-practices that emphasized prudent choices over those that are simply allowable. Although the licensee had previously identified the leak in valve AC-898 and determined that the leak had compromised the structural integrity of the system, the licensee failed to fix the leak. (H.14)
05000285/FIN-2015002-032015Q2Fort CalhounFailure to Establish Adequate Work Instructions to Clean and Inspect the Reactor Vessel HeadThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure to establish adequate work instructions to clean and inspect the reactor vessel head. Specifically, the work instructions for the required visual examination of the reactor vessel head failed to specify what constituted a relevant condition as defined by ASME Code Case N-729-1, Alternative Enclosure Examination Requirements for PWR Reactor Vessel Upper Head with Nozzles Having Pressure Retaining Partial Penetration Welds. As a result, the licensee failed to identify several relevant conditions that required additional inspections to adequately assure that the structural integrity of the reactor vessel head was not compromised. This issue was entered into the licensees corrective action program as Condition Report 2015-05995. The failure to establish adequate work instructions to clean and inspect the reactor vessel head was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not result in exceeding the RCS leak rate for a small lossof-coolant accident, and did not affect other systems used to mitigate a loss-of-coolant accident resulting in a total loss of their function. The inspectors determined that the finding had a teamwork cross-cutting aspect in the area of human performance because individuals and work groups failed to communicate and coordinate their activities within and across organizational boundaries to ensure nuclear safety is maintained. (H.4)
05000285/FIN-2015002-042015Q2Fort CalhounFailure to Incorporate Vendor Manual Recommendations for Conducting Preventative Maintenance on the Reactor Vessel Head Vent ValveThe inspectors identified a non-cited violation of Technical Specification 5.8.1.a associated with the failure to establish a preventative maintenance schedule for the reactor vessel head vent manual isolation valve, RC-100. Specifically, engineering personnel failed to consider vendor recommended maintenance activities/schedules, and determined that the valve could be run to failure. As a result, when the valve packing failed during operation, boric acid leaked onto the reactor vessel head. The licensee replaced the valve internals during refueling outage RFO 27 under Work Order 551054. This issue was entered into the licensees corrective action program as Condition Report 2015-05432. The failure of engineering personnel to establish a preventative maintenance schedule for the reactor vessel head vent manual isolation valve was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the equipment performance attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not result in exceeding the RCS leak rate for a small loss-of-coolant accident, and did not affect other systems used to mitigate a loss-of-coolant accident resulting in a total loss of their function. No cross-cutting aspect was assigned because the inspectors determined that the finding was not indicative of current performance.
05000285/FIN-2015002-052015Q2Fort CalhounFailure to Promptly Identify and Correct a Condition Adverse to Quality Involving a Spent Fuel Pool Cooling Vent Valve LeakThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions, for the failure to promptly identify and correct a condition adverse to quality. Specifically, the licensee failed to take corrective action to replace spent fuel pool cooling system discharge header vent valve AC-898 after a leak was identified. A work order for the condition was opened in 2009 but was never implemented. Subsequently, a pressure boundary leak was identified in 2013 and misidentified in 2014 but was never addressed. The licensee replaced vent valve AC-898 and repaired the affected weld in April 2015. This issue was entered into the licensees corrective action program as Condition Report 2015-05038. The failure to promptly identify and correct a condition adverse to quality was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the design control attribute of the Barrier Integrity Cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not adversely affect decay heat removal capabilities from the spent fuel pool causing the pool temperature to exceed the maximum analyzed temperature limit specified in the site-specific licensing basis, did not result from fuel handling errors, dropped fuel assembly, dropped storage cask, or crane operations over the SFP that caused mechanical damage to fuel clad and a detectible release of radionuclides, did not result in a loss of spent fuel pool water inventory decreasing below the minimum analyzed level limit specified in the site-specific licensing basis, and did not affect the SFP neutron absorber, fuel bundle misplacement or soluble boron concentration. The inspectors determined that the finding had a basis for decision cross-cutting aspect in the area of human performance because leaders failed to ensure that the bases for operational and organizational decisions were communicated during multiple instances where the leak in valve AC-898 could have been repaired. (H.10)
05000285/FIN-2015002-062015Q2Fort CalhounFailure to Identify and Correct Loose Incore Instrument Nozzle ConnectionThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure to identify and correct a condition adverse to quality. Specifically, maintenance personnel failed to document a loose connection on incore instrument port 44 in the corrective action program. As a result, the connection was not tightened and boric acid leaked onto the reactor vessel head during operation. This issue was entered into the licensees corrective action program as Condition Report 2015-05864. The failure of maintenance personnel to document a loose connection on incore instrument port 44 in the corrective action program was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the equipment performance attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 1, Initiating Events Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not result in exceeding the RCS leak rate for a small loss-of-coolant accident, and did not affect other systems used to mitigate a loss-of-coolant accident resulting in a total loss of their function. The inspectors determined that the finding had a field presence cross-cutting aspect in the area of human performance because the licensee did not ensure supervisory and management oversight of work activities, including contractors and supplemental personnel. (H.2)
05000285/FIN-2015002-072015Q2Fort CalhounFailure to Perform Functionality Assessments for the Spent Fuel Pool Cooling SystemThe inspectors identified a finding associated with the failure of operations personnel to follow procedures used to perform functionality assessments. Specifically, operations personnel failed to provide sufficient technical justification for the reasonable assurance of functionality of the spent fuel pool cooling system when boric acid leaks were identified on discharge header vent valve AC-898. Vent valve AC-898 was replaced and the issue was entered into the licensees corrective action program as Condition Report 2015-05856. The failure of operations personnel to follow station procedures to perform functionality assessments was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it adversely affected the design control attribute of the Barrier Integrity Cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 3, Barrier Integrity Screening Questions, the issue screened as having very low safety significance (Green) because the finding did not adversely affect decay heat removal capabilities from the spent fuel pool causing the pool temperature to exceed the maximum analyzed temperature limit specified in the site-specific licensing basis, did not result from fuel handling errors, dropped fuel assembly, dropped storage cask, or crane operations over the SFP that caused mechanical damage to fuel clad and a detectible release of radionuclides, did not result in a loss of spent fuel pool water inventory decreasing below the minimum analyzed level limit specified in the site-specific licensing basis, and did not affect the SFP neutron absorber, fuel bundle misplacement or soluble boron concentration. The inspectors determined that the finding had a training cross-cutting aspect in the area of human performance because the licensee did not provide training and ensure knowledge transfer to maintain a knowledgeable, technically competent workforce and instill nuclear safety values. (H.9)
05000285/FIN-2015002-082015Q2Fort CalhounFailure to Submit Summaries of the Impact of Changes to the Emergency Plan and Implementing ProceduresThe inspector identified a non-cited violation of 10 CFR 50.54(q)(5) for the licensees failure to submit reports of its analysis of the impact of changes to the emergency plan and implementing procedures on the emergency plan. Specifically, the inspector identified three examples between February 21 and June 18, 2015, of the licensee submitting changes to the emergency plan and implementing procedures without the required summaries. The issue was entered into the licensees corrective action program as Condition Report CR 2015-04934. The failure to submit a summary of the analysis of the effect of changes to emergency plan implementing procedures on the site emergency plan is a performance deficiency within the licensees ability to foresee and correct. The issue is more than minor because the licensees failure to submit the required summary affects the NRCs ability to perform its regulatory function, and the licensee has not incorporated this requirement into its program. The inspectors evaluated the issue using Section 6.6.d of the NRC Enforcement Policy, dated July 12, 2011, and determined it to be a Severity Level IV violation because the issue involved the licensees ability to implement a regulatory requirement not related to assessment or notification. Traditional enforcement violations are not assigned a crosscutting aspect.
05000285/FIN-2015002-092015Q2Fort CalhounFailure to Follow Instructions and Procedures Related to Snubber ActivitiesThe inspectors identified a non-cited violation of very low safety significance of 10 CFR Part 50, Appendix B, Criterion V Instructions, Procedures, and Drawings, because activities affecting quality were not accomplished in accordance with instructions and procedures established by the licensee. Specifically, the licensee failed to document a degraded condition associated with a safety related seismic snubber affecting the auxiliary feedwater system, did not notify operations of the degraded condition, and did not assess the risk of the inoperable snubber in accordance with licensee instructions and procedures. The licensee entered this violation into their corrective action program. Immediate actions taken to address this violation included a review of all other snubber inspections that were rejected to ensure that other degraded conditions were reported to the control room, a review of all planned snubber maintenance with respect to online risk, and the issuance of interim guidance to all Shift Managers on the subject of snubber operability and risk. The inspectors determined that the licensees failure to follow instructions and procedures associated with safety related snubbers was a performance deficiency. The finding is more than minor because if left uncorrected, the performance deficiency could have led to a more significant safety concern. Specifically, the failure to follow instructions and procedures associated with safety related snubbers could result in unacceptable risk configurations that are not analyzed under technical specifications and could challenge the reliability of safety related equipment during a seismic event. Using NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2 Mitigating System Screening Questions Part B, dated July 1, 2012, the inspectors determined the finding to be of very low safety significance (Green) since the finding did not result in the loss of equipment specifically designed to mitigate a seismic initiating event. The finding has a cross-cutting aspect in the area of Human Performance, the Work Management aspect, since the licensee did not implement a work process that ensured the identification and management of risk commensurate to the work. (H.5)
05000285/FIN-2016001-012016Q1Fort CalhounImplementing a Procedure Change for Alternative Shutdown Cooling that would have Required NRC ApprovalThe inspectors identified a Severity Level IV non-cited violation of 10 CFR 50.59, Changes, Tests, and Experiments, for the failure to recognize that a change to the facility as described in the Updated Safety Analysis Report would require prior NRC review and approval. Specifically, the 10 CFR 50.59 evaluation revised a site procedure, without NRC approval, to substitute automatic flow control of shutdown cooling flow and temperature with manual control using the low pressure safety injection loop injection valves. The licensees corrective actions included revising the affected procedure to reflect the original automatic flow control. The licensee entered this issue in the corrective action program as Condition Report 2013-15342. The licensees failure to implement the requirements of 10 CFR 50.59 and adequately evaluate changes to determine if prior NRC approval is required was a performance deficiency. Because this violation had the potential to impact the NRCs ability to perform its regulatory function, the inspectors evaluated the violation using traditional enforcement. In accordance with Section 2.1.3.E.6 of the NRC Enforcement Manual, the team evaluated this finding using the significance determination process to assess its significance. The inspectors performed an initial screening of the finding in accordance with NRC Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated July 1, 2012. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the finding was determined to have very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensees Maintenance Rule program. Therefore, in accordance with Section 6.1.d.2 of the NRC Enforcement Policy, the inspectors characterized this performance deficiency as a Severity Level IV violation. The inspectors determined that a cross-cutting aspect was not applicable because the issue involving the failure to perform an adequate 10 CFR 50.59 evaluation was strictly associated with a traditional enforcement violation.
05000285/FIN-2016001-022016Q1Fort CalhounLicensee-Identified ViolationTechnical Specification 2.6(1) requires containment integrity to be maintained unless the reactor is in a cold or refueling shutdown condition. If containment integrity is not maintained and the reactor does not meet these cold or refueling shutdown conditions, then containment integrity must be restored within one hour or the reactor is required to be in hot shutdown within the next six hours. From November 22, 2013, through June 27, 2014, a test connection cap was left off of a containment penetration which constituted a loss of containment integrity. Upon discovery of this condition on June 27, 2014, the licensee entered Technical Specification 2.6(1) and Abnormal Operating Procedure 12 for loss of containment integrity. The cap was re-installed and containment integrity was restored within one hour. The violation is more than minor because it is associated with the configuration control attribute of the Barrier Integrity Cornerstone. Failure to install the containment penetration cap following local leak rate testing on November 22, 2013, resulted in a loss of containment integrity until it was discovered missing on June 27, 2014. This adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (i.e., containment) protect the public from radionuclide releases caused by accidents or events. The violation was reviewed by a Senior Reactor Analyst and was determined to be of very low safety significance because the test connection fitting was a 14-inch diameter opening. Inspection Manual Chapter 0609, Significance Determination Process, Appendix H, identifies that small lines (less than 1 to 2 inches in diameter) would not generally contribute to large early release frequency. Therefore, this finding screens to Green. The licensee entered the issue into their corrective action program as Condition Report 2014-07958.
05000298/FIN-2011006-012011Q2CooperFailure to Promptly Identify and Correct Conditions Adverse to QualityThe inspectors identified a noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, associated with four examples of the licensees failure to promptly identify and correct conditions adverse to quality. Specifically, the licensee failed to identify and correct excessive setpoint drift of reactor core isolation cooling system pressure switches, the leak of oil from the service water booster pump, a vulnerability that allowed non-quality controlled material to be installed in safety related applications, and the cause of a failure of the high pressure coolant injection steam line high flow instrument. The licensee entered the finding into the corrective action program as Condition Reports 2011-07060, 2011-07105, 2011-07151, and 2011-06653. The performance deficiency was determined to be more than minor because if left uncorrected, the continued failure to promptly identify and correct conditions adverse to quality could result in more risk significant equipment being inoperable, and is therefore a finding. This finding affected the Mitigating Systems Cornerstone. Using Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the finding was determined to have very low safety significance because the finding: (1) was not a design or qualification issue confirmed not to result in a loss of operability or functionality; (2) did not represent an actual loss of safety function of the system or train; (3) did not result in the loss of one or more trains of nontechnical specification equipment; and (4) did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The finding was determined to have a crosscutting aspect in the area of problem identification and resolution, associated with the corrective action program component, in that, the licensee failed to implement a corrective action program with a low threshold for identifying issues; issues are identified completely, accurately and in a timely manner commensurate with their safety significance.
05000298/FIN-2011006-022011Q2CooperFailure to Report Conditions Prohibited by Technical Specifications and Safety System Functional FailuresThe inspectors identified a noncited violation of 10 CFR 50.73, Licensee Event Report System, associated with the licensees failure to submit a licensee event report within 60 days following discovery of an event meeting the reportability criteria as specified. Specifically, a condition prohibited by technical specifications occurred when a zurn strainer failure rendered the service water system inoperable for longer than the action statement and would have prevented fulfillment of a safety function. The licensee entered the finding into the corrective action program as Condition Report 2011-06778. The inspectors reviewed this issue in accordance with NRC Inspection Manual Chapter 0612 and the NRC Enforcement Manual. Through this review, the inspectors determined that traditional enforcement was applicable to this issue because the NRC\'s regulatory ability was affected. Specifically, the NRC relies on the licensees to identify and report conditions or events meeting the criteria specified in regulations in order to perform its regulatory function; and when this is not done, the regulatory function is impacted. The inspectors determined that this finding was not suitable for evaluation using the significance determination process, and as such, was evaluated in accordance with the NRC Enforcement Policy. The finding was a violation determined to be of very low safety significance, was not repetitive or willful, and was entered into the corrective action program. Therefore, this violation is being treated as a Severity Level IV noncited violation consistent with the NRC Enforcement Policy. This finding had a crosscutting aspect in the area of problem identification and resolution associated with the corrective action component, in that, the licensee failed to appropriately and thoroughly evaluate for reportability aspects all factors associated with the equipment failure.
05000298/FIN-2011006-032011Q2CooperFailure to Perform 10 CFR 50.59 Evaluation for Design ChangeThe inspectors identified a noncited violation of 10 CFR 50.59, Changes, Tests, and Experiments, associated with the failure to adequately evaluate a change in order to ensure that it did not require prior NRC approval. Specifically, the licensee revised a residual heat removal pump motor cable sizing calculation to a smaller sized cable without a change evaluation. The licensee entered the issue into the corrective action program as Condition Report 2011-01730. The finding was determined to be more than minor because the licensee failed to perform a 10 CFR 50.59 evaluation when required. Specifically, the NRC relies on licensees to identify and report conditions or events meeting the criteria specified in regulations in order to perform its regulatory function, and when this is not done the regulatory function is impacted, and is therefore more than minor. Violations of 10 CFR 50.59 are considered to impede or impact the regulatory process, so they are dispositioned using the traditional enforcement process. The enforcement manual specifies that the severity level is determined in parallel with the Significance Determination Process (SDP). The inspectors performed a Phase 1 screening in accordance with Manual Chapter 0609, Attachment 4, Phase 1 Initial Screening and Characterization of Findings, and determined that the finding was of very low safety significance (Green) because the finding: (1) was not a design or qualification issue confirmed not to result in a loss of operability or functionality; (2) did not represent an actual loss of safety function of the system or train; (3) did not result in the loss of one or more trains of nontechnical specification equipment; and (4) did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. Therefore, the inspectors categorized the finding as Severity Level IV in accordance with the enforcement manual. The finding was a violation determined to be of very low safety significance, was not repetitive or willful, and was entered into the corrective action program. Therefore, this violation is being treated as a noncited violation consistent with the NRC Enforcement Policy. The inspectors determined the cause of the finding through interviews and document reviews. This finding was determined to have a crosscutting aspect in the area of problem identification and resolution associated with the corrective action program in that the licensee failed to appropriately and thoroughly evaluate all factors associated with the design change.
05000298/FIN-2011006-042011Q2CooperFailure to Take Action for an Ineffective Corrective ActionThe inspectors identified a noncited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, for the failure to correct a condition adverse to quality. Specifically, the licensee determined that an interim corrective action to prevent recurrence was ineffective, yet it took no effective corrective action. As a result, the licensee was vulnerable to a repetitive condition adverse to quality. The licensee entered the issue into the corrective action program as Condition Report 2011-07152. The finding was determined to be more than minor because the performance deficiency could be reasonably viewed as a precursor to an event in that the interim action was not effective as a barrier to prevent recurrence of an event. The finding is associated with the Mitigating Systems Cornerstone. The inspectors performed a Phase 1 screening in accordance with Manual Chapter 0609, Attachment 4, Phase 1 Initial Screening and Characterization of Findings, and determined that the finding was of very low safety significance (Green) because the finding: (1) was not a design or qualification issue confirmed not to result in a loss of operability or functionality; (2) did not represent an actual loss of safety function of the system or train; (3) did not result in the loss of one or more trains of nontechnical specification equipment; and (4) did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The inspectors determined that this finding had a crosscutting aspect in the area of problem identification and resolution associated with corrective actions because the licensee failed to prioritize and thoroughly evaluate a condition report that documented an inadequate interim corrective action to prevent recurrence.
05000298/FIN-2011006-052011Q2CooperFailure to Correctly Translate Design Requirements into Installed Plant ConfigurationThe inspectors identified a cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, for the licensees failure to assure that the applicable design basis for applicable structures, systems, and components were correctly translated into specifications, procedures, and instructions. Specifically, the licensee failed to justify through evaluation that the diesel generator fuel oil day tanks would be available following a tornado missile strike on the tank vents. The violation was cited because the licensee failed to restore compliance in a reasonable time following documentation of the issue as a noncited violation in NRC Inspection Report 2010007 (issued December 3, 2010). The licensee entered this issue into the corrective action program as Condition Report 2011-06655. The performance deficiency was determined to be more than minor because it was associated with the protection against the external factors attribute of the Mitigating Systems Cornerstone, and affected the associated cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences, and is therefore a finding. Using Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the finding was determined to have very low safety significance because the finding: (1) was not a design or qualification issue confirmed not to result in a loss of operability or functionality; (2) did not represent an actual loss of safety function of the system or train; (3) did not result in the loss of one or more trains of nontechnical specification equipment; and (4) did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. The finding was determined to have a crosscutting aspect in the area of human performance, associated with the decision making component in that the licensee failed to use conservative assumptions in decision making and adopt a requirement to demonstrate that the proposed action is safe in order to proceed rather than a requirement to demonstrate it is unsafe in order to disapprove the action.
05000298/FIN-2017001-012017Q1CooperFailure to Maintain Alternate Shutdown Emergency ProcedureThe inspectors identified a non-cited violation of Technical Specification 5.4.1.a for the licensees failure to maintain Emergency Procedure 5.1ASD, Alternate Shutdown, Revision 17, for establishing reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit. Specifically, the licensee failed to maintain Emergency Procedure 5.1ASD with adequate instructions to place the reactor equipment cooling system north or south critical loop in service and verify reactor equipment system flow to the high pressure cooling injection system fan coil unit during some control room evacuation scenarios. The immediate corrective actions were to assess operability of the high pressure coolant injection system during control room evacuations that are not related to fire scenarios, and to revise Emergency Procedure 5.1ASD with instructions to open the criticalloop supply valves (REC-MOV-711 or REC-MOV-714) in the control room or locally, and verify reactor equipment system flow to the high pressure coolant injection fan coil unit. The licensee entered this deficiency into the corrective action program as Condition ReportCR-CNS-2017-01403. The licensees failure to maintain Emergency Procedure 5.1ASD to establish reactor equipment cooling system flow to the high pressure coolant injection fan coil unit during some control room evacuation scenarios, in violation of Technical Specification 5.4.1.a, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the procedural quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, the licensee did not provide instructions to establish reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit, which would have complicated operator response during a control room evacuation. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant nontechnical specification train. The finding had a cross-cutting aspect in the area of problem identification and resolution associated with identification. Specifically, the licensee failed to implement a corrective action program with a low threshold for identifying issues during the required annual review of emergency procedures (P.1).
05000298/FIN-2017001-022017Q1CooperFailure to Identify a Condition Adverse to Quality Associated with the 250 Vdc Electrical SystemThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to identify a condition adverse to quality associated with Station Procedure 2.2.24.1, 250 Vdc Electrical System (Div 1), Revision 14, in accordance with Station Procedure 0-CNS-LI-102, Corrective Action Process, Revision 6. Specifically, the licensee failed to identify that Station Procedure 2.2.24.1 contained inadequate instructions to ensure the oncoming charger 1C output voltage was matched with the bus 1A voltage when transferring bus 1A from charger 1A to charger 1C, so that technical specification bus voltage requirements would remain met. This resulted in an unexpected and initially unrecognized decline in voltage on the bus to below the required minimum of 260.4 Vdc. This condition required the licensee to declare the Division 1 250 Vdc electrical system and Division 1 residual heat removal low pressure coolant injection system inoperable. The immediate corrective action was to adjust the charger 1C float voltage greater than 260.4 Vdc to restore operability of the Division 1 250 Vdc electrical and residual heat removal low pressure coolant injection systems. The licensee entered this deficiency into the corrective action program as Condition Reports CR-CNS-2016-08658 and CR-CNS-2017-00750. The licensees failure to identify a condition adverse to quality associated with Station Procedure 2.2.24.1, to ensure technical specification bus voltage requirements were met, in violation of Station Procedure 0-CNS-LI-102, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the procedural quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, charger 1C, when in service, did not maintain battery 1A terminal voltage within the requirements of Surveillance Requirement 3.8.4.1, which required the licensee to declare the Division 1 250 Vdc electrical system and the Division 1 residual heat removal low pressure coolant injection system inoperable. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant, nontechnical specification train. The finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate the charger 1C float voltage issue to ensure that the resolution addressed the cause and extent of condition commensurate with the safety significance (P.2).
05000298/FIN-2017001-032017Q1CooperFailure to Identify a Condition Adverse to QualityThe inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to identify a condition adverse to quality for Division 1 residual heat removal service water booster pump A, in accordance with Station Procedure 0-CNS-LI-102, Corrective Action Process, Revision 6. Specifically, on January 5, 2017, the inspectors identified an oil level lower than normally expected, oil on the pump skid, and an oil droplet formed on the Division 1 residual heat removal service water booster pump A inboard bearing sight glass. The inspectors informed the control room of this condition, and the licensee determined the oil leakage from the pumps sight glass would have prevented the pump from operating for the required 30 days during a design basis accident. The immediate corrective action was to repair the Division 1 residual heat removal service water booster pump A inboard bearing sight glass, restoring operability of the pump. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2017-00054. The licensees failure to identify a condition adverse to quality for Division 1 residual heat removal service water booster pump A, in violation of Station Procedure 0-CNS-LI-102, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, the oil leakage from the service water booster pump A inboard bearing sight glass would have prevented the pump from operating for its required 30-day mission time during a design basis accident and resulted in the pump being declared inoperable. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety significant nontechnical specification train. The finding had a cross-cutting aspect in the area of human performance associated with challenge the unknown because the licensee failed to stop when faced with uncertain conditions and failed to ensure that risks are evaluated and managed before proceeding. Specifically, the licensee did not maintain a questioning attitude during job-site reviews to identify and resolve unexpected conditions, including lower than the expected oil level in the service water booster pump A inboard bearing sight glass, oil on the pump skid, and an oil droplet formed on the bottom of the sight glass (H.11).
05000298/FIN-2017001-042017Q1CooperFailure to Address Nonconforming Pipe Thinning in Accordance with the ASME CodeThe inspectors identified a non-cited violation of 10 CFR 50.55a(g)(4) for the licensees failure to use an approved method to disposition an American Society of Mechanical Engineers Code nonconforming condition in the residual heat removal service water system. Specifically, the licensee identified multiple locations with localized pipe thinning below the American Society of Mechanical Engineers Code B31.1 design minimum pipe-wall thickness during an ultrasonic examination but failed to use an approved method to calculate a new acceptable pipe-wall thickness. As a corrective action to restore compliance, the licensee replaced this section of piping on November 1, 2016, during Refueling Outage 29. The licensee entered this issue into the corrective action program as Condition Reports CR-CNS-2016-05558 and CR-CNS-2016-05963. The licensees failure to use an approved method to calculate a new minimum allowable pipe-wall thickness, in violation of 10 CFR 50.55a(g)(4), was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the design control attribute of the Mitigating System Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, calculating an allowable minimum pipe-wall thickness value that is below the American Society of Mechanical Engineers code design minimum value reduces the pipings structural integrity, potentially leading to the failure of the piping. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings AtPower, dated June 19, 2012, inspectors determined the finding screened as having very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant nontechnical specification train. This finding had a cross-cutting aspect in the area of human performance associated with design margins because the licensee failed to operate and maintain the residual heat removal service water system within the American Society of Mechanical Engineers code minimum pipe-wall thickness. Specifically, having identified that the affected pipe location was below the allowable pipe-wall thickness, the licensee opted to calculate and accept a new minimum pipe-wall thickness value that was not consistent with code requirements instead of repairing the affected piping at the time of discovery (H.6).
05000298/FIN-2017001-052017Q1CooperLoss of Shutdown Cooling due to Relay MaintenanceThe inspectors reviewed a self-revealed, non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to implement Maintenance Procedure 7.3.16, Low Voltage Relay Removal and Installation, Revision 22, for relay replacement work. Specifically, on October 28, 2016, the licensee failed to evaluate the potential impact of primary containment isolation system relay PCIS-REL-K27 work on shutdown cooling relay PCIS-REL-K30, which was mounted next to K27 and shared a common mounting rail. As a result, the licensee did not identify the potential of losing residual heat removal shutdown cooling, and while installing the K27 relay and snapping it into the mounting rail, workers caused a momentary actuation of relay K30 and a loss of residual heat removal shutdown cooling. Corrective actions to restore compliance included restoration of shutdown cooling, completion of the K27 relay maintenance with shutdown cooling out of service, and an outage risk management procedure change that prohibited work on or near shutdown cooling relays while the system was required to be in service. The licensee entered this deficiency into the corrective action program as Condition Report CR-CNS-2016-07645. The licensees failure to implement Maintenance Procedure 7.3.16, in violation of Technical Specification 5.4.1.a, was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Initiating Events Cornerstone and affected the associated cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown operations. Using Inspection Manual Chapter 0609, Appendix G, Attachment 1, Shutdown Operations Significance Process Phase 1 Initial Screening and Characterization of Findings, dated May 9, 2014, the inspectors determined that the finding did not require a quantitative assessment because the event occurred when the refuel canal/cavity was flooded. Therefore, the finding screened as very low safety significance (Green). The finding had a cross-cutting aspect in the area of human performance associated with work management, because the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the need for coordination with different work groups or job activities. Specifically, the licensee failed to control, execute, and coordinate safety-related primary containment isolation system relay work activities to ensure residual heat removal shutdown cooling was not adversely impacted (H.5).