05000298/FIN-2017001-01
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Finding | |
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Title | Failure to Maintain Alternate Shutdown Emergency Procedure |
Description | The inspectors identified a non-cited violation of Technical Specification 5.4.1.a for the licensees failure to maintain Emergency Procedure 5.1ASD, Alternate Shutdown, Revision 17, for establishing reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit. Specifically, the licensee failed to maintain Emergency Procedure 5.1ASD with adequate instructions to place the reactor equipment cooling system north or south critical loop in service and verify reactor equipment system flow to the high pressure cooling injection system fan coil unit during some control room evacuation scenarios. The immediate corrective actions were to assess operability of the high pressure coolant injection system during control room evacuations that are not related to fire scenarios, and to revise Emergency Procedure 5.1ASD with instructions to open the criticalloop supply valves (REC-MOV-711 or REC-MOV-714) in the control room or locally, and verify reactor equipment system flow to the high pressure coolant injection fan coil unit. The licensee entered this deficiency into the corrective action program as Condition ReportCR-CNS-2017-01403. The licensees failure to maintain Emergency Procedure 5.1ASD to establish reactor equipment cooling system flow to the high pressure coolant injection fan coil unit during some control room evacuation scenarios, in violation of Technical Specification 5.4.1.a, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the procedural quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events. Specifically, the licensee did not provide instructions to establish reactor equipment cooling system flow to the high pressure coolant injection system fan coil unit, which would have complicated operator response during a control room evacuation. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it: was not a design deficiency; did not represent a loss of system and/or function; did not represent an actual loss of function; did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and did not result in the loss of a high safety-significant nontechnical specification train. The finding had a cross-cutting aspect in the area of problem identification and resolution associated with identification. Specifically, the licensee failed to implement a corrective action program with a low threshold for identifying issues during the required annual review of emergency procedures [P.1]. |
Site: | Cooper |
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Report | IR 05000298/2017001 Section 1R04 |
Date counted | Mar 31, 2017 (2017Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.04 |
Inspectors (proximate) | C Henderson E Uribe G Warnick I Anchondo J Watkins P Elkmann P Voss R Deese |
Violation of: | Technical Specification |
CCA | P.1, Identification |
INPO aspect | PI.1 |
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Finding - Cooper - IR 05000298/2017001 | |||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Cooper) @ 2017Q1
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