Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARNRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr1994-04-25025 April 1994 LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr NRC-93-0058, LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr1993-06-18018 June 1993 LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr1993-05-20020 May 1993 LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr NRC-91-0058, LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr1991-05-24024 May 1991 LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr NRC-91-0069, LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr1991-05-24024 May 1991 LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr NRC-91-0055, LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr1991-05-10010 May 1991 LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr NRC-91-0004, LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr1991-01-28028 January 1991 LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr NRC-90-0144, LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr1990-09-28028 September 1990 LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr NRC-90-0107, LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr1990-06-22022 June 1990 LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr NRC-90-0087, LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr1990-06-0808 June 1990 LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr NRC-90-0075, LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr1990-05-18018 May 1990 LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr NRC-90-0073, LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr1990-05-0808 May 1990 LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr NRC-90-0048, LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr1990-03-22022 March 1990 LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr NRC-90-0027, LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr1990-02-21021 February 1990 LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr NRC-90-0021, LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr1990-02-0707 February 1990 LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr NRC-90-0019, LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr1990-01-31031 January 1990 LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr NRC-90-0018, LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr1990-01-25025 January 1990 LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr NRC-90-0008, LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr1990-01-19019 January 1990 LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr NRC-90-0007, LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr1990-01-17017 January 1990 LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr ML19354E0971990-01-12012 January 1990 LER 89-038-00:on 891223,reactor Scrammed When Fire Occurred in Vicinity of High Pressure Turbine.Caused by Oil Soaked Inlagging Pads & Ignited When Turbine Casing Heated Up to Oil Flashpoint.Insulation Pads replaced.W/900122 Ltr NRC-90-0005, LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr1990-01-11011 January 1990 LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr NRC-90-0004, LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr1990-01-0909 January 1990 LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr NRC-90-0002, LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr1990-01-0808 January 1990 LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr NRC-90-0003, LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr1990-01-0808 January 1990 LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr NRC-89-0261, LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr1989-12-28028 December 1989 LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr NRC-89-0260, LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr1989-12-21021 December 1989 LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr NRC-89-0255, LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr1989-12-20020 December 1989 LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr NRC-89-0259, LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr1989-12-15015 December 1989 LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr NRC-89-0256, LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr1989-12-15015 December 1989 LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr NRC-89-0258, LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr1989-12-15015 December 1989 LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr NRC-89-0251, LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr1989-11-30030 November 1989 LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr NRC-89-0249, LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr1989-11-22022 November 1989 LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr NRC-89-0246, LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr1989-11-20020 November 1989 LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr NRC-89-0244, LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr1989-11-20020 November 1989 LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr NRC-89-0194, LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr1989-11-14014 November 1989 LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr NRC-89-0193, LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr1989-11-0909 November 1989 LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr NRC-89-0192, LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr1989-11-0606 November 1989 LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr NRC-89-0190, LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr1989-10-24024 October 1989 LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr NRC-89-0189, LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr1989-10-23023 October 1989 LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr NRC-89-0186, LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr1989-10-0606 October 1989 LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr NRC-89-0185, LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr1989-10-0606 October 1989 LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr 1994-04-25
[Table view] Category:RO)
MONTHYEARNRC-94-0025, LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr1994-04-25025 April 1994 LER 93-014-01:on 931225,turbine Generator Tripped When Mechanical Overspeed Device Was Activated.Caused by Severe Vibration.Corrective Action:Assessment of Structural Integrity of Pedestal Was conducted.W/940425 Ltr NRC-93-0058, LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr1993-06-18018 June 1993 LER 93-008-00:on 930518,discovered That Recorder T50-R802A Could Not Be Considered Operable Per TS 3.3.7.5.Caused by Personnel Error.Lessons Learned Will Be Incorporated Into Training Programs & Plant procedures.W/930618 Ltr NRC-93-0055, LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr1993-05-20020 May 1993 LER 93-007-00:on 930420,reactor Tripped on Intermediate Range Monitor Upscale During Reactor Pressure & Feedwater Transient.Caused by Personnel Error.Affected Pressure Transmitters replaced.W/930520 Ltr NRC-91-0058, LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr1991-05-24024 May 1991 LER 91-008-00:on 910424,reactor Bldg HVAC Tripped,Div I SGTS Auto Started & Div I Control Ctr HVAC Shifted to Recirculation Mode Due to Mispositioned Trip Output Logic switch.W/910524 Ltr NRC-91-0069, LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr1991-05-24024 May 1991 LER 90-012-01:on 901016,HPIC Steam Line Flow Transmitter Failed Due to Short Circuit Across Capacitor Plates.Circuit Boards Replaced & Failure Analysis Performed by Rosemount,Inc.W/910524 Ltr NRC-91-0055, LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr1991-05-10010 May 1991 LER 91-006-00:on 910410,balance of Plant Breaker Opened Causing Reactor Bldg HVAC Isolation.Caused by Component Failures.Nprds Search Conducted for Similiar Problems. W/910510 Ltr NRC-91-0004, LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr1991-01-28028 January 1991 LER 90-013-00:on 901228,determined That Inadequate Control Could Occur During Air Grab Sampling Process.Caused by Lack of Proper Administrative Controls in Sampling Procedure. Sample Suction added.W/910128 Ltr NRC-90-0144, LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr1990-09-28028 September 1990 LER 90-007-00:on 900829,control Ctr Ventilation Shifted to Recirculation Due to Blown Fuse.Caused by Design Deficiency in Div 1 & 2 Radiation Monitor Trip Circuitry.Design Change Implemented to Eliminate Trip Relay logic.W/900928 Ltr NRC-90-0107, LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr1990-06-22022 June 1990 LER 88-034-01:on 880831,RWCU Outboard Isolation Valve Closed,Causing RWCU Pumps to Trip.Caused by Loss of Continuity to Relay Due to Deposits Built Up on Surface of Contacts.Relay in Isolation Circuits replaced.W/900622 Ltr NRC-90-0087, LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr1990-06-0808 June 1990 LER 90-002-01:on 900202,determined That Area Radiation Surveillance Procedure 44.080.301 Listed Incorrect Values for Alarm Setpoints.Caused by Unavailable Setpoint Calculations.Procedure revised.W/900608 Ltr NRC-90-0075, LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr1990-05-18018 May 1990 LER 87-045-02:on 870908,operator Removed Fuse Which Deenergized Dc Control Power to Bus 72C,resulting in Loss of Power Supply to Swing Bus & to LPCI Loop Selection Valves. Caused by Design Flaw.Design Change initiated.W/900518 Ltr NRC-90-0073, LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr1990-05-0808 May 1990 LER 90-003-00:on 900410,Div I Reactor Protection Sys Power Supply Failure & Subsequent MSIV Closure.Caused by Coil Burn Up.Relays Replaced & MG Sets Returned to svc.W/900508 Ltr NRC-90-0048, LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr1990-03-22022 March 1990 LER 89-037-01:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed Prior to Expiration on 891125. Caused by Personnel Error.Procedure revised.W/900322 Ltr NRC-90-0027, LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr1990-02-21021 February 1990 LER 89-034-01:on 891208,two Members of Fire Watch Did Not Complete Assigned Hourly Rounds from 891002-1207 in Reactor & Auxiliary Bldgs.Both Individuals Terminated & Fire Stations Equipped W/Unique Bar code.W/900221 Ltr NRC-90-0021, LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr1990-02-0707 February 1990 LER 90-001-00:on 900108,annunciator 2D5 Alarmed for Div II ECCS Testability Logic/Power Failure.Caused by Blown Fuse. Fuse Installed During Course of Troubleshooting W/No Subsequent Problems noted.W/900207 Ltr NRC-90-0019, LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr1990-01-31031 January 1990 LER 89-028-01:on 891028,eight Safety Relief Valves Failed Set Pressure Tolerance Test.Cause Under Review by Util & Generically by BWR Owners Group Safety Relief Valve Set Point Drift Committee.Valves Removed & cleaned.W/900131 Ltr NRC-90-0018, LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr1990-01-25025 January 1990 LER 89-039-00:on 891226,Div I Emergency Equipment Cooling Water & Svc Water Sys Automatically Started Due to Partial Load Shed of Bus 72E.Caused by Personnel Error. Accountability Meeting Held on 900117.W/900125 Ltr NRC-90-0008, LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr1990-01-19019 January 1990 LER 89-037-00:on 891220,determined That Tech Spec Stroke Time Testing for Outboard Reactor Water Sample Line Isolation Valve Not Performed.Caused by Personnel Error. Critique of Event Being developed.W/900119 Ltr NRC-90-0007, LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr1990-01-17017 January 1990 LER 89-036-00:on 891218,control Room Operator Inadvertently Depressed Closed Push Buttons on Inboard MSIVs A,B & C & Reactor Scram Resulted.Caused by Operator Error.Operator Involved Was Removed from Licensed duties.W/900117 Ltr ML19354E0971990-01-12012 January 1990 LER 89-038-00:on 891223,reactor Scrammed When Fire Occurred in Vicinity of High Pressure Turbine.Caused by Oil Soaked Inlagging Pads & Ignited When Turbine Casing Heated Up to Oil Flashpoint.Insulation Pads replaced.W/900122 Ltr NRC-90-0005, LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr1990-01-11011 January 1990 LER 89-035-00:on 891210,steam Jet Air Ejectors Placed in Svc W/O Required Surveillance Completed & Required Grab Sample Not Started Until 891213.Caused by Personnel Error.Off Gas Sys Operating Procedure Will Be revised.W/900111 Ltr NRC-90-0004, LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr1990-01-0909 January 1990 LER 89-030-00:on 891026,Channel C Level 1 & 2 Replacement Transmitter Found to Be Installed Incorrectly & Condition Recognized on 891210,when Level 2 Trip Unit Was Reading Upscale.Caused by Personnel error.W/900109 Ltr NRC-90-0002, LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr1990-01-0808 January 1990 LER 89-033-00:on 891207,volt-ohm Meter Connected to Incorrect Terminal,Causing Div II of Emergency Equipment Cooling Water Sys to Actuate.Caused by Personnel Error.Sys Secured & Channel Test Successfully completed.W/900108 Ltr NRC-90-0003, LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr1990-01-0808 January 1990 LER 89-034-00:on 891208,review of Key Card Transactions Showed That Fire Watch Personnel Missed Assigned Hourly Fire Watch from 891020-1207.Fire Watch Person Discharged.Plan Re Improvement of Fire Watches developed.W/900108 Ltr NRC-89-0261, LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr1989-12-28028 December 1989 LER 89-028-00:on 891129,ESF Actuations Occurred During Set Up for Surveillance.Caused by Blown Fuse.Blown Fuse Replaced & Affected Sys Returned to Normal Operation Following Completion of surveillance.W/891228 Ltr NRC-89-0260, LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr1989-12-21021 December 1989 LER 89-021-01:on 890906,35 of 237 Containment Isolation Valves Exceeded Administrative Allowable Leakage Rate When Tested.Caused by Normal Wear & Degradation During Specified Time Interval.Valves Cleaned & repaired.W/891221 Ltr NRC-89-0255, LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr1989-12-20020 December 1989 LER 89-031-00:on 891120,both Div II Emergency Equipment Cooling Water (EECW) & Emergency Equipment Svc Water Sys Pumps Tripped Immediately.Caused by Inadequacies in Stated Procedures.Procedures revised.W/891220 Ltr NRC-89-0259, LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr1989-12-15015 December 1989 LER 89-017-01:on 890810,new Analysis of Feedwater Line Break Scenario Assumes Failure of Feedwater Startup Control Valve in Open Position.Review of Pipe Break Documentation Conducted.Updated FSAR Change to Be submitted.W/891215 Ltr NRC-89-0256, LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr1989-12-15015 December 1989 LER 89-022-01:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse C71A-F15B Blew.On 890928, Reactor Bldg HVAC Isolated.Caused by Personnel Error. Procedures Will Be revised.W/891215 Ltr NRC-89-0258, LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr1989-12-15015 December 1989 LER 89-025-00:on 891115,low Level 2 Signal Unintentionally Induced During Reactor Pressure Vessel Hydrostatic Pressure Test.Caused by Personnel Error.Personnel Counseled on Notifying & Coordinating Instrument lineups.W/891215 Ltr NRC-89-0251, LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr1989-11-30030 November 1989 LER 89-019-01:on 890819,discovered That Div I Recirculation Fan Not Rotating Which Resulted in Decrease in Control Room Air Pressure.Caused by Lack of Lubrication in Bearings. Lubrication Program Improvements evaluated.W/891130 Ltr NRC-89-0249, LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr1989-11-22022 November 1989 LER 89-029-00:on 891023,half Scram Signal Received When Power Was Lost on Reactor Protection Sys Bus B,Resulting in Several ESFs Actuation.Caused by Location of Breaker Operating Switch in High Traffic area.W/891122 Ltr NRC-89-0246, LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr1989-11-20020 November 1989 LER 89-028-00:on 891020,eight safety-related Valves Failed Set Pressure Test.Cause Under Review.All Valves Removed for Testing Being Refurbished,Cleaned,Retested & Recertified to Be within Plant Accepted tolerances.W/891120 Ltr NRC-89-0244, LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr1989-11-20020 November 1989 LER 89-024-00:on 891019,recognized That Secondary Containment Dampers Not Tested as Required by Tech Spec 3.6.5.2.Caused by Operations Personnel Error.Event Critique to Be Included in Required Reading program.W/891120 Ltr NRC-89-0194, LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr1989-11-14014 November 1989 LER 89-027-00:on 891015,reactor Bldg Hvac,Control Ctr HVAC & Drywell Floor & Equipment Drain Sumps Isolated & Standby Gas Treatment Sys & Noninterrruptalbe Control Air Compressors Started.Caused by Personnel error.W/891114 Ltr NRC-89-0193, LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr1989-11-0909 November 1989 LER 89-026-00:on 891010,control Ctr HVAC Shifted to Recirculation Mode of Operaton Due to Short Circuit.Caused by Failure of Lamp Filament When Being Tightened.Fuse & Lamp Replaced & Sys Returned to Normal operation.W/891109 Ltr NRC-89-0192, LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr1989-11-0606 November 1989 LER 87-045-01:on 870908,fuse Removed Which Deenergized Dc Control Power to Bus 72C & Resulted in Loss of Power Supply to Swing Bus & LPCI Loop Selection Valves.Caused by Design Error.Undervoltage Relay Added & Training held.W/891106 Ltr NRC-89-0190, LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr1989-10-24024 October 1989 LER 89-023-00:on 890924,personnel Inadvertently Caused Trip of Essential Safety Sys Buses 64B & 64C.Caused by Failure of Personnel Involved to Review Applicable Prints Prior to Performing Test.Event Reviewed w/personnel.W/891024 Ltr NRC-89-0189, LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr1989-10-23023 October 1989 LER 89-022-00:on 890923 & 24,reactor Protection Sys Logic Actuations Occurred When Fuse Blew.On 890928,reactor Bldg HVAC Isolated When Jumper Lifted Per Incorrect Work Plan Instruction.Caused by Personnel error.W/891023 Ltr NRC-89-0186, LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr1989-10-0606 October 1989 LER 89-016-01:on 890711,Div 1 of RHR Svc Water Sys Declared Inoperable Due to Low Nitrogen Pressure for Cooling Tower Fan Brake.Caused by Leak in One Hose.Leaking Hose Replaced & Nitrogen Pressure restored.W/891006 Ltr NRC-89-0185, LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr1989-10-0606 October 1989 LER 89-021-00:on 890906,local Leak Rate Testing of Containment Isolation Valves & Penetrations Exceeded Tech Spec Limit.Caused by Excessive Containment Isolation Valve Leakage Due to Degradation of valve.W/891006 Ltr 1994-04-25
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N4381999-10-25025 October 1999 Safety Evaluation Supporting Amend 17 to License DPR-9 ML20217P3551999-10-22022 October 1999 LER 99-S01-00:on 990922,loaded 9mm Handgun Was Discovered on Truck Cargo Area of Vehicle Inside Protected Area.Caused by Inadequate Vehicle Search.Guidance in Procedures & Security Training to Address Multiple Vehicle Searches Was Provided NRC-99-0095, Monthly Operating Rept for Sept 1999 for Fermi 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Fermi 2.With NRC-99-0067, Monthly Operating Rept for Aug 1999 for Fermi 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Fermi 2.With NRC-99-0065, Monthly Operating Rept for July 1999 for Fermi 2.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Fermi 2.With NRC-99-0088, Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with1999-06-30030 June 1999 Detroit Edison Co Enrico Fermi Atomic Power Plant,Unit 1 Annual Rept for Period 980701-990630. with NRC-99-0064, Monthly Operating Rept for June 1999 for Fermi 2.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Fermi 2.With NRC-99-0062, Monthly Operating Rept for May 1999 for Fermi 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Fermi 2.With ML20206J9301999-05-10010 May 1999 SER Concluding That Util Adequately Addressed Actions Requested in GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Powered-Operated Gate Valves ML20206G5081999-05-0505 May 1999 Safety Evaluation Approving Request for Relief PR-8,Rev 2 on Basis That Licensee Committed to Meet All Related Requirements of ASME OM-6 Std & PR-12 on Basis That Proposed Alternative Will Provide Acceptable Level of Safety NRC-99-0022, Monthly Operating Rept for Apr 1999 for Fermi 2.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Fermi 2.With ML20205Q7141999-04-15015 April 1999 Safety Evaluation Supporting Amend 16 to License DPR-9 ML20205P9721999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Fermi 2 ML20204E0371999-03-17017 March 1999 Safety Evaluation Accepting Licensee Request for NRC Approval of Alternative Rv Weld Exam,Per Provisions of 10CFR50.55a(a)(3)(i) & 10CFR50.55a(g)(6)(ii)(A)(5) for Plant,Unit 2 for 40-month Period ML20204D0361999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Fermi 2 ML20198S3341999-01-0606 January 1999 Safety Evaluation Supporting Amend 15 to License DPR-9 NRC-99-0005, Monthly Operating Rept for Dec 1998 for Fermi 2.With1998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Fermi 2.With ML20207B7491998-12-31031 December 1998 1998 Annual Operating Rept for Fermi 2 ML20205Q9621998-12-31031 December 1998 Revised Monthly Operating Rept for Dec 1998 for Fermi 2 NRC-99-0021, 1998 Annual Financial Rept for Detroit Edison Co. with1998-12-31031 December 1998 1998 Annual Financial Rept for Detroit Edison Co. with NRC-98-0153, Monthly Operating Rept for Nov 1998 for Fermi 2.With1998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Fermi 2.With NRC-98-0160, Monthly Operating Rept for Oct 1998 for Fermi 2.With1998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Fermi 2.With ML20154R2331998-10-21021 October 1998 Safety Evaluation Supporting Amend 13 to License DPR-9 ML20154L1031998-10-14014 October 1998 Safety Evaluation Accepting Licensee Response to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode NRC-98-0139, Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With1998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Fermi,Unit 2.With ML20154H8161998-09-30030 September 1998 Rev 0 to COLR Cycle 7 for Fermi 2 ML20153B8811998-09-18018 September 1998 Safety Evaluation Accepting Request for Relief from Certain Requirements of ASME Boiler & Pressure Vessel Code,Section Xi,For Plant,Unit 2 ML20151X0651998-09-11011 September 1998 Safety Evaluation Re Inservice Testing Program Relief Request VR-63 for Plant NRC-98-0111, Monthly Operating Rept for Aug 1998 for Fermi 2.With1998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Fermi 2.With ML20153B7921998-08-31031 August 1998 Rev 0 to Fermi 1 Sar ML20237E1171998-08-25025 August 1998 Safety Evaluation Accepting Licensee Relief Requests for First 10-yr Interval Inservice Insp Nondestructive Exam Program ML20236X8611998-08-0505 August 1998 SER Related to Revised Feedwater Nozzle Analysis to Facility Operating License NPF-43,Enrico Fermi Nuclear Power Plant, Unit 2 NRC-98-0109, Monthly Operating Rept for July 1998 for Fermi 21998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Fermi 2 ML20236K3261998-07-0101 July 1998 SER Accepting Licensee Response Related to Revised Feedwater Nozzle Analysis to License NPF-43 for Enrico Fermi Nuclear Power Plant,Unit 2 NRC-98-0097, Monthly Operating Rept for June 1998 for Fermi,Unit 21998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Fermi,Unit 2 NRC-98-0127, Annual Rept for Period 970701-9806301998-06-30030 June 1998 Annual Rept for Period 970701-980630 NRC-98-0079, Monthly Operating Rept for May 1998 for Fermi 21998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Fermi 2 NRC-98-0076, Monthly Operating Rept for Apr 1998 for Fermi 21998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Fermi 2 NRC-98-0072, Monthly Operating Rept for Mar 1998 for Fermi 21998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Fermi 2 NRC-98-0050, Monthly Operating Rept for Feb 1998 for Fermi 21998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Fermi 2 NRC-98-0019, Monthly Operating Rept for Jan 1998 for Fermi 21998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Fermi 2 ML20198L4241998-01-0808 January 1998 Safety Evaluation Accepting Proposed Rev 2 to Relief Request VR-51 Under Fermi 2 Pump & Valve Inservice Testing Program Per 10CFR50.55a(f)(6)(i) for First 10-yr Interval NRC-98-0015, Monthly Operating Rept for Dec 1997 for Fermi 21997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Fermi 2 ML20217N3821997-12-31031 December 1997 Annual Operating Rept for 970101-1231 NRC-98-0053, 1997 Annual Financial Rept for Detroit Edison Company1997-12-31031 December 1997 1997 Annual Financial Rept for Detroit Edison Company ML20205Q9601997-12-31031 December 1997 Revised Monthly Operating Rept for Dec 1997 for Fermi 2 NRC-97-0141, Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility1997-12-23023 December 1997 Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility ML20197A9921997-12-15015 December 1997 Rev 0 to Efp,Unit 1 Fermi 1 Sar NRC-97-0131, Monthly Operating Rept for Nov 1997 for Fermi 21997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Fermi 2 ML20248H1151997-10-31031 October 1997 Rev 1 to Colr,Cycle 6 for Fermi 2 1999-09-30
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