ML072210843
ML072210843 | |
Person / Time | |
---|---|
Site: | Davis Besse |
Issue date: | 08/07/2007 |
From: | Caldwell J L Region 3 Administrator |
To: | Reyes L A NRC/EDO |
References | |
Download: ML072210843 (5) | |
Text
August 2, 2007MEMORANDUM TO:Luis A. ReyesExecutive Director for OperationsTHRU: James E. Dyer, Director/RA/Office of Nuclear Reactor RegulationFROM: James L. Caldwell/RA/Regional Administrator
SUBJECT:
REQUEST FOR RENEWAL OF DEVIATION TO THE REACTOROVERSIGHT PROCESS ACTION MATRIX FOR DAVIS-BESSE NUCLEAR POWER STATIONThis memorandum requests your approval to deviate from the Reactor Oversight Process(ROP) Action Matrix for the Davis-Besse Nuclear Power Station in order to continue heightened Nuclear Regulatory Commission (NRC) oversight for the time period of August 2007 through July 2009. This action is necessary to continue to monitor the licensee's efforts to sustain improved plant performance following resolution of the long-standing underlying problems that culminated in a Red finding associated with the severe wastage that was discovered on the reactor vessel head. Davis-Besse was placed under the IMC 0350 process for about three years. After the Oversight Panel's recommendation, and in consultation with the Director of NRR and the Deputy Executive Director for Reactor Programs, I authorized Davis-Besse's return to the ROP on July 1, 2005. In anticipation of the plant's transition from the IMC 0350 process, a deviation from the ROP was authorized on May 16, 2005, for the period of July 2005 through June 2006, and again on August 17, 2006, for the period of August 2006 through July 2007. The actions we propose in this memorandum are planned for Davis-Besse for the time period ofAugust 2007 through July 2009. This approach is consistent with our previously approved ROP deviation memoranda and the underlying concept of IMC 0305, in which the NRC, through its assessment process, has recognized that long-standing performance issues at a plant may require a more tailored, plant-specific followup over an extended period of time.CONTACT:Bruce Burgess, DRP(630) 829-9629 L. Reyes-2-BackgroundThe Davis-Besse facility entered the IMC 0350 Oversight Process as a result of the issues thatled to the wastage of the reactor vessel head, which was discovered during the 2002 refueling outage. In particular, significant programmatic concerns in the areas of Operations, Engineering, Corrective Action, and Safety Culture/Safety Conscious Work Environment (SCWE) were identified through NRC inspections that were conducted after the wastage was discovered on the reactor vessel head.To address the programmatic issues that resulted in the reactor head degradation, and priorto restart of the facility, the licensee submitted its "Integrated Report to Support Restart of the Davis-Besse Nuclear Power Station and Request for Restart Approval." This report documented specific corrective actions that were implemented and commitments for actions targeting sustained performance improvement at Davis-Besse. Prior to granting restart authority to the licensee, the NRC performed special inspection activities that were sufficiently comprehensive to be in excess of that required by IP 95002 and IP 95003.The NRC concluded that the licensee had taken sufficient actions to correct the deficienciesthat led to the Red finding. To ensure that the licensee had implemented lasting corrective actions and was able to sustain safe performance at Davis-Besse following restart, the NRC determined that a Confirmatory Order was necessary to modify their license to require annual independent assessments for five years in the areas of Operations, Engineering, Corrective Action, and Safety Culture/SCWE. The licensee previously completed the first and second set of independent assessmentsrequired through our Confirmatory Order during calendar year (CY) 2004 and 2005. During CY 2004 through CY 2006, inspectors evaluated the results of these independent assessments through previously approved deviation from the ROP and determined that these assessments were adequately conducted to satisfy the requirements of the Order. The licensee has also completed the third set of independent assessments for CY 2006required through our Confirmatory Order. During CY 2006 and to date in CY 2007, inspectors have evaluated the results of these assessments and determined that they were adequately conducted to satisfy the requirements of the Order. The licensee has recently started to perform the fourth set of independent assessmentsfor CY 2007. These assessments are scheduled to be completed between June and November 2007; the results of which are planned to be submitted to the NRC between August 2007 and January 2008. The current deviation from the ROP to review these independent self-assessment activities expires on July 31, 2007. A renewal of the ROP deviation is required to continue our independent self-assessment review effort for the final two sets of annual assessments. This effort will include a review the CY 2007 and CY 2008 assessment results in the Operations, Engineering, Corrective Action, and Safety Culture/SCWE areas.
L. Reyes-3-Deviation BasisWhen Davis-Besse exited the IMC 0350 process, it was placed in the Regulatory Responsecolumn of the Action Matrix based on one White finding in the Emergency Preparedness cornerstone. On January 1, 2006, Davis-Besse transitioned into the Licensee Response column of the Action Matrix and has remained in the Licensee Response column since.
Although performance at Davis-Besse indicates that improvements have been realized, Region III believes that Davis-Besse continues to warrant NRC inspection beyond that whichis prescribed by the ROP baseline inspection program to ensure compliance with the Order. In the case of Davis-Besse, the March 8, 2004, Confirmatory Order required, in part, thatFirstEnergy Nuclear Operating Company (FENOC) contract with external organizations to conduct comprehensive performance assessments in the areas of Operations, Engineering, Corrective Action, and Safety Culture/SCWE. The NRC required these additional measures to provide reasonable assurance that long-term corrective actions remain effective for those conditions that resulted in the risk-significant performance deficiencies that occurred at Davis-Besse. These independent assessments provide important confirmation of the effectiveness of the licensee's self-assessments and long-term improvement actions.
Therefore, Region III believes that to adequately evaluate these independent assessmentactivities, some continued inspection beyond that which is prescribed by the ROP baseline inspection program for the period of August 2007 through July 2009 is appropriate. The estimated additional inspection resources required to perform these inspections in the areas of Operations, Engineering, and Corrective Action, is about 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of direct inspection per area, per year for the next 2 years; and 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br /> of direct inspection for the Safety Culture/SCWE area per year, for the next 2 years. The results of these inspections will be documented in the Davis-Besse quarterly integrated inspection reports. Deviation RequestDavis-Besse is currently categorized within the Licensee Response column of the ActionMatrix. Region III requests your approval to deviate from the Action Matrix for the period ofAugust 2007 through July 2009 to perform additional inspections beyond that prescribed by the ROP baseline inspection program to evaluate the independent assessments conducted in the four areas described in our March 8, 2004, Confirmatory Order. These four areas are Operations, Engineering, Corrective Action, and Safety Culture/SCWE. Inspection activities associated with the review of each independent assessment would be similar to those approved through the previous ROP deviation memoranda and would include: 1) a review of each independent assessment plan prior to each assessment; 2) an evaluation of in-process assessment activities; and 3) a review of each final independent assessment report and associated action plans to resolve any areas for improvement as detailed in the reports. The additional inspection resources required to perform these inspections is estimated to be about 40 direct inspection hours per area, per year, for the Operations, Engineering, and Corrective Action Program areas, for the next 2 years; and 80 direct inspection hours for the Safety Culture/SCWE area, per year, for the next 2 years, for a total of approximately 400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br />.
These inspections will continue to be performed under IP 95003.
L. Reyes-4-This request for 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> of direct inspection for each of the final two CY assessment setsrepresents a reduction of 50 inspection hours from the 250 hours0.00289 days <br />0.0694 hours <br />4.133598e-4 weeks <br />9.5125e-5 months <br /> that was approved in the previous ROP deviation request for the review of the CY 2006 assessment set. Additionally, this request represents a reduction of two-thirds from the 600 hours0.00694 days <br />0.167 hours <br />9.920635e-4 weeks <br />2.283e-4 months <br /> that was approved for the review of the CY 2005 assessment set. We are seeking your approval of this ROP deviation to perform assessments of the licensee's final two required sets of annual independent
assessments.Inspection Manual Chapter 0305, Section 06.06.h, recognizes that for a period of up toone year after a plant has exited the IMC 0350 process, the regional offices may utilize some actions that are consistent with the Degraded Cornerstone or Multiple/Repetitive Degraded Cornerstone column of the Action Matrix to ensure the appropriate level of oversight of licensee improvement initiatives. There are no provisions in IMC 0305 for additional inspection resources for facilities that have exited the IMC 0350 process after one year. Region III requests a Reactor Oversight Process Action Matrix Deviation to conduct the additional inspections as described above.Approval: /RA by William F. Kane Acting for/
Date: 08/07/07 Luis A. Reyes Executive Director for Operationscc:J. Wiggins, NRRB. Boger, NRR T. Reis, NRR C. Haney, NRR M. Case, NRR S. Richards, NRR J. Anderson, NRR R. Gibbs, NRR T. Wengert, NRR M. Satorius, DRA, RIII C. Pederson, DRP, RIII A. Boland, DRS, RIII J. Rutkowski, SRI, RIII August 2, 2007MEMORANDUM TO:Luis A. ReyesExecutive Director for OperationsTHRU: James E. Dyer, Director/RA/Office of Nuclear Reactor RegulationFROM: James L. Caldwell/RA/Regional Administrator
SUBJECT:
REQUEST FOR RENEWAL OF DEVIATION TO THE REACTOROVERSIGHT PROCESS ACTION MATRIX FOR DAVIS-BESSE NUCLEAR POWER STATIONThis memorandum requests your approval to deviate from the Reactor Oversight Process(ROP) Action Matrix for the Davis-Besse Nuclear Power Station in order to continue heightened Nuclear Regulatory Commission (NRC) oversight for the time period of August 2007 through July 2008. This action is necessary to continue to monitor the licensee's efforts to sustain improved plant performance following resolution of the long-standing underlying problems that culminated in a Red finding associated with the severe wastage that was discovered on the reactor vessel head. Davis-Besse was placed under the IMC 0350 process for about three years. After the Oversight Panel's recommendation, and in consultation with the Director of NRR and the Deputy Executive Director for Reactor Programs, I authorized Davis-Besse's return to the ROP on July 1, 2005. In anticipation of the plant's transition from the IMC 0350 process, a deviation from the ROP was authorized on May 16, 2005, for the period of July 2005 through June 2006, and again on August 17, 2006, for the period of August 2006 through July 2007. The actions we propose in this memorandum are planned for Davis-Besse for the time period ofAugust 2007 through July 2009. This approach is consistent with our previously approved ROP deviation memoranda and the underlying concept of IMC 0305, in which the NRC, through its assessment process, has recognized that long-standing performance issues at a plant may require a more tailored, plant-specific followup over an extended period of time.CONTACT:Bruce Burgess, DRP, RIII(630) 829-9629See Previous ConcurrenceDOCUMENT NAME:C:\FileNet\ML072210843.wpd G Publicly Available G Non-Publicly Available G Sensitive G Non-SensitiveTo receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copyOFFICERIIIRIIIRIIINRRNRRRIIINAMEBBurgess*KO'Brien*JKH3 forCPederson*KSW forJAndersen*RKF forJDyer*JCaldwellDATE07/23/0707/24/0707/24/0707/26/0708/02/0708/01/07OFFICIAL RECORD COPY