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{{#Wiki_filter:A | {{#Wiki_filter:A REACTOR COOLANT PUMP FLOW TEST INSTRUMENTATION | ||
B | ~RSCHEL TYPE 24" x 17 1/2'~ VENTURI | ||
REACTOR | |||
.-~~~~~~~~~~ | |||
BARTON No. I, 0-20 MOD 200..._ psi _ __. | |||
:!: 2.5% | t 0.5% F.S. | ||
CASE AP | |||
MEASURED TEST | BARTON MOD 2 No.~ 0-20 -0.5% F.S. psi | ||
BARTON No.4, 0-15 MOD 200 psi ___ _. | |||
+/-0.5% F.S. | |||
: 6. p | |||
No.33898, BARTON MOD 200 0-15 psi..._ _ __. | |||
+/-0.5% F.S. | |||
I : | |||
I I I I I ' | ROYLYN No. 5 - BARTON MOD 227 1o----i CROSBY No. 4 0-3000 | ||
I I I I | * O. 25o/o psi... - 0-150 i: 0.5% psid F.S. 0-3000 t 0.5% F.S. psi | ||
92 500 | BALTIMORE Figure A GAS & ELECTRIC CO. REACTOR COOLANT PUMP FLOW Calvert Cliffs TEST INSTRUMENTATION Rev.18 Nuclear Power Plant | ||
:!: 0.5% OF READING t::.Pmin 84.57 PSI'------~ | Rev. 18 B ERROR IN ESTABLISHMENT OF FLOW | ||
BALTIMORE Figure B GAS & ELECTRIC CO. | |||
TEST LOOP TRUE FLOW" TRUE. Q = 92,500 ~PM REACTOR SYSTEM FLOW COOLANT | |||
VENTURI t::.P | |||
+ 1%0F THEORETICAL | |||
' t::,. Pc( 8. + (. 02518. 64 x 64 xl09 109 TRUE PUMP AP* 85 PSI VENTURI AP MEASURED | |||
:!: 2.5% A Pm~x B. 86 x 109 CASE AP OF READING t Q=./4E T. | |||
MEASURED TEST AP.. 85. CALCULATED LOOP AP + 0. 75 PSI Q.)s.86x109 | |||
+ 0.5% FS = AP max 85. 75 PSI TEST LOOP FLOW qr.ax 94, 100 GPM | |||
+ 0. 75 PSI | |||
: 6. p INDIVIDUAL PUMP ALLOWANCE FOR | |||
.__._!o1oo1~ CURVE PUMP CASE AREA Offiax94, 940 GPM VARIATION | |||
I : 840 GPM I I I I I ' | |||
I I ~ | |||
I I | |||
'f \\ I 92 ' 94, 500.) 940 MEASURED PUMP APPARENT REACTOR A P IN REACTOR COOLANT SYSTEM 0niax = 96,100 GPM COOLANT SYSTEM !::. p = 85 -85 PSI (Q.005) FLOW, WORST | |||
:!: 0.5% OF READING t::.Pmin 84.57 PSI'------~ CASE ERRORS | |||
BALTIMORE Figure B GAS & ELECTRIC CO. ERROR IN ESTABLISHMENT OF FLOW Calvert Cliffs Rev. 18 Nuclear Power Plant | |||
Rev. 18}} |
Revision as of 19:45, 19 November 2024
Text
A REACTOR COOLANT PUMP FLOW TEST INSTRUMENTATION
~RSCHEL TYPE 24" x 17 1/2'~ VENTURI
.-~~~~~~~~~~
BARTON No. I, 0-20 MOD 200..._ psi _ __.
t 0.5% F.S.
BARTON MOD 2 No.~ 0-20 -0.5% F.S. psi
BARTON No.4, 0-15 MOD 200 psi ___ _.
+/-0.5% F.S.
No.33898, BARTON MOD 200 0-15 psi..._ _ __.
+/-0.5% F.S.
ROYLYN No. 5 - BARTON MOD 227 1o----i CROSBY No. 4 0-3000
- O. 25o/o psi... - 0-150 i: 0.5% psid F.S. 0-3000 t 0.5% F.S. psi
BALTIMORE Figure A GAS & ELECTRIC CO. REACTOR COOLANT PUMP FLOW Calvert Cliffs TEST INSTRUMENTATION Rev.18 Nuclear Power Plant
Rev. 18 B ERROR IN ESTABLISHMENT OF FLOW
TEST LOOP TRUE FLOW" TRUE. Q = 92,500 ~PM REACTOR SYSTEM FLOW COOLANT
VENTURI t::.P
+ 1%0F THEORETICAL
' t::,. Pc( 8. + (. 02518. 64 x 64 xl09 109 TRUE PUMP AP* 85 PSI VENTURI AP MEASURED
- !: 2.5% A Pm~x B. 86 x 109 CASE AP OF READING t Q=./4E T.
MEASURED TEST AP.. 85. CALCULATED LOOP AP + 0. 75 PSI Q.)s.86x109
+ 0.5% FS = AP max 85. 75 PSI TEST LOOP FLOW qr.ax 94, 100 GPM
+ 0. 75 PSI
- 6. p INDIVIDUAL PUMP ALLOWANCE FOR
.__._!o1oo1~ CURVE PUMP CASE AREA Offiax94, 940 GPM VARIATION
I : 840 GPM I I I I I '
I I ~
I I
'f \\ I 92 ' 94, 500.) 940 MEASURED PUMP APPARENT REACTOR A P IN REACTOR COOLANT SYSTEM 0niax = 96,100 GPM COOLANT SYSTEM !::. p = 85 -85 PSI (Q.005) FLOW, WORST
- !: 0.5% OF READING t::.Pmin 84.57 PSI'------~ CASE ERRORS
BALTIMORE Figure B GAS & ELECTRIC CO. ERROR IN ESTABLISHMENT OF FLOW Calvert Cliffs Rev. 18 Nuclear Power Plant
Rev. 18