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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION  
{{#Wiki_filter:UNITED STATES
REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352  
                            NUCLEAR REGULATORY COMMISSION
  January 27, 2010  
                                              REGION III
                                2443 WARRENVILLE ROAD, SUITE 210
  Mr. Charles G. Pardee  
                                          LISLE, IL 60532-4352
Senior Vice President, Exelon Generation Company, LLC  
                                            January 27, 2010
President and Chief Nuclear Officer (CNO), Exelon Nuclear  
Mr. Charles G. Pardee
Senior Vice President, Exelon Generation Company, LLC
President and Chief Nuclear Officer (CNO), Exelon Nuclear
4300 Winfield Road
Warrenville, IL 60555
SUBJECT:        QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2
                NRC INTEGRATED INSPECTION REPORT 05000254/2009005;
                05000265/2009005
Dear Mr. Pardee:
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed
report documents the inspection findings, which were discussed on January 5, 2010, with
Mr. T. Tulon and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, three self-revealed findings of very low safety
significance were identified. Two of the findings involved a violation of NRC requirements.
However, because of their very low safety significance, and because the issues were entered
into your corrective action program, the NRC is treating the issues as non-cited violations
(NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally,
a licensee-identified violation is listed in Section 4OA7 of this report.
If you contest the subject or severity of an NCV, you should provide a response within 30 days
of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
Office at the Quad Cities Nuclear Power Station. In addition, if you disagree with the
characterization of any finding in this report, you should provide a response within 30 days of
the date of this inspection report, with the basis for your disagreement, to the Regional
Administrator, Region III, and the NRC Resident Inspector at the Quad Cities Nuclear Power
Station. The information that you provide will be considered in accordance with Inspection
Manual Chapter 0305.


4300 Winfield Road
C. Pardee                                    -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter
and its enclosure will be made available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                            Sincerely,
                                            /RA/
                                            Mark A. Ring, Chief
                                            Branch 1
                                            Division of Reactor Projects
Docket Nos. 50-254; 50-265
License Nos. DPR-29; DPR-30
Enclosure:    Inspection Report 05000254/2009005; 05000265/2009005
                w/Attachment: Supplemental Information
cc w/encl:    Distribution via ListServ


Warrenville, IL  60555
          U.S. NUCLEAR REGULATORY COMMISSION
SUBJECT: QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000254/2009005;
                          REGION III
Docket Nos:        50-254, 50-265
License Nos:       DPR-29, DPR-30
Report No:          05000254/2009005 and 05000265/2009005
Licensee:          Exelon Nuclear
Facility:          Quad Cities Nuclear Power Station, Units 1 and 2
Location:          Cordova, IL
Dates:              October 1 through December 31, 2009
Inspectors:        J. McGhee, Senior Resident Inspector
                    B. Cushman, Resident Inspector
                    R. Orlikowski, Senior Resident Inspector - Duane Arnold
                    M. Bielby, Senior Operations Engineer
                    C. Moore, Operations Engineer
                    M. Mitchell, Senior Radiation Protection Inspector
                    R. Jickling, Senior Emergency Preparedness Inspector
                    C. Mathews, Illinois Emergency Management Agency
Approved by:        M. Ring, Chief
                    Branch 1
                    Division of Reactor Projects
                                                                      Enclosure


05000265/2009005 Dear Mr. Pardee: On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed
                                          TABLE OF CONTENTS
report documents the inspection findings, which were discussed on January 5, 2010, with
SUMMARY OF FINDINGS ...........................................................................................................1
Mr. T. Tulon and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.   Based on the results of this inspection, three self-revealed findings of very low safety significance were identified. Two of the findings involved a violation of NRC requirements.
REPORT DETAILS .......................................................................................................................4
However, because of their very low safety significance, and because the issues were entered
Summary of Plant Status...........................................................................................................4
into your corrective action program, the NRC is
  1.    REACTOR SAFETY .......................................................................................................4
treating the issues as non-cited violations (NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally,
      1R01    Adverse Weather Protection (71111.01)..............................................................4
a licensee-identified violation is listed in Section 4OA7 of this report.   If you contest the subject or severity of an NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
      1R04    Equipment Alignment (71111.04) ........................................................................5
Regulatory Commission, ATTN:  Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
      1R05    Fire Protection (71111.05) ...................................................................................6
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
      1R11    Licensed Operator Requalification Program (71111.11)......................................7
Office at the Quad Cities Nuclear Power Station. In addition, if you disagree with the
      1R12    Maintenance Effectiveness (71111.12)..............................................................11
characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Quad Cities Nuclear Power
      1R13    Maintenance Risk Assessments and Emergent Work Control (71111.13) ........12
Station. The information that you provide will be considered in accordance with Inspection
      1R15    Operability Evaluations (71111.15) ....................................................................12
Manual Chapter 0305.  
      1R19    Post-Maintenance Testing (71111.19) ...............................................................13
  C. Pardee    -2-
      1R22    Surveillance Testing (71111.22) ........................................................................14
   
      1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ................15
  In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be made available electronically for public inspection in the
      1EP6 Drill Evaluation (71114.06).................................................................................17
NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS)ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).         Sincerely,        /RA/ 
  4.    OTHER ACTIVITIES.....................................................................................................18
      Mark A. Ring, Chief      Branch 1      Division of Reactor Projects
      4OA1 Performance Indicator Verification (71151) .......................................................18
      4OA2 Identification and Resolution of Problems (71152) ............................................21
      4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............27
      4OA5 Other Activities ...................................................................................................30
      4OA6 Management Meetings ......................................................................................30
      4OA7 Licensee-Identified Violations ............................................................................31
SUPPLEMENTAL INFORMATION ...............................................................................................1
  Key Points of Contact ................................................................................................................1
  List of Items Opened, Closed and Discussed............................................................................1
List of Documents Reviewed .....................................................................................................2
  List of Acronyms Used ..............................................................................................................8
                                                                                                                        Enclosure


                                      SUMMARY OF FINDINGS
Docket Nos. 50-254; 50-265
IR 05000254/2009005, 05000265/2009005; 10/01/09 - 12/31/09; Quad Cities Nuclear Power
Station, Units 1 & 2; Other Activities.
This report covers a 3-month period of inspection by resident inspectors and announced
baseline inspections by regional inspectors. Three Green findings were identified by the
inspectors. Two of the findings were considered Non-Cited Violations (NCVs) of NRC
regulations. The significance of most findings is indicated by their color (Green, White, Yellow,
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process
(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity
level after NRC management review. The NRCs program for overseeing the safe operation of
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
Revision 4, dated December 2006.
A.      NRC-Identified and Self-Revealed Findings
        Cornerstone: Mitigating Systems
    *  Green. A finding of very low safety significance and a NCV of 10 CFR 50 Appendix B,
        Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the
        installation of an inappropriate component into the Unit 2 emergency diesel generator
        coolant system. Specifically, the licensee failed to properly perform a part evaluation for
        a replacement temperature indicator (TI) designated as augmented quality. This
        resulted in the TI probe shearing off in the coolant flow stream and causing foreign
        material to enter the coolant system. Immediate corrective actions included the
        installation of an appropriately approved TI and recovery of foreign material from the
        system.
        The same part evaluation process was used for risk-significant components independent
        of the system being worked. Therefore, this finding was more than minor because, if left
        uncorrected, this performance deficiency could lead to unplanned unavailability of
        safety-related or risk-significant equipment and would become a more significant safety
        concern. The inspectors performed a Phase 1 SDP screening and concluded that the
        issue was of very low safety significance (Green) because the failure of the TI did not
        result in unplanned inoperability or loss of function of the diesel generator. The
        inspectors determined that this finding did not have a cross-cutting aspect. This
        performance deficiency is not indicative of current licensee performance. The decision
        to install this type of TI was made in October 2007. The process which allowed this
        performance deficiency was identified and corrected through procedure and policy
        revisions in February 2008. (Section 4OA2)
    *  Green: A finding of very low safety significance and a NCV of TS 3.6.2.4,
        Residual Heat Removal (RHR) Suppression Pool Spray, was self-revealed for the
        licensees failure to meet the Technical Specification (TS) limiting conditions of operation
        (LCO) requirement prior to transitioning into an operating mode where the LCO was
        required to be satisfied. Specifically, Motor Operator (MO) 1-1001-37B for the Unit 1
        RHR torus (suppression pool) spray isolation valve was found to have been inoperable
        when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009.
        The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the
        valve was not demonstrated operable by stroking the valve electrically after the actuator
                                                  1                                      Enclosure


License Nos. DPR-29; DPR-30
  motor was declutched. Inspectors determined that the finding was cross-cutting in the
Enclosure: Inspection Report 05000254/2009005; 05000265/2009005   w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ 
  area of Problem Identification and Resolution - Corrective Action (P.1(a)) because plant
Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos: 50-254, 50-265 License Nos: DPR-29, DPR-30 Report No: 05000254/2009005 and 05000265/2009005
  personnel failed to identify the physical contact with the valve actuator that resulted in
Licensee: Exelon Nuclear
  the valve being declutched; therefore, operators incorrectly assessed the system
Facility: Quad Cities Nuclear Power Station, Units 1 and 2
   condition as in compliance with TS 3.6.2.4. Immediate licensee corrective actions
Location: Cordova, IL
  included engagement of the motor and stroke testing of the valve.
Dates: October 1 through December 31, 2009 Inspectors: J. McGhee, Senior Resident Inspector  B. Cushman, Resident Inspector
  The finding is more than minor because it was associated with the equipment
R. Orlikowski, Senior Resident Inspector - Duane Arnold
  performance quality attribute of the Mitigating Systems Cornerstone and affected the
M. Bielby, Senior Operations Engineer
  objective of ensuring availability, reliability, and capability of systems that respond to
C. Moore, Operations Engineer  M. Mitchell, Senior Radiation Protection Inspector  R. Jickling, Senior Emergency Preparedness Inspector
  initiating events to prevent undesirable consequences. Specifically, failure to verify
C. Mathews, Illinois Emergency Management Agency 
  system availability and capability prior to entering the required modes resulted in fewer
  available mitigating systems than assumed in the operating risk evaluations. The
  inspectors determined the finding could be evaluated using the SDP in accordance with
  IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial
  Screening and Characterization of findings, Table 4a. Inspectors answered all of the
  questions for the Mitigating Systems Cornerstone No. Therefore, the finding screened
  as Green or very low safety significance. (Section 4OA3)
  Cornerstone: Barrier Integrity
* Green. A finding of very low safety significance was self-revealed for the failure to
  perform maintenance that would ensure the portable emergency flooding pump (Darley
  pump) was in a standby condition and readily available to accomplish the requirements
  of QCOA 0010-16, Flood Emergency Procedure. Specifically, the failure to perform
  adequate maintenance resulted in the need to replace the battery and gasoline for the
  pump and, upon pump start, fuel sprayed out of the fuel pump. Although the staged
  portable pump would not have supported the external flooding emergency response
  procedure, no violation of regulatory requirements occurred. The inspectors did not
  identify a cross-cutting aspect associated with this finding because the issue is not
  reflective of current licensee performance. Immediate corrective actions included
  replacement of the degraded battery and overhaul of the pumps fuel pump. Other
  actions included identification of preventative maintenance tasks and establishing a
  program owner of the pump and support equipment.
  This issue was more than minor because it was associated with the Structures,
  Systems, and Components (SSC) Performance attribute of the Barrier Integrity
  Cornerstone objective of maintaining the functionality of spent fuel pool cooling.
  The finding affected the cornerstone objective of providing assurance that physical
  design barriers protect the public from radionuclide releases caused by events including
  external flooding. Specifically, the pump could fail due to maintenance preventable
  component failure resulting in inadequate or degraded makeup to the spent fuel pool
  during an external flooding event. The inspectors determined the finding could be
  evaluated using the SDP in accordance with IMC 0609, Significance Determination
  Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of
  findings, Tables 4a and 4b. The inspectors determined that even though this equipment
  is assumed to completely fail, the licensee could provide an alternate portable pump
  already located on site and capable of performing the safety function during this slow
  developing event. Since alternate equipment was available and the delay in mobilizing
  the alternate equipment would not have resulted in loss of capability to mitigate the
                                              2                                      Enclosure


  impact of the flooding event, the issue is of very low safety significance or Green.
Approved by: M. Ring, Chief
  (Section 4OA2)
Branch 1 Division of Reactor Projects
B. Licensee-Identified Violations
 
  A violation of very low safety significance that was identified by the licensee was
Enclosure TABLE OF CONTENTS SUMMARY OF FINDINGS...........................................................................................................1
  reviewed by inspectors. Corrective actions planned or taken by the licensee have been
REPORT DETAILS.......................................................................................................................4 Summary of Plant Status...........................................................................................................4 1. REACTOR SAFETY.......................................................................................................4
  entered into the licensees corrective action program. This violation and associated
1R01 Adverse Weather Protection (71111.01)..............................................................4
  corrective action tracking number are listed in Section 4OA7 of this report.
1R04 Equipment Alignment (71111.04)........................................................................5
                                            3                                      Enclosure
1R05 Fire Protection (71111.05)...................................................................................6
1R11 Licensed Operator Requalification Program (71111.11)......................................7
1R12 Maintenance Effectiveness (71111.12)..............................................................11
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)........12
1R15 Operability Evaluations (71111.15)....................................................................12
1R19 Post-Maintenance Testing (71111.19)...............................................................13
1R22 Surveillance Testing (71111.22)........................................................................14
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)................15
1EP6 Drill Evaluation (71114.06).................................................................................17
4. OTHER ACTIVITIES.....................................................................................................18
4OA1 Performance Indicator Verification (71151).......................................................18
4OA2 Identification and Resolution of Problems (71152)............................................21
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)...............27
4OA5 Other Activities...................................................................................................30
4OA6  Management Meetings......................................................................................30
4OA7 Licensee-Identified Violations............................................................................31
SUPPLEMENTAL INFORMATION...............................................................................................1
Key Points of Contact................................................................................................................1 List of Items Opened, Closed and Discussed............................................................................1
List of Documents Reviewed.....................................................................................................
2 List of Acronyms Used..............................................................................................................8 
  1 Enclosure SUMMARY OF FINDINGS IR 05000254/2009005, 05000265/2009005; 10/01/09 - 12/31/09; Quad Cities Nuclear Power Station, Units 1 & 2; Other Activities.  This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.
  Three Green findings were identified by the inspectors.  Two of the findings were considered Non-Cited Violations (NCVs) of NRC
regulations.  The significance of most findings is indicated by their color (Green, White, Yellow,
Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process"
(SDP).  Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.  The NRC's program for overseeing the safe operation of
commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process,"
Revision 4, dated December 2006.   A. NRC-Identified and Self-Revealed Findings
Cornerstone:  Mitigating Systems  Green.  A finding of very low safety significance and a NCV of 10 CFR 50 Appendix B, Criterion V, "Instructions, Procedures, and Drawings," was self-revealed for the installation of an inappropriate component into the Unit 2 emergency diesel generator coolant system. Specifically, the licensee failed to properly perform a part evaluation for a replacement temperature indicator (TI) designated as "augmented quality."  This
resulted in the TI probe shearing off in the coolant flow stream and causing foreign


material to enter the coolant system.  Immediate corrective actions included the installation of an appropriately approved TI and recovery of foreign material from the system.  The same part evaluation process was used for risk-significant components independent of the system being worked.  Therefore, this finding was more than minor because, if left
                                          REPORT DETAILS
uncorrected, this performance deficiency could lead to unplanned unavailability of
Summary of Plant Status
safety-related or risk-significant equipment and would become a more significant safety concern.  The inspectors performed a Phase 1 SDP screening and concluded that the issue was of very low safety significance (Green) because the failure of the TI did not
Unit 1
result in unplanned inoperability or loss of function of the diesel generator.  The
Unit 1 operated at 100 percent thermal power throughout the evaluated period from October 1
inspectors determined that this finding did not have a cross-cutting aspect.  This
until December 31, 2009, with the exception of planned power reductions for routine
performance deficiency is not indicative of current licensee performance.  The decision
surveillances, planned equipment repair, and control rod maneuvers.
to install this type of TI was made in Oc
Unit 2
tober 2007.  The process which allowed this performance deficiency was identified and corrected through procedure and policy
Unit 2 operated at or near 100 percent thermal power from October 1 until December 16 with
revisions in February 2008.  (Section 4OA2)  Green:  A finding of very low safety significance and a NCV of TS 3.6.2.4, "Residual Heat Removal (RHR) Suppression Pool Spray," was self-revealed for the licensee's failure to meet the Technical Specification (TS) limiting conditions of operation
the exception of planned power reductions for routine surveillances and control rod maneuvers.
(LCO) requirement prior to transitioning into an operating mode where the LCO was
On December 16, 2009, operators attempted to replace a light bulb in the indication circuit for
required to be satisfied.  Specifically, Motor Operator (MO) 1-1001-37B for the Unit 1 RHR torus (suppression pool) spray isolation valve was found to have been inoperable when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. 
the extraction steam check valve A on the 2D feedwater heaters. The light bulb separated with
The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the
the base remaining in the socket. During the evolution the D heaters tripped, resulting in a
valve was not demonstrated operable by stroking the valve electrically after the actuator 
partial loss of feedwater heating and a resulting change in reactor power. Operators lowered
  2 Enclosure motor was declutched.  Inspectors determined that the finding was cross-cutting in the area of Problem Identification and Resolution - Corrective Action (P.1(a)) because plant
power about 150 MWth (50 MWe) by inserting one high reactivity-worth control rod. Power
personnel failed to identify the physical contact with the valve actuator that resulted in the valve being declutched; therefore, operators incorrectly assessed the system condition as in compliance with TS 3.6.2.4.  Immediate licensee corrective actions
increased by 0.59 percent during the loss of feedwater heating transient. By 10:45 a.m. that
included engagement of the motor and stroke testing of the valve.  The finding is more than minor because it was associated with the equipment performance quality attribute of the Mitigating Systems Cornerstone and affected the
same morning, feedwater heaters had been restored and the control rod was withdrawn to
objective of ensuring availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, failure to verify system availability and capability prior to entering the required modes resulted in fewer
restore the unit to 100 percent thermal power. The unit remained at 100 percent power for the
available mitigating systems than assumed in the operating risk evaluations.  The
duration of the evaluated period.
inspectors determined the finding could be evaluated using the SDP in accordance with
1.       REACTOR SAFETY
IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of findings," Table 4a.  Inspectors answered all of the questions for the Mitigating Systems Cornerstone "No."  Therefore, the finding screened
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
as Green or very low safety significance. (Section 4OA3) Cornerstone:  Barrier Integrity  Green.  A finding of very low safety significance was self-revealed
1R01 Adverse Weather Protection (71111.01)
for the failure to perform maintenance that would ensure the portable emergency flooding pump (Darley pump) was in a standby condition and readily available to accomplish the requirements of QCOA 0010-16, "Flood Emergency Procedure."  Specifically, the failure to perform adequate maintenance resulted in the need to replace the battery and gasoline for the
  .1     Winter Seasonal Readiness Preparations
pump and, upon pump start, fuel sprayed out of the fuel pump.  Although the staged
    a.   Inspection Scope
portable pump would not have supported the external flooding emergency response
        The inspectors conducted a review of the licensees preparations for winter conditions to
procedure, no violation of regulatory requirements occurred.  The inspectors did not
        verify that the plants design features and implementation of procedures were sufficient
identify a cross-cutting aspect associated with this finding because the issue is not reflective of current licensee performance.  Immediate corrective actions included replacement of the degraded battery and overhaul of the pump's fuel pump.  Other
        to protect mitigating systems from the effects of adverse weather. Documentation for
actions included identification of preventative maintenance tasks and establishing a
        selected risk-significant systems was reviewed to ensure that these systems would
program owner of the pump and support equipment. This issue was more than minor because it was associated with the Structures, Systems, and Components (SSC) Performance attribute of the Barrier Integrity Cornerstone objective of maintaining the functionality of spent fuel pool cooling. 
        remain functional when challenged by inclement weather. During the inspection, the
The finding affected the cornerstone objective of providing assurance that physical
        inspectors focused on plant-specific design features and the licensees procedures used
design barriers protect the public from radionuclide releases caused by events including external flooding.  Specifically, the pump could fail due to maintenance preventable
        to mitigate or respond to adverse weather conditions. Additionally, the inspectors
component failure resulting in inadequate or degraded makeup to the spent fuel pool during an external flooding event.  The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination
        reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of
        requirements for systems selected for inspection, and verified that operator actions were
findings," Tables 4a and 4b.  The inspectors determined that even though this equipment
        appropriate as specified by plant-specific procedures. Cold weather protection, such as
is assumed to completely fail, the licensee could provide an alternate portable pump already located on site and capable of performing the safety function during this slow developing event.  Since alternate equipment was available and the delay in mobilizing
        heat tracing and area heaters, was verified to be in operation where applicable. The
the alternate equipment would not have resulted in loss of capability to mitigate the 
        inspectors also reviewed corrective action program (CAP) items to verify that the
  3 Enclosure impact of the flooding event, the issue is of very low safety significance or Green.  (Section 4OA2) B. Licensee-Identified Violations
        licensee was identifying adverse weather issues at an appropriate threshold and
A violation of very low safety significance that was identified by the licensee was reviewed by inspectors.  Corrective actions planned or taken by the licensee have been
        entering them into the CAP in accordance with station corrective action procedures.
entered into the licensee's corrective action program.  This violation and associated
        Specific documents reviewed during this inspection are listed in the Attachment to this
corrective action tracking number are listed in Section 4OA7 of this report. 
        report. The inspectors reviews focused specifically on the following plant systems due
  4 Enclosure REPORT DETAILS
        to their risk significance or susceptibility to cold weather issues:
Summary of Plant Status
                                                      4                                  Enclosure
Unit 1 Unit 1 operated at 100 percent thermal power throughout the evaluated period from October 1 until December 31, 2009, with the exception of planned power reductions for routine  
surveillances, planned equipment repair, and control rod maneuvers.  
Unit 2 Unit 2 operated at or near 100 percent thermal power from October 1 until December 16 with the exception of planned power reductions for ro
utine surveillances and control rod maneuvers. On December 16, 2009, operators attempted to replace a light bulb in the indication circuit for  
the extraction steam check valve 'A' on the 2D feedwater heaters. The light bulb separated with the base remaining in the socket. During the evolution the 'D' heaters tripped, resulting in a  
partial loss of feedwater heating and a resulting change in reactor power. Operators lowered  
power about 150 MWth (50 MWe) by inserting one high reactivity-worth control rod. Power increased by 0.59 percent during the loss of feedwater heating transient. By 10:45 a.m. that same morning, feedwater heaters had been restored and the control rod was withdrawn to  
restore the unit to 100 percent thermal power. The unit remained at 100 percent power for the  
duration of the evaluated period.   1. REACTOR SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01) .1 Winter Seasonal Readiness Preparations
a. Inspection Scope
The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather. Documentation for  
selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather. During the inspection, the  
inspectors focused on plant-specific design features and the licensee's procedures used  
to mitigate or respond to adverse weather conditions. Additionally, the inspectors  
reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for systems selected for inspection, and verified that operator actions were  
appropriate as specified by plant-specific procedures. Cold weather protection, such as  
heat tracing and area heaters, was verified to be in operation where applicable. The  
inspectors also reviewed corrective action program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into the CAP in accordance with station corrective action procedures. Specific documents reviewed during this inspection are listed in the Attachment to this report. The inspectors' reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues:  
  5 Enclosure heating steam, and  circulating water/de-icing valve. This inspection constituted one winter seasonal readiness preparations sample as defined in Inspection Procedure (IP) 71111.01-05. b. Findings
No findings of significance were identified.  1R04 Equipment Alignment (71111.04) .1 Quarterly Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant systems:    1/2 'B' diesel driven fire pump; and  Unit 1 emergency diesel generator and diesel generator cooling water pump.  The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstone at the time they were inspected.  The inspectors attempted
to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
orders (WOs), condition reports, and the impact of ongoing work activities on redundant
trains of equipment in order to identify conditions that could have rendered the systems
incapable of performing their intended functions.  The inspectors also walked down
accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the components and observed operating parameter
s of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly
identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the Attachment to this report.  These activities constituted two partial system walkdown samples as defined in
IP 71111.04-05. b. Findings
No findings of significance were identified. 
  6 Enclosure .2 Semi-Annual Complete System Walkdown
a. Inspection Scope
On November 5, 2009, the inspectors performed a complete system alignment inspection of the Unit 2 emergency diesel generator to verify the functional capability of the system.  This system was selected because
it was considered both safety significant and risk significant in the licensee's probabilistic risk assessment.  The inspectors
walked down the system to review mechanical and electrical equipment lineups;
electrical power availability; system pressure and temperature indications, as
appropriate; component labeling; component lubrication; component and equipment cooling; hangers and supports; operability of support systems; and to ensure that ancillary equipment or debris did not interfere with equipment operation.  A review of a


sample of past and outstanding work orders was performed to determine whether any
      *        heating steam, and
deficiencies significantly affected the system
      *        circulating water/de-icing valve.
function.  In addition, the inspectors reviewed the CAP database to ensure that system equipment alignment problems were being identified and appropriately resolved.  Documents reviewed are listed in the Attachment to this report. These activities constituted one complete system walkdown sample as defined in  
      This inspection constituted one winter seasonal readiness preparations sample as
IP 71111.04-05.   b. Findings
      defined in Inspection Procedure (IP) 71111.01-05.
No findings of significance were identified.   1R05 Fire Protection (71111.05) .1 Routine Resident Inspector Tours (71111.05Q) a. Inspection Scope
  b. Findings
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:   Unit 2 Reactor Bldg. El. 554'0", NW Corner Room - 2A Core Spray, Fire Zone
      No findings of significance were identified.
11.3.3;  Unit 1 Turbine Bldg. El. 595'0", Diesel Generator, Fire Zone 9.1;  Unit 1 Turbine Bldg. El. 595'0", Reactor Feed Pumps, Fire Zone 8.2.6.A;  Crib House Bldg. El. 559'8", Basement, Fire Zone 11.4.A; and  Crib House Bldg. El. 595'0", Ground Floor/Service Water Pumps, Fire Zone
1R04 Equipment Alignment (71111.04)
11.4.B. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained
.1   Quarterly Partial System Walkdowns
passive fire protection features in good material condition, and implemented adequate
  a. Inspection Scope
compensatory measures for out-of-service, degraded or inoperable fire protection
      The inspectors performed partial system walkdowns of the following risk-significant
equipment, systems, or features in accordance with the licensee's fire plan.
      systems:
The inspectors selected fire areas based on their overall contribution to internal fire risk 
      *        1/2 B diesel driven fire pump; and
  7 Enclosure as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a
      *        Unit 1 emergency diesel generator and diesel generator cooling water pump.
plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the Attachment to this report, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for
      The inspectors selected these systems based on their risk significance relative to the
immediate use; that fire detectors and sprinklers were unobstructed; that transient
      Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted
material loading was within the analyzed limits; and fire doors, dampers, and penetration
      to identify any discrepancies that could impact the function of the system, and, therefore,
seals appeared to be in satisfactory condition. The inspectors also verified that minor
      potentially increase risk. The inspectors reviewed applicable operating procedures,
issues identified during the inspection were entered into the licensee's CAP.  Documents reviewed are listed in the Attachment to this report.  These activities constituted five quarterly fire protection inspection samples as defined in
      system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
IP 71111.05-05.  b. Findings
      orders (WOs), condition reports, and the impact of ongoing work activities on redundant
No findings of significance were identified.  1R11 Licensed Operator Requalification Program (71111.11) .1 Resident Inspector Quarterly Review (71111.11Q) a. Inspection Scope
      trains of equipment in order to identify conditions that could have rendered the systems
On November 4, 2009, the inspectors observed licensed operator continuing training to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures.  The inspectors evaluated the following areas:    licensed operator performance;  crew's communications and accuracy of documentation;  ability to take timely actions in the conservative direction;  correct use and implementation of abnormal and emergency procedures;  control board manipulations;  oversight and direction from supervisors; and  ability to identify and implement Emergency Plan actions and notifications.  The crew's performance in these areas was compared to pre-established operator action expectations and lesson objectives.  Documents reviewed are listed in the Attachment to
      incapable of performing their intended functions. The inspectors also walked down
this report.  This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.  b. Findings
      accessible portions of the systems to verify system components and support equipment
No findings of significance were identified.   
      were aligned correctly and operable. The inspectors examined the material condition of
  8 Enclosure .2 Facility Operating History (71111.11B) a. Inspection Scope
      the components and observed operating parameters of equipment to verify that there
The inspectors reviewed the plant's operating history from January 2007 through September 2009 to identify operating experience that was expected to be addressed by the Licensed Operator Requalification Training (LORT) program.  The inspectors verified
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
that the identified operating experience had been addressed by the facility licensee in
      identified and resolved equipment alignment problems that could cause initiating events
accordance with the station's approved Systems Approach to Training (SAT) program to satisfy the requirements of 10 CFR 55.59(c).  The documents reviewed during this
      or impact the capability of mitigating systems or barriers and entered them into the CAP
inspection are listed in the Attachment to this report.  b. Findings
      with the appropriate significance characterization. Documents reviewed are listed in the
No findings of significance were identified.  .3 Licensee Requalification Examinations
      Attachment to this report.
a. Inspection Scope
      These activities constituted two partial system walkdown samples as defined in
The inspectors performed an inspection of the licensee's LORT test/examination program for compliance with the station's SAT program which would satisfy the requirements of 10 CFR 55.59(c)(4).  The reviewed operating examination material  
      IP 71111.04-05.
consisted of two operating tests, each containing two dynamic simulator scenarios and
  b. Findings
five job performance measures (JPMs).  The two biennial written examinations reviewed
      No findings of significance were identified.
consisted of two parts.  Each written examination contained 30 questions consisting of 15 written exam questions and 15 static exam questions.  The inspectors reviewed the annual requalification operating test and biennial written examination material to  
                                                5                                     Enclosure
evaluate general quality, construction, and difficulty level. The inspectors assessed the  
level of examination material duplication fr
om week to week during the current year operating test.  The examiners assessed the amount of written examination material duplication from week to week for the biennial written examination administered in calendar year 2009.  The inspectors reviewed the methodology for developing the examinations, including the LORT program 2-year sample plan, probabilistic risk assessment insights, previously identified operator performance deficiencies, and plant modifications. The documents reviewed during this inspection are listed in the  
Attachment to this report.   b. Findings
No findings of significance were identified.  .4 Licensee Administration of Requalification Examinations
a. Inspection Scope
The inspectors observed the administration of a requalification operating test to assess the licensee's effectiveness in conducting the test to ensure compliance with 10 CRF 55.59(c)(4).  The inspectors evaluated the performance of one operating crew in parallel with the facility evaluators dur
ing four dynamic simulator scenarios and evaluated various licensed crew members concurrently with facility evaluators during the 
  9 Enclosure administration of several JPMs. The inspectors assessed the facility evaluators' ability to determine adequate crew and individual performance using objective, measurable
standards.  The inspectors observed the training staff personnel administer the operating test, including conducting pre-examination briefings, evaluations of operator performance, and individual and crew evaluations upon completion of the operating test.
The inspectors evaluated the ability of the simulator to support the examinations.  b. Findings
No findings of significance were identified.   .5 Examination Security
a. Inspection Scope
The inspectors observed and reviewed the licensee's overall licensed operator requalification examination security program related to examination physical security (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability
and bias) to verify compliance with 10 CFR 55.49, "Integrity of Examinations and Tests."  The inspectors also reviewed the facility licensee's examination security procedure and the implementation of security and integr
ity measures (e.g., security agreements, sampling criteria, bank use, and test item repetition) throughout the examination
process.  No examination security compromises occurred during these observations. 


The documents reviewed during this inspection are listed in the Attachment to this  
.2  Semi-Annual Complete System Walkdown
report.   b. Findings
  a. Inspection Scope
No findings of significance were identified.  .6 Licensee Training Feedback System
      On November 5, 2009, the inspectors performed a complete system alignment
a. Inspection Scope
      inspection of the Unit 2 emergency diesel generator to verify the functional capability of
The inspectors assessed the methods and effectiveness of the licensee's processes for revising and maintaining its LORT program up-to-date, including the use of feedback
      the system. This system was selected because it was considered both safety significant
from plant events and industry experience information. The inspectors reviewed the licensee's quality assurance oversight activities, including licensee training department self-assessment reports. The inspectors evaluated the licensee's ability to assess the
      and risk significant in the licensees probabilistic risk assessment. The inspectors
      walked down the system to review mechanical and electrical equipment lineups;
      electrical power availability; system pressure and temperature indications, as
      appropriate; component labeling; component lubrication; component and equipment
      cooling; hangers and supports; operability of support systems; and to ensure that
      ancillary equipment or debris did not interfere with equipment operation. A review of a
      sample of past and outstanding work orders was performed to determine whether any
      deficiencies significantly affected the system function. In addition, the inspectors
      reviewed the CAP database to ensure that system equipment alignment problems were
      being identified and appropriately resolved. Documents reviewed are listed in the
      Attachment to this report.
      These activities constituted one complete system walkdown sample as defined in
      IP 71111.04-05.
  b. Findings
      No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1   Routine Resident Inspector Tours (71111.05Q)
  a. Inspection Scope
      The inspectors conducted fire protection walkdowns which were focused on availability,
      accessibility, and the condition of firefighting equipment in the following risk-significant
      plant areas:
      *      Unit 2 Reactor Bldg. El. 5540, NW Corner Room - 2A Core Spray, Fire Zone
              11.3.3;
      *      Unit 1 Turbine Bldg. El. 5950, Diesel Generator, Fire Zone 9.1;
      *      Unit 1 Turbine Bldg. El. 5950, Reactor Feed Pumps, Fire Zone 8.2.6.A;
      *      Crib House Bldg. El. 5598, Basement, Fire Zone 11.4.A; and
      *      Crib House Bldg. El. 5950, Ground Floor/Service Water Pumps, Fire Zone
              11.4.B.
      The inspectors reviewed areas to assess if the licensee had implemented a fire
      protection program that adequately controlled combustibles and ignition sources within
      the plant, effectively maintained fire detection and suppression capability, maintained
      passive fire protection features in good material condition, and implemented adequate
      compensatory measures for out-of-service, degraded or inoperable fire protection
      equipment, systems, or features in accordance with the licensees fire plan.
      The inspectors selected fire areas based on their overall contribution to internal fire risk
                                                  6                                      Enclosure


effectiveness of its LORT program and their ability to implement appropriate corrective actions.  This evaluation was performed to verify compliance with 10 CFR 55.59(c) and the licensee's SAT based program.  The documents reviewed during this inspection are listed in the Attachment to this report.  b. Findings
      as documented in the plants Individual Plant Examination of External Events with later
No findings of significance were identified.   
      additional insights, their potential to impact equipment which could initiate or mitigate a
  10 Enclosure .7 Licensee Remedial Training Program
      plant transient, or their impact on the plants ability to respond to a security event.
a. Inspection Scope
      Using the documents listed in the Attachment to this report, the inspectors verified that
The inspectors assessed the adequacy and effectiveness of the remedial training conducted since the previous biennial requalification examinations and the training from the current examination cycle to ensure that they addressed weaknesses in licensed operator or crew performance identified during training and plant operations. The  
      fire hoses and extinguishers were in their designated locations and available for
inspectors reviewed remedial training procedur
      immediate use; that fire detectors and sprinklers were unobstructed; that transient
es and individual remedial training plans.  This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to
      material loading was within the analyzed limits; and fire doors, dampers, and penetration
the licensee's SAT based program.  The documents reviewed during this inspection are listed in the Attachment to this report.   b. Findings
      seals appeared to be in satisfactory condition. The inspectors also verified that minor
No findings of significance were identified. .8 Conformance With Operator License Conditions
      issues identified during the inspection were entered into the licensees CAP.
  a. Inspection Scope
      Documents reviewed are listed in the Attachment to this report.
The inspectors reviewed the facility and individual operator licensees' conformance with the requirements of 10 CFR Part 55.  The inspectors reviewed the facility licensee's
      These activities constituted five quarterly fire protection inspection samples as defined in
program for maintaining active operator licenses and to assess compliance with
      IP 71111.05-05.
10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the  
  b. Findings
process for tracking on-shift hours for licensed operators and which control room positions were granted watch-standing credit for maintaining active operator licenses.  The inspectors reviewed the facility licensee's LORT program to assess compliance with
      No findings of significance were identified.
the requalification program requirements as described by 10 CFR 55.59(c).  Additionally, medical records for 10 licensed operators were reviewed for compliance with
1R11 Licensed Operator Requalification Program (71111.11)
10 CFR 55.53(I).  The documents reviewed during this inspection are listed in the  
  .1  Resident Inspector Quarterly Review (71111.11Q)
Attachment to this report.  b. Findings
  a. Inspection Scope
No findings of significance were identified.  .9 Annual Operating Test Results and Biennial Written Examination Results (71111.11B) a. Inspection Scope
      On November 4, 2009, the inspectors observed licensed operator continuing training to
The inspectors reviewed the overall pass/fail results of the individual JPM operating tests, the simulator operating tests, and the biennial written examination (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from September 2009
      verify that operator performance was adequate, evaluators were identifying and
through November 2009 as part of the licensee's operator licensing requalification cycle.  These results were compared to the thresholds established in Inspection Manual
      documenting crew performance problems, and training was being conducted in
Chapter 0609, Appendix I, "Licensed Operator Requalification Significance
      accordance with licensee procedures. The inspectors evaluated the following areas:
Determination Process (SDP)."  The evaluations were also performed to determine if the licensee effectively implemented operator requalification guidelines established in NUREG 1021, "Operator Licensing Examination Standards for Power Reactors," and
      *        licensed operator performance;
  11 Enclosure IP 71111.11, "Licensed Operator Requalification Program."  The documents reviewed during this inspection are listed in the Attachment to this report.   This inspection constituted one inspection sample as defined in IP 71111.11.   b. Findings
      *        crews communications and accuracy of documentation;
No findings of significance were identified.   1R12 Maintenance Effectiveness (71111.12) .1 Routine Quarterly Evaluations (71111.12Q) a. Inspection Scope
      *        ability to take timely actions in the conservative direction;
The inspectors evaluated degraded performance issues involving the following risk-significant systems:  Z2900; Safe Shutdown Makeup Pump, and  Z4700; Instrument Air. The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and
      *        correct use and implementation of abnormal and emergency procedures;
independently verified the licensee's actions to address system performance or condition
      *        control board manipulations;
      *        oversight and direction from supervisors; and
      *        ability to identify and implement Emergency Plan actions and notifications.
      The crews performance in these areas was compared to pre-established operator action
      expectations and lesson objectives. Documents reviewed are listed in the Attachment to
      this report.
      This inspection constituted one quarterly licensed operator requalification program
      sample as defined in IP 71111.11.
  b. Findings
      No findings of significance were identified.
                                                  7                                      Enclosure


problems in terms of the following:    implementing appropriate work practices;  identifying and addressing common cause failures;  scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  characterizing system reliability issues for performance;  charging unavailability for performance;  trending key parameters for condition monitoring;  ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying appropriate performance criteria for SSCs/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified
.2  Facility Operating History (71111.11B)
as (a)(1).   The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.   This inspection constituted two quarterly maintenance effectiveness samples as defined in IP 71111.12-05.   b. Findings
  a. Inspection Scope
No findings of significance were identified.  
    The inspectors reviewed the plants operating history from January 2007 through
   12 Enclosure 1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) .1 Maintenance Risk Assessments and Emergent Work Control
    September 2009 to identify operating experience that was expected to be addressed by
a. Inspection Scope
    the Licensed Operator Requalification Training (LORT) program. The inspectors verified
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related
    that the identified operating experience had been addressed by the facility licensee in
equipment listed below to verify that the appropriate risk assessments were performed
    accordance with the stations approved Systems Approach to Training (SAT) program to
    satisfy the requirements of 10 CFR 55.59(c). The documents reviewed during this
    inspection are listed in the Attachment to this report.
  b. Findings
    No findings of significance were identified.
.3  Licensee Requalification Examinations
  a. Inspection Scope
    The inspectors performed an inspection of the licensees LORT test/examination
    program for compliance with the stations SAT program which would satisfy the
    requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material
    consisted of two operating tests, each containing two dynamic simulator scenarios and
    five job performance measures (JPMs). The two biennial written examinations reviewed
    consisted of two parts. Each written examination contained 30 questions consisting of
    15 written exam questions and 15 static exam questions. The inspectors reviewed the
    annual requalification operating test and biennial written examination material to
    evaluate general quality, construction, and difficulty level. The inspectors assessed the
    level of examination material duplication from week to week during the current year
    operating test. The examiners assessed the amount of written examination material
    duplication from week to week for the biennial written examination administered in
    calendar year 2009. The inspectors reviewed the methodology for developing the
    examinations, including the LORT program 2-year sample plan, probabilistic risk
    assessment insights, previously identified operator performance deficiencies, and plant
    modifications. The documents reviewed during this inspection are listed in the
    Attachment to this report.
   b. Findings
    No findings of significance were identified.
.4   Licensee Administration of Requalification Examinations
  a. Inspection Scope
    The inspectors observed the administration of a requalification operating test to
    assess the licensees effectiveness in conducting the test to ensure compliance with
    10 CRF 55.59(c)(4). The inspectors evaluated the performance of one operating crew in
    parallel with the facility evaluators during four dynamic simulator scenarios and
    evaluated various licensed crew members concurrently with facility evaluators during the
                                                8                                    Enclosure


prior to removing equipment for work:  Work Week 45 - 1A residual heat removal (RHR) room cooler, 1A RHR service water (RHRSW) loop, 1B RHR seal cooler, 1-1001-16A boroscope and Votes testing, 1-1001-37A MOV equipment qualification inspection; and  Work Week 51 - Unit 1 250 Vdc battery reconfiguration using Unit 1 125 Vdc alternate battery with emergent Unit 2 125 Vdc battery low specific gravity
    administration of several JPMs. The inspectors assessed the facility evaluators ability
problems, 2A RHR loop and 2B RHRSW pump unavailability.   These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
    to determine adequate crew and individual performance using objective, measurable
and complete. When emergent work was performed, the inspectors verified that the
    standards. The inspectors observed the training staff personnel administer the operating
plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were
    test, including conducting pre-examination briefings, evaluations of operator
consistent with the risk assessment.  The inspectors also reviewed TS requirements and  
    performance, and individual and crew evaluations upon completion of the operating test.
walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.   These maintenance risk assessments and emergent work control activities constituted
    The inspectors evaluated the ability of the simulator to support the examinations.
two samples as defined in IP 71111.13-05.  b. Findings
  b. Findings
No findings of significance were identified.  1R15 Operability Evaluations (71111.15) .1 Operability Evaluations
    No findings of significance were identified.
a. Inspection Scope
.5  Examination Security
The inspectors reviewed the following issues:  IR 987904:  1A RHR Room Cooler Tube Sheet Has Pitting, and IR 994823:  TS SR 3.8.4.8 Frequency Not Met. The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical
  a. Inspection Scope
adequacy of the evaluations to ensure that TS operability was properly justified and the  
    The inspectors observed and reviewed the licensees overall licensed operator
subject component or system remained available such that no unrecognized increase in
    requalification examination security program related to examination physical security
   13 Enclosure risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensee's evaluations to determine
    (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability
    and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.
    The inspectors also reviewed the facility licensees examination security procedure and
    the implementation of security and integrity measures (e.g., security agreements,
    sampling criteria, bank use, and test item repetition) throughout the examination
    process. No examination security compromises occurred during these observations.
    The documents reviewed during this inspection are listed in the Attachment to this
    report.
   b. Findings
    No findings of significance were identified.
.6   Licensee Training Feedback System
  a. Inspection Scope
    The inspectors assessed the methods and effectiveness of the licensees processes for
    revising and maintaining its LORT program up-to-date, including the use of feedback
    from plant events and industry experience information. The inspectors reviewed the
    licensees quality assurance oversight activities, including licensee training department
    self-assessment reports. The inspectors evaluated the licensees ability to assess the
    effectiveness of its LORT program and their ability to implement appropriate corrective
    actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and
    the licensees SAT based program. The documents reviewed during this inspection are
    listed in the Attachment to this report.
   b. Findings
    No findings of significance were identified.
                                              9                                        Enclosure


whether the components or systems were
.7  Licensee Remedial Training Program
operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors  
  a. Inspection Scope
determined, where appropriate, compliance with bounding limitations associated with the  
    The inspectors assessed the adequacy and effectiveness of the remedial training
evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
    conducted since the previous biennial requalification examinations and the training from
documents to verify that the licensee was identifying and correcting any deficiencies
    the current examination cycle to ensure that they addressed weaknesses in licensed
associated with operability evaluations. Documents reviewed are listed in the Attachment to this report.   This operability inspection constituted two samples as defined in IP 71111.15-05.   b. Findings
    operator or crew performance identified during training and plant operations. The
No findings of significance were identified.  1R19 Post-Maintenance Testing (71111.19) .1 Post-Maintenance Testing
    inspectors reviewed remedial training procedures and individual remedial training plans.
a. Inspection Scope
    This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to
The inspectors reviewed the following post-maintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional
    the licensees SAT based program. The documents reviewed during this inspection are
    listed in the Attachment to this report.
  b. Findings
    No findings of significance were identified.
.8  Conformance With Operator License Conditions
  a. Inspection Scope
    The inspectors reviewed the facility and individual operator licensees' conformance with
    the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's
    program for maintaining active operator licenses and to assess compliance with
    10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the
    process for tracking on-shift hours for licensed operators and which control room
    positions were granted watch-standing credit for maintaining active operator licenses.
    The inspectors reviewed the facility licensee's LORT program to assess compliance with
    the requalification program requirements as described by 10 CFR 55.59(c). Additionally,
    medical records for 10 licensed operators were reviewed for compliance with
    10 CFR 55.53(I). The documents reviewed during this inspection are listed in the
    Attachment to this report.
   b. Findings
    No findings of significance were identified.
.9   Annual Operating Test Results and Biennial Written Examination Results (71111.11B)
  a. Inspection Scope
    The inspectors reviewed the overall pass/fail results of the individual JPM operating
    tests, the simulator operating tests, and the biennial written examination (required to be
    given per 10 CFR 55.59(a)(2)) administered by the licensee from September 2009
    through November 2009 as part of the licensees operator licensing requalification cycle.
    These results were compared to the thresholds established in Inspection Manual
    Chapter 0609, Appendix I, Licensed Operator Requalification Significance
    Determination Process (SDP)." The evaluations were also performed to determine if the
    licensee effectively implemented operator requalification guidelines established in
    NUREG 1021, Operator Licensing Examination Standards for Power Reactors, and
                                              10                                      Enclosure


capability:  WO 1121775, 250 Vdc Battery Charger #2 4-Hour Load Test;  WO 1261246, Replace Battery Changeover Relay R12 EC 376690; QCMMS 4100-33, 1/2-4101B Diesel Driven Fire Pump Annual Capacity Test;  WO 1130535, OP PMT Filter 'B' Train Control Room HVAC; and WO1107582, Replace Unit 2 DGCWP Alternate Feed Contactor. These activities were selected based upon the structure, system, or component's ability to impact risk.  The inspectors evaluated these activities for the following (as applicable):
      IP 71111.11, Licensed Operator Requalification Program. The documents reviewed
the effect of testing on the plant had been adequately addressed; testing was adequate
      during this inspection are listed in the Attachment to this report.
for the maintenance performed; acceptance criteria were clear and demonstrated
      This inspection constituted one inspection sample as defined in IP 71111.11.
operational readiness; test instrumentation was appropriate; tests were performed as
  b. Findings
written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion); and test
      No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12)
  .1   Routine Quarterly Evaluations (71111.12Q)
  a. Inspection Scope
      The inspectors evaluated degraded performance issues involving the following
      risk-significant systems:
      *      Z2900; Safe Shutdown Makeup Pump, and
      *      Z4700; Instrument Air.
      The inspectors reviewed events such as where ineffective equipment maintenance had
      resulted in valid or invalid automatic actuations of engineered safeguards systems and
      independently verified the licensee's actions to address system performance or condition
      problems in terms of the following:
      *      implementing appropriate work practices;
      *      identifying and addressing common cause failures;
      *      scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
      *      characterizing system reliability issues for performance;
      *      charging unavailability for performance;
      *      trending key parameters for condition monitoring;
      *      ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
      *      verifying appropriate performance criteria for SSCs/functions classified as (a)(2)
              or appropriate and adequate goals and corrective actions for systems classified
              as (a)(1).
      The inspectors assessed performance issues with respect to the reliability, availability,
      and condition monitoring of the system. In addition, the inspectors verified maintenance
      effectiveness issues were entered into the CAP with the appropriate significance
      characterization. Documents reviewed are listed in the Attachment to this report.
      This inspection constituted two quarterly maintenance effectiveness samples as defined
      in IP 71111.12-05.
  b. Findings
      No findings of significance were identified.
                                                11                                      Enclosure


documentation was properly evaluated.  The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements.  In addition, the inspectors
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
reviewed corrective action documents associated with post-maintenance tests to
  .1   Maintenance Risk Assessments and Emergent Work Control
determine whether the licensee was identifying problems and entering them in the CAP
  a. Inspection Scope
and that the problems were being corrected commensurate with their importance to
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
safety.  Documents reviewed are listed in the Attachment to this report. 
      maintenance and emergent work activities affecting risk-significant and safety-related
  14 Enclosure This inspection constituted five post-maintenance testing samples as defined in
      equipment listed below to verify that the appropriate risk assessments were performed
IP 71111.19-05. b. Findings
      prior to removing equipment for work:
  No findings of significance were identified1R22 Surveillance Testing (71111.22) .1 Surveillance Testing
      *        Work Week 45 - 1A residual heat removal (RHR) room cooler, 1A RHR service
a. Inspection Scope
              water (RHRSW) loop, 1B RHR seal cooler, 1-1001-16A boroscope and Votes
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural
              testing, 1-1001-37A MOV equipment qualification inspection; and
and TS requirements:   QCOS 1400-01, 2A Core Spray Pump Performance Test (IST);  QCIS 0300-02, Unit 1 Division 1 Scram Discharge Volume Calibration and Functional Test (Routine);  QCOS 7500-05, 1/2 'B' Standby Gas Treatment Operability Test (Routine);  QCOS 1600-07, Reactor Coolant Leakage in the Drywell (RCS); QCEMS 0230-11, Modified Performance Test of Unit 1(2) 125 Vdc Normal or
      *        Work Week 51 - Unit 1 250 Vdc battery reconfiguration using Unit 1 125 Vdc
Alternate Battery (Routine); and   QCOS 6900-14, Station Battery Allowable Value Verification Surveillance (Routine).   The inspectors observed in plant activities and reviewed procedures and associated records to determine the following:    did preconditioning occur;  were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;  were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;  plant equipment calibration was correct, accurate, and properly documented;  as-left setpoints were within required ranges, and the calibration frequency were in accordance with TS, the UFSAR, procedures, and applicable commitments;  measuring and test equipment calibration was current;  test equipment was used within the required range and accuracy, applicable prerequisites described in the test procedures were satisfied;  test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other
              alternate battery with emergent Unit 2 125 Vdc battery low specific gravity
applicable procedures, jumpers and lifted leads were controlled and restored
              problems, 2A RHR loop and 2B RHRSW pump unavailability.
where used;  test data and results were accurate, complete, within limits, and valid;  test equipment was removed after testing;  where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of 
      These activities were selected based on their potential risk significance relative to the
  15 Enclosure Mechanical Engineers code, and reference values were consistent with the  
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
system design basis;  where applicable, test results not meeting acceptance criteria were addressed
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
with an adequate operability evaluation or the system or component was declared inoperable;  where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;  where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;  prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;  equipment was returned to a position or status required to support the performance of its safety functions; and all problems identified during the testing were appropriately documented and dispositioned in the CAP.  Documents reviewed are listed in the Attachment to this report.  This inspection constituted four routine surveillance testing samples, one inservice testing sample, and one reactor coolant system leak detection inspection samples as  
      and complete. When emergent work was performed, the inspectors verified that the
defined in IP 71111.22, Sections -02 and -05.   b. Findings
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
No findings of significance were identified.   1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) .1 Emergency Action Level and Emergency Plan Changes
      of maintenance work, discussed the results of the assessment with the licensee's
a. Inspection Scope
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
Since the last NRC inspection of this program area, Emergency Plan Annex, Revisions 26 and 27 were implemented based on the licensee's determination, in accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the Plan, and that the revised Plan as changed continues to meet the
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50.  The inspectors  
      walked down portions of redundant safety systems, when applicable, to verify risk
conducted a sampling review of the Emergency Plan changes and a review of the
      analysis assumptions were valid and applicable requirements were met.
Emergency Action Level (EAL) changes to evaluate for potential decreases in effectiveness of the Plan.  However, this review does not constitute formal NRC approval
      These maintenance risk assessments and emergent work control activities constituted
of the changes.  Therefore, these changes remain subject to future NRC inspection in
      two samples as defined in IP 71111.13-05.
their entirety.  This emergency action level and emergency plan changes inspection constituted one sample as defined in IP 71114.04-05.   
  b. Findings
  16 Enclosure b. Findings
      No findings of significance were identified.
(1) Unresolved Item (URI) 05000254/2009005-01: "Changes to EAL HU6 Potentially Decrease the Effectiveness of the Plans without Prior NRC Approval"
1R15 Operability Evaluations (71111.15)
Introduction: The inspectors reviewed changes implemented to the Quad Cities Station Radiological Emergency Plan Annex EALs and EAL Basis.  In Revision 26, the licensee
.1   Operability Evaluations
changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection
  a. Inspection Scope
within the protected area boundary," by adding two statements.  The two changes added
      The inspectors reviewed the following issues:
to the EAL basis stated that if the alarm could not be verified by redundant control room
      *        IR 987904: 1A RHR Room Cooler Tube Sheet Has Pitting, and
or nearby fire panel indications, notification from the field that a fire exists starts the 15-minute classification and fire extinguishment clocks.  The second change stated the 15-minute period to extinguish the fire does not start until either the fire alarm is verified
      *        IR 994823: TS SR 3.8.4.8 Frequency Not Met.
to be valid by additional control room or nearby fire panel instrumentation, or upon
      The inspectors selected these potential operability issues based on the risk significance
notification of a fire from the field.  These statements conflict with the previous
      of the associated components and systems. The inspectors evaluated the technical
Quad Cities Station Annex, Revision 25, basis statements and potentially decrease the effectiveness of the Plans. 
      adequacy of the evaluations to ensure that TS operability was properly justified and the
Description: Quad Cities Station Radiological Emergency Plan Annex, Revision 25, EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of
      subject component or system remained available such that no unrecognized increase in
detection, or explosion, within the protected area boundary."  The threshold values for
                                                12                                        Enclosure
HU6 were, in part:  1) Fire in any Table H2 area not extinguished within 15 minutes of control room notification or verification of a control room alarm; or 2) Fire outside any Table H2 area with the potential to damage safety systems in any Table H2 area not
extinguished within 15 minutes
of control room notification or verification of a control room alarm. Table H2, Vital Areas, were identified as main control room, reactor
building, diesel generator rooms, 4 kilovolt switchgear area, battery rooms, 'B' train control room heating-ventilation and air conditioning, service water pumps, and turbine building cable tunnel. The basis defined fire as "combustion characterized by heat and light.  Sources of smoke such as slipping
drive belts or overheated electrical equipment do not constitute fires. Observation of flame is preferred but is not required if large
quantities of smoke and heat are observed."  The basis for Revision 25, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of this threshold is to address the magnitude and extent of fires that may be potentially significant precursors to damage to safety syst
ems. As used here, notification is visual observation and report by plant personnel or sensor alarm indication.  The 15-minute
period begins with a credible notification that a fire is occurring or indication of a valid fire
detection system alarm.  A verified alarm is assumed to be an indication of a fire unless
personnel dispatched to the scene disprove the alarm within the 15-minute period.  The report, however, shall not be required to verify the alarm.  The intent of the 15-minute period is to size the fire and discriminate against small fires that are readily extinguished (e.g., smoldering waste paper basket, etc.). 
Revision 26 of the Quad Cities Station Radiological Emergency Plan Annex, changed the threshold basis for EAL HU6 by adding the following two statements:  1)"If the alarm cannot be verified by redundant control room or nearby fire panel indications, notification
from the field that a fire exists starts the 15-minute classification and fire extinguishment
clocks," and 2) "The 15-minute period to extinguish the fire does not start until either the  
fire alarm is verified to be valid by utilization of additional control room or nearby fire panel instrumentation, or upon notification of a fire from the field." 
  17 Enclosure The two statements added to the basis in Revision 26 conflict with the Revision 25 threshold basis and initiating condition.  The changed threshold basis in Revision 26
could add an indeterminate amount of time to declaring an actual emergency until a person responded to the area of the fire and made a notification to the control room of a fire in the event that redundant control room or nearby fire panel indications were not


available.  
      risk occurred. The inspectors compared the operability and design criteria in the
Pending further review and verification by the NRC to determine if the changes to EAL
      appropriate sections of the TS and UFSAR to the licensees evaluations to determine
HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue was considered an unresolved item (URI 05000254/2009005-01; 05000265/2009005-01).  1EP6 Drill Evaluation (71114.06) .1 Emergency Preparedness Drill Observation
      whether the components or systems were operable. Where compensatory measures
a. Inspection Scope
      were required to maintain operability, the inspectors determined whether the measures
The inspectors evaluated the conduct of an after-hours licensee emergency drill on November 11, 2009, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities.  The
      in place would function as intended and were properly controlled. The inspectors
after-hours drill was preceded by an unannounced, after-hours drive-in drill. 
      determined, where appropriate, compliance with bounding limitations associated with the
The inspectors observed emergency response operations in the Technical Support
      evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
Center to determine whether the event classification, notifications, and protective action recommendations were performed in accordance with procedures.  The inspectors also attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify
      documents to verify that the licensee was identifying and correcting any deficiencies
whether the licensee staff was properly identifying weaknesses and entering them into the corrective action program. As part of the inspection, the inspectors reviewed the drill
      associated with operability evaluations. Documents reviewed are listed in the
package and other documents listed in the Attachment to this report.  This emergency preparedness drill inspection constituted one sample as defined in
      Attachment to this report.
IP 71114.06-05.  b. Findings
      This operability inspection constituted two samples as defined in IP 71111.15-05.
No findings of significance were identified.   .2 Emergency Preparedness Termination and Recovery Drill Observation
  b. Findings
a. Inspection Scope
      No findings of significance were identified.
The inspectors evaluated the conduct of an emergency preparedness termination and recovery drill on December 2, 2009, to identify any weaknesses and deficiencies in the
1R19 Post-Maintenance Testing (71111.19)
conduct of the drill and to assess the licensee's ability to assess performance via a
.1   Post-Maintenance Testing
formal critique process in order to identify and correct Emergency Preparedness
  a. Inspection Scope
weaknesses. The inspectors observed emergency response operations in the Technical Support Center to determine whether the recovery and termination activities associated with the drill were performed in accordance with procedures.  The inspectors also  
      The inspectors reviewed the following post-maintenance activities to verify that
attended the licensee drill critique to compare any inspector-observed weakness with those identified by the licensee staff in order to evaluate the critique and to verify  
      procedures and test activities were adequate to ensure system operability and functional
whether the licensee staff was properly identifying weaknesses and entering them into 
      capability:
  18 Enclosure the corrective action program. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment to this report.   This emergency preparedness drill inspection constituted one sample as defined in  
      *      WO 1121775, 250 Vdc Battery Charger #2 4-Hour Load Test;
IP 71114.06-05.   b. Findings
      *      WO 1261246, Replace Battery Changeover Relay R12 EC 376690;
No findings of significance were identified.   4. OTHER ACTIVITIES 4OA1 Performance Indicator Verification (71151) .1 Mitigating Systems Performance Index -  
      *      QCMMS 4100-33, 1/2-4101B Diesel Driven Fire Pump Annual Capacity Test;
Emergency Alternating Current Power System
      *      WO 1130535, OP PMT Filter B Train Control Room HVAC; and
a. Inspection Scope
      *      WO1107582, Replace Unit 2 DGCWP Alternate Feed Contactor.
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index (MSPI) - Emergency Alternating
      These activities were selected based upon the structure, system, or component's ability
Current (AC) Power System performance indicator for Quad Cities Units 1 and 2 for the period from the 4th quarter 2008 through
      to impact risk. The inspectors evaluated these activities for the following (as applicable):
the 3rd quarter 2009.  To determine the accuracy of the performance indicator (PI) data reported during those periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator
      the effect of testing on the plant had been adequately addressed; testing was adequate
Guideline," Revision 6, were used.  The inspectors reviewed the licensee's operator
      for the maintenance performed; acceptance criteria were clear and demonstrated
narrative logs, MSPI derivation reports, issue reports, event reports and NRC integrated
      operational readiness; test instrumentation was appropriate; tests were performed as
inspection reports for the period of October 1, 2008, through September 30, 2009, to validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the
      written in accordance with properly reviewed and approved procedures; equipment was
previous inspection, and if so, that the change was in accordance with applicable
      returned to its operational status following testing (temporary modifications or jumpers
guidance.  The inspectors also reviewed the licensee's issue report database to
      required for test performance were properly removed after test completion); and test
determine if any problems had been identified with the PI data collected or transmitted
      documentation was properly evaluated. The inspectors evaluated the activities against
for this indicator, and none were identified.  Documents reviewed are listed in the Attachment to this report.  This inspection constituted two MSPI emergency AC power system samples as defined
      TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
in IP 71151-05.  b. Findings
      NRC generic communications to ensure that the test results adequately ensured that the
No findings of significance were identified.  .2 Mitigating Systems Performance Index - High Pressure Injection Systems
      equipment met the licensing basis and design requirements. In addition, the inspectors
a. Inspection Scope
      reviewed corrective action documents associated with post-maintenance tests to
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - High Pressure Injection Systems performance indicator for Quad Cities Units 1  
      determine whether the licensee was identifying problems and entering them in the CAP
and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009.  To
      and that the problems were being corrected commensurate with their importance to
determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory Assessment Performance 
      safety. Documents reviewed are listed in the Attachment to this report.
  19 Enclosure Indicator Guideline," Revision 6, were used. The inspectors reviewed the licensee's
                                                13                                      Enclosure
operator narrative logs, issue reports, M
SPI derivation reports, event reports and NRC integrated inspection reports for the period of October 1, 2008, through September 30, 2009, to validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more
than 25 percent in value since the previous inspection, and if so, that the change was in
accordance with applicable guidance.  The inspectors also reviewed the licensee's issue
report database to determine if any problems had been identified with the PI data
collected or transmitted for this indicator, and none were identified. Documents reviewed are listed in the Attachment to this report.  This inspection constituted two MSPI high pressure injection system samples as defined
in IP 71151-05.  b. Findings
No findings of significance were identified.  .3 Mitigating Systems Performance Index - Heat Removal System
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Heat Removal System performance indicator for Quad Cities Units 1 and 2 for
the period from the 4th quarter 2008 through the 3rd quarter 2009.  To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, "Regulatory Assessment Performance Indicator
Guideline," Revision 6, were used.  The inspectors reviewed the licensee's operator
narrative logs, issue reports, event reports, MSPI derivation reports, and NRC integrated
inspection reports for the period of October 1, 2008, through September 30, 2009, to
validate the accuracy of the submittals.  The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable
guidance.  The inspectors also reviewed the licensee's issue report database to  
determine if any problems had been identified with the PI data collected or transmitted
for this indicator, and none were identified.  Documents reviewed are listed in the Attachment to this report.  This inspection constituted two MSPI heat removal system samples as defined in
IP 71151-05.   b. Findings
No findings of significance were identified.  .4 Mitigating Systems Performance Index - Residual Heat Removal System
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Residual Heat Removal System performance indicator for Quad Cities Units 1 
  20 Enclosure and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009.  To determine the accuracy of the PI data reported during those periods, the PI definitions
and guidance contained in the NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, were used.  The inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated inspection reports for the period of October 1, 2008, through
September 30, 2009, to validate the accuracy of the submittals.  The inspectors
reviewed the MSPI component risk coefficient to determine if it had changed by more
than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable guidance.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data
collected or transmitted for this indicator, and none were identified.  Documents
reviewed are listed in the Attachment to this report.  This inspection constituted two MSPI residual heat removal system samples as defined
in IP 71151-05.  b. Findings
No findings of significance were identified.  .5 Mitigating Systems Performanc
e Index - Cooling Water Systems
a. Inspection Scope
The inspectors sampled licensee submittals for the Mitigating Systems Performance Index - Cooling Water Systems performance indicator for Quad Cities Units 1 and 2 for
the period from the 4th quarter 2008 through the 3rd quarter 2009.  To determine the
accuracy of the PI data reported during those periods, PI definitions and guidance
contained in the NEI Document 99-02, "Regulatory Assessment Performance Indicator
Guideline," Revision 6, were used.  The inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated inspection reports for the period of October 1, 2008, through September 30, 2009, to
validate the accuracy of the submittals.  The inspectors reviewed the MSPI component
risk coefficient to determine if it had changed by more than 25 percent in value since the  
previous inspection, and if so, that the change was in accordance with applicable guidance.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted
for this indicator, and none were identified. Documents reviewed are listed in the  
Attachment to this report.   This inspection constituted two MSPI cooling water system samples as defined in
IP 71151-05.  b. Findings
No findings of significance were identified.   
  21 Enclosure .6 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
Radiological Effluent Occurrences
a. Inspection Scope
The inspectors sampled licensee submittals for the Radiological Effluent Technical Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent
Occurrences performance indicator for the period of December 2008 through
November 2009.  The inspectors used PI definitions and guidance contained in the
NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline,"


Revision 6 to determine the accuracy of the PI data reported during those periods.  The inspectors reviewed the licensee's issue report database and selected individual reports generated since this indicator was last reviewed to identify any potential
      This inspection constituted five post-maintenance testing samples as defined in
occurrences such as unmonitored, uncontrolled, or improperly calculated effluent
      IP 71111.19-05.
releases that may have impacted offsite dose.  The inspectors reviewed gaseous
  b. Findings
effluent summary data and the results of associated offsite dose calculations for selected dates between December 2008 and November 2009 to determine if indicator results were accurately reported.  The inspectors also reviewed the licensee's methods for
      No findings of significance were identified.
quantifying gaseous and liquid effluents and determining effluent dose.  Documents
1R22 Surveillance Testing (71111.22)
reviewed are listed in the Attachment to this report.  This inspection constituted one RETS/ODCM radiological effluent occurrences sample
  .1   Surveillance Testing
as defined in IP 71151-05.   b. Findings
  a. Inspection Scope
No findings of significance were identified.   4OA2 Identification and Resolution of Problems (71152) Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection .1 Routine Review of Items Entered into the Corrective Action Program (CAP)
      The inspectors reviewed the test results for the following activities to determine whether
a. Inspection Scope
      risk-significant systems and equipment were capable of performing their intended safety
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's CAP at an appropriate threshold, that adequate attention was being given to timely corrective
      function and to verify testing was conducted in accordance with applicable procedural
actions, and that adverse trends were identified and addressed.  Attributes reviewed
      and TS requirements:
included:  the complete and accurate identification of the problem; that timeliness was  
      *      QCOS 1400-01, 2A Core Spray Pump Performance Test (IST);
commensurate with the safety significance; that evaluation and disposition of
      *      QCIS 0300-02, Unit 1 Division 1 Scram Discharge Volume Calibration and
performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective
              Functional Test (Routine);
actions were commensurate with safety and sufficient to prevent recurrence of the issue. 
      *      QCOS 7500-05, 1/2 B Standby Gas Treatment Operability Test (Routine);
Minor issues entered into the licensee's CAP as a result of the inspectors' observations
      *      QCOS 1600-07, Reactor Coolant Leakage in the Drywell (RCS);
are included in the attached List of Documents Reviewed.   
      *      QCEMS 0230-11, Modified Performance Test of Unit 1(2) 125 Vdc Normal or
  22 Enclosure These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples.  Instead, by procedure they were considered an
              Alternate Battery (Routine); and
integral part of the inspections performed during the quarter and documented in Section 1 of this report.  b. Findings
      *      QCOS 6900-14, Station Battery Allowable Value Verification Surveillance
No findings of significance were identified.  .2 Daily Corrective Action Program Reviews
              (Routine).
a. Inspection Scope
      The inspectors observed in plant activities and reviewed procedures and associated
In order to assist with the identification of repetitive equipment failures and specific human performance issues for followup, the inspectors performed a daily screening of items entered into the licensee's CAP. This review was accomplished through
      records to determine the following:
inspection of the station's daily condition report packages. These daily reviews were performed by procedure as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.  b. Findings
      *      did preconditioning occur;
No findings of significance were identified. .3 Semi-Annual Trend Review
      *      were the effects of the testing adequately addressed by control room personnel
a. Inspection Scope
              or engineers prior to the commencement of the testing;
The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue.  The
      *      were acceptance criteria clearly stated, demonstrated operational readiness, and
inspectors' review was focused on repetitive equipment issues and associated corrective
              consistent with the system design basis;
actions, but also considered the results of daily inspector CAP item screening discussed
      *      plant equipment calibration was correct, accurate, and properly documented;
in Section 4OA2.2 above, licensee trending efforts, and licensee human performance
      *      as-left setpoints were within required ranges, and the calibration frequency were
results.  The inspectors' review nominally considered the 6-month period of
              in accordance with TS, the UFSAR, procedures, and applicable commitments;
January 1, 2009, through June 30, 2009, although some examples expanded beyond those dates where the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental
      *      measuring and test equipment calibration was current;
problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments.  The inspectors compared and contrasted their results with the results contained in the licensee's
      *      test equipment was used within the required range and accuracy, applicable
CAP trending reports.  Corrective actions associated with a sample of the issues
              prerequisites described in the test procedures were satisfied;
identified in the licensee's trending reports were reviewed for adequacy.  Additionally,  
      *      test frequencies met TS requirements to demonstrate operability and reliability;
the inspectors reviewed CAP open priority 1, 2, and 3 corrective actions for timeliness. 
              tests were performed in accordance with the test procedures and other
In addition, all open priority 4 action tracking items (ACITs) were reviewed to ensure they were properly categorized and that the justifications for extension were appropriate and  
              applicable procedures, jumpers and lifted leads were controlled and restored
properly documented.   
              where used;
  23 Enclosure This review constituted a single semi-annual trend inspection sample as defined in
      *      test data and results were accurate, complete, within limits, and valid;
IP 71152-05.  b. Findings
      *      test equipment was removed after testing;
No findings of significance were identified.  .4 Selected Issue Followup Inspection:  Issue Report 966501, "Darley Pump Leaking Gasoline from the Fuel Pump"
      *      where applicable for inservice testing activities, testing was performed in
a. Inspection Scope
              accordance with the applicable version of Section XI, American Society of
During a review of items entered in the licensee's CAP, the inspectors followed up on a corrective action item documenting gasoline leaking from the fuel pump of the portable emergency flooding pump (Darley pump) on September 17, 2009, during preparations for a pump capacity demonstration run.  The pump capacity demonstration was a new
                                              14                                      Enclosure
procedure developed in response to a non-cited violation (NCV) documented in
Inspection Report 05000254/2007005.  This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05.  b. Findings
Introduction:  A finding of very low safety significance was self-revealed
for the failure to maintain the portable emergency flooding pump and supporting equipment in a condition
required to support implementation of QCOA 0010-16, "Flood Emergency Procedure."
Description:  In Inspection Report 05000254/2007005, inspectors documented a NCV of TS 5.4.1 for the licensee's failure to develop adequate surveillance procedures for
equipment used during an external flooding event.  Corrective action for this issue
included revising the external flooding procedure and developing and implementing a
procedure to test a portable pump used as the sole source of makeup water to the spent


fuel pool following an external flooding event.  The action to develop and implement the pump test procedure was issued in May and stated, "Develop test procedure and conduct test to confirm flow of greater than or equal to 200 gpm by mid-JulyBrief
              Mechanical Engineers code, and reference values were consistent with the
NRC Resident as appropriate.The action was closed to an Engineering Change (EC)  
              system design basis;
366481, on July 18, 2007, with no actual test performed.   The documented justification
      *      where applicable, test results not meeting acceptance criteria were addressed
              with an adequate operability evaluation or the system or component was
              declared inoperable;
      *      where applicable for safety-related instrument control surveillance tests,
              reference setting data were accurately incorporated in the test procedure;
      *      where applicable, actual conditions encountering high resistance electrical
              contacts were such that the intended safety function could still be accomplished;
      *      prior procedure changes had not provided an opportunity to identify problems
              encountered during the performance of the surveillance or calibration test;
      *      equipment was returned to a position or status required to support the
              performance of its safety functions; and
      *      all problems identified during the testing were appropriately documented and
              dispositioned in the CAP.
      Documents reviewed are listed in the Attachment to this report.
      This inspection constituted four routine surveillance testing samples, one inservice
      testing sample, and one reactor coolant system leak detection inspection samples as
      defined in IP 71111.22, Sections -02 and -05.
  b. Findings
      No findings of significance were identified.
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
  .1  Emergency Action Level and Emergency Plan Changes
  a. Inspection Scope
      Since the last NRC inspection of this program area, Emergency Plan Annex,
      Revisions 26 and 27 were implemented based on the licensees determination, in
      accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in
      effectiveness of the Plan, and that the revised Plan as changed continues to meet the
      requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors
      conducted a sampling review of the Emergency Plan changes and a review of the
      Emergency Action Level (EAL) changes to evaluate for potential decreases in
      effectiveness of the Plan. However, this review does not constitute formal NRC approval
      of the changes. Therefore, these changes remain subject to future NRC inspection in
      their entirety.
      This emergency action level and emergency plan changes inspection constituted one
      sample as defined in IP 71114.04-05.
                                                15                                    Enclosure


for this closure stated that discussions with the NRC resident clarified the intent of the action and no physical testing needed to be performedFollowup discussions with the resident inspectors stationed at Quad Cities in July 2007 had no recollection of the
bFindings
conversation and their understanding of the intended action remained unchanged from
(1) Unresolved Item (URI) 05000254/2009005-01: Changes to EAL HU6 Potentially
the original report. Licensee staff generated Issue Report (IR) 738335 in February 2008 to document the review of the NCV response and generate a closure package of all related IRs.  The lack of preventative maintenance (PM) testing was identified and an action tracking item was
    Decrease the Effectiveness of the Plans without Prior NRC Approval
generated to "Develop PM/testing requirements for the Darley pump associated with the  
    Introduction: The inspectors reviewed changes implemented to the Quad Cities Station
external flooding event."  The original corrective action due date was July 16, 2008.  The action was extended several times, and on May 18, 2009, during a review of
    Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 26, the licensee
corrective actions for NRC-identified issues, the licensee staff identified that a CAP 
    changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection
  24 Enclosure action item (ACIT 624645-03) had been inappropriately closed. In addition, the licensee determined that ACIT 624645-03 was inappropriately tagged as an Action Tracking Item
    within the protected area boundary, by adding two statements. The two changes added
(ACIT) and should have been a corrective action.  Issue Report 921197 was generated and ACIT 624645 was upgraded to a corrective action with a July 31, 2009, due date.  The test procedure was developed and the pump was scheduled to run on
    to the EAL basis stated that if the alarm could not be verified by redundant control room
September 17, 2009. The capacity test was implemented with WO 01247374.  When mechanics pulled the pump and support components from the storage location, they found that the engine
    or nearby fire panel indications, notification from the field that a fire exists starts the
battery had to be replaced and the gasoline stored with the motor had to be replaced.  Since the mechanics performing the test had never operated the pump, they decided to run it in the weld shop before taking it down to the river.  When the mechanics started
    15-minute classification and fire extinguishment clocks. The second change stated the
the pump, fuel was spraying out of the fuel pump.  They immediately shut down the  
    15-minute period to extinguish the fire does not start until either the fire alarm is verified
pump and contained the fuel leak (IR 966501).   The Darley pump fuel system was repaired and the capacity test was completed satisfactorily on September 25, 2009.  Review of recent pump operating history and PM tasks revealed that the pump had not been operated since the NCV was identified in
    to be valid by additional control room or nearby fire panel instrumentation, or upon
2007.  The annual maintenance performed under PM 164250 in July of 2009 changed
    notification of a fire from the field. These statements conflict with the previous
the oil and inspected the filters and spark plugs with no post-maintenance operation
    Quad Cities Station Annex, Revision 25, basis statements and potentially decrease the
required.  The PM also failed to identify that the battery was beyond the expected life and did not determine that the battery would maintain its charge. 
    effectiveness of the Plans.
Analysis:  The inspectors determined that the failure to perform maintenance that would ensure the pump was in a standby condition and readily available to accomplish the
    Description: Quad Cities Station Radiological Emergency Plan Annex, Revision 25,
requirements of QCOA 0010-16 was a performance deficiency fully within the licensee's ability to control, and therefore a finding. This issue was more than minor because it
    EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of
was associated with the SSC Performance attribute of the Barrier Integrity Cornerstone element of maintaining the functionality of spent fuel pool cooling. The finding affected the cornerstone objective of providing assurance that physical design barriers protect the
    detection, or explosion, within the protected area boundary." The threshold values for
public from radionuclide releases caused by events including external flooding. 
    HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of
Specifically, the pump could fail due to
    control room notification or verification of a control room alarm; or 2) Fire outside any
a maintenance preventable component failure resulting in inadequate or degraded makeup to the spent fuel pool during an external flooding event. The inspectors did not identify a cross-cutting aspect associated with this finding because the maintenance issue is a legacy issue and not reflective of current
    Table H2 area with the potential to damage safety systems in any Table H2 area not
licensee performance. The pump and PM tasks had been in place for several years. 
    extinguished within 15 minutes of control room notification or verification of a control
Inspectors reviewed maintenance requirements for other temporary equipment staged in
    room alarm. Table H2, Vital Areas, were identified as main control room, reactor
support of external events and emergency operating procedures, some of which was put
    building, diesel generator rooms, 4 kilovolt switchgear area, battery rooms, B train
in place after the Darley pump was staged, and did not identify any similar issues.  The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 -  
    control room heating-ventilation and air conditioning, service water pumps, and turbine
Initial Screening and Characterization of findings," Tables 4a and 4b.  The inspectors
    building cable tunnel. The basis defined fire as "combustion characterized by heat and
determined that even though this equipment is assumed to completely fail, the licensee
    light. Sources of smoke such as slipping drive belts or overheated electrical equipment
could provide an alternate portable pump already located on site and capable of performing the safety function during this
    do not constitute fires. Observation of flame is preferred but is not required if large
slow developing event. The alternate pump had maintenance and test procedures in place to provide a basis for reliability. Since
    quantities of smoke and heat are observed."
alternate equipment was available and the delay in mobilizing the alternate equipment  
    The basis for Revision 25, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of
would not have resulted in loss of capability to mitigate the impact of the flooding event,
    this threshold is to address the magnitude and extent of fires that may be potentially
the issue is of very low safety significance or Green.  
    significant precursors to damage to safety systems. As used here, notification is visual
  25 Enclosure
    observation and report by plant personnel or sensor alarm indication. The 15-minute
Enforcement:  Technical Specification 5.4.1 required that written procedures be established, implemented, and maintained for the items specified in Regulatory
    period begins with a credible notification that a fire is occurring or indication of a valid fire
Guide 1.33, "Quality Assurance Program Requirements."  QCOA 0010-16, "Flood Emergency Procedure," was the licensee procedure used to meet the Regulatory Guide 1.33 requirement for an emergency flooding event.  The procedure
    detection system alarm. A verified alarm is assumed to be an indication of a fire unless
specified that the portable pump staged in the protected area warehouse is to be used to  
    personnel dispatched to the scene disprove the alarm within the 15-minute period.
respond to the event. Although the regulatory guide did not specifically require
    The report, however, shall not be required to verify the alarm. The intent of the
maintenance procedures for portable equipment, failure to maintain the staged
    15-minute period is to size the fire and discriminate against small fires that are readily
equipment in a condition to be used to mitigate the event does not support timely implementation of the procedure to provide spent fuel pool makeup and is a finding.  Enforcement action does not apply because the performance deficiency did not involve a violation of a regulatory requirement. Because the finding does not involve a violation of  
    extinguished (e.g., smoldering waste paper basket, etc.).
regulatory requirements and has a very low safety significance, it is identified as
    Revision 26 of the Quad Cities Station Radiological Emergency Plan Annex, changed
(FIN 05000254/2009005-02; 05000265/2009005-02). The issue was added to the licensee's CAP program as IR 966501 and IR 968809. Immediate corrective actions included replacement of the degraded battery and overhaul of the pump's fuel pump. 
    the threshold basis for EAL HU6 by adding the following two statements: 1)"If the alarm
Other actions included identification of preventative maintenance tasks and establishing
    cannot be verified by redundant control room or nearby fire panel indications, notification
a program owner of the pump.   .5 Selected Issue Followup Inspection:  Incident Report 984769, "Temperature Indicating Probe Found Broken in the Unit 2 Diesel Generator Coolant System"
    from the field that a fire exists starts the 15-minute classification and fire extinguishment
a. Inspection Scope
    clocks," and 2) "The 15-minute period to extinguish the fire does not start until either the
During a review of items entered in the licensee's CAP, the inspectors followed up on a corrective action item documenting a failed temperature indicating probe (TI) in the Unit 2 diesel generator coolant system on October 27, 2009, during planned
    fire alarm is verified to be valid by utilization of additional control room or nearby fire
maintenance on the Unit 2 emergency diesel generator (EDG).  This review constituted one in-depth problem identification and resolution sample as defined in IP 71152-05.  b. Findings
    panel instrumentation, or upon notification of a fire from the field."
Introduction:  A finding of very low safety significance and associated NCV were self-revealed when a TI failed in the Unit 2 diesel generator coolant system.
                                                16                                        Enclosure
Description:  On October 27, 2009, while performing corrective maintenance on TI 2-6641-8205, technicians noted that the tip had broken off the probe when comparing
it to the length of the new TI.  This TI provides local indication of the jacket coolant water
temperature at the inlet to the diesel engine and provides no alarm function.  The TI was scheduled for replacement in October 2008 when Operations identified the TI reading abnormally at zero degrees.  A work order was written and scheduled for October 2009.  During the performance of the maintenance, it was noted that the new TI was longer than the one recently removed.  A new work order was written to retrieve any
foreign material from the system. The broken tip was recovered from the diesel
generator coolant system.   
  26 Enclosure The licensee investigation discovered that the installation analysis for this TI was approved under the non-safety below level of design detail (NSBLD) process in October


2007 under Revision 3 of SM-AA-300, "Procurement Engineering Support Activities."  Using this provision, "NSBLD changes must be documented and shall identify the change with justification of the change's technical acceptability.The length of the probe
      The two statements added to the basis in Revision 26 conflict with the Revision 25
was the only difference to the previously installed TI.  The TI was installed with a  
      threshold basis and initiating condition. The changed threshold basis in Revision 26
3.25 inch probe, which was longer than the previous 2 inch probe. The added length
      could add an indeterminate amount of time to declaring an actual emergency until a
increased the shear force from the coolant flow and caused the probe to break off.   An operating experience (OPEX) review would have revealed an event at another nuclear facility where the same make
      person responded to the area of the fire and made a notification to the control room of a
and model TI experienced the same failure mechanism in a diesel generator coolant system. Under Revision 3 of SM-AA-300, OPEX reviews for NSBLD were not required, nor were additional peer reviews required.
      fire in the event that redundant control room or nearby fire panel indications were not
The lack of an OPEX review was an identified vulnerability by the licensee's corporate
      available.
supply organization in a common cause analysis which was performed for a lack of technical rigor issued in February 2008.  A corrective action from this common cause analysis was to implement Revision 4 of SM-AA-300 which limited NSBLD reviews to  
      Pending further review and verification by the NRC to determine if the changes to EAL
non-safety host component applications. Revi
      HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue was
sion 4 was implemented at Quad Cities in February 2008. Since this specific TI is classified as "augmented quality," Revision 4
      considered an unresolved item (URI 05000254/2009005-01; 05000265/2009005-01).
would prevent use of the NSBLD process of a non-identical replacementA full item equivalency evaluation would be required for any non-identical replacementAn extent of condition review is scheduled to be performed at Quad Cities by Procurement Engineering for all NSBLD reviews that were performed under Revision 3
1EP6 Drill Evaluation (71114.06)
of SM-AA-300 from August 2007 through February 2008.  
.1  Emergency Preparedness Drill Observation
Analysis:  The inspectors determined that the approval of an inappropriate component designated as "augmented quality" was a performance deficiency and a finding.  The same parts evaluation process was used for risk-significant components independent of the system being worked.  Therefore, this finding was more than minor because, if left
  a. Inspection Scope
uncorrected, this performance deficiency could lead to unplanned unavailability of  
      The inspectors evaluated the conduct of an after-hours licensee emergency drill on
safety-related or risk-significant equipment and would become a more significant safety
      November 11, 2009, to identify any weaknesses and deficiencies in classification,
concern.  This performance deficiency challenged the Mitigating Systems Cornerstone attribute of Equipment Performance by challenging equipment availability and reliability.   The inspectors performed a Phase 1 SDP screening and concluded that the issue was of very low safety significance (Green) because the failure of the TI did not result in  
      notification, and protective action recommendation development activities. The
unplanned inoperability or loss of function of the diesel generator. The inspectors  
      after-hours drill was preceded by an unannounced, after-hours drive-in drill.
determined that this finding did not have a cross-cutting aspect.  This performance
      The inspectors observed emergency response operations in the Technical Support
deficiency is not indicative of current licensee performance.  The decision to install this
      Center to determine whether the event classification, notifications, and protective action
type of TI was made in October 2007.  The process which allowed this performance deficiency was identified and corrected through procedure and policy revisions to
      recommendations were performed in accordance with procedures. The inspectors also
      attended the licensee drill critique to compare any inspector-observed weakness with
      those identified by the licensee staff in order to evaluate the critique and to verify
      whether the licensee staff was properly identifying weaknesses and entering them into
      the corrective action program. As part of the inspection, the inspectors reviewed the drill
      package and other documents listed in the Attachment to this report.
      This emergency preparedness drill inspection constituted one sample as defined in
      IP 71114.06-05.
  b. Findings
      No findings of significance were identified.
  .2   Emergency Preparedness Termination and Recovery Drill Observation
  a. Inspection Scope
      The inspectors evaluated the conduct of an emergency preparedness termination and
      recovery drill on December 2, 2009, to identify any weaknesses and deficiencies in the
      conduct of the drill and to assess the licensees ability to assess performance via a
      formal critique process in order to identify and correct Emergency Preparedness
      weaknesses. The inspectors observed emergency response operations in the Technical
      Support Center to determine whether the recovery and termination activities associated
      with the drill were performed in accordance with procedures. The inspectors also
      attended the licensee drill critique to compare any inspector-observed weakness with
      those identified by the licensee staff in order to evaluate the critique and to verify
      whether the licensee staff was properly identifying weaknesses and entering them into
                                                17                                        Enclosure


SM-AA-300 in February 2008.  
      the corrective action program. As part of the inspection, the inspectors reviewed the drill
Enforcement:  The TI was designated "augmented quality" in the licensee's quality assurance program.  The licensee's quality assurance program applied controls equivalent to safety-related components for Class 1E equipment qualification to "augmented quality" equipment and systems. This correlation is applicable to several
      package and other documents listed in the Attachment to this report.
Appendix B criteria included in the program such as both Section 3 - "Design Control,"
      This emergency preparedness drill inspection constituted one sample as defined in
and Section 5 - "Instructions Procedures and Drawings," of the licensee's Quality
      IP 71114.06-05.
Assurance program for "augmented quality." 
  b. Findings
  27 Enclosure Title 10 CFR 50, Appendix B, Criterion V states in part that activities affecting quality shall be prescribed by instructions and procedures of a type appropriate to the  
      No findings of significance were identified.
circumstances and shall be accomplished in accordance with these instructions or procedures.   Contrary to the above, on October 30, 2007, SM-AA-300 was not appropriate to the circumstances in that it did not require an approval process with technical rigor
4.   OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
  .1  Mitigating Systems Performance Index - Emergency Alternating Current Power System
  a. Inspection Scope
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
      Index (MSPI) - Emergency Alternating Current (AC) Power System performance
      indicator for Quad Cities Units 1 and 2 for the period from the 4th quarter 2008 through
      the 3rd quarter 2009. To determine the accuracy of the performance indicator (PI) data
      reported during those periods, PI definitions and guidance contained in the Nuclear
      Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
      Guideline, Revision 6, were used. The inspectors reviewed the licensees operator
      narrative logs, MSPI derivation reports, issue reports, event reports and NRC integrated
      inspection reports for the period of October 1, 2008, through September 30, 2009, to
      validate the accuracy of the submittals. The inspectors reviewed the MSPI component
      risk coefficient to determine if it had changed by more than 25 percent in value since the
      previous inspection, and if so, that the change was in accordance with applicable
      guidance. The inspectors also reviewed the licensees issue report database to
      determine if any problems had been identified with the PI data collected or transmitted
      for this indicator, and none were identified. Documents reviewed are listed in the
      Attachment to this report.
      This inspection constituted two MSPI emergency AC power system samples as defined
      in IP 71151-05.
  b. Findings
      No findings of significance were identified.
.2  Mitigating Systems Performance Index - High Pressure Injection Systems
  a. Inspection Scope
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
      Index - High Pressure Injection Systems performance indicator for Quad Cities Units 1
      and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To
      determine the accuracy of the PI data reported during those periods, PI definitions and
      guidance contained in the NEI Document 99-02, Regulatory Assessment Performance
                                                18                                    Enclosure


equivalent to the process used for safety-related components when a non-identical
    Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees
temperature indicating probe designated "augmented quality" was approved for use. 
    operator narrative logs, issue reports, MSPI derivation reports, event reports and
That part was approved for use through a NSBLD review per Revision 3 of SM-AA-300 instead of undergoing a full item equivalency evaluation, and the part subsequently failed resulting in foreign material in the diesel generator coolant system. The foreign
    NRC integrated inspection reports for the period of October 1, 2008, through
material did not cause any adverse consequences in this instance.  Because this issue is of very low safety significance, and this issue has been entered into the licensee's corrective action program as Issue Report 984769, this issue is being
    September 30, 2009, to validate the accuracy of the submittals. The inspectors
treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000265/2009005-03).
    reviewed the MSPI component risk coefficient to determine if it had changed by more
Corrective actions for this event included replacement of the TI with an appropriately approved TI. The licensee has also scheduled to perform an extent of condition review
    than 25 percent in value since the previous inspection, and if so, that the change was in
of NSBLD reviews performed under Revision 3 of SM-AA-300 from August 2007 through
    accordance with applicable guidance. The inspectors also reviewed the licensees issue
February 2008.   4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) .1 (Closed) Licensee Event Report 05000254/2009-003-00:  "Failure of RHR Torus Spray Isolation Valve to Open Due to Declutch Mechanism Problems"
    report database to determine if any problems had been identified with the PI data
a. Inspection Scope
    collected or transmitted for this indicator, and none were identified. Documents
Inspectors reviewed the event, evaluation, and corrective actions for the motor operated valve failure reported in Licensee Event Report (LER) 05000254/2009-003.   Documents reviewed as part of this inspection are listed in the Attachment to this report. This LER is
    reviewed are listed in the Attachment to this report.
    This inspection constituted two MSPI high pressure injection system samples as defined
    in IP 71151-05.
  b. Findings
    No findings of significance were identified.
.3  Mitigating Systems Performance Index - Heat Removal System
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
    Index - Heat Removal System performance indicator for Quad Cities Units 1 and 2 for
    the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the
    accuracy of the PI data reported during those periods, PI definitions and guidance
    contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator
    Guideline, Revision 6, were used. The inspectors reviewed the licensees operator
    narrative logs, issue reports, event reports, MSPI derivation reports, and NRC integrated
    inspection reports for the period of October 1, 2008, through September 30, 2009, to
    validate the accuracy of the submittals. The inspectors reviewed the MSPI component
    risk coefficient to determine if it had changed by more than 25 percent in value since the
    previous inspection, and if so, that the change was in accordance with applicable
    guidance. The inspectors also reviewed the licensees issue report database to
    determine if any problems had been identified with the PI data collected or transmitted
    for this indicator, and none were identified. Documents reviewed are listed in the
    Attachment to this report.
    This inspection constituted two MSPI heat removal system samples as defined in
    IP 71151-05.
  b. Findings
    No findings of significance were identified.
.4  Mitigating Systems Performance Index - Residual Heat Removal System
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
    Index - Residual Heat Removal System performance indicator for Quad Cities Units 1
                                                19                                    Enclosure


closed.   This event follow-up review constituted one sample as defined in IP 71153-05.  b. Findings
    and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To
Introduction:  A finding of very low safety significance and an NCV of Technical Specification (TS) 3.6.2.4, "Residual Heat Removal (RHR) Suppression Pool Spray,"
    determine the accuracy of the PI data reported during those periods, the PI definitions
was self-revealed for the licensee's failure to meet the TS limiting condition for operation
    and guidance contained in the NEI Document 99-02, Regulatory Assessment
(LCO) requirements prior to transitioning into an operating mode where the LCO was
    Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the
required to be satisfied. Specifically, MO 1-1001-37B, motor operator for the Unit 1 RHR torus (suppression pool) spray isolation valve, was found to have been inoperable when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the valve
    licensees operator narrative logs, issue reports, MSPI derivation reports, event reports
was not demonstrated operable by stroking the valve electrically after the actuator motor
    and NRC integrated inspection reports for the period of October 1, 2008, through
    September 30, 2009, to validate the accuracy of the submittals. The inspectors
    reviewed the MSPI component risk coefficient to determine if it had changed by more
    than 25 percent in value since the previous inspection, and if so, that the change was in
    accordance with applicable guidance. The inspectors also reviewed the licensees issue
    report database to determine if any problems had been identified with the PI data
    collected or transmitted for this indicator, and none were identified. Documents
    reviewed are listed in the Attachment to this report.
    This inspection constituted two MSPI residual heat removal system samples as defined
    in IP 71151-05.
   b. Findings
    No findings of significance were identified.
.5  Mitigating Systems Performance Index - Cooling Water Systems
  a. Inspection Scope
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
    Index - Cooling Water Systems performance indicator for Quad Cities Units 1 and 2 for
    the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the
    accuracy of the PI data reported during those periods, PI definitions and guidance
    contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator
    Guideline, Revision 6, were used. The inspectors reviewed the licensees operator
    narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated
    inspection reports for the period of October 1, 2008, through September 30, 2009, to
    validate the accuracy of the submittals. The inspectors reviewed the MSPI component
    risk coefficient to determine if it had changed by more than 25 percent in value since the
    previous inspection, and if so, that the change was in accordance with applicable
    guidance. The inspectors also reviewed the licensees issue report database to
    determine if any problems had been identified with the PI data collected or transmitted
    for this indicator, and none were identified. Documents reviewed are listed in the
    Attachment to this report.
    This inspection constituted two MSPI cooling water system samples as defined in
    IP 71151-05.
  b. Findings
    No findings of significance were identified.
                                                20                                    Enclosure


was declutched.     
.6  Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
  28 Enclosure Discussion:  On June 4, 2009, with Unit 1 in Mode 1 at 100 percent power following startup from a forced outage, MO 1-1001-37B, torus spray shutoff valve, was determined
      Radiological Effluent Occurrences
to be  inoperable because it would not open remotely using the control switch during performance of the residual heat removal power operated valve test surveillance. The torus spray valve had been closed using the motor and a clearance order had been placed on the valve during the outage. Another motor operated valve in the residual
   a. Inspection Scope
heat removal system on that same clearance, MO 1-1001-7C, RHR 'C' torus suction line
      The inspectors sampled licensee submittals for the Radiological Effluent Technical
isolation valve, had failed to open on May 28, 2009, when the clearance tag was
      Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent
removed and valve stroking was being performed to restore the component to a standby configuration. Operators reported manually declutching (disengaging the actuator motor) the 7C valve while placing the clearance tag in order to verify the valve was
      Occurrences performance indicator for the period of December 2008 through
closed.  Inspectors identified that the action of manually verifying valve position was not
      November 2009. The inspectors used PI definitions and guidance contained in the
a normal practice as supported by OP-AA-103-105, "Limitorque Motor-Operated Valve
      NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
Operations," and Operations department management.  Investigation into the 7C failure revealed that the actuator lubricant was degraded in the area of the clutch return spring preventing the motor from engaging when called upon from the control circuit.  The
      Revision 6 to determine the accuracy of the PI data reported during those periods.
RHR 'C' valve actuator was rebuilt using MOV Long Life grease, new tripper cams, new
      The inspectors reviewed the licensees issue report database and selected individual
trip lever assembly, and a new outer declutch arm snap ring.  The rebuilt actuator was
      reports generated since this indicator was last reviewed to identify any potential
verified to operate correctly in all modes and returned to service prior to unit restart on May 30, 2009.  Inspectors interviewed operating personnel regarding the positioning of MO 1-1001-37B torus spray valve.  Operators stated that they did not manually declutch the 37B valve since the valve was already closed (normal position) when they hung the tag. The
      occurrences such as unmonitored, uncontrolled, or improperly calculated effluent
licensee's investigation attempted to identify both how the motor on the 37B valve was
      releases that may have impacted offsite dose. The inspectors reviewed gaseous
declutched and why the actuator did not return to the motor mode of operation automatically as designed. The licensee verified that the actuator was not able to transition from the motor mode to the manual mode without external (human)
      effluent summary data and the results of associated offsite dose calculations for selected
      dates between December 2008 and November 2009 to determine if indicator results
      were accurately reported. The inspectors also reviewed the licensees methods for
      quantifying gaseous and liquid effluents and determining effluent dose. Documents
      reviewed are listed in the Attachment to this report.
      This inspection constituted one RETS/ODCM radiological effluent occurrences sample
      as defined in IP 71151-05.
  b. Findings
      No findings of significance were identified.
4OA2 Identification and Resolution of Problems (71152)
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
      Physical Protection
.1  Routine Review of Items Entered into the Corrective Action Program (CAP)
  a. Inspection Scope
      As part of the various baseline inspection procedures discussed in previous sections of
      this report, the inspectors routinely reviewed issues during baseline inspection activities
      and plant status reviews to verify that they were being entered into the licensees CAP at
      an appropriate threshold, that adequate attention was being given to timely corrective
      actions, and that adverse trends were identified and addressed. Attributes reviewed
      included: the complete and accurate identification of the problem; that timeliness was
      commensurate with the safety significance; that evaluation and disposition of
      performance issues, generic implications, common causes, contributing factors, root
      causes, extent of condition reviews, and previous occurrences reviews were proper and
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
      Minor issues entered into the licensees CAP as a result of the inspectors observations
      are included in the attached List of Documents Reviewed.
                                                21                                        Enclosure


interventionAlthough the licensee could not identify how or when the valve actuator motor was declutched, the licensee's investigators concluded that the declutch lever was most likely bumped during work activities on top of the Torus during the recent outage with the unit in Mode 4. Investigation further determined that with the valve motor disengaged,  
    These routine reviews for the identification and resolution of problems did not constitute
increased friction in the actuator caused by degraded lubricant in the area of the clutch
    any additional inspection samples. Instead, by procedure they were considered an
return spring prevented the engagement of the motor to open the valve. The actuator
    integral part of the inspections performed during the quarter and documented in
motor was engaged by manually manipulating the declutch lever and stroke testing the
    Section 1 of this report.
   b. Findings
    No findings of significance were identified.
.2  Daily Corrective Action Program Reviews
  a. Inspection Scope
    In order to assist with the identification of repetitive equipment failures and specific
    human performance issues for followup, the inspectors performed a daily screening of
    items entered into the licensees CAP. This review was accomplished through
    inspection of the stations daily condition report packages.
    These daily reviews were performed by procedure as part of the inspectors daily plant
    status monitoring activities and, as such, did not constitute any separate inspection
    samples.
  b. Findings
    No findings of significance were identified.
.3  Semi-Annual Trend Review
  a. Inspection Scope
    The inspectors performed a review of the licensees CAP and associated documents to
    identify trends that could indicate the existence of a more significant safety issue. The
    inspectors review was focused on repetitive equipment issues and associated corrective
    actions, but also considered the results of daily inspector CAP item screening discussed
    in Section 4OA2.2 above, licensee trending efforts, and licensee human performance
    results. The inspectors review nominally considered the 6-month period of
    January 1, 2009, through June 30, 2009, although some examples expanded beyond
    those dates where the scope of the trend warranted.
    The review also included issues documented outside the normal CAP in major
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
    problem/challenges lists, system health reports, quality assurance audit/surveillance
    reports, self assessment reports, and Maintenance Rule assessments. The inspectors
    compared and contrasted their results with the results contained in the licensees
    CAP trending reports. Corrective actions associated with a sample of the issues
    identified in the licensees trending reports were reviewed for adequacy. Additionally,
    the inspectors reviewed CAP open priority 1, 2, and 3 corrective actions for timeliness.
    In addition, all open priority 4 action tracking items (ACITs) were reviewed to ensure they
    were properly categorized and that the justifications for extension were appropriate and
    properly documented.
                                                22                                    Enclosure


valveInspectors reviewed the grease sampling methodology and the preventative maintenance frequency for the SMP-00 type actuators and determined that both were  
    This review constituted a single semi-annual trend inspection sample as defined in
conducted in accordance with the industry standards for these type valves.   
    IP 71152-05.
Analysis:  The failure of plant personnel to demonstrate operability of MO 1-1001-37B by stroking the valve electrically prior to changing modes was a performance deficiency. The finding is more than minor because it was associated with the equipment performance quality attribute of the Mitigating Systems Cornerstone and affected the  
   b. Findings
objective of ensuring availability, reliability and capability of systems that respond to  
    No findings of significance were identified.
initiating events to prevent undesirable consequences. Specifically, failure to verify
.4   Selected Issue Followup Inspection: Issue Report 966501, Darley Pump Leaking
system availability and capability prior to entering the required modes resulted in fewer 
    Gasoline from the Fuel Pump
   29 Enclosure available mitigating systems than assumed in the operating risk evaluations. Inspectors determined that the finding was cross-cutting in the area of Problem Identification and
  a. Inspection Scope
Resolution - Corrective Action because plant personnel failed to identify the valve actuator contact that resulted in the valve being declutched; therefore, operators incorrectly assessed the system condition as in compliance with TS 3.6.2.4 (P.1(a)).  The inspectors determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 -
    During a review of items entered in the licensees CAP, the inspectors followed up on a
Initial Screening and Characterization of Findings," Table 4a.  Inspectors answered all of  
    corrective action item documenting gasoline leaking from the fuel pump of the portable
the questions for the Mitigating Systems Cornerstone "No."  Therefore, the finding screened as Green or very low safety significance. 
    emergency flooding pump (Darley pump) on September 17, 2009, during preparations
Enforcement:  Technical Specification 3.0, "Limiting Condition for Operation (LCO) Applicability," LCO 3.0.4 stated in part that when an LCO is not met, entry into a mode in
    for a pump capacity demonstration run. The pump capacity demonstration was a new
the Applicability shall only be made:    when the associated actions to be entered permit continued operation while in the mode or other specified condition in the Applicability for an unlimited time;  after performance of a risk assessment addressing inoperable systems and components, and acceptability of entering the mode; or when an allowance is stated in the specification.   Technical Specification 3.6.2.4, "Residual Heat Removal (RHR) Suppression Pool Spray," required two RHR suppression pool spray subsystems to be operable in
    procedure developed in response to a non-cited violation (NCV) documented in
Modes 1, 2 and 3.  Contrary to the above, on May 30, 2009, the licensee changed operating modes from Mode 4 to Mode 2 with the MO 1-1001-37B valve inoperable in violation of TS 3.6.2.4
    Inspection Report 05000254/2007005.
LCO conditions since only one RHR suppression pool (Torus) spray subsystem was operable.  Specifically, TS 3.6.2.4 had no allowance provided to permit mode change with less than two subsystems operable, no prior risk assessment was performed, and the specification did not permit operation for an unlimited time, the mode change
    This review constituted one in-depth problem identification and resolution sample as
resulted in non-compliance with TS LCO 3.6.2.4.  Because this finding is of very low safety significance, and this issue has been entered into the licensee's corrective action program as IR 928048, this violation is being treated
    defined in IP 71152-05.
as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000254/2009005-04).  Immediate corrective actions for this event included engagement of the actuator motor by manually manipulating the declutch lever and stroke testing the valve. Since the
   b. Findings
hardened grease in this area of the actuator assembly was only an issue if the actuator
    Introduction: A finding of very low safety significance was self-revealed for the failure to
was manually declutched, the valve was left in standby, and overhaul of the valve actuator was scheduled for the next refueling outage.   
    maintain the portable emergency flooding pump and supporting equipment in a condition
  30 Enclosure 4OA5 Other Activities
    required to support implementation of QCOA 0010-16, Flood Emergency Procedure.
.1 World Association of Nuclear Operators Plant Assessment Report Review
    Description: In Inspection Report 05000254/2007005, inspectors documented a NCV of
a. Inspection Scope
    TS 5.4.1 for the licensees failure to develop adequate surveillance procedures for
The inspectors reviewed the final report for the World Association of Nuclear Operators plant assessment conducted in February 2009.  The inspectors reviewed the report to
    equipment used during an external flooding event. Corrective action for this issue
    included revising the external flooding procedure and developing and implementing a
    procedure to test a portable pump used as the sole source of makeup water to the spent
    fuel pool following an external flooding event. The action to develop and implement the
    pump test procedure was issued in May and stated, Develop test procedure and
    conduct test to confirm flow of greater than or equal to 200 gpm by mid-July. Brief
    NRC Resident as appropriate. The action was closed to an Engineering Change (EC)
    366481, on July 18, 2007, with no actual test performed. The documented justification
    for this closure stated that discussions with the NRC resident clarified the intent of the
    action and no physical testing needed to be performed. Followup discussions with the
    resident inspectors stationed at Quad Cities in July 2007 had no recollection of the
    conversation and their understanding of the intended action remained unchanged from
    the original report.
    Licensee staff generated Issue Report (IR) 738335 in February 2008 to document the
    review of the NCV response and generate a closure package of all related IRs. The lack
    of preventative maintenance (PM) testing was identified and an action tracking item was
    generated to Develop PM/testing requirements for the Darley pump associated with the
    external flooding event. The original corrective action due date was July 16, 2008.
    The action was extended several times, and on May 18, 2009, during a review of
    corrective actions for NRC-identified issues, the licensee staff identified that a CAP
                                              23                                      Enclosure


ensure that issues identified were consistent with the NRC perspectives of licensee performance and to verify if any significant safety issues were identified that required
action item (ACIT 624645-03) had been inappropriately closed. In addition, the licensee
determined that ACIT 624645-03 was inappropriately tagged as an Action Tracking Item
(ACIT) and should have been a corrective action. Issue Report 921197 was generated
and ACIT 624645 was upgraded to a corrective action with a July 31, 2009, due date.
The test procedure was developed and the pump was scheduled to run on
September 17, 2009.
The capacity test was implemented with WO 01247374. When mechanics pulled the
pump and support components from the storage location, they found that the engine
battery had to be replaced and the gasoline stored with the motor had to be replaced.
Since the mechanics performing the test had never operated the pump, they decided to
run it in the weld shop before taking it down to the river. When the mechanics started
the pump, fuel was spraying out of the fuel pump. They immediately shut down the
pump and contained the fuel leak (IR 966501).
The Darley pump fuel system was repaired and the capacity test was completed
satisfactorily on September 25, 2009. Review of recent pump operating history and
PM tasks revealed that the pump had not been operated since the NCV was identified in
2007. The annual maintenance performed under PM 164250 in July of 2009 changed
the oil and inspected the filters and spark plugs with no post-maintenance operation
required. The PM also failed to identify that the battery was beyond the expected life
and did not determine that the battery would maintain its charge.
Analysis: The inspectors determined that the failure to perform maintenance that would
ensure the pump was in a standby condition and readily available to accomplish the
requirements of QCOA 0010-16 was a performance deficiency fully within the licensees
ability to control, and therefore a finding. This issue was more than minor because it
was associated with the SSC Performance attribute of the Barrier Integrity Cornerstone
element of maintaining the functionality of spent fuel pool cooling. The finding affected
the cornerstone objective of providing assurance that physical design barriers protect the
public from radionuclide releases caused by events including external flooding.
Specifically, the pump could fail due to a maintenance preventable component failure
resulting in inadequate or degraded makeup to the spent fuel pool during an external
flooding event. The inspectors did not identify a cross-cutting aspect associated with
this finding because the maintenance issue is a legacy issue and not reflective of current
licensee performance. The pump and PM tasks had been in place for several years.
Inspectors reviewed maintenance requirements for other temporary equipment staged in
support of external events and emergency operating procedures, some of which was put
in place after the Darley pump was staged, and did not identify any similar issues.
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of findings, Tables 4a and 4b. The inspectors
determined that even though this equipment is assumed to completely fail, the licensee
could provide an alternate portable pump already located on site and capable of
performing the safety function during this slow developing event. The alternate pump
had maintenance and test procedures in place to provide a basis for reliability. Since
alternate equipment was available and the delay in mobilizing the alternate equipment
would not have resulted in loss of capability to mitigate the impact of the flooding event,
the issue is of very low safety significance or Green.
                                          24                                      Enclosure


further NRC followup.   b. Findings
    Enforcement: Technical Specification 5.4.1 required that written procedures be
No findings of significance were identified. .2 Quarterly Resident Inspector Observations of Security Personnel and Activities
    established, implemented, and maintained for the items specified in Regulatory
a. Inspection Scope
    Guide 1.33, Quality Assurance Program Requirements. QCOA 0010-16,
During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.  These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples.  Rather, they were considered an
    Flood Emergency Procedure, was the licensee procedure used to meet the
integral part of the inspectors' normal plant status review and inspection activities.   b. Findings
    Regulatory Guide 1.33 requirement for an emergency flooding event. The procedure
No findings of significance were identified.   4OA6 Management Meetings
    specified that the portable pump staged in the protected area warehouse is to be used to
.1 Exit Meeting Summary
    respond to the event. Although the regulatory guide did not specifically require
On January 5, 2010, the inspectors presented the inspection results to T. Tulon and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.   .2 Interim Exit Meetings
    maintenance procedures for portable equipment, failure to maintain the staged
Interim exits were conducted for:    The results of the licensed operator requalification training program inspection and with the site vice president, Mr. T. Tulon, on October 2, 2009. 
    equipment in a condition to be used to mitigate the event does not support timely
  The licensed operator requalification training biennial written examination and annual operating test examination materials were discussed with the training manager, Mr. K. Moser, on November 12, 2009.   
    implementation of the procedure to provide spent fuel pool makeup and is a finding.
  31 Enclosure  The licensed operator requalification training program annual inspection results with operations training manager, Mr. D. Snook, on November 20, 2009, via telephone.    The results of the Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent Occurrences performance indicator verification program inspection with the plant manager, Mr. R. Gideon, on December 16, 2009.    The annual review of Emergency Action Level and Emergency Plan changes with the licensee's emergency preparedness coordinator, Mr. F. Swan, via telephone on December 21, 2009The inspectors confirmed that none of the potential report input discussed was considered proprietary. Proprietary material received during the inspection was returned
    Enforcement action does not apply because the performance deficiency did not involve a
to the licensee. 4OA7 Licensee-Identified Violations
    violation of a regulatory requirement. Because the finding does not involve a violation of
The following violation of very low significance (Green) was identified by the licensee and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, fo
    regulatory requirements and has a very low safety significance, it is identified as
r being dispositioned as an NCV.    Technical Specification 5.5.1 requires implementation of the Offsite Dose Calculation Manual.  Offsite Dose Calculation Manual, Revision 8, Part 12.2.1, Radioactive Liquid Effluent Monitoring Instrumentation, Section C requires that  
    (FIN 05000254/2009005-02; 05000265/2009005-02). The issue was added to the
when the service water effluent gross activity monitor is operated with less than
    licensees CAP program as IR 966501 and IR 968809. Immediate corrective actions
the minimum number of operable channels, the licensee shall collect and analyze
    included replacement of the degraded battery and overhaul of the pumps fuel pump.
grab samples for beta or gamma activity once per 12 hours. Contrary to the above, grab samples were not collected while the Unit 1 service water effluent gross activity monitor was inoperable from June 2-20, 2009.  Specifically, following fuse replacement, the licensee failed to recognize that the instrument
    Other actions included identification of preventative maintenance tasks and establishing
remained uninitialized; therefore, that compensatory samples were required.  The  
    a program owner of the pump.
finding was documented in the licensee's corrective action program as IR 933472. Corrective actions included returning the monitor to service and reviewing captured monitor data from June 2-20, 2009, to ensure that no release
.5  Selected Issue Followup Inspection: Incident Report 984769, Temperature Indicating
events occurred during the monitor outage, revising the monitor repair and
    Probe Found Broken in the Unit 2 Diesel Generator Coolant System
maintenance procedures to clear direct communication with the Chemistry
   a. Inspection Scope
Department subject matter experts during work on the system, and reinforcing
    During a review of items entered in the licensees CAP, the inspectors followed up on a
the expectation that control room operators turn over all abnormal indications to supervisors each shift. The finding was determined to be of very low safety significance because, although the finding related to the effluent release
    corrective action item documenting a failed temperature indicating probe (TI) in the
    Unit 2 diesel generator coolant system on October 27, 2009, during planned
    maintenance on the Unit 2 emergency diesel generator (EDG).
    This review constituted one in-depth problem identification and resolution sample as
    defined in IP 71152-05.
   b. Findings
    Introduction: A finding of very low safety significance and associated NCV were
    self-revealed when a TI failed in the Unit 2 diesel generator coolant system.
    Description: On October 27, 2009, while performing corrective maintenance on
    TI 2-6641-8205, technicians noted that the tip had broken off the probe when comparing
    it to the length of the new TI. This TI provides local indication of the jacket coolant water
    temperature at the inlet to the diesel engine and provides no alarm function.
    The TI was scheduled for replacement in October 2008 when Operations identified the
    TI reading abnormally at zero degrees. A work order was written and scheduled for
    October 2009. During the performance of the maintenance, it was noted that the new TI
    was longer than the one recently removed. A new work order was written to retrieve any
    foreign material from the system. The broken tip was recovered from the diesel
    generator coolant system.
                                              25                                        Enclosure


program, it was not a failure to implement the effluent program or an event that resulted in a dose to the public in excess of Appendix I criterion or
The licensee investigation discovered that the installation analysis for this TI was
approved under the non-safety below level of design detail (NSBLD) process in October
2007 under Revision 3 of SM-AA-300, Procurement Engineering Support Activities.
Using this provision, NSBLD changes must be documented and shall identify the
change with justification of the changes technical acceptability. The length of the probe
was the only difference to the previously installed TI. The TI was installed with a
3.25 inch probe, which was longer than the previous 2 inch probe. The added length
increased the shear force from the coolant flow and caused the probe to break off.
An operating experience (OPEX) review would have revealed an event at another
nuclear facility where the same make and model TI experienced the same failure
mechanism in a diesel generator coolant system. Under Revision 3 of SM-AA-300,
OPEX reviews for NSBLD were not required, nor were additional peer reviews required.
The lack of an OPEX review was an identified vulnerability by the licensees corporate
supply organization in a common cause analysis which was performed for a lack of
technical rigor issued in February 2008. A corrective action from this common cause
analysis was to implement Revision 4 of SM-AA-300 which limited NSBLD reviews to
non-safety host component applications. Revision 4 was implemented at Quad Cities in
February 2008. Since this specific TI is classified as augmented quality, Revision 4
would prevent use of the NSBLD process of a non-identical replacement. A full item
equivalency evaluation would be required for any non-identical replacement.
An extent of condition review is scheduled to be performed at Quad Cities by
Procurement Engineering for all NSBLD reviews that were performed under Revision 3
of SM-AA-300 from August 2007 through February 2008.
Analysis: The inspectors determined that the approval of an inappropriate component
designated as augmented quality was a performance deficiency and a finding. The
same parts evaluation process was used for risk-significant components independent of
the system being worked. Therefore, this finding was more than minor because, if left
uncorrected, this performance deficiency could lead to unplanned unavailability of
safety-related or risk-significant equipment and would become a more significant safety
concern. This performance deficiency challenged the Mitigating Systems Cornerstone
attribute of Equipment Performance by challenging equipment availability and reliability.
The inspectors performed a Phase 1 SDP screening and concluded that the issue was
of very low safety significance (Green) because the failure of the TI did not result in
unplanned inoperability or loss of function of the diesel generator. The inspectors
determined that this finding did not have a cross-cutting aspect. This performance
deficiency is not indicative of current licensee performance. The decision to install this
type of TI was made in October 2007. The process which allowed this performance
deficiency was identified and corrected through procedure and policy revisions to
SM-AA-300 in February 2008.
Enforcement: The TI was designated augmented quality in the licensees quality
assurance program. The licensees quality assurance program applied controls
equivalent to safety-related components for Class 1E equipment qualification to
augmented quality equipment and systems. This correlation is applicable to several
Appendix B criteria included in the program such as both Section 3 - Design Control,
and Section 5 - Instructions Procedures and Drawings, of the licensees Quality
Assurance program for augmented quality.
                                          26                                    Enclosure


10 CFR 20.1301(e).  ATTACHMENT: SUPPLEMENTAL INFORMATION 
      Title 10 CFR 50, Appendix B, Criterion V states in part that activities affecting quality
  1 Attachment SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT
      shall be prescribed by instructions and procedures of a type appropriate to the
Licensee T. Tulon, Site Vice President
      circumstances and shall be accomplished in accordance with these instructions or
R. Gideon, Plant Manager
      procedures.
D. Kimler, Shift Operations Superintendent
      Contrary to the above, on October 30, 2007, SM-AA-300 was not appropriate to the
      circumstances in that it did not require an approval process with technical rigor
      equivalent to the process used for safety-related components when a non-identical
      temperature indicating probe designated augmented quality was approved for use.
      That part was approved for use through a NSBLD review per Revision 3 of SM-AA-300
      instead of undergoing a full item equivalency evaluation, and the part subsequently
      failed resulting in foreign material in the diesel generator coolant system. The foreign
      material did not cause any adverse consequences in this instance.
      Because this issue is of very low safety significance, and this issue has been entered
      into the licensees corrective action program as Issue Report 984769, this issue is being
      treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy
      (NCV 05000265/2009005-03).
      Corrective actions for this event included replacement of the TI with an appropriately
      approved TI. The licensee has also scheduled to perform an extent of condition review
      of NSBLD reviews performed under Revision 3 of SM-AA-300 from August 2007 through
      February 2008.
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)
.1   (Closed) Licensee Event Report 05000254/2009-003-00: Failure of RHR Torus Spray
      Isolation Valve to Open Due to Declutch Mechanism Problems
  a. Inspection Scope
      Inspectors reviewed the event, evaluation, and corrective actions for the motor operated
      valve failure reported in Licensee Event Report (LER) 05000254/2009-003. Documents
      reviewed as part of this inspection are listed in the Attachment to this report. This LER is
      closed.
      This event follow-up review constituted one sample as defined in IP 71153-05.
  b. Findings
      Introduction: A finding of very low safety significance and an NCV of Technical
      Specification (TS) 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool Spray,
      was self-revealed for the licensees failure to meet the TS limiting condition for operation
      (LCO) requirements prior to transitioning into an operating mode where the LCO was
      required to be satisfied. Specifically, MO 1-1001-37B, motor operator for the Unit 1 RHR
      torus (suppression pool) spray isolation valve, was found to have been inoperable when
      the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. The
      valve actuator had been inadvertently declutched (i.e., motor disengaged) and the valve
      was not demonstrated operable by stroking the valve electrically after the actuator motor
      was declutched.
                                                27                                      Enclosure


S. Darin, Engineering Manager
Discussion: On June 4, 2009, with Unit 1 in Mode 1 at 100 percent power following
startup from a forced outage, MO 1-1001-37B, torus spray shutoff valve, was determined
to be inoperable because it would not open remotely using the control switch during
performance of the residual heat removal power operated valve test surveillance.
The torus spray valve had been closed using the motor and a clearance order had been
placed on the valve during the outage. Another motor operated valve in the residual
heat removal system on that same clearance, MO 1-1001-7C, RHR C torus suction line
isolation valve, had failed to open on May 28, 2009, when the clearance tag was
removed and valve stroking was being performed to restore the component to a standby
configuration. Operators reported manually declutching (disengaging the actuator
motor) the 7C valve while placing the clearance tag in order to verify the valve was
closed. Inspectors identified that the action of manually verifying valve position was not
a normal practice as supported by OP-AA-103-105, Limitorque Motor-Operated Valve
Operations, and Operations department management. Investigation into the 7C failure
revealed that the actuator lubricant was degraded in the area of the clutch return spring
preventing the motor from engaging when called upon from the control circuit. The
RHR C valve actuator was rebuilt using MOV Long Life grease, new tripper cams, new
trip lever assembly, and a new outer declutch arm snap ring. The rebuilt actuator was
verified to operate correctly in all modes and returned to service prior to unit restart on
May 30, 2009.
Inspectors interviewed operating personnel regarding the positioning of MO 1-1001-37B
torus spray valve. Operators stated that they did not manually declutch the 37B valve
since the valve was already closed (normal position) when they hung the tag. The
licensees investigation attempted to identify both how the motor on the 37B valve was
declutched and why the actuator did not return to the motor mode of operation
automatically as designed. The licensee verified that the actuator was not able to
transition from the motor mode to the manual mode without external (human)
intervention.
Although the licensee could not identify how or when the valve actuator motor was
declutched, the licensees investigators concluded that the declutch lever was most likely
bumped during work activities on top of the Torus during the recent outage with the unit
in Mode 4. Investigation further determined that with the valve motor disengaged,
increased friction in the actuator caused by degraded lubricant in the area of the clutch
return spring prevented the engagement of the motor to open the valve. The actuator
motor was engaged by manually manipulating the declutch lever and stroke testing the
valve.
Inspectors reviewed the grease sampling methodology and the preventative
maintenance frequency for the SMP-00 type actuators and determined that both were
conducted in accordance with the industry standards for these type valves.
Analysis: The failure of plant personnel to demonstrate operability of MO 1-1001-37B by
stroking the valve electrically prior to changing modes was a performance deficiency.
The finding is more than minor because it was associated with the equipment
performance quality attribute of the Mitigating Systems Cornerstone and affected the
objective of ensuring availability, reliability and capability of systems that respond to
initiating events to prevent undesirable consequences. Specifically, failure to verify
system availability and capability prior to entering the required modes resulted in fewer
                                            28                                      Enclosure


W. Beck, Regulatory Assurance Manager
available mitigating systems than assumed in the operating risk evaluations. Inspectors
J. Burkhead, Nuclear Oversight Manager
determined that the finding was cross-cutting in the area of Problem Identification and
J. Garrity, Work Control Manager
Resolution - Corrective Action because plant personnel failed to identify the valve
K. Moser, Training Manager
actuator contact that resulted in the valve being declutched; therefore, operators
V. Neels, Chemistry/Environ/Radwaste Manager
incorrectly assessed the system condition as in compliance with TS 3.6.2.4 (P.1(a)).
D. Collins, Radiation Protection Manager
The inspectors determined the finding could be evaluated using the SDP in accordance
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Initial Screening and Characterization of Findings, Table 4a. Inspectors answered all of
the questions for the Mitigating Systems Cornerstone No. Therefore, the finding
screened as Green or very low safety significance.
Enforcement: Technical Specification 3.0, Limiting Condition for Operation (LCO)
Applicability, LCO 3.0.4 stated in part that when an LCO is not met, entry into a mode in
the Applicability shall only be made:
*        when the associated actions to be entered permit continued operation while in
        the mode or other specified condition in the Applicability for an unlimited time;
*        after performance of a risk assessment addressing inoperable systems and
        components, and acceptability of entering the mode; or
*        when an allowance is stated in the specification.
Technical Specification 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool
Spray, required two RHR suppression pool spray subsystems to be operable in
Modes 1, 2 and 3.
Contrary to the above, on May 30, 2009, the licensee changed operating modes from
Mode 4 to Mode 2 with the MO 1-1001-37B valve inoperable in violation of TS 3.6.2.4
LCO conditions since only one RHR suppression pool (Torus) spray subsystem was
operable. Specifically, TS 3.6.2.4 had no allowance provided to permit mode change
with less than two subsystems operable, no prior risk assessment was performed, and
the specification did not permit operation for an unlimited time, the mode change
resulted in non-compliance with TS LCO 3.6.2.4.
Because this finding is of very low safety significance, and this issue has been entered
into the licensees corrective action program as IR 928048, this violation is being treated
as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy
(NCV 05000254/2009005-04).
Immediate corrective actions for this event included engagement of the actuator motor
by manually manipulating the declutch lever and stroke testing the valve. Since the
hardened grease in this area of the actuator assembly was only an issue if the actuator
was manually declutched, the valve was left in standby, and overhaul of the valve
actuator was scheduled for the next refueling outage.
                                          29                                        Enclosure


D. Thompson, Security Manager
4OA5 Other Activities
  Nuclear Regulatory Commission
.1  World Association of Nuclear Operators Plant Assessment Report Review
    
  a. Inspection Scope
M. Ring, Chief, Reactor Projects Branch 1
      The inspectors reviewed the final report for the World Association of Nuclear Operators
      plant assessment conducted in February 2009. The inspectors reviewed the report to
      ensure that issues identified were consistent with the NRC perspectives of licensee
      performance and to verify if any significant safety issues were identified that required
      further NRC followup.
  b. Findings
      No findings of significance were identified.
.2  Quarterly Resident Inspector Observations of Security Personnel and Activities
  a. Inspection Scope
      During the inspection period, the inspectors conducted observations of security force
      personnel and activities to ensure that the activities were consistent with licensee
      security procedures and regulatory requirements relating to nuclear plant security.
      These observations took place during both normal and off-normal plant working hours.
      These quarterly resident inspector observations of security force personnel and activities
      did not constitute any additional inspection samples. Rather, they were considered an
      integral part of the inspectors' normal plant status review and inspection activities.
  b. Findings
      No findings of significance were identified.
4OA6 Management Meetings
  .1  Exit Meeting Summary
      On January 5, 2010, the inspectors presented the inspection results to T. Tulon and
      other members of the licensee staff. The licensee acknowledged the issues presented.
      The inspectors confirmed that none of the potential report input discussed was
      considered proprietary.
.2   Interim Exit Meetings
      Interim exits were conducted for:
      *      The results of the licensed operator requalification training program inspection
              and with the site vice president, Mr. T. Tulon, on October 2, 2009.
      *      The licensed operator requalification training biennial written examination and
              annual operating test examination materials were discussed with the training
              manager, Mr. K. Moser, on November 12, 2009.
                                                30                                      Enclosure


Illinois Emergency Management Agency
    *        The licensed operator requalification training program annual inspection results
 
              with operations training manager, Mr. D. Snook, on November 20, 2009, via
R. Zuffa, Unit Supervisor, Resident Inspector Section LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
              telephone.
Opened 05000254/2009005-01;  
    *        The results of the Radiological Effluent TS/Offsite Dose Calculation Manual
05000265/2009005-01 URI Changes to EAL HU6 Potentially Decrease the Effectiveness of the Plans without Prior NRC Approval
              Radiological Effluent Occurrences performance indicator verification program
05000254/2009005-02;
              inspection with the plant manager, Mr. R. Gideon, on December 16, 2009.
    *        The annual review of Emergency Action Level and Emergency Plan changes
              with the licensee's emergency preparedness coordinator, Mr. F. Swan, via
              telephone on December 21, 2009.
    The inspectors confirmed that none of the potential report input discussed was
    considered proprietary. Proprietary material received during the inspection was returned
    to the licensee.
4OA7 Licensee-Identified Violations
    The following violation of very low significance (Green) was identified by the licensee
    and is a violation of NRC requirements which meets the criteria of Section VI of the
    NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
    *        Technical Specification 5.5.1 requires implementation of the Offsite Dose
              Calculation Manual. Offsite Dose Calculation Manual, Revision 8, Part 12.2.1,
              Radioactive Liquid Effluent Monitoring Instrumentation, Section C requires that
              when the service water effluent gross activity monitor is operated with less than
              the minimum number of operable channels, the licensee shall collect and analyze
              grab samples for beta or gamma activity once per 12 hours. Contrary to the
              above, grab samples were not collected while the Unit 1 service water effluent
              gross activity monitor was inoperable from June 2-20, 2009. Specifically,
              following fuse replacement, the licensee failed to recognize that the instrument
              remained uninitialized; therefore, that compensatory samples were required. The
              finding was documented in the licensees corrective action program as
              IR 933472. Corrective actions included returning the monitor to service and
              reviewing captured monitor data from June 2-20, 2009, to ensure that no release
              events occurred during the monitor outage, revising the monitor repair and
              maintenance procedures to clear direct communication with the Chemistry
              Department subject matter experts during work on the system, and reinforcing
              the expectation that control room operators turn over all abnormal indications to
              supervisors each shift. The finding was determined to be of very low safety
              significance because, although the finding related to the effluent release
              program, it was not a failure to implement the effluent program or an event that
              resulted in a dose to the public in excess of Appendix I criterion or
              10 CFR 20.1301(e).
ATTACHMENT: SUPPLEMENTAL INFORMATION
                                                31                                      Enclosure


05000265/2009005-02 FIN Darley Pump Leaking Gasoline from the Fuel Pump 05000265/2009005-03 NCV Temperature Indicating Probe Found Broken in the Unit 2  
                              SUPPLEMENTAL INFORMATION
Diesel Generator Coolant System 05000254/2009005-04 NCV Failure of RHR Torus Spray Isolation Valve to Open Due to  
                                  KEY POINTS OF CONTACT
Declutch Mechanism Problems  
Licensee
Closed 05000254/2009005-02;  
T. Tulon, Site Vice President
05000265/2009005-02 FIN Darley Pump Leaking Gasoline from the Fuel Pump 05000265/2009005-03 NCV Temperature Indicating Probe Found Broken in the Unit 2  
R. Gideon, Plant Manager
Diesel Generator Coolant System 05000254/2009005-04 NCV Failure of RHR Torus Spray Isolation Valve to Open Due to  
D. Kimler, Shift Operations Superintendent
Declutch Mechanism Problems 05000254/2009003-00 LER Failure of RHR Torus Spray Isolation Valve to Open Due to  
S. Darin, Engineering Manager
Declutch Mechanism Problems  
W. Beck, Regulatory Assurance Manager
 
J. Burkhead, Nuclear Oversight Manager
  2 Attachment LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection. Inclusion on this list does  
J. Garrity, Work Control Manager
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
K. Moser, Training Manager
any part of it, unless this is stated in the body of the inspection report.  
V. Neels, Chemistry/Environ/Radwaste Manager
D. Collins, Radiation Protection Manager
D. Thompson, Security Manager
Nuclear Regulatory Commission
M. Ring, Chief, Reactor Projects Branch 1
Illinois Emergency Management Agency
R. Zuffa, Unit Supervisor, Resident Inspector Section
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
05000254/2009005-01;      URI    Changes to EAL HU6 Potentially Decrease the Effectiveness
05000265/2009005-01              of the Plans without Prior NRC Approval
05000254/2009005-02;      FIN   Darley Pump Leaking Gasoline from the Fuel Pump
05000265/2009005-02
05000265/2009005-03       NCV   Temperature Indicating Probe Found Broken in the Unit 2
                                  Diesel Generator Coolant System
05000254/2009005-04       NCV   Failure of RHR Torus Spray Isolation Valve to Open Due to
                                  Declutch Mechanism Problems
Closed
05000254/2009005-02;       FIN   Darley Pump Leaking Gasoline from the Fuel Pump
05000265/2009005-02
05000265/2009005-03       NCV   Temperature Indicating Probe Found Broken in the Unit 2
                                  Diesel Generator Coolant System
05000254/2009005-04       NCV   Failure of RHR Torus Spray Isolation Valve to Open Due to
                                  Declutch Mechanism Problems
05000254/2009003-00       LER   Failure of RHR Torus Spray Isolation Valve to Open Due to
                                  Declutch Mechanism Problems
                                                1                                  Attachment
 
                                  LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
selected sections of portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
Section 1R01
Section 1R01
- QCOP 0010-01; Winterizing Checklist; Revision 48 - QCOP 0010-02; Required Cold Weather Routines; Revision 28 - WC-AA-107; Seasonal Readiness; Revision 06 - IR 99493; U-2 FW Heater LCV Response to Lowering Circulating Water Inlet Temp  
- QCOP 0010-01; Winterizing Checklist; Revision 48
- WO 1183498; Cycle CW De-Ice Valve  
- QCOP 0010-02; Required Cold Weather Routines; Revision 28
- WO 1282535; Ice Melt Valve Stuck Shut  
- WC-AA-107; Seasonal Readiness; Revision 06
- QCOP 4400-06; Circulating Water System De-icing; Revision 14 - ECR 59777; Design Alternate Method for Operation of Ice Melt Valve - IR 993018; Wire Rope Rating on Ice Melt Valve  
- IR 99493; U-2 FW Heater LCV Response to Lowering Circulating Water Inlet Temp
- IR 986355; Ice Melt Valve Stuck Shut  
- WO 1183498; Cycle CW De-Ice Valve
- WO 01194645; MM Union Leaking Inside U1 Cond Demin Vault (HTG STM)  
- WO 1282535; Ice Melt Valve Stuck Shut
- WO 01215488; MM Repair Piping Leak Underground Next to Cribhouse - WO 01242820; MM Seal Cracks in Ceiling Above Bus 23-1  
- QCOP 4400-06; Circulating Water System De-icing; Revision 14
- ECR 59777; Design Alternate Method for Operation of Ice Melt Valve
- IR 993018; Wire Rope Rating on Ice Melt Valve
- IR 986355; Ice Melt Valve Stuck Shut
- WO 01194645; MM Union Leaking Inside U1 Cond Demin Vault (HTG STM)
- WO 01215488; MM Repair Piping Leak Underground Next to Cribhouse
- WO 01242820; MM Seal Cracks in Ceiling Above Bus 23-1
Section 1R04
Section 1R04
- QCOP 4100-01; Firewater System Lineup for Standby Operation; Revision 4 - QCOP 6600-01: Diesel Generator 1(2) Preparation For Standby Operation; Revision 38  
- QCOP 4100-01; Firewater System Lineup for Standby Operation; Revision 4
- WO #01272234; EM Change RMS-9 Setting at SWGR 19 CUB 5D Per EC 377092  
- QCOP 6600-01: Diesel Generator 1(2) Preparation For Standby Operation; Revision 38
- WO #01107582; EM Replace U2 DGCWP Alternate Feed Contactor - WO #920850; IM CAL DG HX 2-6661B Cooling Water Inlet PI 2-3941-67A - WO #945963; IM CAL DG HX 2-6661B Cooling Water Outlet PI 2-3941-67B  
- WO #01272234; EM Change RMS-9 Setting at SWGR 19 CUB 5D Per EC 377092
- WO #01107581; EM Replace U2 DGCWP Normal Feed Contactor  
- WO #01107582; EM Replace U2 DGCWP Alternate Feed Contactor
- WO #01245102; EM Support OP QCOS 6600-17 U2 DGCW Pump Alternate Feed Test  
- WO #920850; IM CAL DG HX 2-6661B Cooling Water Inlet PI 2-3941-67A
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for Appendix R; Revision 15 - EC 360507; Unit 2 EDG Voltage Regulator (Place EDG in Droop Mode Prior to  
- WO #945963; IM CAL DG HX 2-6661B Cooling Water Outlet PI 2-3941-67B
Synchronization to the Grid) - EC 377665; TMOD to Bypass Faulty SSES Switch Local/Remote Contact at U2 Diesel  
- WO #01107581; EM Replace U2 DGCWP Normal Feed Contactor
Generator  
- WO #01245102; EM Support OP QCOS 6600-17 U2 DGCW Pump Alternate Feed Test
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for
  Appendix R; Revision 15
- EC 360507; Unit 2 EDG Voltage Regulator (Place EDG in Droop Mode Prior to
  Synchronization to the Grid)
- EC 377665; TMOD to Bypass Faulty SSES Switch Local/Remote Contact at U2 Diesel
  Generator
Section 1R05
Section 1R05
- OP-AA-201-008; Pre-fire Plan Manual Index - Pre-Plan RB-16; Revision 2 - Pre-plan TB-74; Fire Zone 9.1, Unit 1 Turbine Bldg. El. 595'-0", Diesel Generator; Revision 24  
- OP-AA-201-008; Pre-fire Plan Manual Index - Pre-Plan RB-16; Revision 2
- Pre-plan TB-73; Fire Zone 8.2.6.A, Unit 1 Turbine Bldg. El. 595'-0", Reactor Feed Pumps;  
- Pre-plan TB-74; Fire Zone 9.1, Unit 1 Turbine Bldg. El. 595-0, Diesel Generator; Revision 24
Revision 24 - Pre-plan CH-44; Fire Zone 11.4.A, Crib House Bldg. El. 559'-8" Basement; Revision 0 - Pre-plan CH-45; Fire Zone 11.4.B, Ground Floor/Service Water Pumps; Revision 22
- Pre-plan TB-73; Fire Zone 8.2.6.A, Unit 1 Turbine Bldg. El. 595-0, Reactor Feed Pumps;
  3 Attachment  
  Revision 24
- Pre-plan CH-44; Fire Zone 11.4.A, Crib House Bldg. El. 559-8 Basement; Revision 0
- Pre-plan CH-45; Fire Zone 11.4.B, Ground Floor/Service Water Pumps; Revision 22
                                                    2                                  Attachment
 
Section 1R11
Section 1R11
- SY-AA-101-132; Assessment and Response to Suspicious Activity and Security Threats;  
- SY-AA-101-132; Assessment and Response to Suspicious Activity and Security Threats;
Revision 14 - QCOA 0010-20; Security Event; Revision 25 - EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27  
  Revision 14
- Requalification Examination Results/Calendar Year 2009  
- QCOA 0010-20; Security Event; Revision 25
- Quad Cities, Units 1 and 2 NRC Integrated Inspection Reports; dated various from  
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27
January 2007 through September 2009 - OP-AA-105-102; Attachment 1; Active License Tracking Log (for 1st & 2nd Quarters of 2009);  
- Requalification Examination Results/Calendar Year 2009
Revision 9 - OP-AA-105-102; Attachment 2, Reactivation of License Log (2 for LSRO, 2 RO); Revision 9  
- Quad Cities, Units 1 and 2 NRC Integrated Inspection Reports; dated various from
- Quad Cities Classroom Sample Plan for Training Years 2008 and 2009; 6/18/2009  
  January 2007 through September 2009
- Quad Cities Simulator Sample Plan for Training Years 2008 and 2009  
- OP-AA-105-102; Attachment 1; Active License Tracking Log (for 1st & 2nd Quarters of 2009);
- 71111.11 Appendix C Responses/Justifications; 9/28/2009 - TQ-AA-224-F070; Evaluation Feedback Summary, LORT Cycle 08-1 through 08-5; LORT  
  Revision 9
Cycle 09-1 through 09-4 - TQ-AA-1002; Attachment 3; LORT Quarterly Curriculum Review Committee Meeting Minutes; all of 2008 and first two quarters of 2009 - Special LORT CRC Meeting Minutes; 1/23/2009 - TQ-AA-150; Operator Training Programs; Revision 2 - TQ-AA-150-F07; Simulator Evaluation Form - STA or IA  
- OP-AA-105-102; Attachment 2, Reactivation of License Log (2 for LSRO, 2 RO); Revision 9
- TQ-AA-150-F08; Simulator Evaluation Form - Individual  
- Quad Cities Classroom Sample Plan for Training Years 2008 and 2009; 6/18/2009
- TQ-AA-150-F09; Simulator Evaluation Form - Crew  
- Quad Cities Simulator Sample Plan for Training Years 2008 and 2009
- TQ-AA-210-5101; Training Observation Forms; dated various  
- 71111.11 Appendix C Responses/Justifications; 9/28/2009
- TQ-AA-306; Simulator Management - TQ-AA-306-F06; BWR Critical Condition for Cold Startup; Revision 0 - TQ-AA-306-F07; BWR Power Coefficient of Reactivity and Control Rod Worth; Revision 0  
- TQ-AA-224-F070; Evaluation Feedback Summary, LORT Cycle 08-1 through 08-5; LORT
- TQ-AA-306-F08; BWR Xenon Worth; Revision 0  
  Cycle 09-1 through 09-4
- TQ-AA-306-F06; BWR Site Specific Shutdow
- TQ-AA-1002; Attachment 3; LORT Quarterly Curriculum Review Committee Meeting Minutes;
n Margin and Reactivity Anomaly Tests - TQ-AA-306-JA-02; Simulator Testing Report Update - Differences between the Quad Cities Simula
  all of 2008 and first two quarters of 2009
tor and Quad Cities U-1 & U-2; Revision 14;  
- Special LORT CRC Meeting Minutes; 1/23/2009
7/17/09 - Differences between the Quad Cities Simula
- TQ-AA-150; Operator Training Programs; Revision 2
tor and Quad Cities U-1 & U-2; Revision 15;  
- TQ-AA-150-F07; Simulator Evaluation Form - STA or IA
9/29/09 - LS-AA-126-1005; Attachment 2; Check-In Self-Assessment Report Template  
- TQ-AA-150-F08; Simulator Evaluation Form - Individual
- LS-AA-126-1001; Attachment 2; FASA Self-Assessment Report - Simulator Malfunction Test Procedure, Grid Frequency Disturbance (ED16) - Simulator Malfunction Test Procedure, Reactor Building Instrument Air System (IA02)  
- TQ-AA-150-F09; Simulator Evaluation Form - Crew
- Simulator Malfunction Test Procedure, Main Steam Isolation Valve Closure (MS01)  
- TQ-AA-210-5101; Training Observation Forms; dated various
- Quad Cities Simulator Malfunction Testing Schedule; Revision 8; 5/5/2008  
- TQ-AA-306; Simulator Management
- Simulator Transient Tests; dated various - Safety System Functional Failure, Rolling Twelve Months Unit 1 and Unit 2; 9/28/09 - Action Request Reports; various dates for LORT 2009  
- TQ-AA-306-F06; BWR Critical Condition for Cold Startup; Revision 0
- LORT Attendance Sheets; 2009
- TQ-AA-306-F07; BWR Power Coefficient of Reactivity and Control Rod Worth; Revision 0
  4 Attachment  
- TQ-AA-306-F08; BWR Xenon Worth; Revision 0
- TQ-AA-306-F06; BWR Site Specific Shutdown Margin and Reactivity Anomaly Tests
- TQ-AA-306-JA-02; Simulator Testing Report Update
- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 14;
  7/17/09
- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 15;
  9/29/09
- LS-AA-126-1005; Attachment 2; Check-In Self-Assessment Report Template
- LS-AA-126-1001; Attachment 2; FASA Self-Assessment Report
- Simulator Malfunction Test Procedure, Grid Frequency Disturbance (ED16)
- Simulator Malfunction Test Procedure, Reactor Building Instrument Air System (IA02)
- Simulator Malfunction Test Procedure, Main Steam Isolation Valve Closure (MS01)
- Quad Cities Simulator Malfunction Testing Schedule; Revision 8; 5/5/2008
- Simulator Transient Tests; dated various
- Safety System Functional Failure, Rolling Twelve Months Unit 1 and Unit 2; 9/28/09
- Action Request Reports; various dates for LORT 2009
- LORT Attendance Sheets; 2009
                                              3                                    Attachment
 
Section 1R12
Section 1R12
- Enterprise Maintenance Rule Production Database for the following systems: Z2900; Safe Shutdown Makeup Pump Z4700; Instrument Air - System Engineer Notebook and Accountability Logs for the following systems: Safe Shutdown Makeup Pump Instrument Air - IR 712670; Safe shutdown makeup pump failed surveillance; 12/17/07 - IR 713041; Broken SSMP part not found during repairs; 12/18/07  
- Enterprise Maintenance Rule Production Database for the following systems:
- IR 711934; SSMP Suction line did not fill during fill; 12/14/07  
      *      Z2900; Safe Shutdown Makeup Pump
- IR 712059; SSMP fails to sustain flow and pressure; 12/15/07 - IR 731013; SSMP Sparking on Startup; 2/4/08 - IR 729984; SSMP failed operability test per TIC-1982; 2/1/08  
      *      Z4700; Instrument Air
- IR 729951; SSMP Local FIC failed PMT; 1/31/08  
- System Engineer Notebook and Accountability Logs for the following systems:
- IR 734472; MRULE A-1 determination for SSMP required; 2/11/08  
      *      Safe Shutdown Makeup Pump
- IR 741838; SSMP feed breaker problems during system restoration; 2/27/08 - IR 787063; Local SSMP flow controller not reading correctly; 6/16/08 - IR 890904; SSMP controller connector degraded; 3/10/09  
      *      Instrument Air
- IR 930013; Historical FME identified in SSMP piping inspection; 6/10/09  
- IR 712670; Safe shutdown makeup pump failed surveillance; 12/17/07
- IR 956294; SSMP FIC Valve position discrepancy with local valve indication; 8/21/09  
- IR 713041; Broken SSMP part not found during repairs; 12/18/07
- IR 947201; FPI - SSMP Breaker and fuse coordination for CT-2; 7/29/08  
- IR 711934; SSMP Suction line did not fill during fill; 12/14/07
- IR 1003024; SSMP Draws a vacuum when starting for PMT; 12/09/09 - IR 1002036; Drain valve for SSMP room cooler may be blocked; 12/06/09 - IR 991490; NCV 09-006-02 Closure package - SSMP Breaker coordination 11/10/09  
- IR 712059; SSMP fails to sustain flow and pressure; 12/15/07
- IR 673268; 1B Instrument Air Compressor Excessive Leakage; 9/20/07  
- IR 731013; SSMP Sparking on Startup; 2/4/08
- IR 762652; 1A Instrument Air Compressor Trip; 04/12/08  
- IR 729984; SSMP failed operability test per TIC-1982; 2/1/08
- IR 856509; Red Trend Code for 1/2B Instrument Air Compressor - EC 364602 - IR 871161; 1A Instrument Air Compressor Trip; 01/24/09 - IR 871939; 1A Instrument Air Compressor Trip; 01/26/09  
- IR 729951; SSMP Local FIC failed PMT; 1/31/08
- IR 977823; 1A Instrument Air Compressor Tripped Due to Low Oil Pressure; 2/7/09  
- IR 734472; MRULE A-1 determination for SSMP required; 2/11/08
- IR 936122; Compressor does not auto start; 6/27/09  
- IR 741838; SSMP feed breaker problems during system restoration; 2/27/08
- IR 787063; Local SSMP flow controller not reading correctly; 6/16/08
- IR 890904; SSMP controller connector degraded; 3/10/09
- IR 930013; Historical FME identified in SSMP piping inspection; 6/10/09
- IR 956294; SSMP FIC Valve position discrepancy with local valve indication; 8/21/09
- IR 947201; FPI - SSMP Breaker and fuse coordination for CT-2; 7/29/08
- IR 1003024; SSMP Draws a vacuum when starting for PMT; 12/09/09
- IR 1002036; Drain valve for SSMP room cooler may be blocked; 12/06/09
- IR 991490; NCV 09-006-02 Closure package - SSMP Breaker coordination 11/10/09
- IR 673268; 1B Instrument Air Compressor Excessive Leakage; 9/20/07
- IR 762652; 1A Instrument Air Compressor Trip; 04/12/08
- IR 856509; Red Trend Code for 1/2B Instrument Air Compressor - EC 364602
- IR 871161; 1A Instrument Air Compressor Trip; 01/24/09
- IR 871939; 1A Instrument Air Compressor Trip; 01/26/09
- IR 977823; 1A Instrument Air Compressor Tripped Due to Low Oil Pressure; 2/7/09
- IR 936122; Compressor does not auto start; 6/27/09
Section 1R13
Section 1R13
- WO #01075655; EM Perform Boroscope INSP of MO 1-1001-16A MOV - WO #01120751; EM MOV 1-1001-37A MOV EQ Inspection - WO #01123089; MM Inspect/Clean 1B RHR Pump Seal Cooler  
- WO #01075655; EM Perform Boroscope INSP of MO 1-1001-16A MOV
- WO #01131318; EM Votes Test MOV 1-1001-16A  
- WO #01120751; EM MOV 1-1001-37A MOV EQ Inspection
- WO #01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
- WO #01123089; MM Inspect/Clean 1B RHR Pump Seal Cooler
- WO #01131318; EM Votes Test MOV 1-1001-16A
- WO #01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
Section 1R15
Section 1R15
- IR 849245; 1B RHR Room Cooler Heat Exchanger Has Tube Sheet Pitting - WO 862709; 1B RHR Air/Water Side Room CLR CLN/INSP  
- IR 849245; 1B RHR Room Cooler Heat Exchanger Has Tube Sheet Pitting
- IR 987904; 1A RHR Room Cooler Heat Exchanger Tube Sheet Has Pitting  
- WO 862709; 1B RHR Air/Water Side Room CLR CLN/INSP
- WO 01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
- IR 987904; 1A RHR Room Cooler Heat Exchanger Tube Sheet Has Pitting
  5 Attachment - IR 849681; 1B RHR Room Cooler Reassembled at Risk - EC 373177; Determination of Minimum Wall Thickness of Tubesheet for RHR Room  
- WO 01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
Cooler 1-574B - IR 994823; TS SR 3.8.4.8 Frequency Not Met - QC-SURV-01; Risk Assessment for Missed Surveillance for U2 125 Vdc Battery  
                                                4                                  Attachment
 
- IR 849681; 1B RHR Room Cooler Reassembled at Risk
- EC 373177; Determination of Minimum Wall Thickness of Tubesheet for RHR Room
  Cooler 1-574B
- IR 994823; TS SR 3.8.4.8 Frequency Not Met
- QC-SURV-01; Risk Assessment for Missed Surveillance for U2 125 Vdc Battery
Section 1R19
Section 1R19
- QCMMS 4100-32; 1/2 -4101A Diesel Driven Fire Pump Annual Capacity Test; Revision 24 - WO 1261246; Replace Battery Changeover Relay R12 EC 376690  
- QCMMS 4100-32; 1/2 -4101A Diesel Driven Fire Pump Annual Capacity Test; Revision 24
- EC 376690; 1/2 A Fire Pump Controller Replace Battery Changeover Relay R12; Revision 1 - QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 28 - QCOP 4100-03; Diesel Fire Pump Operation; Revision 17  
- WO 1261246; Replace Battery Changeover Relay R12 EC 376690
- QCMMS 4100-33; 1/2 - 4101B Diesel Driven Fire Pump Annual Capacity Test; Revision 24 - WO 1121775; 250 Vdc Battery Charger #2 4 Hour Load Test  
- EC 376690; 1/2 A Fire Pump Controller Replace Battery Changeover Relay R12; Revision 1
- WO 1130534; Control RM HVAC Air Filter Unit In Place DOP LK Test - QCOS 5750-02; Control Room Emergency Filter System Test; Revision 45 - QCIS 5700-04; Main Control Room Air Filter Unit DOP-Freon Test; Revision 0  
- QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 28
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for Appendix R; Revision 15 - QCEPM 0400-15; Emergency Diesel Generator Transfer Panel Inspection; Revision 9 - WO 01107582; Replace Unit 2 DGCWP Alternate Feed Contactor  
- QCOP 4100-03; Diesel Fire Pump Operation; Revision 17
- QCMMS 4100-33; 1/2 - 4101B Diesel Driven Fire Pump Annual Capacity Test; Revision 24
- WO 1121775; 250 Vdc Battery Charger #2 4 Hour Load Test
- WO 1130534; Control RM HVAC Air Filter Unit In Place DOP LK Test
- QCOS 5750-02; Control Room Emergency Filter System Test; Revision 45
- QCIS 5700-04; Main Control Room Air Filter Unit DOP-Freon Test; Revision 0
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for
  Appendix R; Revision 15
- QCEPM 0400-15; Emergency Diesel Generator Transfer Panel Inspection; Revision 9
- WO 01107582; Replace Unit 2 DGCWP Alternate Feed Contactor
Section 1R22
Section 1R22
- QCOS 1400-01; Quarterly Core Spray System Flow Rate Test; Revision 38 - QCOS 1400-07; Core Spray Pump Performance Test; Revision 10  
- QCOS 1400-01; Quarterly Core Spray System Flow Rate Test; Revision 38
- QCOS 7500-05; Standby Gas Treatment System Monthly Operability Test; Revision 30  
- QCOS 1400-07; Core Spray Pump Performance Test; Revision 10
- QCIS 0300-02; Unit 1 Division 1 Scram Discharge Volume Rochester Instruments Calibration and Functional Test; Revision 09 - QCOS 1600-07, Revision 027; Reactor Coolant Leakage in the Drywell  
- QCOS 7500-05; Standby Gas Treatment System Monthly Operability Test; Revision 30
- QCEMS 0230-11; Modified Performance Test of Unit 1(2) 125 Vdc Normal or Alternate Battery; Revision 0 - QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 33 - QCOP 6900-24; Transfer of Unit 2 125 Vdc Battery Bus Between Normal and Alternate Battery; Revision 12 - QCOS 6900-14; Station Battery Allowable Value Verification Surveillance; Revision 13  
- QCIS 0300-02; Unit 1 Division 1 Scram Discharge Volume Rochester Instruments Calibration
  and Functional Test; Revision 09
- QCOS 1600-07, Revision 027; Reactor Coolant Leakage in the Drywell
- QCEMS 0230-11; Modified Performance Test of Unit 1(2) 125 Vdc Normal or Alternate
  Battery; Revision 0
- QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 33
- QCOP 6900-24; Transfer of Unit 2 125 Vdc Battery Bus Between Normal and Alternate
  Battery; Revision 12
- QCOS 6900-14; Station Battery Allowable Value Verification Surveillance; Revision 13
Section 1EP4
Section 1EP4
- Quad Cities Station Radiological Emergency Plan Annex; Revisions 25, 26, and 27  
- Quad Cities Station Radiological Emergency Plan Annex; Revisions 25, 26, and 27
Section 1EP6
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27
- Quad Cities Generating Station 2009 Termination and Recovery Drill Briefing Package;
  December 2, 2009
- EP-AA-115; Termination and Recovery; Revision 7
- EP-AA-111-F-01; Termination/Recovery Checklist; Revision A
                                              5                                    Attachment


Section 1EP6
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27 - Quad Cities Generating Station 2009 Termination and Recovery Drill Briefing Package; December 2, 2009 - EP-AA-115; Termination and Recovery; Revision 7
- EP-AA-111-F-01; Termination/Recovery Checklist; Revision A 
  6 Attachment
Section 4OA1
Section 4OA1
- CY-QC-120-724; Continuous Liquid Effluent Analysis; Revision 1 - CY-QC-120, 723; Allocation of Radioactive Liquid Discharges; Revision 0 - CY-QC-120-720; Plant Effluent Dose Calculations; Revision 4 - CY-QC-120-725; Gaseous Release of Tritium Calculation; Revision 1  
- CY-QC-120-724; Continuous Liquid Effluent Analysis; Revision 1
- Cy-QC-120-726; Fe-55, Sr-89, Sr-90 and Gaseous Alpha Release; Revision 3  
- CY-QC-120, 723; Allocation of Radioactive Liquid Discharges; Revision 0
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline, Revision 6  
- CY-QC-120-720; Plant Effluent Dose Calculations; Revision 4
- Enterprise Maintenance Rule Production Database for the following systems: Z2300; High Pressure Coolant Injection System Z1000; Residual Heat Removal System Z6600; Diesel Generator System Z1300; Reactor Core Isolation Cooling System Z9700; 345 kV Switchyard - System Engineer Notebook and Accountability Logs for the following systems: Residual Heat Removal RHR Service Water Reactor Core Isolation Cooling HPCI Emergency Diesel Generators  
- CY-QC-120-725; Gaseous Release of Tritium Calculation; Revision 1
- Cy-QC-120-726; Fe-55, Sr-89, Sr-90 and Gaseous Alpha Release; Revision 3
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline, Revision 6
- Enterprise Maintenance Rule Production Database for the following systems:
      *      Z2300; High Pressure Coolant Injection System
      *      Z1000; Residual Heat Removal System
      *      Z6600; Diesel Generator System
      *      Z1300; Reactor Core Isolation Cooling System
      *      Z9700; 345 kV Switchyard
- System Engineer Notebook and Accountability Logs for the following systems:
      *      Residual Heat Removal
      *      RHR Service Water
      *      Reactor Core Isolation Cooling
      *      HPCI
      *      Emergency Diesel Generators
Section 4OA2Q
Section 4OA2Q
- IR 984769; Well Broke Off TI in Diesel Generator Coolant System - WO 1198663; U-2 EDG Eng Temp Indicator TI-2-6641-8205 Not Working - WO 1280197; Well Broke Off TI In U2  
- IR 984769; Well Broke Off TI in Diesel Generator Coolant System
Diesel Generator Coolant System - SM-AA-300; Procurement Engineering Support Activities; Revision 5  
- WO 1198663; U-2 EDG Eng Temp Indicator TI-2-6641-8205 Not Working
- IR 624645; Flood Emergency Pump Testing Documentation; 05/02/07  
- WO 1280197; Well Broke Off TI In U2 Diesel Generator Coolant System
- IR 638004; Clarify UFSAR 3.4.1.1 Required Flow Rate to SFP During Flood; 06/07/07  
- SM-AA-300; Procurement Engineering Support Activities; Revision 5
- IR 738335; NCV 07-005-02 GR NCV & X-cutting WRT External Flooding Event; 02/19/08  
- IR 624645; Flood Emergency Pump Testing Documentation; 05/02/07
- IR 921197; Inappropriate ACIT Closure of Darley Pump NCV; 05/18/09 - IR 927463; Request For Darley Pump Testing in On-line Schedule; 06/03/09 - IR 966501; Darley Pump Leaking Gasoline from the Fuel Pump; 09/17/09  
- IR 638004; Clarify UFSAR 3.4.1.1 Required Flow Rate to SFP During Flood; 06/07/07
- IR 968809; Adequacy of Preventative Maintenance on Darley Pump; 09/22/09  
- IR 738335; NCV 07-005-02 GR NCV & X-cutting WRT External Flooding Event; 02/19/08
- WO 01247374; Darley Pump Baseline Testing; 9/17/09  
- IR 921197; Inappropriate ACIT Closure of Darley Pump NCV; 05/18/09
- QCOA 0010-16; Flood Emergency Procedure; Revision 12 - QCMMS 1500-12; Portable Emergency Flood Pump Capacity Test; Revision 0 - QCOP 4100-19; Emergency Portable Pump Operations; Revision 7  
- IR 927463; Request For Darley Pump Testing in On-line Schedule; 06/03/09
- PMID/RQ 164250; Perform Maintenance on the External Portable Pump; 09/17/09  
- IR 966501; Darley Pump Leaking Gasoline from the Fuel Pump; 09/17/09
- IR 968809; Adequacy of Preventative Maintenance on Darley Pump; 09/22/09
- WO 01247374; Darley Pump Baseline Testing; 9/17/09
- QCOA 0010-16; Flood Emergency Procedure; Revision 12
- QCMMS 1500-12; Portable Emergency Flood Pump Capacity Test; Revision 0
- QCOP 4100-19; Emergency Portable Pump Operations; Revision 7
- PMID/RQ 164250; Perform Maintenance on the External Portable Pump; 09/17/09
Section 4OA3
Section 4OA3
- 10 Medical Files for Licensed Operators; Various Dates - Licensee Event Report 254/09-003; "Failure of RHR Torus Spray Isolation Valve Due to  
- 10 Medical Files for Licensed Operators; Various Dates
Declutch Mechanism Problems; 8/3/09 - IR 928048; MO 1-1001-37B Failed to Open During QCOS 1000-09; 6/4/09  
- Licensee Event Report 254/09-003; Failure of RHR Torus Spray Isolation Valve Due to
- IR 924666; 1-1001-7C Will Not Open; 5/28/09  
  Declutch Mechanism Problems; 8/3/09
- OP-AA-103-105; Limitorque Motor-operated Valve Operations; Revision 1
- IR 928048; MO 1-1001-37B Failed to Open During QCOS 1000-09; 6/4/09
  7 Attachment  
- IR 924666; 1-1001-7C Will Not Open; 5/28/09
- OP-AA-103-105; Limitorque Motor-operated Valve Operations; Revision 1
                                                6                                Attachment
 
Section 4OA7
Section 4OA7
- AR 933472, Service Water Effluent Radiation Monitor Inoperable; 6/20/09
- AR 933472, Service Water Effluent Radiation Monitor Inoperable; 6/20/09
  8 Attachment  
                                              7                          Attachment
LIST OF ACRONYMS USED  AC Alternating Current ADAMS Agencywide Document Access Management System ACIT Action Tracking Item CAP Corrective Action Program
CFR Code of Federal Regulations
DGCWP Diesel Generator Cooling Water Pump
EAL Emergency Action Level
EC Engineering Change EDG Emergency Diesel Generator IMC Inspection Manual Chapter
IP Inspection Procedure
IR Issue Report
IST Inservice Test JPM Job Performance Measure LCO Limiting Condition for Operation
LER Licensee Event Report
LORT Licensed Operator Requalification Training
MO Motor Operator MOV Motor Operated Valve MSPI Mitigating System Performance Index
NCV Non-Cited Violation
NEI Nuclear Energy Institute
NRC U.S. Nuclear Regulatory Commission
NSBLD Non-Safety Below Level of Design Detail OP Operations OPEX Operating Experience
ODCM Offsite Dose Calculation Manual
PARS Publicly Available Records
PI Performance Indicator PM Planned or Preventative Maintenance PMT Post Maintenance Test
RCS Reactor Coolant System
RETS Radiological Effluent Technical Specification
RHR Residual Heat Removal
RHRSW Residual Heat Removal Service Water SAT Systems Approach to Training SDP Significance Determination Process
SSC Systems, Structures, and Components
TI Temperature Indicator
TS Technical Specification UFSAR Updated Final Safety Analysis Report URI Unresolved Item
Vdc Volt direct current
WO Work Order 
  C. Pardee    -2-
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be made available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS).  ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). 
      Sincerely,        /RA/        Mark A. Ring, Chief      Branch 1
      Division of Reactor Projects
 
Docket Nos. 50-254; 50-265
License Nos. DPR-29; DPR-30
Enclosure: Inspection Report 05000254/2009005; 05000265/2009005  w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ
 
 
 
  DOCUMENT NAME:  G:\1-Secy\1-Work In Progress\QUA 2009005.doc  Publicly Available  Non-Publicly Available  Sensitive  Non-Sensitive To receive a copy of this document, indicate in th
e concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE RIII E RIII        NAME MRing:cms    DATE 01/27/2010   
OFFICIAL RECORD COPY 
  Letter to C. Pardee from M. Ring dated January 27, 2010
 
SUBJECT: QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 INTEGRATED INSPECTION REPORT 05000254/2009005; 05000265/2009005 DISTRIBUTION
: Susan Bagley
 
RidsNrrDorlLpl3-2 Resource
 
RidsNrrPMQuad Cities


RidsNrrDirsIrib Resource Cynthia Pederson Steven Orth
                          LIST OF ACRONYMS USED
Jared Heck
AC    Alternating Current
ADAMS Agencywide Document Access Management System
ACIT  Action Tracking Item
CAP  Corrective Action Program
CFR  Code of Federal Regulations
DGCWP Diesel Generator Cooling Water Pump
EAL  Emergency Action Level
EC    Engineering Change
EDG  Emergency Diesel Generator
IMC  Inspection Manual Chapter
IP    Inspection Procedure
IR    Issue Report
IST  Inservice Test
JPM  Job Performance Measure
LCO  Limiting Condition for Operation
LER  Licensee Event Report
LORT  Licensed Operator Requalification Training
MO    Motor Operator
MOV  Motor Operated Valve
MSPI  Mitigating System Performance Index
NCV  Non-Cited Violation
NEI  Nuclear Energy Institute
NRC  U.S. Nuclear Regulatory Commission
NSBLD Non-Safety Below Level of Design Detail
OP    Operations
OPEX  Operating Experience
ODCM  Offsite Dose Calculation Manual
PARS  Publicly Available Records
PI    Performance Indicator
PM    Planned or Preventative Maintenance
PMT  Post Maintenance Test
RCS  Reactor Coolant System
RETS  Radiological Effluent Technical Specification
RHR  Residual Heat Removal
RHRSW Residual Heat Removal Service Water
SAT  Systems Approach to Training
SDP  Significance Determination Process
SSC  Systems, Structures, and Components
TI    Temperature Indicator
TS    Technical Specification
UFSAR Updated Final Safety Analysis Report
URI  Unresolved Item
Vdc  Volt direct current
WO    Work Order
                                      8            Attachment


Allan Barker
C. Pardee                                            -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter
and its enclosure will be made available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                    Sincerely,
                                                    /RA/
                                                    Mark A. Ring, Chief
                                                    Branch 1
                                                    Division of Reactor Projects
Docket Nos. 50-254; 50-265
License Nos. DPR-29; DPR-30
Enclosure:        Inspection Report 05000254/2009005; 05000265/2009005
                    w/Attachment: Supplemental Information
cc w/encl:        Distribution via ListServ
DOCUMENT NAME: G:\1-Secy\1-Work In Progress\QUA 2009005.doc
Publicly Available            Non-Publicly Available      Sensitive    Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl
"E" = Copy with attach/encl "N" = No copy
OFFICE          RIII          E RIII
NAME            MRing:cms
DATE            01/27/2010
                                          OFFICIAL RECORD COPY


Carole Ariano  
Letter to C. Pardee from M. Ring dated January 27, 2010
Linda Linn  
SUBJECT:      QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 INTEGRATED
DRPIII  
              INSPECTION REPORT 05000254/2009005; 05000265/2009005
DRSIII  
DISTRIBUTION:
Patricia Buckley  
Susan Bagley
Tammy Tomczak ROPreports Resource
RidsNrrDorlLpl3-2 Resource
RidsNrrPMQuad Cities
RidsNrrDirsIrib Resource
Cynthia Pederson
Steven Orth
Jared Heck
Allan Barker
Carole Ariano
Linda Linn
DRPIII
DRSIII
Patricia Buckley
Tammy Tomczak
ROPreports Resource
}}
}}

Revision as of 22:22, 13 November 2019

IR 05000254-09-005 and 05000265-09-005 on 10/01/09 - 12/31/09 for Quad Cities Nuclear Power Station, Units 1 & 2
ML100271264
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 01/27/2010
From: Ring M
NRC/RGN-III/DRP/B1
To: Pardee C
Exelon Generation Co, Exelon Nuclear
References
FOIA/PA-2010-0209 IR-09-005
Download: ML100271264 (45)


See also: IR 05000254/2009005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

January 27, 2010

Mr. Charles G. Pardee

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000254/2009005;

05000265/2009005

Dear Mr. Pardee:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed

report documents the inspection findings, which were discussed on January 5, 2010, with

Mr. T. Tulon and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, three self-revealed findings of very low safety

significance were identified. Two of the findings involved a violation of NRC requirements.

However, because of their very low safety significance, and because the issues were entered

into your corrective action program, the NRC is treating the issues as non-cited violations

(NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally,

a licensee-identified violation is listed in Section 4OA7 of this report.

If you contest the subject or severity of an NCV, you should provide a response within 30 days

of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Quad Cities Nuclear Power Station. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region III, and the NRC Resident Inspector at the Quad Cities Nuclear Power

Station. The information that you provide will be considered in accordance with Inspection

Manual Chapter 0305.

C. Pardee -2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter

and its enclosure will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Enclosure: Inspection Report 05000254/2009005; 05000265/2009005

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-254, 50-265

License Nos: DPR-29, DPR-30

Report No: 05000254/2009005 and 05000265/2009005

Licensee: Exelon Nuclear

Facility: Quad Cities Nuclear Power Station, Units 1 and 2

Location: Cordova, IL

Dates: October 1 through December 31, 2009

Inspectors: J. McGhee, Senior Resident Inspector

B. Cushman, Resident Inspector

R. Orlikowski, Senior Resident Inspector - Duane Arnold

M. Bielby, Senior Operations Engineer

C. Moore, Operations Engineer

M. Mitchell, Senior Radiation Protection Inspector

R. Jickling, Senior Emergency Preparedness Inspector

C. Mathews, Illinois Emergency Management Agency

Approved by: M. Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ...........................................................................................................1

REPORT DETAILS .......................................................................................................................4

Summary of Plant Status...........................................................................................................4

1. REACTOR SAFETY .......................................................................................................4

1R01 Adverse Weather Protection (71111.01)..............................................................4

1R04 Equipment Alignment (71111.04) ........................................................................5

1R05 Fire Protection (71111.05) ...................................................................................6

1R11 Licensed Operator Requalification Program (71111.11)......................................7

1R12 Maintenance Effectiveness (71111.12)..............................................................11

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ........12

1R15 Operability Evaluations (71111.15) ....................................................................12

1R19 Post-Maintenance Testing (71111.19) ...............................................................13

1R22 Surveillance Testing (71111.22) ........................................................................14

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ................15

1EP6 Drill Evaluation (71114.06).................................................................................17

4. OTHER ACTIVITIES.....................................................................................................18

4OA1 Performance Indicator Verification (71151) .......................................................18

4OA2 Identification and Resolution of Problems (71152) ............................................21

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............27

4OA5 Other Activities ...................................................................................................30

4OA6 Management Meetings ......................................................................................30

4OA7 Licensee-Identified Violations ............................................................................31

SUPPLEMENTAL INFORMATION ...............................................................................................1

Key Points of Contact ................................................................................................................1

List of Items Opened, Closed and Discussed............................................................................1

List of Documents Reviewed .....................................................................................................2

List of Acronyms Used ..............................................................................................................8

Enclosure

SUMMARY OF FINDINGS

IR 05000254/2009005, 05000265/2009005; 10/01/09 - 12/31/09; Quad Cities Nuclear Power

Station, Units 1 & 2; Other Activities.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Three Green findings were identified by the

inspectors. Two of the findings were considered Non-Cited Violations (NCVs) of NRC

regulations. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity

level after NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the

installation of an inappropriate component into the Unit 2 emergency diesel generator

coolant system. Specifically, the licensee failed to properly perform a part evaluation for

a replacement temperature indicator (TI) designated as augmented quality. This

resulted in the TI probe shearing off in the coolant flow stream and causing foreign

material to enter the coolant system. Immediate corrective actions included the

installation of an appropriately approved TI and recovery of foreign material from the

system.

The same part evaluation process was used for risk-significant components independent

of the system being worked. Therefore, this finding was more than minor because, if left

uncorrected, this performance deficiency could lead to unplanned unavailability of

safety-related or risk-significant equipment and would become a more significant safety

concern. The inspectors performed a Phase 1 SDP screening and concluded that the

issue was of very low safety significance (Green) because the failure of the TI did not

result in unplanned inoperability or loss of function of the diesel generator. The

inspectors determined that this finding did not have a cross-cutting aspect. This

performance deficiency is not indicative of current licensee performance. The decision

to install this type of TI was made in October 2007. The process which allowed this

performance deficiency was identified and corrected through procedure and policy

revisions in February 2008. (Section 4OA2)

  • Green: A finding of very low safety significance and a NCV of TS 3.6.2.4,

Residual Heat Removal (RHR) Suppression Pool Spray, was self-revealed for the

licensees failure to meet the Technical Specification (TS) limiting conditions of operation

(LCO) requirement prior to transitioning into an operating mode where the LCO was

required to be satisfied. Specifically, Motor Operator (MO) 1-1001-37B for the Unit 1

RHR torus (suppression pool) spray isolation valve was found to have been inoperable

when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009.

The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the

valve was not demonstrated operable by stroking the valve electrically after the actuator

1 Enclosure

motor was declutched. Inspectors determined that the finding was cross-cutting in the

area of Problem Identification and Resolution - Corrective Action (P.1(a)) because plant

personnel failed to identify the physical contact with the valve actuator that resulted in

the valve being declutched; therefore, operators incorrectly assessed the system

condition as in compliance with TS 3.6.2.4. Immediate licensee corrective actions

included engagement of the motor and stroke testing of the valve.

The finding is more than minor because it was associated with the equipment

performance quality attribute of the Mitigating Systems Cornerstone and affected the

objective of ensuring availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, failure to verify

system availability and capability prior to entering the required modes resulted in fewer

available mitigating systems than assumed in the operating risk evaluations. The

inspectors determined the finding could be evaluated using the SDP in accordance with

IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial

Screening and Characterization of findings, Table 4a. Inspectors answered all of the

questions for the Mitigating Systems Cornerstone No. Therefore, the finding screened

as Green or very low safety significance. (Section 4OA3)

Cornerstone: Barrier Integrity

  • Green. A finding of very low safety significance was self-revealed for the failure to

perform maintenance that would ensure the portable emergency flooding pump (Darley

pump) was in a standby condition and readily available to accomplish the requirements

of QCOA 0010-16, Flood Emergency Procedure. Specifically, the failure to perform

adequate maintenance resulted in the need to replace the battery and gasoline for the

pump and, upon pump start, fuel sprayed out of the fuel pump. Although the staged

portable pump would not have supported the external flooding emergency response

procedure, no violation of regulatory requirements occurred. The inspectors did not

identify a cross-cutting aspect associated with this finding because the issue is not

reflective of current licensee performance. Immediate corrective actions included

replacement of the degraded battery and overhaul of the pumps fuel pump. Other

actions included identification of preventative maintenance tasks and establishing a

program owner of the pump and support equipment.

This issue was more than minor because it was associated with the Structures,

Systems, and Components (SSC) Performance attribute of the Barrier Integrity

Cornerstone objective of maintaining the functionality of spent fuel pool cooling.

The finding affected the cornerstone objective of providing assurance that physical

design barriers protect the public from radionuclide releases caused by events including

external flooding. Specifically, the pump could fail due to maintenance preventable

component failure resulting in inadequate or degraded makeup to the spent fuel pool

during an external flooding event. The inspectors determined the finding could be

evaluated using the SDP in accordance with IMC 0609, Significance Determination

Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of

findings, Tables 4a and 4b. The inspectors determined that even though this equipment

is assumed to completely fail, the licensee could provide an alternate portable pump

already located on site and capable of performing the safety function during this slow

developing event. Since alternate equipment was available and the delay in mobilizing

the alternate equipment would not have resulted in loss of capability to mitigate the

2 Enclosure

impact of the flooding event, the issue is of very low safety significance or Green.

(Section 4OA2)

B. Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee was

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees corrective action program. This violation and associated

corrective action tracking number are listed in Section 4OA7 of this report.

3 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1

Unit 1 operated at 100 percent thermal power throughout the evaluated period from October 1

until December 31, 2009, with the exception of planned power reductions for routine

surveillances, planned equipment repair, and control rod maneuvers.

Unit 2

Unit 2 operated at or near 100 percent thermal power from October 1 until December 16 with

the exception of planned power reductions for routine surveillances and control rod maneuvers.

On December 16, 2009, operators attempted to replace a light bulb in the indication circuit for

the extraction steam check valve A on the 2D feedwater heaters. The light bulb separated with

the base remaining in the socket. During the evolution the D heaters tripped, resulting in a

partial loss of feedwater heating and a resulting change in reactor power. Operators lowered

power about 150 MWth (50 MWe) by inserting one high reactivity-worth control rod. Power

increased by 0.59 percent during the loss of feedwater heating transient. By 10:45 a.m. that

same morning, feedwater heaters had been restored and the control rod was withdrawn to

restore the unit to 100 percent thermal power. The unit remained at 100 percent power for the

duration of the evaluated period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Winter Seasonal Readiness Preparations

a. Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant-specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant-specific procedures. Cold weather protection, such as

heat tracing and area heaters, was verified to be in operation where applicable. The

inspectors also reviewed corrective action program (CAP) items to verify that the

licensee was identifying adverse weather issues at an appropriate threshold and

entering them into the CAP in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the Attachment to this

report. The inspectors reviews focused specifically on the following plant systems due

to their risk significance or susceptibility to cold weather issues:

4 Enclosure

  • heating steam, and
  • circulating water/de-icing valve.

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • 1/2 B diesel driven fire pump; and

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders (WOs), condition reports, and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment to this report.

These activities constituted two partial system walkdown samples as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

5 Enclosure

.2 Semi-Annual Complete System Walkdown

a. Inspection Scope

On November 5, 2009, the inspectors performed a complete system alignment

inspection of the Unit 2 emergency diesel generator to verify the functional capability of

the system. This system was selected because it was considered both safety significant

and risk significant in the licensees probabilistic risk assessment. The inspectors

walked down the system to review mechanical and electrical equipment lineups;

electrical power availability; system pressure and temperature indications, as

appropriate; component labeling; component lubrication; component and equipment

cooling; hangers and supports; operability of support systems; and to ensure that

ancillary equipment or debris did not interfere with equipment operation. A review of a

sample of past and outstanding work orders was performed to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the CAP database to ensure that system equipment alignment problems were

being identified and appropriately resolved. Documents reviewed are listed in the

Attachment to this report.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Unit 2 Reactor Bldg. El. 5540, NW Corner Room - 2A Core Spray, Fire Zone

11.3.3;

  • Unit 1 Turbine Bldg. El. 5950, Diesel Generator, Fire Zone 9.1;
  • Unit 1 Turbine Bldg. El. 5950, Reactor Feed Pumps, Fire Zone 8.2.6.A;
  • Crib House Bldg. El. 5598, Basement, Fire Zone 11.4.A; and
  • Crib House Bldg. El. 5950, Ground Floor/Service Water Pumps, Fire Zone

11.4.B.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

6 Enclosure

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

On November 4, 2009, the inspectors observed licensed operator continuing training to

verify that operator performance was adequate, evaluators were identifying and

documenting crew performance problems, and training was being conducted in

accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews communications and accuracy of documentation;
  • ability to take timely actions in the conservative direction;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and lesson objectives. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

7 Enclosure

.2 Facility Operating History (71111.11B)

a. Inspection Scope

The inspectors reviewed the plants operating history from January 2007 through

September 2009 to identify operating experience that was expected to be addressed by

the Licensed Operator Requalification Training (LORT) program. The inspectors verified

that the identified operating experience had been addressed by the facility licensee in

accordance with the stations approved Systems Approach to Training (SAT) program to

satisfy the requirements of 10 CFR 55.59(c). The documents reviewed during this

inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.3 Licensee Requalification Examinations

a. Inspection Scope

The inspectors performed an inspection of the licensees LORT test/examination

program for compliance with the stations SAT program which would satisfy the

requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material

consisted of two operating tests, each containing two dynamic simulator scenarios and

five job performance measures (JPMs). The two biennial written examinations reviewed

consisted of two parts. Each written examination contained 30 questions consisting of

15 written exam questions and 15 static exam questions. The inspectors reviewed the

annual requalification operating test and biennial written examination material to

evaluate general quality, construction, and difficulty level. The inspectors assessed the

level of examination material duplication from week to week during the current year

operating test. The examiners assessed the amount of written examination material

duplication from week to week for the biennial written examination administered in

calendar year 2009. The inspectors reviewed the methodology for developing the

examinations, including the LORT program 2-year sample plan, probabilistic risk

assessment insights, previously identified operator performance deficiencies, and plant

modifications. The documents reviewed during this inspection are listed in the

Attachment to this report.

b. Findings

No findings of significance were identified.

.4 Licensee Administration of Requalification Examinations

a. Inspection Scope

The inspectors observed the administration of a requalification operating test to

assess the licensees effectiveness in conducting the test to ensure compliance with

10 CRF 55.59(c)(4). The inspectors evaluated the performance of one operating crew in

parallel with the facility evaluators during four dynamic simulator scenarios and

evaluated various licensed crew members concurrently with facility evaluators during the

8 Enclosure

administration of several JPMs. The inspectors assessed the facility evaluators ability

to determine adequate crew and individual performance using objective, measurable

standards. The inspectors observed the training staff personnel administer the operating

test, including conducting pre-examination briefings, evaluations of operator

performance, and individual and crew evaluations upon completion of the operating test.

The inspectors evaluated the ability of the simulator to support the examinations.

b. Findings

No findings of significance were identified.

.5 Examination Security

a. Inspection Scope

The inspectors observed and reviewed the licensees overall licensed operator

requalification examination security program related to examination physical security

(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability

and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.

The inspectors also reviewed the facility licensees examination security procedure and

the implementation of security and integrity measures (e.g., security agreements,

sampling criteria, bank use, and test item repetition) throughout the examination

process. No examination security compromises occurred during these observations.

The documents reviewed during this inspection are listed in the Attachment to this

report.

b. Findings

No findings of significance were identified.

.6 Licensee Training Feedback System

a. Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes for

revising and maintaining its LORT program up-to-date, including the use of feedback

from plant events and industry experience information. The inspectors reviewed the

licensees quality assurance oversight activities, including licensee training department

self-assessment reports. The inspectors evaluated the licensees ability to assess the

effectiveness of its LORT program and their ability to implement appropriate corrective

actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and

the licensees SAT based program. The documents reviewed during this inspection are

listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

9 Enclosure

.7 Licensee Remedial Training Program

a. Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial training

conducted since the previous biennial requalification examinations and the training from

the current examination cycle to ensure that they addressed weaknesses in licensed

operator or crew performance identified during training and plant operations. The

inspectors reviewed remedial training procedures and individual remedial training plans.

This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to

the licensees SAT based program. The documents reviewed during this inspection are

listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.8 Conformance With Operator License Conditions

a. Inspection Scope

The inspectors reviewed the facility and individual operator licensees' conformance with

the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's

program for maintaining active operator licenses and to assess compliance with

10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the

process for tracking on-shift hours for licensed operators and which control room

positions were granted watch-standing credit for maintaining active operator licenses.

The inspectors reviewed the facility licensee's LORT program to assess compliance with

the requalification program requirements as described by 10 CFR 55.59(c). Additionally,

medical records for 10 licensed operators were reviewed for compliance with

10 CFR 55.53(I). The documents reviewed during this inspection are listed in the

Attachment to this report.

b. Findings

No findings of significance were identified.

.9 Annual Operating Test Results and Biennial Written Examination Results (71111.11B)

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of the individual JPM operating

tests, the simulator operating tests, and the biennial written examination (required to be

given per 10 CFR 55.59(a)(2)) administered by the licensee from September 2009

through November 2009 as part of the licensees operator licensing requalification cycle.

These results were compared to the thresholds established in Inspection Manual

Chapter 0609, Appendix I, Licensed Operator Requalification Significance

Determination Process (SDP)." The evaluations were also performed to determine if the

licensee effectively implemented operator requalification guidelines established in

NUREG 1021, Operator Licensing Examination Standards for Power Reactors, and

10 Enclosure

IP 71111.11, Licensed Operator Requalification Program. The documents reviewed

during this inspection are listed in the Attachment to this report.

This inspection constituted one inspection sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

  • Z4700; Instrument Air.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for SSCs/functions classified as (a)(2)

or appropriate and adequate goals and corrective actions for systems classified

as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

No findings of significance were identified.

11 Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

water (RHRSW) loop, 1B RHR seal cooler, 1-1001-16A boroscope and Votes

testing, 1-1001-37A MOV equipment qualification inspection; and

  • Work Week 51 - Unit 1 250 Vdc battery reconfiguration using Unit 1 125 Vdc

alternate battery with emergent Unit 2 125 Vdc battery low specific gravity

problems, 2A RHR loop and 2B RHRSW pump unavailability.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

two samples as defined in IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • IR 987904: 1A RHR Room Cooler Tube Sheet Has Pitting, and

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

12 Enclosure

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted two samples as defined in IP 71111.15-05.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • WO 1121775, 250 Vdc Battery Charger #2 4-Hour Load Test;
  • QCMMS 4100-33, 1/2-4101B Diesel Driven Fire Pump Annual Capacity Test;

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

13 Enclosure

This inspection constituted five post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Functional Test (Routine);

  • QCOS 7500-05, 1/2 B Standby Gas Treatment Operability Test (Routine);
  • QCEMS 0230-11, Modified Performance Test of Unit 1(2) 125 Vdc Normal or

Alternate Battery (Routine); and

  • QCOS 6900-14, Station Battery Allowable Value Verification Surveillance

(Routine).

The inspectors observed in plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges, and the calibration frequency were

in accordance with TS, the UFSAR, procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy, applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures, jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

14 Enclosure

Mechanical Engineers code, and reference values were consistent with the

system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing samples, one inservice

testing sample, and one reactor coolant system leak detection inspection samples as

defined in IP 71111.22, Sections -02 and -05.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

Since the last NRC inspection of this program area, Emergency Plan Annex,

Revisions 26 and 27 were implemented based on the licensees determination, in

accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in

effectiveness of the Plan, and that the revised Plan as changed continues to meet the

requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors

conducted a sampling review of the Emergency Plan changes and a review of the

Emergency Action Level (EAL) changes to evaluate for potential decreases in

effectiveness of the Plan. However, this review does not constitute formal NRC approval

of the changes. Therefore, these changes remain subject to future NRC inspection in

their entirety.

This emergency action level and emergency plan changes inspection constituted one

sample as defined in IP 71114.04-05.

15 Enclosure

b. Findings

(1) Unresolved Item (URI) 05000254/2009005-01: Changes to EAL HU6 Potentially

Decrease the Effectiveness of the Plans without Prior NRC Approval

Introduction: The inspectors reviewed changes implemented to the Quad Cities Station

Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 26, the licensee

changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection

within the protected area boundary, by adding two statements. The two changes added

to the EAL basis stated that if the alarm could not be verified by redundant control room

or nearby fire panel indications, notification from the field that a fire exists starts the

15-minute classification and fire extinguishment clocks. The second change stated the

15-minute period to extinguish the fire does not start until either the fire alarm is verified

to be valid by additional control room or nearby fire panel instrumentation, or upon

notification of a fire from the field. These statements conflict with the previous

Quad Cities Station Annex, Revision 25, basis statements and potentially decrease the

effectiveness of the Plans.

Description: Quad Cities Station Radiological Emergency Plan Annex, Revision 25,

EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of

detection, or explosion, within the protected area boundary." The threshold values for

HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of

control room notification or verification of a control room alarm; or 2) Fire outside any

Table H2 area with the potential to damage safety systems in any Table H2 area not

extinguished within 15 minutes of control room notification or verification of a control

room alarm. Table H2, Vital Areas, were identified as main control room, reactor

building, diesel generator rooms, 4 kilovolt switchgear area, battery rooms, B train

control room heating-ventilation and air conditioning, service water pumps, and turbine

building cable tunnel. The basis defined fire as "combustion characterized by heat and

light. Sources of smoke such as slipping drive belts or overheated electrical equipment

do not constitute fires. Observation of flame is preferred but is not required if large

quantities of smoke and heat are observed."

The basis for Revision 25, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of

this threshold is to address the magnitude and extent of fires that may be potentially

significant precursors to damage to safety systems. As used here, notification is visual

observation and report by plant personnel or sensor alarm indication. The 15-minute

period begins with a credible notification that a fire is occurring or indication of a valid fire

detection system alarm. A verified alarm is assumed to be an indication of a fire unless

personnel dispatched to the scene disprove the alarm within the 15-minute period.

The report, however, shall not be required to verify the alarm. The intent of the

15-minute period is to size the fire and discriminate against small fires that are readily

extinguished (e.g., smoldering waste paper basket, etc.).

Revision 26 of the Quad Cities Station Radiological Emergency Plan Annex, changed

the threshold basis for EAL HU6 by adding the following two statements: 1)"If the alarm

cannot be verified by redundant control room or nearby fire panel indications, notification

from the field that a fire exists starts the 15-minute classification and fire extinguishment

clocks," and 2) "The 15-minute period to extinguish the fire does not start until either the

fire alarm is verified to be valid by utilization of additional control room or nearby fire

panel instrumentation, or upon notification of a fire from the field."

16 Enclosure

The two statements added to the basis in Revision 26 conflict with the Revision 25

threshold basis and initiating condition. The changed threshold basis in Revision 26

could add an indeterminate amount of time to declaring an actual emergency until a

person responded to the area of the fire and made a notification to the control room of a

fire in the event that redundant control room or nearby fire panel indications were not

available.

Pending further review and verification by the NRC to determine if the changes to EAL

HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue was

considered an unresolved item (URI 05000254/2009005-01; 05000265/2009005-01).

1EP6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of an after-hours licensee emergency drill on

November 11, 2009, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. The

after-hours drill was preceded by an unannounced, after-hours drive-in drill.

The inspectors observed emergency response operations in the Technical Support

Center to determine whether the event classification, notifications, and protective action

recommendations were performed in accordance with procedures. The inspectors also

attended the licensee drill critique to compare any inspector-observed weakness with

those identified by the licensee staff in order to evaluate the critique and to verify

whether the licensee staff was properly identifying weaknesses and entering them into

the corrective action program. As part of the inspection, the inspectors reviewed the drill

package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b. Findings

No findings of significance were identified.

.2 Emergency Preparedness Termination and Recovery Drill Observation

a. Inspection Scope

The inspectors evaluated the conduct of an emergency preparedness termination and

recovery drill on December 2, 2009, to identify any weaknesses and deficiencies in the

conduct of the drill and to assess the licensees ability to assess performance via a

formal critique process in order to identify and correct Emergency Preparedness

weaknesses. The inspectors observed emergency response operations in the Technical

Support Center to determine whether the recovery and termination activities associated

with the drill were performed in accordance with procedures. The inspectors also

attended the licensee drill critique to compare any inspector-observed weakness with

those identified by the licensee staff in order to evaluate the critique and to verify

whether the licensee staff was properly identifying weaknesses and entering them into

17 Enclosure

the corrective action program. As part of the inspection, the inspectors reviewed the drill

package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index - Emergency Alternating Current Power System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Emergency Alternating Current (AC) Power System performance

indicator for Quad Cities Units 1 and 2 for the period from the 4th quarter 2008 through

the 3rd quarter 2009. To determine the accuracy of the performance indicator (PI) data

reported during those periods, PI definitions and guidance contained in the Nuclear

Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, were used. The inspectors reviewed the licensees operator

narrative logs, MSPI derivation reports, issue reports, event reports and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator, and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI emergency AC power system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Mitigating Systems Performance Index - High Pressure Injection Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - High Pressure Injection Systems performance indicator for Quad Cities Units 1

and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To

determine the accuracy of the PI data reported during those periods, PI definitions and

guidance contained in the NEI Document 99-02, Regulatory Assessment Performance

18 Enclosure

Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees

operator narrative logs, issue reports, MSPI derivation reports, event reports and

NRC integrated inspection reports for the period of October 1, 2008, through

September 30, 2009, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable guidance. The inspectors also reviewed the licensees issue

report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator, and none were identified. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI high pressure injection system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.3 Mitigating Systems Performance Index - Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Heat Removal System performance indicator for Quad Cities Units 1 and 2 for

the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, were used. The inspectors reviewed the licensees operator

narrative logs, issue reports, event reports, MSPI derivation reports, and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator, and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI heat removal system samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.4 Mitigating Systems Performance Index - Residual Heat Removal System

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Residual Heat Removal System performance indicator for Quad Cities Units 1

19 Enclosure

and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To

determine the accuracy of the PI data reported during those periods, the PI definitions

and guidance contained in the NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the

licensees operator narrative logs, issue reports, MSPI derivation reports, event reports

and NRC integrated inspection reports for the period of October 1, 2008, through

September 30, 2009, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable guidance. The inspectors also reviewed the licensees issue

report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator, and none were identified. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI residual heat removal system samples as defined

in IP 71151-05.

b. Findings

No findings of significance were identified.

.5 Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Cooling Water Systems performance indicator for Quad Cities Units 1 and 2 for

the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, were used. The inspectors reviewed the licensees operator

narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator, and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI cooling water system samples as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

20 Enclosure

.6 Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent Technical

Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent

Occurrences performance indicator for the period of December 2008 through

November 2009. The inspectors used PI definitions and guidance contained in the

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6 to determine the accuracy of the PI data reported during those periods.

The inspectors reviewed the licensees issue report database and selected individual

reports generated since this indicator was last reviewed to identify any potential

occurrences such as unmonitored, uncontrolled, or improperly calculated effluent

releases that may have impacted offsite dose. The inspectors reviewed gaseous

effluent summary data and the results of associated offsite dose calculations for selected

dates between December 2008 and November 2009 to determine if indicator results

were accurately reported. The inspectors also reviewed the licensees methods for

quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample

as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1 Routine Review of Items Entered into the Corrective Action Program (CAP)

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

21 Enclosure

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for followup, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues and associated corrective

actions, but also considered the results of daily inspector CAP item screening discussed

in Section 4OA2.2 above, licensee trending efforts, and licensee human performance

results. The inspectors review nominally considered the 6-month period of

January 1, 2009, through June 30, 2009, although some examples expanded beyond

those dates where the scope of the trend warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy. Additionally,

the inspectors reviewed CAP open priority 1, 2, and 3 corrective actions for timeliness.

In addition, all open priority 4 action tracking items (ACITs) were reviewed to ensure they

were properly categorized and that the justifications for extension were appropriate and

properly documented.

22 Enclosure

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings of significance were identified.

.4 Selected Issue Followup Inspection: Issue Report 966501, Darley Pump Leaking

Gasoline from the Fuel Pump

a. Inspection Scope

During a review of items entered in the licensees CAP, the inspectors followed up on a

corrective action item documenting gasoline leaking from the fuel pump of the portable

emergency flooding pump (Darley pump) on September 17, 2009, during preparations

for a pump capacity demonstration run. The pump capacity demonstration was a new

procedure developed in response to a non-cited violation (NCV) documented in

Inspection Report 05000254/2007005.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

Introduction: A finding of very low safety significance was self-revealed for the failure to

maintain the portable emergency flooding pump and supporting equipment in a condition

required to support implementation of QCOA 0010-16, Flood Emergency Procedure.

Description: In Inspection Report 05000254/2007005, inspectors documented a NCV of

TS 5.4.1 for the licensees failure to develop adequate surveillance procedures for

equipment used during an external flooding event. Corrective action for this issue

included revising the external flooding procedure and developing and implementing a

procedure to test a portable pump used as the sole source of makeup water to the spent

fuel pool following an external flooding event. The action to develop and implement the

pump test procedure was issued in May and stated, Develop test procedure and

conduct test to confirm flow of greater than or equal to 200 gpm by mid-July. Brief

NRC Resident as appropriate. The action was closed to an Engineering Change (EC) 366481, on July 18, 2007, with no actual test performed. The documented justification

for this closure stated that discussions with the NRC resident clarified the intent of the

action and no physical testing needed to be performed. Followup discussions with the

resident inspectors stationed at Quad Cities in July 2007 had no recollection of the

conversation and their understanding of the intended action remained unchanged from

the original report.

Licensee staff generated Issue Report (IR) 738335 in February 2008 to document the

review of the NCV response and generate a closure package of all related IRs. The lack

of preventative maintenance (PM) testing was identified and an action tracking item was

generated to Develop PM/testing requirements for the Darley pump associated with the

external flooding event. The original corrective action due date was July 16, 2008.

The action was extended several times, and on May 18, 2009, during a review of

corrective actions for NRC-identified issues, the licensee staff identified that a CAP

23 Enclosure

action item (ACIT 624645-03) had been inappropriately closed. In addition, the licensee

determined that ACIT 624645-03 was inappropriately tagged as an Action Tracking Item

(ACIT) and should have been a corrective action. Issue Report 921197 was generated

and ACIT 624645 was upgraded to a corrective action with a July 31, 2009, due date.

The test procedure was developed and the pump was scheduled to run on

September 17, 2009.

The capacity test was implemented with WO 01247374. When mechanics pulled the

pump and support components from the storage location, they found that the engine

battery had to be replaced and the gasoline stored with the motor had to be replaced.

Since the mechanics performing the test had never operated the pump, they decided to

run it in the weld shop before taking it down to the river. When the mechanics started

the pump, fuel was spraying out of the fuel pump. They immediately shut down the

pump and contained the fuel leak (IR 966501).

The Darley pump fuel system was repaired and the capacity test was completed

satisfactorily on September 25, 2009. Review of recent pump operating history and

PM tasks revealed that the pump had not been operated since the NCV was identified in

2007. The annual maintenance performed under PM 164250 in July of 2009 changed

the oil and inspected the filters and spark plugs with no post-maintenance operation

required. The PM also failed to identify that the battery was beyond the expected life

and did not determine that the battery would maintain its charge.

Analysis: The inspectors determined that the failure to perform maintenance that would

ensure the pump was in a standby condition and readily available to accomplish the

requirements of QCOA 0010-16 was a performance deficiency fully within the licensees

ability to control, and therefore a finding. This issue was more than minor because it

was associated with the SSC Performance attribute of the Barrier Integrity Cornerstone

element of maintaining the functionality of spent fuel pool cooling. The finding affected

the cornerstone objective of providing assurance that physical design barriers protect the

public from radionuclide releases caused by events including external flooding.

Specifically, the pump could fail due to a maintenance preventable component failure

resulting in inadequate or degraded makeup to the spent fuel pool during an external

flooding event. The inspectors did not identify a cross-cutting aspect associated with

this finding because the maintenance issue is a legacy issue and not reflective of current

licensee performance. The pump and PM tasks had been in place for several years.

Inspectors reviewed maintenance requirements for other temporary equipment staged in

support of external events and emergency operating procedures, some of which was put

in place after the Darley pump was staged, and did not identify any similar issues.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of findings, Tables 4a and 4b. The inspectors

determined that even though this equipment is assumed to completely fail, the licensee

could provide an alternate portable pump already located on site and capable of

performing the safety function during this slow developing event. The alternate pump

had maintenance and test procedures in place to provide a basis for reliability. Since

alternate equipment was available and the delay in mobilizing the alternate equipment

would not have resulted in loss of capability to mitigate the impact of the flooding event,

the issue is of very low safety significance or Green.

24 Enclosure

Enforcement: Technical Specification 5.4.1 required that written procedures be

established, implemented, and maintained for the items specified in Regulatory

Guide 1.33, Quality Assurance Program Requirements. QCOA 0010-16,

Flood Emergency Procedure, was the licensee procedure used to meet the

Regulatory Guide 1.33 requirement for an emergency flooding event. The procedure

specified that the portable pump staged in the protected area warehouse is to be used to

respond to the event. Although the regulatory guide did not specifically require

maintenance procedures for portable equipment, failure to maintain the staged

equipment in a condition to be used to mitigate the event does not support timely

implementation of the procedure to provide spent fuel pool makeup and is a finding.

Enforcement action does not apply because the performance deficiency did not involve a

violation of a regulatory requirement. Because the finding does not involve a violation of

regulatory requirements and has a very low safety significance, it is identified as

(FIN 05000254/2009005-02; 05000265/2009005-02). The issue was added to the

licensees CAP program as IR 966501 and IR 968809. Immediate corrective actions

included replacement of the degraded battery and overhaul of the pumps fuel pump.

Other actions included identification of preventative maintenance tasks and establishing

a program owner of the pump.

.5 Selected Issue Followup Inspection: Incident Report 984769, Temperature Indicating

Probe Found Broken in the Unit 2 Diesel Generator Coolant System

a. Inspection Scope

During a review of items entered in the licensees CAP, the inspectors followed up on a

corrective action item documenting a failed temperature indicating probe (TI) in the

Unit 2 diesel generator coolant system on October 27, 2009, during planned

maintenance on the Unit 2 emergency diesel generator (EDG).

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

Introduction: A finding of very low safety significance and associated NCV were

self-revealed when a TI failed in the Unit 2 diesel generator coolant system.

Description: On October 27, 2009, while performing corrective maintenance on

TI 2-6641-8205, technicians noted that the tip had broken off the probe when comparing

it to the length of the new TI. This TI provides local indication of the jacket coolant water

temperature at the inlet to the diesel engine and provides no alarm function.

The TI was scheduled for replacement in October 2008 when Operations identified the

TI reading abnormally at zero degrees. A work order was written and scheduled for

October 2009. During the performance of the maintenance, it was noted that the new TI

was longer than the one recently removed. A new work order was written to retrieve any

foreign material from the system. The broken tip was recovered from the diesel

generator coolant system.

25 Enclosure

The licensee investigation discovered that the installation analysis for this TI was

approved under the non-safety below level of design detail (NSBLD) process in October

2007 under Revision 3 of SM-AA-300, Procurement Engineering Support Activities.

Using this provision, NSBLD changes must be documented and shall identify the

change with justification of the changes technical acceptability. The length of the probe

was the only difference to the previously installed TI. The TI was installed with a

3.25 inch probe, which was longer than the previous 2 inch probe. The added length

increased the shear force from the coolant flow and caused the probe to break off.

An operating experience (OPEX) review would have revealed an event at another

nuclear facility where the same make and model TI experienced the same failure

mechanism in a diesel generator coolant system. Under Revision 3 of SM-AA-300,

OPEX reviews for NSBLD were not required, nor were additional peer reviews required.

The lack of an OPEX review was an identified vulnerability by the licensees corporate

supply organization in a common cause analysis which was performed for a lack of

technical rigor issued in February 2008. A corrective action from this common cause

analysis was to implement Revision 4 of SM-AA-300 which limited NSBLD reviews to

non-safety host component applications. Revision 4 was implemented at Quad Cities in

February 2008. Since this specific TI is classified as augmented quality, Revision 4

would prevent use of the NSBLD process of a non-identical replacement. A full item

equivalency evaluation would be required for any non-identical replacement.

An extent of condition review is scheduled to be performed at Quad Cities by

Procurement Engineering for all NSBLD reviews that were performed under Revision 3

of SM-AA-300 from August 2007 through February 2008.

Analysis: The inspectors determined that the approval of an inappropriate component

designated as augmented quality was a performance deficiency and a finding. The

same parts evaluation process was used for risk-significant components independent of

the system being worked. Therefore, this finding was more than minor because, if left

uncorrected, this performance deficiency could lead to unplanned unavailability of

safety-related or risk-significant equipment and would become a more significant safety

concern. This performance deficiency challenged the Mitigating Systems Cornerstone

attribute of Equipment Performance by challenging equipment availability and reliability.

The inspectors performed a Phase 1 SDP screening and concluded that the issue was

of very low safety significance (Green) because the failure of the TI did not result in

unplanned inoperability or loss of function of the diesel generator. The inspectors

determined that this finding did not have a cross-cutting aspect. This performance

deficiency is not indicative of current licensee performance. The decision to install this

type of TI was made in October 2007. The process which allowed this performance

deficiency was identified and corrected through procedure and policy revisions to

SM-AA-300 in February 2008.

Enforcement: The TI was designated augmented quality in the licensees quality

assurance program. The licensees quality assurance program applied controls

equivalent to safety-related components for Class 1E equipment qualification to

augmented quality equipment and systems. This correlation is applicable to several

Appendix B criteria included in the program such as both Section 3 - Design Control,

and Section 5 - Instructions Procedures and Drawings, of the licensees Quality

Assurance program for augmented quality.

26 Enclosure

Title 10 CFR 50, Appendix B, Criterion V states in part that activities affecting quality

shall be prescribed by instructions and procedures of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions or

procedures.

Contrary to the above, on October 30, 2007, SM-AA-300 was not appropriate to the

circumstances in that it did not require an approval process with technical rigor

equivalent to the process used for safety-related components when a non-identical

temperature indicating probe designated augmented quality was approved for use.

That part was approved for use through a NSBLD review per Revision 3 of SM-AA-300

instead of undergoing a full item equivalency evaluation, and the part subsequently

failed resulting in foreign material in the diesel generator coolant system. The foreign

material did not cause any adverse consequences in this instance.

Because this issue is of very low safety significance, and this issue has been entered

into the licensees corrective action program as Issue Report 984769, this issue is being

treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(NCV 05000265/2009005-03).

Corrective actions for this event included replacement of the TI with an appropriately

approved TI. The licensee has also scheduled to perform an extent of condition review

of NSBLD reviews performed under Revision 3 of SM-AA-300 from August 2007 through

February 2008.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000254/2009-003-00: Failure of RHR Torus Spray

Isolation Valve to Open Due to Declutch Mechanism Problems

a. Inspection Scope

Inspectors reviewed the event, evaluation, and corrective actions for the motor operated

valve failure reported in Licensee Event Report (LER) 05000254/2009-003. Documents

reviewed as part of this inspection are listed in the Attachment to this report. This LER is

closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

b. Findings

Introduction: A finding of very low safety significance and an NCV of Technical

Specification (TS) 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool Spray,

was self-revealed for the licensees failure to meet the TS limiting condition for operation

(LCO) requirements prior to transitioning into an operating mode where the LCO was

required to be satisfied. Specifically, MO 1-1001-37B, motor operator for the Unit 1 RHR

torus (suppression pool) spray isolation valve, was found to have been inoperable when

the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. The

valve actuator had been inadvertently declutched (i.e., motor disengaged) and the valve

was not demonstrated operable by stroking the valve electrically after the actuator motor

was declutched.

27 Enclosure

Discussion: On June 4, 2009, with Unit 1 in Mode 1 at 100 percent power following

startup from a forced outage, MO 1-1001-37B, torus spray shutoff valve, was determined

to be inoperable because it would not open remotely using the control switch during

performance of the residual heat removal power operated valve test surveillance.

The torus spray valve had been closed using the motor and a clearance order had been

placed on the valve during the outage. Another motor operated valve in the residual

heat removal system on that same clearance, MO 1-1001-7C, RHR C torus suction line

isolation valve, had failed to open on May 28, 2009, when the clearance tag was

removed and valve stroking was being performed to restore the component to a standby

configuration. Operators reported manually declutching (disengaging the actuator

motor) the 7C valve while placing the clearance tag in order to verify the valve was

closed. Inspectors identified that the action of manually verifying valve position was not

a normal practice as supported by OP-AA-103-105, Limitorque Motor-Operated Valve

Operations, and Operations department management. Investigation into the 7C failure

revealed that the actuator lubricant was degraded in the area of the clutch return spring

preventing the motor from engaging when called upon from the control circuit. The

RHR C valve actuator was rebuilt using MOV Long Life grease, new tripper cams, new

trip lever assembly, and a new outer declutch arm snap ring. The rebuilt actuator was

verified to operate correctly in all modes and returned to service prior to unit restart on

May 30, 2009.

Inspectors interviewed operating personnel regarding the positioning of MO 1-1001-37B

torus spray valve. Operators stated that they did not manually declutch the 37B valve

since the valve was already closed (normal position) when they hung the tag. The

licensees investigation attempted to identify both how the motor on the 37B valve was

declutched and why the actuator did not return to the motor mode of operation

automatically as designed. The licensee verified that the actuator was not able to

transition from the motor mode to the manual mode without external (human)

intervention.

Although the licensee could not identify how or when the valve actuator motor was

declutched, the licensees investigators concluded that the declutch lever was most likely

bumped during work activities on top of the Torus during the recent outage with the unit

in Mode 4. Investigation further determined that with the valve motor disengaged,

increased friction in the actuator caused by degraded lubricant in the area of the clutch

return spring prevented the engagement of the motor to open the valve. The actuator

motor was engaged by manually manipulating the declutch lever and stroke testing the

valve.

Inspectors reviewed the grease sampling methodology and the preventative

maintenance frequency for the SMP-00 type actuators and determined that both were

conducted in accordance with the industry standards for these type valves.

Analysis: The failure of plant personnel to demonstrate operability of MO 1-1001-37B by

stroking the valve electrically prior to changing modes was a performance deficiency.

The finding is more than minor because it was associated with the equipment

performance quality attribute of the Mitigating Systems Cornerstone and affected the

objective of ensuring availability, reliability and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, failure to verify

system availability and capability prior to entering the required modes resulted in fewer

28 Enclosure

available mitigating systems than assumed in the operating risk evaluations. Inspectors

determined that the finding was cross-cutting in the area of Problem Identification and

Resolution - Corrective Action because plant personnel failed to identify the valve

actuator contact that resulted in the valve being declutched; therefore, operators

incorrectly assessed the system condition as in compliance with TS 3.6.2.4 (P.1(a)).

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a. Inspectors answered all of

the questions for the Mitigating Systems Cornerstone No. Therefore, the finding

screened as Green or very low safety significance.

Enforcement: Technical Specification 3.0, Limiting Condition for Operation (LCO)

Applicability, LCO 3.0.4 stated in part that when an LCO is not met, entry into a mode in

the Applicability shall only be made:

  • when the associated actions to be entered permit continued operation while in

the mode or other specified condition in the Applicability for an unlimited time;

  • after performance of a risk assessment addressing inoperable systems and

components, and acceptability of entering the mode; or

  • when an allowance is stated in the specification.

Technical Specification 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool

Spray, required two RHR suppression pool spray subsystems to be operable in

Modes 1, 2 and 3.

Contrary to the above, on May 30, 2009, the licensee changed operating modes from

Mode 4 to Mode 2 with the MO 1-1001-37B valve inoperable in violation of TS 3.6.2.4

LCO conditions since only one RHR suppression pool (Torus) spray subsystem was

operable. Specifically, TS 3.6.2.4 had no allowance provided to permit mode change

with less than two subsystems operable, no prior risk assessment was performed, and

the specification did not permit operation for an unlimited time, the mode change

resulted in non-compliance with TS LCO 3.6.2.4.

Because this finding is of very low safety significance, and this issue has been entered

into the licensees corrective action program as IR 928048, this violation is being treated

as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(NCV 05000254/2009005-04).

Immediate corrective actions for this event included engagement of the actuator motor

by manually manipulating the declutch lever and stroke testing the valve. Since the

hardened grease in this area of the actuator assembly was only an issue if the actuator

was manually declutched, the valve was left in standby, and overhaul of the valve

actuator was scheduled for the next refueling outage.

29 Enclosure

4OA5 Other Activities

.1 World Association of Nuclear Operators Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the World Association of Nuclear Operators

plant assessment conducted in February 2009. The inspectors reviewed the report to

ensure that issues identified were consistent with the NRC perspectives of licensee

performance and to verify if any significant safety issues were identified that required

further NRC followup.

b. Findings

No findings of significance were identified.

.2 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary

On January 5, 2010, the inspectors presented the inspection results to T. Tulon and

other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The results of the licensed operator requalification training program inspection

and with the site vice president, Mr. T. Tulon, on October 2, 2009.

  • The licensed operator requalification training biennial written examination and

annual operating test examination materials were discussed with the training

manager, Mr. K. Moser, on November 12, 2009.

30 Enclosure

  • The licensed operator requalification training program annual inspection results

with operations training manager, Mr. D. Snook, on November 20, 2009, via

telephone.

  • The results of the Radiological Effluent TS/Offsite Dose Calculation Manual

Radiological Effluent Occurrences performance indicator verification program

inspection with the plant manager, Mr. R. Gideon, on December 16, 2009.

  • The annual review of Emergency Action Level and Emergency Plan changes

with the licensee's emergency preparedness coordinator, Mr. F. Swan, via

telephone on December 21, 2009.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was returned

to the licensee.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meets the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

Calculation Manual. Offsite Dose Calculation Manual, Revision 8, Part 12.2.1,

Radioactive Liquid Effluent Monitoring Instrumentation, Section C requires that

when the service water effluent gross activity monitor is operated with less than

the minimum number of operable channels, the licensee shall collect and analyze

grab samples for beta or gamma activity once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to the

above, grab samples were not collected while the Unit 1 service water effluent

gross activity monitor was inoperable from June 2-20, 2009. Specifically,

following fuse replacement, the licensee failed to recognize that the instrument

remained uninitialized; therefore, that compensatory samples were required. The

finding was documented in the licensees corrective action program as

IR 933472. Corrective actions included returning the monitor to service and

reviewing captured monitor data from June 2-20, 2009, to ensure that no release

events occurred during the monitor outage, revising the monitor repair and

maintenance procedures to clear direct communication with the Chemistry

Department subject matter experts during work on the system, and reinforcing

the expectation that control room operators turn over all abnormal indications to

supervisors each shift. The finding was determined to be of very low safety

significance because, although the finding related to the effluent release

program, it was not a failure to implement the effluent program or an event that

resulted in a dose to the public in excess of Appendix I criterion or

10 CFR 20.1301(e).

ATTACHMENT: SUPPLEMENTAL INFORMATION

31 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Tulon, Site Vice President

R. Gideon, Plant Manager

D. Kimler, Shift Operations Superintendent

S. Darin, Engineering Manager

W. Beck, Regulatory Assurance Manager

J. Burkhead, Nuclear Oversight Manager

J. Garrity, Work Control Manager

K. Moser, Training Manager

V. Neels, Chemistry/Environ/Radwaste Manager

D. Collins, Radiation Protection Manager

D. Thompson, Security Manager

Nuclear Regulatory Commission

M. Ring, Chief, Reactor Projects Branch 1

Illinois Emergency Management Agency

R. Zuffa, Unit Supervisor, Resident Inspector Section

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000254/2009005-01; URI Changes to EAL HU6 Potentially Decrease the Effectiveness05000265/2009005-01 of the Plans without Prior NRC Approval

05000254/2009005-02; FIN Darley Pump Leaking Gasoline from the Fuel Pump

05000265/2009005-02

05000265/2009005-03 NCV Temperature Indicating Probe Found Broken in the Unit 2

Diesel Generator Coolant System

05000254/2009005-04 NCV Failure of RHR Torus Spray Isolation Valve to Open Due to

Declutch Mechanism Problems

Closed

05000254/2009005-02; FIN Darley Pump Leaking Gasoline from the Fuel Pump

05000265/2009005-02

05000265/2009005-03 NCV Temperature Indicating Probe Found Broken in the Unit 2

Diesel Generator Coolant System

05000254/2009005-04 NCV Failure of RHR Torus Spray Isolation Valve to Open Due to

Declutch Mechanism Problems05000254/2009003-00 LER Failure of RHR Torus Spray Isolation Valve to Open Due to

Declutch Mechanism Problems

1 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01

- QCOP 0010-01; Winterizing Checklist; Revision 48

- QCOP 0010-02; Required Cold Weather Routines; Revision 28

- WC-AA-107; Seasonal Readiness; Revision 06

- IR 99493; U-2 FW Heater LCV Response to Lowering Circulating Water Inlet Temp

- WO 1183498; Cycle CW De-Ice Valve

- WO 1282535; Ice Melt Valve Stuck Shut

- QCOP 4400-06; Circulating Water System De-icing; Revision 14

- ECR 59777; Design Alternate Method for Operation of Ice Melt Valve

- IR 993018; Wire Rope Rating on Ice Melt Valve

- IR 986355; Ice Melt Valve Stuck Shut

- WO 01194645; MM Union Leaking Inside U1 Cond Demin Vault (HTG STM)

- WO 01215488; MM Repair Piping Leak Underground Next to Cribhouse

- WO 01242820; MM Seal Cracks in Ceiling Above Bus 23-1

Section 1R04

- QCOP 4100-01; Firewater System Lineup for Standby Operation; Revision 4

- QCOP 6600-01: Diesel Generator 1(2) Preparation For Standby Operation; Revision 38

- WO #01272234; EM Change RMS-9 Setting at SWGR 19 CUB 5D Per EC 377092

- WO #01107582; EM Replace U2 DGCWP Alternate Feed Contactor

- WO #920850; IM CAL DG HX 2-6661B Cooling Water Inlet PI 2-3941-67A

- WO #945963; IM CAL DG HX 2-6661B Cooling Water Outlet PI 2-3941-67B

- WO #01107581; EM Replace U2 DGCWP Normal Feed Contactor

- WO #01245102; EM Support OP QCOS 6600-17 U2 DGCW Pump Alternate Feed Test

- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for

Appendix R; Revision 15

- EC 360507; Unit 2 EDG Voltage Regulator (Place EDG in Droop Mode Prior to

Synchronization to the Grid)

- EC 377665; TMOD to Bypass Faulty SSES Switch Local/Remote Contact at U2 Diesel

Generator

Section 1R05

- OP-AA-201-008; Pre-fire Plan Manual Index - Pre-Plan RB-16; Revision 2

- Pre-plan TB-74; Fire Zone 9.1, Unit 1 Turbine Bldg. El. 595-0, Diesel Generator; Revision 24

- Pre-plan TB-73; Fire Zone 8.2.6.A, Unit 1 Turbine Bldg. El. 595-0, Reactor Feed Pumps;

Revision 24

- Pre-plan CH-44; Fire Zone 11.4.A, Crib House Bldg. El. 559-8 Basement; Revision 0

- Pre-plan CH-45; Fire Zone 11.4.B, Ground Floor/Service Water Pumps; Revision 22

2 Attachment

Section 1R11

- SY-AA-101-132; Assessment and Response to Suspicious Activity and Security Threats;

Revision 14

- QCOA 0010-20; Security Event; Revision 25

- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27

- Requalification Examination Results/Calendar Year 2009

- Quad Cities, Units 1 and 2 NRC Integrated Inspection Reports; dated various from

January 2007 through September 2009

- OP-AA-105-102; Attachment 1; Active License Tracking Log (for 1st & 2nd Quarters of 2009);

Revision 9

- OP-AA-105-102; Attachment 2, Reactivation of License Log (2 for LSRO, 2 RO); Revision 9

- Quad Cities Classroom Sample Plan for Training Years 2008 and 2009; 6/18/2009

- Quad Cities Simulator Sample Plan for Training Years 2008 and 2009

- 71111.11 Appendix C Responses/Justifications; 9/28/2009

- TQ-AA-224-F070; Evaluation Feedback Summary, LORT Cycle 08-1 through 08-5; LORT

Cycle 09-1 through 09-4

- TQ-AA-1002; Attachment 3; LORT Quarterly Curriculum Review Committee Meeting Minutes;

all of 2008 and first two quarters of 2009

- Special LORT CRC Meeting Minutes; 1/23/2009

- TQ-AA-150; Operator Training Programs; Revision 2

- TQ-AA-150-F07; Simulator Evaluation Form - STA or IA

- TQ-AA-150-F08; Simulator Evaluation Form - Individual

- TQ-AA-150-F09; Simulator Evaluation Form - Crew

- TQ-AA-210-5101; Training Observation Forms; dated various

- TQ-AA-306; Simulator Management

- TQ-AA-306-F06; BWR Critical Condition for Cold Startup; Revision 0

- TQ-AA-306-F07; BWR Power Coefficient of Reactivity and Control Rod Worth; Revision 0

- TQ-AA-306-F08; BWR Xenon Worth; Revision 0

- TQ-AA-306-F06; BWR Site Specific Shutdown Margin and Reactivity Anomaly Tests

- TQ-AA-306-JA-02; Simulator Testing Report Update

- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 14;

7/17/09

- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 15;

9/29/09

- LS-AA-126-1005; Attachment 2; Check-In Self-Assessment Report Template

- LS-AA-126-1001; Attachment 2; FASA Self-Assessment Report

- Simulator Malfunction Test Procedure, Grid Frequency Disturbance (ED16)

- Simulator Malfunction Test Procedure, Reactor Building Instrument Air System (IA02)

- Simulator Malfunction Test Procedure, Main Steam Isolation Valve Closure (MS01)

- Quad Cities Simulator Malfunction Testing Schedule; Revision 8; 5/5/2008

- Simulator Transient Tests; dated various

- Safety System Functional Failure, Rolling Twelve Months Unit 1 and Unit 2; 9/28/09

- Action Request Reports; various dates for LORT 2009

- LORT Attendance Sheets; 2009

3 Attachment

Section 1R12

- Enterprise Maintenance Rule Production Database for the following systems:

  • Z4700; Instrument Air

- System Engineer Notebook and Accountability Logs for the following systems:

  • Instrument Air

- IR 712670; Safe shutdown makeup pump failed surveillance; 12/17/07

- IR 713041; Broken SSMP part not found during repairs; 12/18/07

- IR 711934; SSMP Suction line did not fill during fill; 12/14/07

- IR 712059; SSMP fails to sustain flow and pressure; 12/15/07

- IR 731013; SSMP Sparking on Startup; 2/4/08

- IR 729984; SSMP failed operability test per TIC-1982; 2/1/08

- IR 729951; SSMP Local FIC failed PMT; 1/31/08

- IR 734472; MRULE A-1 determination for SSMP required; 2/11/08

- IR 741838; SSMP feed breaker problems during system restoration; 2/27/08

- IR 787063; Local SSMP flow controller not reading correctly; 6/16/08

- IR 890904; SSMP controller connector degraded; 3/10/09

- IR 930013; Historical FME identified in SSMP piping inspection; 6/10/09

- IR 956294; SSMP FIC Valve position discrepancy with local valve indication; 8/21/09

- IR 947201; FPI - SSMP Breaker and fuse coordination for CT-2; 7/29/08

- IR 1003024; SSMP Draws a vacuum when starting for PMT; 12/09/09

- IR 1002036; Drain valve for SSMP room cooler may be blocked; 12/06/09

- IR 991490; NCV 09-006-02 Closure package - SSMP Breaker coordination 11/10/09

- IR 673268; 1B Instrument Air Compressor Excessive Leakage; 9/20/07

- IR 762652; 1A Instrument Air Compressor Trip; 04/12/08

- IR 856509; Red Trend Code for 1/2B Instrument Air Compressor - EC 364602

- IR 871161; 1A Instrument Air Compressor Trip; 01/24/09

- IR 871939; 1A Instrument Air Compressor Trip; 01/26/09

- IR 977823; 1A Instrument Air Compressor Tripped Due to Low Oil Pressure; 2/7/09

- IR 936122; Compressor does not auto start; 6/27/09

Section 1R13

- WO #01075655; EM Perform Boroscope INSP of MO 1-1001-16A MOV

- WO #01120751; EM MOV 1-1001-37A MOV EQ Inspection

- WO #01123089; MM Inspect/Clean 1B RHR Pump Seal Cooler

- WO #01131318; EM Votes Test MOV 1-1001-16A

- WO #01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect

Section 1R15

- IR 849245; 1B RHR Room Cooler Heat Exchanger Has Tube Sheet Pitting

- WO 862709; 1B RHR Air/Water Side Room CLR CLN/INSP

- IR 987904; 1A RHR Room Cooler Heat Exchanger Tube Sheet Has Pitting

- WO 01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect

4 Attachment

- IR 849681; 1B RHR Room Cooler Reassembled at Risk

- EC 373177; Determination of Minimum Wall Thickness of Tubesheet for RHR Room

Cooler 1-574B

- IR 994823; TS SR 3.8.4.8 Frequency Not Met

- QC-SURV-01; Risk Assessment for Missed Surveillance for U2 125 Vdc Battery

Section 1R19

- QCMMS 4100-32; 1/2 -4101A Diesel Driven Fire Pump Annual Capacity Test; Revision 24

- WO 1261246; Replace Battery Changeover Relay R12 EC 376690

- EC 376690; 1/2 A Fire Pump Controller Replace Battery Changeover Relay R12; Revision 1

- QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 28

- QCOP 4100-03; Diesel Fire Pump Operation; Revision 17

- QCMMS 4100-33; 1/2 - 4101B Diesel Driven Fire Pump Annual Capacity Test; Revision 24

- WO 1121775; 250 Vdc Battery Charger #2 4 Hour Load Test

- WO 1130534; Control RM HVAC Air Filter Unit In Place DOP LK Test

- QCOS 5750-02; Control Room Emergency Filter System Test; Revision 45

- QCIS 5700-04; Main Control Room Air Filter Unit DOP-Freon Test; Revision 0

- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for

Appendix R; Revision 15

- QCEPM 0400-15; Emergency Diesel Generator Transfer Panel Inspection; Revision 9

- WO 01107582; Replace Unit 2 DGCWP Alternate Feed Contactor

Section 1R22

- QCOS 1400-01; Quarterly Core Spray System Flow Rate Test; Revision 38

- QCOS 1400-07; Core Spray Pump Performance Test; Revision 10

- QCOS 7500-05; Standby Gas Treatment System Monthly Operability Test; Revision 30

- QCIS 0300-02; Unit 1 Division 1 Scram Discharge Volume Rochester Instruments Calibration

and Functional Test; Revision 09

- QCOS 1600-07, Revision 027; Reactor Coolant Leakage in the Drywell

- QCEMS 0230-11; Modified Performance Test of Unit 1(2) 125 Vdc Normal or Alternate

Battery; Revision 0

- QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 33

- QCOP 6900-24; Transfer of Unit 2 125 Vdc Battery Bus Between Normal and Alternate

Battery; Revision 12

- QCOS 6900-14; Station Battery Allowable Value Verification Surveillance; Revision 13

Section 1EP4

- Quad Cities Station Radiological Emergency Plan Annex; Revisions 25, 26, and 27

Section 1EP6

- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27

- Quad Cities Generating Station 2009 Termination and Recovery Drill Briefing Package;

December 2, 2009

- EP-AA-115; Termination and Recovery; Revision 7

- EP-AA-111-F-01; Termination/Recovery Checklist; Revision A

5 Attachment

Section 4OA1

- CY-QC-120-724; Continuous Liquid Effluent Analysis; Revision 1

- CY-QC-120, 723; Allocation of Radioactive Liquid Discharges; Revision 0

- CY-QC-120-720; Plant Effluent Dose Calculations; Revision 4

- CY-QC-120-725; Gaseous Release of Tritium Calculation; Revision 1

- Cy-QC-120-726; Fe-55, Sr-89, Sr-90 and Gaseous Alpha Release; Revision 3

- NEI 99-02; Regulatory Assessment Performance Indicator Guideline, Revision 6

- Enterprise Maintenance Rule Production Database for the following systems:

  • Z6600; Diesel Generator System

- System Engineer Notebook and Accountability Logs for the following systems:

Section 4OA2Q

- IR 984769; Well Broke Off TI in Diesel Generator Coolant System

- WO 1198663; U-2 EDG Eng Temp Indicator TI-2-6641-8205 Not Working

- WO 1280197; Well Broke Off TI In U2 Diesel Generator Coolant System

- SM-AA-300; Procurement Engineering Support Activities; Revision 5

- IR 624645; Flood Emergency Pump Testing Documentation; 05/02/07

- IR 638004; Clarify UFSAR 3.4.1.1 Required Flow Rate to SFP During Flood; 06/07/07

- IR 738335; NCV 07-005-02 GR NCV & X-cutting WRT External Flooding Event; 02/19/08

- IR 921197; Inappropriate ACIT Closure of Darley Pump NCV; 05/18/09

- IR 927463; Request For Darley Pump Testing in On-line Schedule; 06/03/09

- IR 966501; Darley Pump Leaking Gasoline from the Fuel Pump; 09/17/09

- IR 968809; Adequacy of Preventative Maintenance on Darley Pump; 09/22/09

- WO 01247374; Darley Pump Baseline Testing; 9/17/09

- QCOA 0010-16; Flood Emergency Procedure; Revision 12

- QCMMS 1500-12; Portable Emergency Flood Pump Capacity Test; Revision 0

- QCOP 4100-19; Emergency Portable Pump Operations; Revision 7

- PMID/RQ 164250; Perform Maintenance on the External Portable Pump; 09/17/09

Section 4OA3

- 10 Medical Files for Licensed Operators; Various Dates

- Licensee Event Report 254/09-003; Failure of RHR Torus Spray Isolation Valve Due to

Declutch Mechanism Problems; 8/3/09

- IR 928048; MO 1-1001-37B Failed to Open During QCOS 1000-09; 6/4/09

- IR 924666; 1-1001-7C Will Not Open; 5/28/09

- OP-AA-103-105; Limitorque Motor-operated Valve Operations; Revision 1

6 Attachment

Section 4OA7

- AR 933472933472 Service Water Effluent Radiation Monitor Inoperable; 6/20/09

7 Attachment

LIST OF ACRONYMS USED

AC Alternating Current

ADAMS Agencywide Document Access Management System

ACIT Action Tracking Item

CAP Corrective Action Program

CFR Code of Federal Regulations

DGCWP Diesel Generator Cooling Water Pump

EAL Emergency Action Level

EC Engineering Change

EDG Emergency Diesel Generator

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Issue Report

IST Inservice Test

JPM Job Performance Measure

LCO Limiting Condition for Operation

LER Licensee Event Report

LORT Licensed Operator Requalification Training

MO Motor Operator

MOV Motor Operated Valve

MSPI Mitigating System Performance Index

NCV Non-Cited Violation

NEI Nuclear Energy Institute

NRC U.S. Nuclear Regulatory Commission

NSBLD Non-Safety Below Level of Design Detail

OP Operations

OPEX Operating Experience

ODCM Offsite Dose Calculation Manual

PARS Publicly Available Records

PI Performance Indicator

PM Planned or Preventative Maintenance

PMT Post Maintenance Test

RCS Reactor Coolant System

RETS Radiological Effluent Technical Specification

RHR Residual Heat Removal

RHRSW Residual Heat Removal Service Water

SAT Systems Approach to Training

SDP Significance Determination Process

SSC Systems, Structures, and Components

TI Temperature Indicator

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

Vdc Volt direct current

WO Work Order

8 Attachment

C. Pardee -2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter

and its enclosure will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Enclosure: Inspection Report 05000254/2009005; 05000265/2009005

w/Attachment: Supplemental Information

cc w/encl: Distribution via ListServ

DOCUMENT NAME: G:\1-Secy\1-Work In Progress\QUA 2009005.doc

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE RIII E RIII

NAME MRing:cms

DATE 01/27/2010

OFFICIAL RECORD COPY

Letter to C. Pardee from M. Ring dated January 27, 2010

SUBJECT: QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 INTEGRATED

INSPECTION REPORT 05000254/2009005; 05000265/2009005

DISTRIBUTION:

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