ML20141K930: Difference between revisions

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| number = ML20141K930
| number = ML20141K930
| issue date = 07/07/1971
| issue date = 07/07/1971
| title = Forwards Category B Repts Re Util 710614 Ltr Transmitting Summary Technical Rept on Primary Containment Leak Rate Test Info.No ACRS Action Warranted
| title = Forwards Category B Repts Re Util Transmitting Summary Technical Rept on Primary Containment Leak Rate Test Info.No ACRS Action Warranted
| author name = Mckinley J
| author name = Mckinley J
| author affiliation = NRC ADVISORY COMMITTEE ON REACTOR SAFEGUARDS (ACRS)
| author affiliation = NRC ADVISORY COMMITTEE ON REACTOR SAFEGUARDS (ACRS)
Line 12: Line 12:
| case reference number = FOIA-91-282
| case reference number = FOIA-91-282
| document report number = NUDOCS 9203260134
| document report number = NUDOCS 9203260134
| title reference date = 06-14-1971
| package number = ML20091A092
| package number = ML20091A092
| document type = INTERNAL OR EXTERNAL MEMORANDUM, MEMORANDUMS-CORRESPONDENCE
| document type = INTERNAL OR EXTERNAL MEMORANDUM, MEMORANDUMS-CORRESPONDENCE

Latest revision as of 10:06, 12 December 2021

Forwards Category B Repts Re Util Transmitting Summary Technical Rept on Primary Containment Leak Rate Test Info.No ACRS Action Warranted
ML20141K930
Person / Time
Site: Oyster Creek
Issue date: 07/07/1971
From: Mckinley J
Advisory Committee on Reactor Safeguards
To: Stratton W
Advisory Committee on Reactor Safeguards
Shared Package
ML20091A092 List: ... further results
References
FOIA-91-282 NUDOCS 9203260134
Download: ML20141K930 (3)


Text

. . . - -- - - - - . .. .. . ._ _ .

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_I July 7, 1971 f - :

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W. R. Stratton, Chairman Oyster Creek Subcuumdttee I C. F. $less, Vice Chairman, JCES CATEGORY 5 REPORTS - 0f87E1 CREEK - JERSIT CENTRAL POWER & L2GRT CONFANY 1.ETTER UNDATED TRANSKITTING St2 MARY TECINIICAL REfott PRIMARY l CONTAllem3rr 17 AKAGL 5ATI TEST MAY 1971; JERSEY CENTRAL POWER & LIGET

.l COMPANT 12TT11s DATED JUIE 14 & 15, 1971, JUNE 15, 1971 TRANSKITTING RESULTS OF A PRELIMINARY INVESTIGATION, AND JUNE 25, 1971 TRANSMITTING OPERATIONAL QUALITY ASSURANCE PROGRAM SUIMARY DESC11FTION

, Attached is e brief summary of the 1sformation presented in the subject i correspondence. No ACRS action appears warranted.

I these items should be incorporated in your set of project documents to maintain an up-tWate description of EM plant, orgeaisatten, procedaes. .

etc.

f Original Signed by J. C luKinley.

( J. C. McKinley

. .j .

Staff Assistant Attachsents:

1) Summary I 2) JCP&L lte date unknown teetg l l Summary Tech. Ept primary l Containment Laakage Rate Test i

May 1971

3) JCP&L ltrs dtd 6/14, 15, 25 (1)/71 p.

l 9 c.

M i

! omer > .. ACRS... .. . . .. . . . ._.. . . . . . . . . . .

sunn ut> . . ..JCMibjw... . . . . . . . . . . . . . . . . . . . . . . . . .

/)/

I DATE> .

7/7/71 _

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Form AEC=318 (P.ev. D 53) u.s covtRautm rn<mine cara iw & meses ,

9203260134 910807 /

PDR FOIA /

DEKOK91-282 PDR /((<

J lf).$C

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1 l

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_- u m y .

StWTsit casali _Jereer central Feuer and u a g e adatadi osbeits a report describias the prhessy 1, .

't eestaineset Lashese sets test osadested am Mf.-

ectober 1979. D e inteersted Primary Osmasteag'"t meat beak ants test was esspleted en esteher 22, 1970. It une condested La enesedanse udth Section 4.5 of the Techsteal Apocifteettens ,

't one within the reestred 12 meethe + 4 usethe of initial eritiestity ( May 3,19I9 ).

h e overall task rate oss ta emcees of asesytabla Itaits. His was due to the lashase throach the torus sayson enslyear isetation yaluer shiek dailmi f to oest propetly. h a Leekage threagh this value i has been estimated to be W botmeen 7

(' .pereest and 9 pereent of the aestained volume per day.

! A leek squares fit of all the data assalted ta' l an overall Leak rate of 0.276 pereest per day.

It uns noted, however, that the data points prier to 1100, 0:taber 21 were gutte erratia. Ekts was due to e drywell recirculaties faa dish tripped I .

and was sta:*.ed neve.ral times duries the test

, , thereby pr..ating the drywell atmosybere from

' reaching en equilibrium asedition until appremi-l mately 1100. October 21. f r g: ~ 1y, a toast l

l squarea fit en the last 13 data peints una calculated resulting is a 0.116 poetent per day i _

'- Leek rate. It is believed that this figure is .

. 1 mera representative of the eetual steady state

! leak rete of the oestaimeemt vessel at 30 pois.

no Acts acties appears warrested.

hsy fetrel Power And teat Comener tatter I dated June _14.197J, esports she failure of

] Contalement spray system Bish.Bryme11 Pressure IF 15A to roast af tet botas tripped for Sommers surveillance testies. Sa malfumation was traced to the misalismeest of a adgmet attached to tbs l

differential pressure bellows of the settah.

aspairs were made and thaspystan returned to normal operation gi ,

?;- ., ,% ,, , ' '

me acas ties e.,uired. 9 .

mm OPTict >

M er M el4L5r1D1-reports-the 1 M e44 Lt&Bt E_collapse.cf._the _ _ _:1

-- ~ ~ ~ - - - - - . . _ . . . . .

g.Juss somut> .. .. ,

eit( peekage bot.(or,dlue.- - - - . .

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~

Furm AEC.338 (Rev.6@ ua .ovtamarm emmms GFx7 de2uu I

^*

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(

9tW11R CatcK I.jgf '

(COIET N ED) h,;; I j

.; 9 '

he 30-taeb esameito flue une erestad AmeMeD plant's vuotilation eteek. It penetmated t s i ventitettom otmak at appresiastely ah*8== M '

feet and see taside the steek to trichia le techos of the top. Its purpees ans to carry off the oeshustion geese from the peehage hattae. He soltepee of the flue reemitad la minor esmeso to the imekiastis pesbo of the etask gaa==14 Ler but eyetan perforesame is met afeested.

t j Aetime one sehen famodtately te onestrust a tem flue for the pechase boiler, outside  ;

et ventilatime eteck, La seder to treturn the '

I boiler and the wasta eencastratar to service me soon as possihte. I At the meat outage of saitable duretten, she isoktaetic probe will be seemined and r u _ied er repaired se required.

> Acas action toquired.

Jereer Centrol Power And Liaht Commeny lotter i

dat.ed June 25,197i reporto preliminary assaults l et the unter hame==r incident in the eere aprey l i eyeten. A jockey puuy woe tastelled to heap L

L 1

I the syntam filled. The 1sttar reports the actions taken or ytanned to evalanta the adequacy of the

't eere spray pipias systene.

l We ACES action appears warranted.

]

Jereer central Power _^-d U-ke causar latter t

dated *~ 15.1971 auhaits a===a===t No. M i

! to the applicottaa. Bis Ansedmont deoerihme

[ the'opeastiment quality assuroese pine and is

' suhaitted La respesos to DEL's Herob 15, 1971

, letter (aes awplasset me.140)

L i

me Acts aaetan required.

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om , . . . . . . . e . .. .1:. .. ,.. . . . . . . . . . . . . . . .-- -

Form MX:-316 (Ro. 941) us sownsince mmins aux m-o me

,, . . . . . _ _ _ - - - . . . _ .