ML19273A978: Difference between revisions

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lgj,gg declared operable.                            The Instrument and Control (I&C) Foreman will now be issued a
lgj,gg declared operable.                            The Instrument and Control (I&C) Foreman will now be issued a
     ,, ,, g
     ,, ,, g
                                                                                                                                                                                                    ;
     ,,,3,            l copy of the I&C' weekly schedule of required testing.
     ,,,3,            l copy of the I&C' weekly schedule of required testing.
l i 4          l                                                                                                                                                                      83 7        8 9 OTHER ST ATUS              DISCO RY                              DISCOVERY DESCRIPTION 32 STA 5                % POWER Ii ls l lE l@ l 0 8[9lg]                                              NA                          l      B l@l Test Coordinator Routine Check l
l i 4          l                                                                                                                                                                      83 7        8 9 OTHER ST ATUS              DISCO RY                              DISCOVERY DESCRIPTION 32 STA 5                % POWER Ii ls l lE l@ l 0 8[9lg]                                              NA                          l      B l@l Test Coordinator Routine Check l

Latest revision as of 03:44, 22 February 2020

LER 79-001/03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator
ML19273A978
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 01/29/1979
From: Borysiak M
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19273A977 List:
References
LER-79-001-03L, LER-79-1-3L, NUDOCS 7902010162
Download: ML19273A978 (3)


Text

. . . a o .

NRC FORM 3GG (7 77)

LICENSEE EVENT REPORT

, CONTROL BLOCK; l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 lo j il JO l11 D l B l S l 1 l@l 0l 0l -l 0]LICENSE 0l Nt.LytiERPl Fl - 0 3lh @l26 4] LICENSE 1l 1] 1l TYPE JJ 1 @l57 C lA T 58l@

7 8 9 LICENSE E CODE 14 15 CON'T lolil R

3gCRTc 9 l L l@l 0 5 0] -l 0l 3l 4l 6l@l0 (M 69 l1 l0 l2 l7 ]9 l@l 075l 1 lREPORT EVENT DATE 74 2 l 9D ATEl 7 l 980 l@

? 8 60 t.1 DOCKET NUYBER EVENT DESCHIPTION AND PRC8 AOLE CONSEQUENCES h

[

o 2 lOn 1/2/79, the Surveillance Test Coordinator discovered that the Monthly Functional The o 3 l Test had not yet been performed on Reactor Protection System (RPS) Channel 2. [

o 4 test late date which includes the maximum allowable extension was 1/2/79 at 0720 hourd.

o s The channel was declared inoperable at 1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br />. There was no danger to the health ]

o 6 and safety of the public or unit personnel. The completion of the required Surveillange RPS Channels 1, 3, and 4 were operable]

o d l Test verified that RPS Channel 2 was operable.

O a lar the time RPS Channel 2 was declared inoperable. (NP-33-79-02) ]

CAUSE COYP. VALVE

$YSTEM CAUSE SUSCODE SU8CCDE COMPONENT CODE SUSCODE CODE CODE o 9 11 lA l @ lA l @ [C l@ lZlZlZlZlZlZl@ y @ y @

12 13 18 19 20 7 8 9 10 11 REVISION SEQUENT:AL OCCURRENCE REPORT CODE TYPE NO.

REPORT NO.

tg g .Ro _ EVENT YE AR

@ REPORT l7l9 l-l l0 l0 l1 l/] Ol3 Ll l_[ 0l 27 28  ?) 3J 31 32

_ 23 22 23 24 2ti FC 9 LB. SL PLIE P,* A FA ER A Ef A O O PL AP T T HOURS 22 S B T IG 33 l@lJ4 Zl@ 1 Z i@

3 '.a 3o.

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010 D I M> I 40 W@ lNj@ lZl@

41 42 43 lZjZlZlZl@

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l

i o !There was a breakdown in communications between testine narconnel arid tho taqr cone-dinator. The Surveillance Test was completed and at 15:125 hours, the channel was _

lgj,gg declared operable. The Instrument and Control (I&C) Foreman will now be issued a

,, ,, g

,,,3, l copy of the I&C' weekly schedule of required testing.

l i 4 l 83 7 8 9 OTHER ST ATUS DISCO RY DISCOVERY DESCRIPTION 32 STA 5  % POWER Ii ls l lE l@ l 0 8[9lg] NA l B l@l Test Coordinator Routine Check l

ACTIVITY CONTENT LOCATION OF RELE ASE RELEASED OF HELF ACE AYOUNT OF ACTIVITY l NA l 7

i c 8 9

{@ 10 Z lgl 11 NA ] 4 45 60 PERSONNEL EXPOSURES NU"B F it TYPE DESCRIPTION l

1 7 l0 l0 0 l@l Z @[ NA *

' uRSONNa'imuh5 Nomn oESCn# TION @ l NA i R 10 l0 c ig 80 7 8 9 18 12 WR##?&'N "" @ 7 9 0 2 010/6 A l li l 91 8 9 IZ l@l10N^ b0 7

PUUllCITY NRC USE ONLY tyE n DEglPTION l ll l[li'I!]gI l 2 l ol Whl "" C4 (. ) ?i

! >t *) 10 233 p DVR 79-00'7 Mike Barysiak PHONE. 419-259-5000, Ex t. 3 NAME Of PinEPAHEH

TOLEDO EDISON COMPANY t DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-02 DATE OF EVENT: January 2, 1979 FACILITY: Davis-Besse Unit 1 Channel 2 of the Reactor Protection System (RPS)

IDENTIFICATION OF OCCURRENCE:

was declared inoperable due to failure to perform requic2d surveillance testing The unit was in Mode 1, wirn Power (MUT) = 2467, and  !

_ Conditions Prior to Occurrence:

Load (Gross MWE) = 839.

Description of Occurrence: On January 2,1979, the Surveillance Test Coordinator dis-covered that ST 5030.02, "RPSlate Monthly Functional Test" had not yet been performed on date (maximum allowable extension) was January 2,1979 RPS Channel 2. The test at 0720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />. Af ter verifying the testing interval was exceeded, the Surveillance Test Coordinator informed the Shif t Foreman, who then declared the channel inoperable at 1125 hours0.013 days <br />0.313 hours <br />0.00186 weeks <br />4.280625e-4 months <br />.

This placed the unit in the Action Statements of Technical Specification 3.3.1.1.

The channel was bypassed to perform the required testing within one hour of the time the channel was declared inoperable.

The Instrument and Control RPS Foreman was notified that the test would have to be per-Channels 1, 3, and 4 were operable at the time RPS Channel 2 formed immediately.

was declared inoperabic.

There was a breakdown in communications Designation of Apparent Cause of Occurrence: coordinator which caused the delay in the per-between testing personnel and the test formance of ST 5030.02.

Analysis of Occurrence: There was no danger to the health and safety of the public or to unit personnel. The completion of the required Surveillance Test verified that RPS Channel 2 was operable.

Corrective Action: At 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, on January 2, 1979, ST 5030.02 was started on RPS Channel 2. The Surveillance Test was completed and at 1925 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.324625e-4 months <br />, the channel was declared operable.

To prevent recurrence, the Instrument and Control Foreman will now be issued a copy of Instrument and Control weekly schedule of required testing so the Instrument and Control Foreman can determine which tests are required without instructions from the Test Coordinator.

LER #79-001

4 TOLEDO EDISON COMPA:;Y g DAVIS-EESSE NUCLEAR POWER STATION U';IT ONE PAGE 2 SUPPLE'1 ENTAL INFOR". ATION FOR LER NP-33-79-02 f

Failure Data:

There have been no previous occurrences of late surveillance testing caused by a breakdown in co=unications.

LER #79-001 1

1 T