ML19270F840: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
Line 18: Line 18:
=Text=
=Text=
{{#Wiki_filter:NRC F ORM 366 (7 77)
{{#Wiki_filter:NRC F ORM 366 (7 77)
LICENSEE EVENT REPORT
LICENSEE EVENT REPORT CONTROL BLOCK: l l  l    l  l    l
-
CONTROL BLOCK: l
                                      .
l  l    l  l    l
                                                                         .h l                  (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1l1l1T YPEll@l                  @
                                                                         .h l                  (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1l1l1T YPEll@l                  @
l lo l i8] 9l 0 ] H 7
l lo l i8] 9l 0 ] H 7
Line 32: Line 28:
o  4      I hours.
o  4      I hours.
Since Group 5 was in asymmetric bypass, TS 3.1.3.3, Action a.2.b requires thatl o  s Group 5 position be verified at least once every 12 hours. There was no danger to                                                                  l The control rods of Group 5                        g l o is l l the health and safety of the public or unit personnel.
Since Group 5 was in asymmetric bypass, TS 3.1.3.3, Action a.2.b requires thatl o  s Group 5 position be verified at least once every 12 hours. There was no danger to                                                                  l The control rods of Group 5                        g l o is l l the health and safety of the public or unit personnel.
O    7    l were not in an asymmetric Condition.                                (NP-33-78-50)                                                                    l
O    7    l were not in an asymmetric Condition.                                (NP-33-78-50)                                                                    l o  s i                                                                                                                                                        80 7          8 9                                                                                                            COMP.          VALVE SYSTEU          CAUSE        CAUSE                                                                                                    %
                                                                                                                                                                        !
o  s i                                                                                                                                                        80 7          8 9                                                                                                            COMP.          VALVE SYSTEU          CAUSE        CAUSE                                                                                                    %
CODE            CODE      SUBCODE                  COMPONENT CODE                  SUSCODE        SU8 CODE lojol                          l Rl B j@ W@ l A l@ lI lN lS lT lR lU l@ l Zl@ W @
CODE            CODE      SUBCODE                  COMPONENT CODE                  SUSCODE        SU8 CODE lojol                          l Rl B j@ W@ l A l@ lI lN lS lT lR lU l@ l Zl@ W @
13                            18          13              20 8                  9          to        it            12 7
13                            18          13              20 8                  9          to        it            12 7
OCCURRENCE          REFORT                  REVISION SEQUENTI AL
OCCURRENCE          REFORT                  REVISION SEQUENTI AL REPOHT NO.                            CODE              TYPE                        No.
_
REPOHT NO.                            CODE              TYPE                        No.
EVENT YE AR LER RO
EVENT YE AR LER RO
                 @ gtar 17 8I                        l-l 23 1014l0[
                 @ gtar 17 8I                        l-l 23 1014l0[
Line 54: Line 46:
i 7      1010 0_j@lZ          TYPE  l      @lNA                                                                                                            '
i 7      1010 0_j@lZ          TYPE  l      @lNA                                                                                                            '
     '        ' '    ,ERSONNEl'IN;unS
     '        ' '    ,ERSONNEl'IN;unS
                                                ''
                                                                                                                                        .
                     ~UveEn          DESCniPTiON@                                                                                                                      l NA 7
                     ~UveEn          DESCniPTiON@                                                                                                                      l NA 7
i  R 8 9 1010 Ol@l    11      12 80 Loss OF On DAYAGE To F ACILITY TYPE    DESCniPTION NA                                                                                                                                          l i o
i  R 8 9 1010 Ol@l    11      12 80 Loss OF On DAYAGE To F ACILITY TYPE    DESCniPTION NA                                                                                                                                          l i o 12 @l Pumav                                            7 9 0 3 27 0 6cro                                                          sacosecyty
              "
12 @l
                '
                                                                                                                                                                      *
    '
Pumav                                            7 9 0 3 27 0 6cro                                                          sacosecyty
* I        IIIIIIIIII!l,i 2 o      ISSU
* I        IIIIIIIIII!l,i 2 o      ISSU
[jij    E  D@DE SCRIPTION l NA                                                                                                      68 69                          63 3 7        8 9          to DVR 78-064                                                                  Y                                        PHON E:
[jij    E  D@DE SCRIPTION l NA                                                                                                      68 69                          63 3 7        8 9          to DVR 78-064                                                                  Y                                        PHON E:
419-239-5000. Ext. 276                  {
419-239-5000. Ext. 276                  {
NAME OF PREPARER
NAME OF PREPARER
                                                                                                                                                                              .


TOLEDO EDISON COMPANY                                      I DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION                              i SUPPLEMENTAL INFORMATION FOR LER NP-33-78-50 DATE OF EVENT _: April 22, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
TOLEDO EDISON COMPANY                                      I DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION                              i SUPPLEMENTAL INFORMATION FOR LER NP-33-78-50 DATE OF EVENT _: April 22, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
Failure to read zone reference light for Group 5 Control Rods when in asymmetric bypass                                                        e
Failure to read zone reference light for Group 5 Control Rods when in asymmetric bypass                                                        e The unit was in Mode 1, with Power (MWT) = 1269 Conditions Prior to Occurrence:
                                                                                                !
The unit was in Mode 1, with Power (MWT) = 1269 Conditions Prior to Occurrence:
and Load (MWE) = 385.
and Load (MWE) = 385.
Description of Occurrence:
Description of Occurrence:
Line 83: Line 64:
Corrective Action: As soon as it was discovered that the zone reference light had not been read, an operator was immediately dispatched to read the zone reference light at 2117 hours on April 22, 1978. A program has been developed for use by the 1    process computer to aid operators in monitoring surveillance tests required at fre-quent intervals when the unit is in an Action Statement.
Corrective Action: As soon as it was discovered that the zone reference light had not been read, an operator was immediately dispatched to read the zone reference light at 2117 hours on April 22, 1978. A program has been developed for use by the 1    process computer to aid operators in monitoring surveillance tests required at fre-quent intervals when the unit is in an Action Statement.
Failure Data: This is not a repetitive occurrence.
Failure Data: This is not a repetitive occurrence.
                                                                          .
LER B78-040
LER B78-040
                                                                                           .}}
                                                                                           .}}

Latest revision as of 18:31, 1 February 2020

LER 78-040/03L-1 on 780422:review of Reactor Operator Log Determined That Group 5 Control Rods 100% Zone Ref Light Had Not Been Checked at Required Frequency.Caused by Personnel Error.Process Computer Reminder Program Developed
ML19270F840
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 05/18/1978
From: Marley J
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19270F837 List:
References
LER-78-040-03L, LER-78-40-3L, NUDOCS 7903270600
Download: ML19270F840 (2)


Text

NRC F ORM 366 (7 77)

LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l

.h l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1l1l1T YPEll@l @

l lo l i8] 9l 0 ] H 7

l D l B l S l14 1 l@l LICENSEE CODE 15 0 ] 0 l - l LICENSE 0 l 0 lNuMBEH N l P l F l - l 025] 3 l@l 26 4LICENSE JU $ 7 C A T 58 CON'T 7

o i 8

[7,"c' 60 L l@l61 0 l 5 l 0 l-l0l3l4 DOCKET NUYBEH 6 hl0l4l2'l2l7l8l@l0l5l1l8l7l8l@

bd 69 EVENT OATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l 2 l l While reviewing the Reactor Operator Log on 4/22/78, it was discovered that the Group [

[olal l 5 Control Rods 100% Zone Reference Light had been last checked on 4/21/78 at 2220 [

o 4 I hours.

Since Group 5 was in asymmetric bypass, TS 3.1.3.3, Action a.2.b requires thatl o s Group 5 position be verified at least once every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. There was no danger to l The control rods of Group 5 g l o is l l the health and safety of the public or unit personnel.

O 7 l were not in an asymmetric Condition. (NP-33-78-50) l o s i 80 7 8 9 COMP. VALVE SYSTEU CAUSE CAUSE  %

CODE CODE SUBCODE COMPONENT CODE SUSCODE SU8 CODE lojol l Rl B j@ W@ l A l@ lI lN lS lT lR lU l@ l Zl@ W @

13 18 13 20 8 9 to it 12 7

OCCURRENCE REFORT REVISION SEQUENTI AL REPOHT NO. CODE TYPE No.

EVENT YE AR LER RO

@ gtar 17 8I l-l 23 1014l0[

24 26 l/l 27 l 0l 3 28 29 lLl 30 l-l 31 W32

_ 21 22 HOURS 22 S B IT FOH 9 UB. SU PPLI E MAN FA TL RFR Er7 A ON PL A T TH A T lZlh 1 0 l0 l0 9I40 Y

@ INlg (Zlg Z lZ lZ lZ g b @lZ @ lZ @

33 34 35 J6 3/ di 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o lThe apparent cause of this occurrence was personnel error. The operator inadvertently [

i i l failed to perform the required observation of the zone reference light. An operator [

at 2117 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.055185e-4 months <br /> on April 22, 1978. A l

,,,7glwas dispatched to read the zone reference light

,,;3; l program has been developed for use by the process computer to aid operators in moni- l

,,g,j ltoring surveillance tests required at frequent intervals when the unit is in Statement.83 an Action l 7 8 9 oTHE R STATUS ISCOV R DISCOVERY DESCRIPTION A S *. PoWE R 4 l A [Ql Operator Log Review l li 15l W @ l 0l 6l@l NA l ACTIVITY CONTENT AMOUNT OF ACTIVITY LOCATION OF RELE ASE RELEASED OF RELE ASE NA l l

7 1 6 8 9 W @ lZ10 l@l NA 11 44 45 80 PERSONNEL E XPOSURES NUVHE R CESCRIPTION I

i 7 1010 0_j@lZ TYPE l @lNA '

' ' ' ,ERSONNEl'IN;unS

~UveEn DESCniPTiON@ l NA 7

i R 8 9 1010 Ol@l 11 12 80 Loss OF On DAYAGE To F ACILITY TYPE DESCniPTION NA l i o 12 @l Pumav 7 9 0 3 27 0 6cro sacosecyty

  • I IIIIIIIIII!l,i 2 o ISSU

[jij E D@DE SCRIPTION l NA 68 69 63 3 7 8 9 to DVR 78-064 Y PHON E:

419-239-5000. Ext. 276 {

NAME OF PREPARER

TOLEDO EDISON COMPANY I DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION i SUPPLEMENTAL INFORMATION FOR LER NP-33-78-50 DATE OF EVENT _: April 22, 1978 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:

Failure to read zone reference light for Group 5 Control Rods when in asymmetric bypass e The unit was in Mode 1, with Power (MWT) = 1269 Conditions Prior to Occurrence:

and Load (MWE) = 385.

Description of Occurrence:

While reviewing the Reactor Operator Log on April 22, s 1978, it was discovered that the Group 5 Control Rods 100% Zone Reference Light had been last checked on April 21, 1978 at 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br />. Since Group 5 was in asym-metric bypass, Technical Specification 3.1.3.3, Action a.2.b requires least that Group once 5

be maintained at 0%, 25%, 50%, 75% or 100% withdrawn and verified at every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The position of Group 5 had not been verified by the 100% Zone Reference Light for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Designation of Apparent Cause of Occurrence: The apparent cause of the occurrence was personnel error. The operator inadvertently failed to perform the required observation of the zone reference light.

Analysis of Occurrence: There was no danger to the health and safety of the public or unit personnel. The control rods of Group 5 were not in an asymmetric condition.

Only the Absolute Position Indication for one control rod was defective requiring operation in asymmetric bypass.

Corrective Action: As soon as it was discovered that the zone reference light had not been read, an operator was immediately dispatched to read the zone reference light at 2117 hours0.0245 days <br />0.588 hours <br />0.0035 weeks <br />8.055185e-4 months <br /> on April 22, 1978. A program has been developed for use by the 1 process computer to aid operators in monitoring surveillance tests required at fre-quent intervals when the unit is in an Action Statement.

Failure Data: This is not a repetitive occurrence.

LER B78-040

.