ML19249B392: Difference between revisions
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NRC FORM 66 U. S. NUCLEAI4 REGULATORY COMMISSION (7-77) | NRC FORM 66 U. S. NUCLEAI4 REGULATORY COMMISSION (7-77) | ||
LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) | LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) | ||
CONTROL BLOCK: l 1 | CONTROL BLOCK: l 1 | ||
l l l l l lh | l l l l l lh O | ||
o i 8 9 l ol Hl Dl 3 l S 1l@l0l0l.-l0l0lNlPjFl- 0l3l@l4 1l1l1 14 15 LICENSE NLMisEH 25 26 LaCENSE TYPE JJ 1l@l l 57 CAT 5d l@ | |||
7 LICENSEE CCOE CON'T | 7 LICENSEE CCOE CON'T | ||
? | ? | ||
0 1 8 | 0 1 8 | ||
5[RCE60 lL @l61 0l 5 l 0DOCKET l- l0 l3 l4 l6 l@l 063 l 7 lEVENT NUMBER t>8 3 l OATE 1 ] 7 l 9 74}@]750l SlREPCRT 21 D71ATE 7 l 9SJl@ | 5[RCE60 lL @l61 0l 5 l 0DOCKET l- l0 l3 l4 l6 l@l 063 l 7 lEVENT NUMBER t>8 3 l OATE 1 ] 7 l 9 74}@]750l SlREPCRT 21 D71ATE 7 l 9SJl@ | ||
EVENT DESCRIPTION AND PROB ABLE CCNSEQUENCES h o 2 l While performing a main turbine steam valve test, operators twice received a control l o 3 l rod drive sequence fault caused by Group 6 rods moving of f their out limit to 95%. [ | EVENT DESCRIPTION AND PROB ABLE CCNSEQUENCES h o 2 l While performing a main turbine steam valve test, operators twice received a control l o 3 l rod drive sequence fault caused by Group 6 rods moving of f their out limit to 95%. [ | ||
o 4 [ This placed the unit in Action Statement (a) of T.S. 3.1.3.6. There was no danger to j o 3 l the health and safety of the public or station personnel. Rod cotion was minimal and ; | o 4 [ This placed the unit in Action Statement (a) of T.S. 3.1.3.6. There was no danger to j o 3 l the health and safety of the public or station personnel. Rod cotion was minimal and ; | ||
o s l caused no noticeable reactivity or core power distribution changes. (NP-33-79-101) ; | o s l caused no noticeable reactivity or core power distribution changes. (NP-33-79-101) ; | ||
o 7 I l | o 7 I l | ||
o 8 l 80 7 8 9 SYSTEM CAUSE CAUSE COYP. VALVE CODE CCDE SUSCOCE COMPCNENT CODE SUBCODE SUSCOOE | o 8 l 80 7 8 9 SYSTEM CAUSE CAUSE COYP. VALVE CODE CCDE SUSCOCE COMPCNENT CODE SUBCODE SUSCOOE 7 | ||
0 9 8 | |||
l Rl B l@ lE ]@ lC l@ l Il Nl Sl Tl Rl Ulh l P l@ l Z l@ | l Rl B l@ lE ]@ lC l@ l Il Nl Sl Tl Rl Ulh l P l@ l Z l@ | ||
9 10 11 12 13 1d 19 20 SEQUENTI AL OCCUAAENCE REPCAT REVISION | 9 10 11 12 13 1d 19 20 SEQUENTI AL OCCUAAENCE REPCAT REVISION | ||
Line 45: | Line 39: | ||
_ 21 22 23 24 26 27 28 29 SJ 31 32 ACTIO N FUTURE ECFECT SH U T OOV.N ATT ACHV ENT NPA04 ?R:YE COYP. COYPONENT TAKEN ACTION O'4 F L A NT *1ETHC3 | _ 21 22 23 24 26 27 28 29 SJ 31 32 ACTIO N FUTURE ECFECT SH U T OOV.N ATT ACHV ENT NPA04 ?R:YE COYP. COYPONENT TAKEN ACTION O'4 F L A NT *1ETHC3 | ||
. dCUBS 22 SLBYlTTED FCPM n8. SUPPLtER YANUFACTURER l03A lglJ4Zl@ lZl@ l36Z l@ l 0 l0 l0 l' l lYlg 41 | . dCUBS 22 SLBYlTTED FCPM n8. SUPPLtER YANUFACTURER l03A lglJ4Zl@ lZl@ l36Z l@ l 0 l0 l0 l' l lYlg 41 | ||
[y 44 Nlg lD l1 l5 l0 lg 44 47 25 3/ 40 42 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS | [y 44 Nlg lD l1 l5 l0 lg 44 47 25 3/ 40 42 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o lrhe cause of this occurrence was a faulty integrated circuit on a logic gate module in) li j i l 1 the auxiliary power supply of the command logic string. Instrument and Control per- ; | ||
i o lrhe cause of this occurrence was a faulty integrated circuit on a logic gate module in) li j i l 1 the auxiliary power supply of the command logic string. Instrument and Control per- ; | |||
i 2 isoanel replaced the integrated circuit and verified proper operation. , | i 2 isoanel replaced the integrated circuit and verified proper operation. , | ||
t 1 l | t 1 l 1 4 l 7 8 9 80 F ACitiTV VETwCOOF STATUS % POW E R CTHER STATUS CISCOV E AY DISCOVERY DESCRIPTION Al@lOperatorobservation t s , l El@ l 0 l 9 l 7 @l NA l l ACTIVliv CONTENT RELEMEO CF RELE ASE AVOUNT CF ACTivlTY LOCATION OF RELEASE c NA l 7 | ||
i 8 3 L11 @ l_zJ @l NA 10 11 44 I I 45 80 PE ASCNNEL EXPOSURES NUv9 E R TYPE OESCRIPTICN lZ 1 l7 l 0l 0l 0 l NA '' 60 l | |||
1 4 l 7 8 9 80 F ACitiTV VETwCOOF STATUS % POW E R CTHER STATUS CISCOV E AY DISCOVERY DESCRIPTION Al@lOperatorobservation | |||
t s , l El@ l 0 l 9 l 7 @l NA l l ACTIVliv CONTENT | |||
RELEMEO CF RELE ASE AVOUNT CF ACTivlTY LOCATION OF RELEASE c NA l 7 | |||
i 8 3 L11 @ l_zJ @l NA 10 11 44 I I 45 80 PE ASCNNEL EXPOSURES NUv9 E R TYPE OESCRIPTICN lZ | |||
1 l7 l 0l 0l 0 l NA '' 60 l | |||
PERSONNEL iN;UR ES *#'# *#*'''- | PERSONNEL iN;UR ES *#'# *#*'''- | ||
NUY8ER DESCaiPTION 1 4 0 )l ) l NA 00 7 3 9 11 12 S LCSS CF CR DAYAGE To FACILtTY TwE CESCn,PTiaN D09040 ' | |||
NUY8ER DESCaiPTION 1 4 0 )l ) l NA 00 7 3 9 11 12 S LCSS CF CR DAYAGE To FACILtTY | |||
TwE CESCn,PTiaN | |||
D09040 ' | |||
7 t 9 4 3 lZ@l 1 ;.) | 7 t 9 4 3 lZ@l 1 ;.) | ||
NA l PU B L ICI TY NRC USE ONLY ISSUED CESCAiPT!ON l ll lllll !l l l l l 0 68 69 60 DVR 79-1:'2 Dean C. Hitchens ,ggyg 419-259-5000, Ext. 231! | NA l PU B L ICI TY NRC USE ONLY ISSUED CESCAiPT!ON l ll lllll !l l l l l 0 68 69 60 DVR 79-1:'2 Dean C. Hitchens ,ggyg 419-259-5000, Ext. 231! | ||
y4yeoppagpaggg 2 | y4yeoppagpaggg 2 | ||
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-101 DATE OF EVENT: July 31, 1979 FAC1Lii Y: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Loss of Group 6 out limit Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2680 and Load (Gross MWE) = 880 Description of Occurrence: On July 31,1979 at 0110 hours and at 0140 hours while performing PT 5193.01, " Main Turbine Steam Valve Tests", operations personnel re-ceived a Control Rod Drive Sequence Fault. In both instances, they noticed that Group 6 had moved off of its out limit to approximately 95%. This placed the unic in the Action Statement (a) of Technical Specification 3.1.3.6. This Tec.hnical Speci-fication requires Group 6 to be within the insertion limits during Modes 1 and 2. | |||
TOLEDO EDISON COMPANY | |||
DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-101 DATE OF EVENT: July 31, 1979 FAC1Lii Y: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Loss of Group 6 out limit Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2680 and Load (Gross MWE) = 880 Description of Occurrence: On July 31,1979 at 0110 hours and at 0140 hours while performing PT 5193.01, " Main Turbine Steam Valve Tests", operations personnel re-ceived a Control Rod Drive Sequence Fault. In both instances, they noticed that Group 6 had moved off of its out limit to approximately 95%. This placed the unic in the Action Statement (a) of Technical Specification 3.1.3.6. This Tec.hnical Speci-fication requires Group 6 to be within the insertion limits during Modes 1 and 2. | |||
Action Statement (a) instructs the unit to restore the rod (s) to within the insertion limit within two hours. | Action Statement (a) instructs the unit to restore the rod (s) to within the insertion limit within two hours. | ||
In each case, operators t=nediately pulled Group 6 back to its out limit which re-moved the unit from the Action Statement (a) of Technical Specification 3.1.3.6. | In each case, operators t=nediately pulled Group 6 back to its out limit which re-moved the unit from the Action Statement (a) of Technical Specification 3.1.3.6. |
Latest revision as of 01:08, 2 February 2020
ML19249B392 | |
Person / Time | |
---|---|
Site: | Davis Besse |
Issue date: | 08/27/1979 |
From: | Hitchens D TOLEDO EDISON CO. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
Shared Package | |
ML19249B386 | List: |
References | |
LER-79-087-03L, LER-79-87-3L, NUDOCS 7909040364 | |
Download: ML19249B392 (2) | |
Text
,
NRC FORM 66 U. S. NUCLEAI4 REGULATORY COMMISSION (7-77)
LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
CONTROL BLOCK: l 1
l l l l l lh O
o i 8 9 l ol Hl Dl 3 l S 1l@l0l0l.-l0l0lNlPjFl- 0l3l@l4 1l1l1 14 15 LICENSE NLMisEH 25 26 LaCENSE TYPE JJ 1l@l l 57 CAT 5d l@
7 LICENSEE CCOE CON'T
?
0 1 8
5[RCE60 lL @l61 0l 5 l 0DOCKET l- l0 l3 l4 l6 l@l 063 l 7 lEVENT NUMBER t>8 3 l OATE 1 ] 7 l 9 74}@]750l SlREPCRT 21 D71ATE 7 l 9SJl@
EVENT DESCRIPTION AND PROB ABLE CCNSEQUENCES h o 2 l While performing a main turbine steam valve test, operators twice received a control l o 3 l rod drive sequence fault caused by Group 6 rods moving of f their out limit to 95%. [
o 4 [ This placed the unit in Action Statement (a) of T.S. 3.1.3.6. There was no danger to j o 3 l the health and safety of the public or station personnel. Rod cotion was minimal and ;
o s l caused no noticeable reactivity or core power distribution changes. (NP-33-79-101) ;
o 7 I l
o 8 l 80 7 8 9 SYSTEM CAUSE CAUSE COYP. VALVE CODE CCDE SUSCOCE COMPCNENT CODE SUBCODE SUSCOOE 7
0 9 8
l Rl B l@ lE ]@ lC l@ l Il Nl Sl Tl Rl Ulh l P l@ l Z l@
9 10 11 12 13 1d 19 20 SEQUENTI AL OCCUAAENCE REPCAT REVISION
,, EVENT YEAR R EPORT NO. CODE TY P E No.
@ ~ LEA-RO l 71 91 l-l 1018171 1/1 1 O l 31 Li 1-1 10 l
_ 21 22 23 24 26 27 28 29 SJ 31 32 ACTIO N FUTURE ECFECT SH U T OOV.N ATT ACHV ENT NPA04 ?R:YE COYP. COYPONENT TAKEN ACTION O'4 F L A NT *1ETHC3
. dCUBS 22 SLBYlTTED FCPM n8. SUPPLtER YANUFACTURER l03A lglJ4Zl@ lZl@ l36Z l@ l 0 l0 l0 l' l lYlg 41
[y 44 Nlg lD l1 l5 l0 lg 44 47 25 3/ 40 42 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o lrhe cause of this occurrence was a faulty integrated circuit on a logic gate module in) li j i l 1 the auxiliary power supply of the command logic string. Instrument and Control per- ;
i 2 isoanel replaced the integrated circuit and verified proper operation. ,
t 1 l 1 4 l 7 8 9 80 F ACitiTV VETwCOOF STATUS % POW E R CTHER STATUS CISCOV E AY DISCOVERY DESCRIPTION Al@lOperatorobservation t s , l El@ l 0 l 9 l 7 @l NA l l ACTIVliv CONTENT RELEMEO CF RELE ASE AVOUNT CF ACTivlTY LOCATION OF RELEASE c NA l 7
i 8 3 L11 @ l_zJ @l NA 10 11 44 I I 45 80 PE ASCNNEL EXPOSURES NUv9 E R TYPE OESCRIPTICN lZ 1 l7 l 0l 0l 0 l NA 60 l
PERSONNEL iN;UR ES *#'# *#*-
NUY8ER DESCaiPTION 1 4 0 )l ) l NA 00 7 3 9 11 12 S LCSS CF CR DAYAGE To FACILtTY TwE CESCn,PTiaN D09040 '
7 t 9 4 3 lZ@l 1 ;.)
NA l PU B L ICI TY NRC USE ONLY ISSUED CESCAiPT!ON l ll lllll !l l l l l 0 68 69 60 DVR 79-1:'2 Dean C. Hitchens ,ggyg 419-259-5000, Ext. 231!
y4yeoppagpaggg 2
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-101 DATE OF EVENT: July 31, 1979 FAC1Lii Y: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Loss of Group 6 out limit Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2680 and Load (Gross MWE) = 880 Description of Occurrence: On July 31,1979 at 0110 hours0.00127 days <br />0.0306 hours <br />1.818783e-4 weeks <br />4.1855e-5 months <br /> and at 0140 hours0.00162 days <br />0.0389 hours <br />2.314815e-4 weeks <br />5.327e-5 months <br /> while performing PT 5193.01, " Main Turbine Steam Valve Tests", operations personnel re-ceived a Control Rod Drive Sequence Fault. In both instances, they noticed that Group 6 had moved off of its out limit to approximately 95%. This placed the unic in the Action Statement (a) of Technical Specification 3.1.3.6. This Tec.hnical Speci-fication requires Group 6 to be within the insertion limits during Modes 1 and 2.
Action Statement (a) instructs the unit to restore the rod (s) to within the insertion limit within two hours.
In each case, operators t=nediately pulled Group 6 back to its out limit which re-moved the unit from the Action Statement (a) of Technical Specification 3.1.3.6.
PT 5193.01 was suspended until the problem could be resolved.
Designation of Annarent Cause of Occurrence: The cause of this occurrence is attri-buted to a faulty integrated circuit (IC 2) on a logic cate module in the auxiliary power supply of the command locic string.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The Group 6 rod motion was minimal and no noticeabla reacti-vity or core power distribution ef fects occurred.
Corrective Action: Instrument an:1 Control personnel were called in and the IC was replaced and proper operation verified under work request IC-055-014-79. FT 5193.01 was successfully completed on July 31, 1979. The unit had been removed from the Action Statement of Technical Specification 3.1.3.6 i==ediately af ter the occurrence when operations personnel pulled Group 6 back to its out limit.
Failure Data: fhere have been no previously reported similar events.
1 LER #79-087
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