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| issue date = 12/27/2011
| issue date = 12/27/2011
| title = Final Significance Determination of White Finding and Notice of Violation - NRC Inspection Report 2011014 and Assessment Follow-up Letter - Brunswick Steam Electric Plant
| title = Final Significance Determination of White Finding and Notice of Violation - NRC Inspection Report 2011014 and Assessment Follow-up Letter - Brunswick Steam Electric Plant
| author name = McCree V M
| author name = Mccree V
| author affiliation = NRC/RGN-II/ORA
| author affiliation = NRC/RGN-II/ORA
| addressee name = Annacone M
| addressee name = Annacone M
Line 19: Line 19:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 December 27, 2011 EA-11-251 Mr. Michael Annacone Vice President Carolina Power and Light Company Brunswick Steam Electric Plant P. O. Box 10429 Southport, NC 28461  
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 December 27, 2011 EA-11-251 Mr. Michael Annacone Vice President Carolina Power and Light Company Brunswick Steam Electric Plant P. O. Box 10429 Southport, NC 28461


==SUBJECT:==
==SUBJECT:==
FINAL SIGNIFICANCE DETERMINATION OF WHITE FINDING AND NOTICE OF VIOLATION - NRC INSPECTION REPORT NOS.: 05000325/2011014 AND 05000324/2011014; AND ASSESSMENT FOLLOW-UP LETTER - BRUNSWICK STEAM ELECTRIC PLANT  
FINAL SIGNIFICANCE DETERMINATION OF WHITE FINDING AND NOTICE OF VIOLATION - NRC INSPECTION REPORT NOS.: 05000325/2011014 AND 05000324/2011014; AND ASSESSMENT FOLLOW-UP LETTER - BRUNSWICK STEAM ELECTRIC PLANT


==Dear Mr. Annacone:==
==Dear Mr. Annacone:==


This letter provides the final significance determination of the preliminary White finding discussed in Brunswick Steam Electric Plant - NRC Inspection Report Nos.: 05000325/2011012 and 05000324/2011012; Preliminary White Finding, dated November 29, 2011. The finding involved an NRC inspector identified violation of 10 CFR Part 50 Appendix B Criterion XVI, Corrective Action, for the failure to identify and correct a condition adverse to quality associated with the entrance enclosures for the Emergency Diesel Generator (EDG) fuel oil tank rooms. Specifically, the enclosures contained openings which would adversely impact their ability to mitigate external flooding of the EDG fuel oil tank rooms in the event of an external event (hurricane). In response to this condition, new sealant material was installed to close the openings of the entrance enclosures for the EDG fuel oil tank rooms, and jersey barriers were installed to limit wave run-up on the enclosures.
This letter provides the final significance determination of the preliminary White finding discussed in Brunswick Steam Electric Plant - NRC Inspection Report Nos.:
05000325/2011012 and 05000324/2011012; Preliminary White Finding, dated November 29, 2011. The finding involved an NRC inspector identified violation of 10 CFR Part 50 Appendix B Criterion XVI, Corrective Action, for the failure to identify and correct a condition adverse to quality associated with the entrance enclosures for the Emergency Diesel Generator (EDG) fuel oil tank rooms. Specifically, the enclosures contained openings which would adversely impact their ability to mitigate external flooding of the EDG fuel oil tank rooms in the event of an external event (hurricane). In response to this condition, new sealant material was installed to close the openings of the entrance enclosures for the EDG fuel oil tank rooms, and jersey barriers were installed to limit wave run-up on the enclosures.
During a telephone conversation with Mr. Randall Musser of NRC, Region II, on December 6, 2011, Licensing Supervisor, Ms. Annette Pope of your staff indicated that Carolina Power and Light Company, Brunswick Steam Electric Plant, did not contest the characterization of the risk significance of this finding and that you declined the opportunity to discuss this issue during a Regulatory Conference or to provide a written response.
During a telephone conversation with Mr. Randall Musser of NRC, Region II, on December 6, 2011, Licensing Supervisor, Ms. Annette Pope of your staff indicated that Carolina Power and Light Company, Brunswick Steam Electric Plant, did not contest the characterization of the risk significance of this finding and that you declined the opportunity to discuss this issue during a Regulatory Conference or to provide a written response.
After considering the information developed during the inspection, the NRC has concluded that the finding is appropriately characterized as White, a finding with low to moderate safety significance that may require additional NRC inspections.
After considering the information developed during the inspection, the NRC has concluded that the finding is appropriately characterized as White, a finding with low to moderate safety significance that may require additional NRC inspections.
Note: According to NRC Inspection Manual Chapter (IMC) 0609, appeal rights only apply to those licensees that have either attended a regulatory conference or submitted a written response to the preliminary determination letter.
Note: According to NRC Inspection Manual Chapter (IMC) 0609, appeal rights only apply to those licensees that have either attended a regulatory conference or submitted a written response to the preliminary determination letter.
CPL 2  The NRC has also determined that the failure to identify and correct a condition adverse to quality associated with the entrance enclosures for the Emergency Diesel Generator (EDG) fuel oil tank rooms is a violation of 10 CFR Part 50 Appendix B Criterion XVI, Corrective Action, as cited in the attached Notice of Violation (Notice). The circumstances surrounding the violation were described in detail in NRC Inspection Report Nos. 05000325/2011012 and 05000324/2011012. In accordance with the NRC Enforcement Policy, the Notice is considered escalated enforcement action because it is associated with a White finding.
You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. If you have additional information that you believe the NRC should consider, you may provide it in your response to the Notice. The NRC's review of your response to the Notice will also determine whether further enforcement action is necessary to ensure compliance with regulatory requirements.
Because plant performance for this issue has been determined to be beyond the licensee response band, the NRC's Action Matrix was used to determine the most appropriate NRC response for this issue. As a result of its continuous review of plant performance, which was completed on December 16, 2011, the NRC updated its assessment of Brunswick Steam Electric Plant, Units 1 and 2. The NRC's evaluation consisted of a review of performance indicators and inspection results.
The NRC determined the performance at Brunswick Steam Electric Plant, Units 1 and 2 to be in the Regulatory Response Column of the Reactor Oversight Process Action Matrix beginning the fourth quarter of 2011. Therefore, in addition to baseline inspections, the NRC plans to conduct a supplemental inspection in accordance with Inspection Procedure 95001, "Inspection for One or Two White Inputs in a Strategic Performance Area," for the review of the White inspection finding. Have your staff notify the NRC of your readiness for us to conduct this supplemental inspection to review the actions taken to address the White inspection finding in the Mitigating Systems Cornerstone.
For administrative purposes, this letter is issued as NRC Inspection Report No. 05000325, 324/2011014. Accordingly, AV 05000325, 324/2011012-01, Failure to Identify and Correct Degradation of the Emergency Diesel Generator Fuel Oil Tank Room Entrance Enclosures is updated as VIO 05000325, 324/2011012-01, Failure to Identify and Correct Degradation of the Emergency Diesel Generator Fuel Oil Tank Room Entrance Enclosures. This violation is associated with a finding with a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee did not identify the issue completely, accurately, and in a timely manner commensurate with its safety significance (P.1(a)).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your CPL 3  response should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the Public without redaction.
Sincerely, 


      /RA by Leonard Wert Acting For/
CPL                                            2 The NRC has also determined that the failure to identify and correct a condition adverse to quality associated with the entrance enclosures for the Emergency Diesel Generator (EDG) fuel oil tank rooms is a violation of 10 CFR Part 50 Appendix B Criterion XVI, Corrective Action, as cited in the attached Notice of Violation (Notice). The circumstances surrounding the violation were described in detail in NRC Inspection Report Nos. 05000325/2011012 and 05000324/2011012. In accordance with the NRC Enforcement Policy, the Notice is considered escalated enforcement action because it is associated with a White finding.
Victor M. McCree Regional Administrator Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62                
You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. If you have additional information that you believe the NRC should consider, you may provide it in your response to the Notice. The NRCs review of your response to the Notice will also determine whether further enforcement action is necessary to ensure compliance with regulatory requirements.
Because plant performance for this issue has been determined to be beyond the licensee response band, the NRCs Action Matrix was used to determine the most appropriate NRC response for this issue. As a result of its continuous review of plant performance, which was completed on December 16, 2011, the NRC updated its assessment of Brunswick Steam Electric Plant, Units 1 and 2. The NRCs evaluation consisted of a review of performance indicators and inspection results.
The NRC determined the performance at Brunswick Steam Electric Plant, Units 1 and 2 to be in the Regulatory Response Column of the Reactor Oversight Process Action Matrix beginning the fourth quarter of 2011. Therefore, in addition to baseline inspections, the NRC plans to conduct a supplemental inspection in accordance with Inspection Procedure 95001, Inspection for One or Two White Inputs in a Strategic Performance Area, for the review of the White inspection finding. Have your staff notify the NRC of your readiness for us to conduct this supplemental inspection to review the actions taken to address the White inspection finding in the Mitigating Systems Cornerstone.
For administrative purposes, this letter is issued as NRC Inspection Report No.
05000325, 324/2011014. Accordingly, AV 05000325, 324/2011012-01, Failure to Identify and Correct Degradation of the Emergency Diesel Generator Fuel Oil Tank Room Entrance Enclosures is updated as VIO 05000325, 324/2011012-01, Failure to Identify and Correct Degradation of the Emergency Diesel Generator Fuel Oil Tank Room Entrance Enclosures.
This violation is associated with a finding with a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee did not identify the issue completely, accurately, and in a timely manner commensurate with its safety significance (P.1(a)).
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your
 
CPL                                        3 response should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the Public without redaction.
Sincerely,
                                            /RA by Leonard Wert Acting For/
Victor M. McCree Regional Administrator Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62


==Enclosure:==
==Enclosure:==
Notice of Violation  
Notice of Violation


__ML113610594___________  X SUNSI REVIEW COMPLETE X FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRP RII:EICS RII:RA HQ: OE HQ:NRR SIGNATURE JSD RAM B. Jones for CFE /RA/ Via email Via email NAME JDodson RMusser RCroteau CEvans LWert  DATE 12/14/2011 12/20/2011 12/20/2011 12/15/2011 12/    /2011 12/19/2011 12/20/2011 E-MAIL COPY?    YES NO      YES NO      YES NO      YES NO      YES NO      YES NO      YES NO CPL 4  cc w/encl: Edward L. Wills, Jr. Director Site Operations Brunswick Steam Electric Plant Electronic Mail Distribution
CPL                                                3 response should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the Public without redaction.
Sincerely,
                                                                /RA by Leonard Wert Acting For/
Victor M. McCree Regional Administrator Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62


Joseph M. Frisco, Jr Plant General Manager Brunswick Steam Electric Plant Progress Energy Electronic Mail Distribution Phyllis N. Mentel Manager, Support Services Brunswick Steam Electric Plant Progress Energy Carolinas, Inc. Electronic Mail Distribution
==Enclosure:==
Notice of Violation XPUBLICLY AVAILABLE              G NON-PUBLICLY AVAILABLE                    G SENSITIVE      X NON-SENSITIVE ADAMS: X Yes    ACCESSION NUMBER:__ML113610594___________                    X SUNSI REVIEW COMPLETE X FORM 665 ATTACHED OFFICE            RII:DRP        RII:DRP        RII:DRP          RII:EICS        RII:RA          HQ: OE          HQ:NRR SIGNATURE          JSD            RAM            B. Jones for    CFE              /RA/            Via email      Via email NAME              JDodson        RMusser        RCroteau        CEvans          LWert DATE                  12/14/2011    12/20/2011      12/20/2011      12/15/2011      12/ /2011    12/19/2011        12/20/2011 E-MAIL COPY?          YES    NO    YES    NO    YES      NO    YES      NO      YES    NO      YES      NO      YES    NO OFFICIAL    RECORD      COPY        DOCUMENT      NAME:          G:\DRPII\RPB4\BRUNSWICK\BRU        FINAL    SI G:\DRPII\RPB4\BRUNSWICK\Reports\2011 Reports\BRU FINAL SIGNIFICANCE LETTER 2011014.DOCX


Annette H. Pope Supervisor, Licensing/Regulatory Programs Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
CPL                                      4 cc w/encl:                                  Senior Resident Inspector Edward L. Wills, Jr.                        U.S. Nuclear Regulatory Commission Director Site Operations                    Brunswick Steam Electric Plant Brunswick Steam Electric Plant              U.S. NRC Electronic Mail Distribution                8470 River Road, SE Southport, NC 28461 Joseph M. Frisco, Jr Plant General Manager                      John H. O'Neill, Jr.
Electronic Mail Distribution Randy C. Ivey Manager, Nuclear Oversight Brunswick Steam Electric Plant Progress Energy Carolinas, Inc. Electronic Mail Distribution Paul E. Dubrouillet, Manager, Training Brunswick Steam Electric Plant Electronic Mail Distribution Kelvin Henderson, General Manager Nuclear Fleet Operations Progress Energy Electronic Mail Distribution Joseph W. Donahue, Vice President Nuclear Oversight Progress Energy Electronic Mail Distribution  
Brunswick Steam Electric Plant              Shaw, Pittman, Potts & Trowbridge Progress Energy                            2300 N. Street, NW Electronic Mail Distribution                Washington, DC 20037-1128 Phyllis N. Mentel                          Peggy Force, Assistant Attorney General Manager, Support Services                  State of North Carolina Brunswick Steam Electric Plant              P.O. Box 629 Progress Energy Carolinas, Inc.            Raleigh, NC 27602 Electronic Mail Distribution Chairman Annette H. Pope                             North Carolina Utilities Commission Supervisor, Licensing/Regulatory Programs   Electronic Mail Distribution Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.             Robert P. Gruber, Executive Director Electronic Mail Distribution               Public Staff - NCUC 4326 Mail Service Center Randy C. Ivey                               Raleigh, NC 27699-4326 Manager, Nuclear Oversight Brunswick Steam Electric Plant             Brunswick County Board of Commissioners Progress Energy Carolinas, Inc.             P.O. Box 249 Electronic Mail Distribution               Bolivia, NC 28422 Paul E. Dubrouillet, Manager, Training     Public Service Commission Brunswick Steam Electric Plant             State of South Carolina Electronic Mail Distribution               P.O. Box 11649 Columbia, SC 29211 Kelvin Henderson, General Manager Nuclear Fleet Operations                   W. Lee Cox, III, Section Chief Progress Energy                             Radiation Protection Section Electronic Mail Distribution               N.C. Department of Environmental Commerce & Natural Resources Joseph W. Donahue, Vice President           Electronic Mail Distribution Nuclear Oversight Progress Energy                             Warren Lee Electronic Mail Distribution                Emergency Management Director New Hanover County Department of David T. Conley, Senior Counsel            Emergency Management Legal Department                            230 Government Center Drive, Suite 115 Progress Energy                            Wilmington, NC 28403 Electronic Mail Distribution


David T. Conley, Senior Counsel Legal Department Progress Energy Electronic Mail Distribution Senior Resident Inspector U.S. Nuclear Regulatory Commission Brunswick Steam Electric Plant U.S. NRC 8470 River Road, SE Southport, NC  28461 John H. O'Neill, Jr. Shaw, Pittman, Potts & Trowbridge 2300 N. Street, NW Washington, DC  20037-1128 Peggy Force, Assistant Attorney General State of North Carolina P.O. Box 629 Raleigh, NC  27602
CPL                                       5 Letter to Michael J. Annacone from Victor M. McCree dated December 27, 2011
 
Chairman North Carolina Utilities Commission Electronic Mail Distribution Robert P. Gruber, Executive Director Public Staff - NCUC 4326 Mail Service Center Raleigh, NC  27699-4326 Brunswick County Board of Commissioners P.O. Box 249 Bolivia, NC  28422 Public Service Commission State of South Carolina P.O. Box 11649 Columbia, SC  29211 W. Lee Cox, III, Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources Electronic Mail Distribution Warren Lee Emergency Management Director New Hanover County Department of Emergency Management 230 Government Center Drive, Suite 115 Wilmington, NC  28403 CPL 5 Letter to Michael J. Annacone from Victor M. McCree dated December 27, 2011  


==SUBJECT:==
==SUBJECT:==
FINAL SIGNIFICANCE DETERMINATION OF WHITE FINDING AND NOTICE OF VIOLATION - NRC INSPECTION REPORT NOS.: 05000325/2011014 AND 05000324/2011014; AND ASSESSMENT FOLLOW-UP LETTER - BRUNSWICK STEAM ELECTRIC PLANT Distribution w/encl:
FINAL SIGNIFICANCE DETERMINATION OF WHITE FINDING AND NOTICE OF VIOLATION - NRC INSPECTION REPORT NOS.: 05000325/2011014 AND 05000324/2011014; AND ASSESSMENT FOLLOW-UP LETTER - BRUNSWICK STEAM ELECTRIC PLANT Distribution w/encl:
C. Evans, RII EICS L. Douglas, RII EICS OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMBrunswick Resource ROPassessment Resource  
C. Evans, RII EICS L. Douglas, RII EICS OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMBrunswick Resource ROPassessment Resource


Enclosure NOTICE OF VIOLATION Carolina Power and Light Company   Docket Nos. 50-325, 50-324 Brunswick Steam Electric Plant   License Nos. DPR-71, DPR-62 EA-11-251 During an NRC inspection conducted on April 20, 2011 a violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy, the violation is listed below:
NOTICE OF VIOLATION Carolina Power and Light Company                                 Docket Nos. 50-325, 50-324 Brunswick Steam Electric Plant                                   License Nos. DPR-71, DPR-62 EA-11-251 During an NRC inspection conducted on April 20, 2011 a violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy, the violation is listed below:
10 CFR Part 50 Appendix B Criterion XVI, Corrective Action states, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected.
10 CFR Part 50 Appendix B Criterion XVI, Corrective Action states, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected.
Contrary to the above, as of April 20, 2011, the licensee failed to identify and promptly correct a condition adverse to quality involving the external flood barrier for the EDG fuel oil tank rooms. Specifically, the entrance enclosures which house the EDG fuel oil tanks had several openings, unsealed pin holes, and a narrow gap along the perimeter of the base walls, which would allow water intrusion into the EDG fuel oil tank rooms during a design basis external event (hurricane).
Contrary to the above, as of April 20, 2011, the licensee failed to identify and promptly correct a condition adverse to quality involving the external flood barrier for the EDG fuel oil tank rooms. Specifically, the entrance enclosures which house the EDG fuel oil tanks had several openings, unsealed pin holes, and a narrow gap along the perimeter of the base walls, which would allow water intrusion into the EDG fuel oil tank rooms during a design basis external event (hurricane).
This violation is associated with a White SDP finding.  
This violation is associated with a White SDP finding.
 
Pursuant to the provisions of 10 CFR 2.201, Carolina Power and Light Company is hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident Inspector at the Brunswick Steam Electric Plant, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of Violation; EA-11-251" and should include for each violation: (1) the reason for the violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will be achieved. Your response may reference or include previously docketed correspondence, if the correspondence adequately addresses the required response. If an adequate reply is not received within the time specified in this Notice, an order or a Demand for Information may be issued as to why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.
Pursuant to the provisions of 10 CFR 2.201, Carolina Power and Light Company is hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident Inspector at the Brunswick Steam Electric Plant, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of Violation; EA-11-251" and should include for each violation: (1) the reason for the violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will be achieved. Your response may reference or include previously docketed correspondence, if the correspondence adequately addresses the required response. If an adequate reply is not received within the time specified in this Notice, an order or a Demand for Information may be issued as to why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.  
 
If you contest this enforcement action, you should also provide a copy of your response, with the basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001.
If you contest this enforcement action, you should also provide a copy of your response, with the basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001.
NOV 2  Enclosure Because your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the public without redaction. If personal privacy or proprietary information is necessary to provide an acceptable response, then please provide a bracketed copy of your response that identifies the information that should be protected and a redacted copy of your response that deletes such information. If you request withholding of such material, you must specifically identify the portions of your response that you seek to have withheld and provide in detail the bases for your claim of withholding (e.g., explain why the disclosure of information will create an unwarranted invasion of personal privacy or provide the information required by  10 CFR 2.390(b) to support a request for withholding confidential commercial or financial information). If safeguards information is necessary to provide an acceptable response, please provide the level of protection described in 10 CFR 73.21.
Enclosure
In accordance with 10 CFR 19.11, you may be required to post this Notice within two working days of receipt. 


Dated this 27th day of December 2011}}
NOV                                              2 Because your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the public without redaction. If personal privacy or proprietary information is necessary to provide an acceptable response, then please provide a bracketed copy of your response that identifies the information that should be protected and a redacted copy of your response that deletes such information. If you request withholding of such material, you must specifically identify the portions of your response that you seek to have withheld and provide in detail the bases for your claim of withholding (e.g., explain why the disclosure of information will create an unwarranted invasion of personal privacy or provide the information required by 10 CFR 2.390(b) to support a request for withholding confidential commercial or financial information). If safeguards information is necessary to provide an acceptable response, please provide the level of protection described in 10 CFR 73.21.
In accordance with 10 CFR 19.11, you may be required to post this Notice within two working days of receipt.
Dated this 27th day of December 2011 Enclosure}}

Latest revision as of 10:15, 12 November 2019

Final Significance Determination of White Finding and Notice of Violation - NRC Inspection Report 2011014 and Assessment Follow-up Letter - Brunswick Steam Electric Plant
ML113610594
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 12/27/2011
From: Mccree V
Region 2 Administrator
To: Annacone M
Carolina Power & Light Co
References
EA-11-251 IR-11-014
Download: ML113610594 (8)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 December 27, 2011 EA-11-251 Mr. Michael Annacone Vice President Carolina Power and Light Company Brunswick Steam Electric Plant P. O. Box 10429 Southport, NC 28461

SUBJECT:

FINAL SIGNIFICANCE DETERMINATION OF WHITE FINDING AND NOTICE OF VIOLATION - NRC INSPECTION REPORT NOS.: 05000325/2011014 AND 05000324/2011014; AND ASSESSMENT FOLLOW-UP LETTER - BRUNSWICK STEAM ELECTRIC PLANT

Dear Mr. Annacone:

This letter provides the final significance determination of the preliminary White finding discussed in Brunswick Steam Electric Plant - NRC Inspection Report Nos.:

05000325/2011012 and 05000324/2011012; Preliminary White Finding, dated November 29, 2011. The finding involved an NRC inspector identified violation of 10 CFR Part 50 Appendix B Criterion XVI, Corrective Action, for the failure to identify and correct a condition adverse to quality associated with the entrance enclosures for the Emergency Diesel Generator (EDG) fuel oil tank rooms. Specifically, the enclosures contained openings which would adversely impact their ability to mitigate external flooding of the EDG fuel oil tank rooms in the event of an external event (hurricane). In response to this condition, new sealant material was installed to close the openings of the entrance enclosures for the EDG fuel oil tank rooms, and jersey barriers were installed to limit wave run-up on the enclosures.

During a telephone conversation with Mr. Randall Musser of NRC, Region II, on December 6, 2011, Licensing Supervisor, Ms. Annette Pope of your staff indicated that Carolina Power and Light Company, Brunswick Steam Electric Plant, did not contest the characterization of the risk significance of this finding and that you declined the opportunity to discuss this issue during a Regulatory Conference or to provide a written response.

After considering the information developed during the inspection, the NRC has concluded that the finding is appropriately characterized as White, a finding with low to moderate safety significance that may require additional NRC inspections.

Note: According to NRC Inspection Manual Chapter (IMC) 0609, appeal rights only apply to those licensees that have either attended a regulatory conference or submitted a written response to the preliminary determination letter.

CPL 2 The NRC has also determined that the failure to identify and correct a condition adverse to quality associated with the entrance enclosures for the Emergency Diesel Generator (EDG) fuel oil tank rooms is a violation of 10 CFR Part 50 Appendix B Criterion XVI, Corrective Action, as cited in the attached Notice of Violation (Notice). The circumstances surrounding the violation were described in detail in NRC Inspection Report Nos. 05000325/2011012 and 05000324/2011012. In accordance with the NRC Enforcement Policy, the Notice is considered escalated enforcement action because it is associated with a White finding.

You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. If you have additional information that you believe the NRC should consider, you may provide it in your response to the Notice. The NRCs review of your response to the Notice will also determine whether further enforcement action is necessary to ensure compliance with regulatory requirements.

Because plant performance for this issue has been determined to be beyond the licensee response band, the NRCs Action Matrix was used to determine the most appropriate NRC response for this issue. As a result of its continuous review of plant performance, which was completed on December 16, 2011, the NRC updated its assessment of Brunswick Steam Electric Plant, Units 1 and 2. The NRCs evaluation consisted of a review of performance indicators and inspection results.

The NRC determined the performance at Brunswick Steam Electric Plant, Units 1 and 2 to be in the Regulatory Response Column of the Reactor Oversight Process Action Matrix beginning the fourth quarter of 2011. Therefore, in addition to baseline inspections, the NRC plans to conduct a supplemental inspection in accordance with Inspection Procedure 95001, Inspection for One or Two White Inputs in a Strategic Performance Area, for the review of the White inspection finding. Have your staff notify the NRC of your readiness for us to conduct this supplemental inspection to review the actions taken to address the White inspection finding in the Mitigating Systems Cornerstone.

For administrative purposes, this letter is issued as NRC Inspection Report No.

05000325, 324/2011014. Accordingly, AV 05000325, 324/2011012-01, Failure to Identify and Correct Degradation of the Emergency Diesel Generator Fuel Oil Tank Room Entrance Enclosures is updated as VIO 05000325, 324/2011012-01, Failure to Identify and Correct Degradation of the Emergency Diesel Generator Fuel Oil Tank Room Entrance Enclosures.

This violation is associated with a finding with a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution area because the licensee did not identify the issue completely, accurately, and in a timely manner commensurate with its safety significance (P.1(a)).

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your

CPL 3 response should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the Public without redaction.

Sincerely,

/RA by Leonard Wert Acting For/

Victor M. McCree Regional Administrator Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62

Enclosure:

Notice of Violation

CPL 3 response should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the Public without redaction.

Sincerely,

/RA by Leonard Wert Acting For/

Victor M. McCree Regional Administrator Docket Nos.: 50-325, 50-324 License Nos.: DPR-71, DPR-62

Enclosure:

Notice of Violation XPUBLICLY AVAILABLE G NON-PUBLICLY AVAILABLE G SENSITIVE X NON-SENSITIVE ADAMS: X Yes ACCESSION NUMBER:__ML113610594___________ X SUNSI REVIEW COMPLETE X FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRP RII:EICS RII:RA HQ: OE HQ:NRR SIGNATURE JSD RAM B. Jones for CFE /RA/ Via email Via email NAME JDodson RMusser RCroteau CEvans LWert DATE 12/14/2011 12/20/2011 12/20/2011 12/15/2011 12/ /2011 12/19/2011 12/20/2011 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICIAL RECORD COPY DOCUMENT NAME: G:\DRPII\RPB4\BRUNSWICK\BRU FINAL SI G:\DRPII\RPB4\BRUNSWICK\Reports\2011 Reports\BRU FINAL SIGNIFICANCE LETTER 2011014.DOCX

CPL 4 cc w/encl: Senior Resident Inspector Edward L. Wills, Jr. U.S. Nuclear Regulatory Commission Director Site Operations Brunswick Steam Electric Plant Brunswick Steam Electric Plant U.S. NRC Electronic Mail Distribution 8470 River Road, SE Southport, NC 28461 Joseph M. Frisco, Jr Plant General Manager John H. O'Neill, Jr.

Brunswick Steam Electric Plant Shaw, Pittman, Potts & Trowbridge Progress Energy 2300 N. Street, NW Electronic Mail Distribution Washington, DC 20037-1128 Phyllis N. Mentel Peggy Force, Assistant Attorney General Manager, Support Services State of North Carolina Brunswick Steam Electric Plant P.O. Box 629 Progress Energy Carolinas, Inc. Raleigh, NC 27602 Electronic Mail Distribution Chairman Annette H. Pope North Carolina Utilities Commission Supervisor, Licensing/Regulatory Programs Electronic Mail Distribution Brunswick Steam Electric Plant Progress Energy Carolinas, Inc. Robert P. Gruber, Executive Director Electronic Mail Distribution Public Staff - NCUC 4326 Mail Service Center Randy C. Ivey Raleigh, NC 27699-4326 Manager, Nuclear Oversight Brunswick Steam Electric Plant Brunswick County Board of Commissioners Progress Energy Carolinas, Inc. P.O. Box 249 Electronic Mail Distribution Bolivia, NC 28422 Paul E. Dubrouillet, Manager, Training Public Service Commission Brunswick Steam Electric Plant State of South Carolina Electronic Mail Distribution P.O. Box 11649 Columbia, SC 29211 Kelvin Henderson, General Manager Nuclear Fleet Operations W. Lee Cox, III, Section Chief Progress Energy Radiation Protection Section Electronic Mail Distribution N.C. Department of Environmental Commerce & Natural Resources Joseph W. Donahue, Vice President Electronic Mail Distribution Nuclear Oversight Progress Energy Warren Lee Electronic Mail Distribution Emergency Management Director New Hanover County Department of David T. Conley, Senior Counsel Emergency Management Legal Department 230 Government Center Drive, Suite 115 Progress Energy Wilmington, NC 28403 Electronic Mail Distribution

CPL 5 Letter to Michael J. Annacone from Victor M. McCree dated December 27, 2011

SUBJECT:

FINAL SIGNIFICANCE DETERMINATION OF WHITE FINDING AND NOTICE OF VIOLATION - NRC INSPECTION REPORT NOS.: 05000325/2011014 AND 05000324/2011014; AND ASSESSMENT FOLLOW-UP LETTER - BRUNSWICK STEAM ELECTRIC PLANT Distribution w/encl:

C. Evans, RII EICS L. Douglas, RII EICS OE Mail RIDSNRRDIRS PUBLIC RidsNrrPMBrunswick Resource ROPassessment Resource

NOTICE OF VIOLATION Carolina Power and Light Company Docket Nos. 50-325, 50-324 Brunswick Steam Electric Plant License Nos. DPR-71, DPR-62 EA-11-251 During an NRC inspection conducted on April 20, 2011 a violation of NRC requirements was identified. In accordance with the NRC Enforcement Policy, the violation is listed below:

10 CFR Part 50 Appendix B Criterion XVI, Corrective Action states, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected.

Contrary to the above, as of April 20, 2011, the licensee failed to identify and promptly correct a condition adverse to quality involving the external flood barrier for the EDG fuel oil tank rooms. Specifically, the entrance enclosures which house the EDG fuel oil tanks had several openings, unsealed pin holes, and a narrow gap along the perimeter of the base walls, which would allow water intrusion into the EDG fuel oil tank rooms during a design basis external event (hurricane).

This violation is associated with a White SDP finding.

Pursuant to the provisions of 10 CFR 2.201, Carolina Power and Light Company is hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001 with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident Inspector at the Brunswick Steam Electric Plant, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be clearly marked as a "Reply to a Notice of Violation; EA-11-251" and should include for each violation: (1) the reason for the violation, or, if contested, the basis for disputing the violation or severity level, (2) the corrective steps that have been taken and the results achieved, (3) the corrective steps that will be taken, and (4) the date when full compliance will be achieved. Your response may reference or include previously docketed correspondence, if the correspondence adequately addresses the required response. If an adequate reply is not received within the time specified in this Notice, an order or a Demand for Information may be issued as to why the license should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response, with the basis for your denial, to the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001.

Enclosure

NOV 2 Because your response will be made available electronically for public inspection in the NRC Public Document Room or from the NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html, to the extent possible, it should not include any personal privacy, proprietary, or safeguards information so that it can be made available to the public without redaction. If personal privacy or proprietary information is necessary to provide an acceptable response, then please provide a bracketed copy of your response that identifies the information that should be protected and a redacted copy of your response that deletes such information. If you request withholding of such material, you must specifically identify the portions of your response that you seek to have withheld and provide in detail the bases for your claim of withholding (e.g., explain why the disclosure of information will create an unwarranted invasion of personal privacy or provide the information required by 10 CFR 2.390(b) to support a request for withholding confidential commercial or financial information). If safeguards information is necessary to provide an acceptable response, please provide the level of protection described in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working days of receipt.

Dated this 27th day of December 2011 Enclosure