05000323/FIN-2018001-02: Difference between revisions

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| finding integer = 02
| finding integer = 02
| quarter = 2018Q1
| quarter = 2018Q1
| IR section = NO CC AREA
| IR section = 4OA2
| finding type = Finding
| finding type = Finding
| significance =  
| significance = Green
| cornerstone = Mitigating Systems
| cornerstone = Mitigating Systems
| violation of = Pending
| violation of = Pending
| identified by = NRC
| identified by = NRC
| Inspection procedure = IP 4OA2
| Inspection procedure = IP 71152
| Inspector = 7115
| Inspector = C Newgent, J Reynoso, W Sifre, L Brookhart, N Greene, J O'Donnell, M Haire
| CCA = N/A for ROP
| CCA =  
| INPO aspect = NO SL
| INPO aspect =  
| description = The inspectors identified a finding of very low safety significance (Green) because PG&E personnel failed to follow the requirements of OM4.ID3, Operating Experience Program, Revision 20.  Specifically, PG&E personnel failed to screen relevant operating experience relating to a safety-related centrifugal charging pump (CCP) journal bearing failure due to non-metallic anti-rotation pin shear failure.  This operating experience notice was received by PG&E September 2011 and was not screened per OM4.ID3, Operating Experience Program, preventing actions from being identified and implemented that could have eliminated vulnerabilities and prevented a similar event from occurring at DCPP.  On November11,2017, CCP 2-1 was declared inoperable and determined to be non-functional due to a damaged journal bearing caused by non-metallic, anti-rotation pin shear failur
| description = The inspectors identified a finding of very low safety significance (Green) because PG&E personnel failed to follow the requirements of OM4.ID3, Operating Experience Program, Revision 20.  Specifically, PG&E personnel failed to screen relevant operating experience relating to a safety-related centrifugal charging pump (CCP) journal bearing failure due to non-metallic anti-rotation pin shear failure.  This operating experience notice was received by PG&E September 2011 and was not screened per OM4.ID3, Operating Experience Program, preventing actions from being identified and implemented that could have eliminated vulnerabilities and prevented a similar event from occurring at DCPP.  On November11,2017, CCP 2-1 was declared inoperable and determined to be non-functional due to a damaged journal bearing caused by non-metallic, anti-rotation pin shear failur


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Latest revision as of 07:59, 30 May 2018

02
Site: Diablo Canyon Pacific Gas & Electric icon.png
Report IR 05000323/2018001 Section 4OA2
Date counted Mar 31, 2018 (2018Q1)
Type: Finding: Green
cornerstone Mitigating Systems
Identified by: NRC identified
Inspection Procedure: IP 71152
Inspectors (proximate) C Newgent
J Reynoso
W Sifre
L Brookhart
N Greene
J O'Donnell
M Haire
Violation of: Pending
INPO aspect
'