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=Text=
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{{#Wiki_filter:' 77)
{{#Wiki_filter:' 77)
              -
                      ,
LICENSEE EVENT REPORT REQUIR ED INFORMATION)
LICENSEE EVENT REPORT REQUIR ED INFORMATION)
NT'.0L BLOCK: l 8
NT'.0L BLOCK: l 8
1    l      I    l  dh  6 (PLEASE FRINT OR TYPE                                                                            ,
1    l      I    l  dh  6 (PLEASE FRINT OR TYPE                                                                            ,
l 1JG l 157lCA1T 36l l@
l 1JG l 157lCA1T 36l l@
l                        f a 1                  lH]D B l S l l '@l 0 l 0 l - UCENSE 14    15 l 010NWl5EH l N l P l F l-25 l 013          26      l@l 4TYPE uCENSE                                    1 l@l            l LICENSEE CCOE
l                        f a 1                  lH]D B l S l l '@l 0 l 0 l - UCENSE 14    15 l 010NWl5EH l N l P l F l-25 l 013          26      l@l 4TYPE uCENSE                                    1 l@l            l LICENSEE CCOE tCN alil                  y'C"7
                                                                                                                                                                                                    '
tCN alil                  y'C"7
                             ,c      l L @l 0 l 5 l 0 l- 10 l 31416                        68
                             ,c      l L @l 0 l 5 l 0 l- 10 l 31416                        68
                                                                                               @l 69 1121016 EVENT 0 ATE l 717 }@li 74      75  l REPORT 212121717 QATE          80l@
                                                                                               @l 69 1121016 EVENT 0 ATE l 717 }@li 74      75  l REPORT 212121717 QATE          80l@
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I l0$8l l T
I l0$8l l T
                                           *Ec a" '            Tc"a*E    Suec$ce                CcMeoNENT CCDE                      SUSC E            S      QE ioisi                              I E I A l@ [C_j@ l Z l@ l Z l Z l Z l Z l Z l Z lh I Z l@20[Zj h                    18          19 9          to          11          12            f3                                                                            REVISION 7        8                                                                                                      OCOUR RENCE          REPORT SEQUENTIAL                                                                                    No.
                                           *Ec a" '            Tc"a*E    Suec$ce                CcMeoNENT CCDE                      SUSC E            S      QE ioisi                              I E I A l@ [C_j@ l Z l@ l Z l Z l Z l Z l Z l Z lh I Z l@20[Zj h                    18          19 9          to          11          12            f3                                                                            REVISION 7        8                                                                                                      OCOUR RENCE          REPORT SEQUENTIAL                                                                                    No.
_
R EPORT NO.                              CCQE                TYPE
R EPORT NO.                              CCQE                TYPE
                   @ a(sy,,po gn        EVENT YEAR g I 71 71                      1-1        1 11 01 61 26 1/1 27 I6l3l 23      29 ILI 30 l-1 31 W
                   @ a(sy,,po gn        EVENT YEAR g I 71 71                      1-1        1 11 01 61 26 1/1 27 I6l3l 23      29 ILI 30 l-1 31 W
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_ 21          22        23          24 S8 i            PoR        8.      SUPP ER                MA UPA      RER O P      T      ME                    hours N AC CN
_ 21          22        23          24 S8 i            PoR        8.      SUPP ER                MA UPA      RER O P      T      ME                    hours N AC CN
                           @lzj@ l Zi@                              l26Zl@        l 01 01 01 01                I41 Yl@          l42N ]@          y@                l44ZI Zl Zl Zl@    47 37                      40                                        43 34                  35 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS on the                I
                           @lzj@ l Zi@                              l26Zl@        l 01 01 01 01                I41 Yl@          l42N ]@          y@                l44ZI Zl Zl Zl@    47 37                      40                                        43 34                  35 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS on the                I
  "
       ;i;o[lThe cause of this occurrence has been attributed to "calionine cnnam *n-="
       ;i;o[lThe cause of this occurrence has been attributed to "calionine cnnam *n-="
b r o n tr o-,    4,    *%                  i i, ,ij        l transmission line which caused a trio of two 345 KV air circuit
b r o n tr o-,    4,    *%                  i i, ,ij        l transmission line which caused a trio of two 345 KV air circuit
Line 56: Line 50:
                                                                                         "        *
                                                                                         "        *
* l
* l
      '
               'Jnv,Ty C#TtNT                                                                                                        LOCATION oP RELEASE utEASEo cP RELEASE -                        AucuNT cP ACTiviry @                      l lNA                                                                  .          l li is l8 I9 Z l @ IZ 7                            10 l@l NA  11                                      44            45 30 PERSONNEL EXPCSURES NUMBER            TYPE        CESCRIPTICN lIlIl                1 PER$0NNEL INJURIES NUM9ER              DESCRIPTION l
               'Jnv,Ty C#TtNT                                                                                                        LOCATION oP RELEASE utEASEo cP RELEASE -                        AucuNT cP ACTiviry @                      l lNA                                                                  .          l li is l8 I9 Z l @ IZ 7                            10 l@l NA  11                                      44            45 30 PERSONNEL EXPCSURES NUMBER            TYPE        CESCRIPTICN lIlIl                1 PER$0NNEL INJURIES NUM9ER              DESCRIPTION l
li la 8l 1010101@l 7            9              11 NA 12
li la 8l 1010101@l 7            9              11 NA 12 oSS OP OR DacAGE TO PACILITY
'
oSS OP OR DacAGE TO PACILITY
!                        E      DESCRIPTION NA l
!                        E      DESCRIPTION NA l
l d 9 Zl@l10                                                                                                                                                            60 l      7 PU8UCITY                                                                .
l d 9 Zl@l10                                                                                                                                                            60 l      7 PU8UCITY                                                                .
NRC USE ONLY oESCRiPTic~ O,p, l
NRC USE ONLY oESCRiPTic~ O,p, l
iSSut0                                                                        8 o o e o 4 c699                                ]      l!llll!!lI!!!!
iSSut0                                                                        8 o o e o 4 c699                                ]      l!llll!!lI!!!!
l2lollNl$al                    NA
l2lollNl$al                    NA l
,
68 69                                  40 3 F      8 9              10 Tom Beeler                                                              (419) 259-5000, Ext. 253)
l 68 69                                  40 3
PHONE:                                                        3 DVR 178-1 & IS@YE OF FREPARER .                                                                                                                                                                  l l
'
F      8 9              10 Tom Beeler                                                              (419) 259-5000, Ext. 253)
PHONE:                                                        3 DVR 178-1 & IS@YE OF FREPARER .                                                                                                                                                                  l
* l


                                                                                                .
TOLEDO EDISON COMPANY p'                          DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-106
                    -                                                                                  .
      *
            ,                                                                                          .
                                        .
            -                                                                                          .
                                                                                                        '
TOLEDO EDISON COMPANY
                                                                                                        !
p'                          DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-106
_
  -
()                                                                                                  r 1
()                                                                                                  r 1
l DATE OF EVENT: December 6 and 7, 1977                                                            ;
l DATE OF EVENT: December 6 and 7, 1977                                                            ;
FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Loss of 02 Startup Transformer due to fault on the Ohio Edison Beaver Line                          ,
FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Loss of 02 Startup Transformer due to fault on the Ohio Edison Beaver Line                          ,
                                                                                                          '
                                                ,
                                              .
                                                                                                          !
Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 1100 and Load (MWE) = 365.                                                                            i Description of Occurrence: At 1741 hours on December 6, 1977 and 0237 hours on December 7,1977, two 345 KV air circuit breakers on "K" Bus tripped due to a fault on the Ohio Edison Beaver Line. This de-energized 02 Startup Transformer and placed the unit into the Action Statement of Technical Specification 3.8.1.I since one of the 345/13.8 KV Startup Transformers was de-energized.          .
Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 1100 and Load (MWE) = 365.                                                                            i Description of Occurrence: At 1741 hours on December 6, 1977 and 0237 hours on December 7,1977, two 345 KV air circuit breakers on "K" Bus tripped due to a fault on the Ohio Edison Beaver Line. This de-energized 02 Startup Transformer and placed the unit into the Action Statement of Technical Specification 3.8.1.I since one of the 345/13.8 KV Startup Transformers was de-energized.          .
                                                                                                  -
Designation of Apparent Cause of Occurrence: The cause of this occurrence has been attributed to " galloping conductors" on the transmission line. "Calloping
Designation of Apparent Cause of Occurrence: The cause of this occurrence has been attributed to " galloping conductors" on the transmission line. "Calloping
         . conductors" is a movement of transmission lines caused by high winds and ice U uildup b      on the transmission lines. This caused the protective relaying scheme to trip two 345 KV air circuit breakers in the switchyard.
         . conductors" is a movement of transmission lines caused by high winds and ice U uildup b      on the transmission lines. This caused the protective relaying scheme to trip two 345 KV air circuit breakers in the switchyard.
Line 99: Line 70:
Corrective Action: At 1742 hours on December 6,1977 and 0237 hours on December 7, 1977, the Load Dispatcher opened the air break switch which cleared the Beaver Line from "K" Bus and at 1743 hours on December 6, 1977 and 0238 hours on Decem-ber 7, 1977, reclosed the two 345 KV air circuit breakers which re-energized "K" Bus from the Toledo Edison Company Bay Shore Line. This removed the unit from the Action Statement of Technical Specification 3.8.1.1. The Transaission and Substation Engineering Division is continuing to study and test proposed resolu-tions to the " galloping conductors" problem.
Corrective Action: At 1742 hours on December 6,1977 and 0237 hours on December 7, 1977, the Load Dispatcher opened the air break switch which cleared the Beaver Line from "K" Bus and at 1743 hours on December 6, 1977 and 0238 hours on Decem-ber 7, 1977, reclosed the two 345 KV air circuit breakers which re-energized "K" Bus from the Toledo Edison Company Bay Shore Line. This removed the unit from the Action Statement of Technical Specification 3.8.1.1. The Transaission and Substation Engineering Division is continuing to study and test proposed resolu-tions to the " galloping conductors" problem.
Failure Data: No previous similar events have occurred.
Failure Data: No previous similar events have occurred.
                                                                                      -
J i
                                                                                          .
;
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                                                      -
i
     -                                                        8002040        .
     -                                                        8002040        .
                                                                                                    ,
l                                                                .
l                                                                .
                                                                                .
                                                                        --
_          _ _}}
_          _ _}}

Latest revision as of 17:39, 18 February 2020

LER 77-106/03L-0:on 771206,two 345 Kv Air Circuit Breakers on K Bus Tripped Due to Fault on Oh Edison Co Beaver Line. Caused by Galloping Conductors on Transmission Line.Load Dispatcher Opened Air Breaker & Reclosed Circuit Breakers
ML19326A508
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 12/22/1977
From: Beeler T
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19326A497 List:
References
LER-77-106-03L, LER-77-106-3L, NUDOCS 8002040689
Download: ML19326A508 (2)


Text

' 77)

LICENSEE EVENT REPORT REQUIR ED INFORMATION)

NT'.0L BLOCK: l 8

1 l I l dh 6 (PLEASE FRINT OR TYPE ,

l 1JG l 157lCA1T 36l l@

l f a 1 lH]D B l S l l '@l 0 l 0 l - UCENSE 14 15 l 010NWl5EH l N l P l F l-25 l 013 26 l@l 4TYPE uCENSE 1 l@l l LICENSEE CCOE tCN alil y'C"7

,c l L @l 0 l 5 l 0 l- 10 l 31416 68

@l 69 1121016 EVENT 0 ATE l 717 }@li 74 75 l REPORT 212121717 QATE 80l@

8 60 68 DOCKET NUMSER EVENT OESCRIPTION AND PRC8 ABLE CONSEQUENCES h breakers I

7) ! 21 l At 1741 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.624505e-4 months <br /> on 12/6/77 and 0237 hours0.00274 days <br />0.0658 hours <br />3.918651e-4 weeks <br />9.01785e-5 months <br /> on 12/7/77, two 345 KV air circuit Bus tripped due to a fault on the Ohio Edison Beaver Line. This de-energized I o i2I l n "K" in the Action Statement of Tech Spec ]

fo,,,;02 Startup Transformer and placed the unit

,o,3, ;3.8.1.1.

There was no danger to the heslth and safety of the public or to unit per- ]

l I o is I l sonnel. At the time of the occurrence, the unit was on the Aux 111arv Transformer l

[a37; gand not on the Startup Transformers. -(NP-33-77-106)

I l0$8l l T

  • Ec a" ' Tc"a*E Suec$ce CcMeoNENT CCDE SUSC E S QE ioisi I E I A l@ [C_j@ l Z l@ l Z l Z l Z l Z l Z l Z lh I Z l@20[Zj h 18 19 9 to 11 12 f3 REVISION 7 8 OCOUR RENCE REPORT SEQUENTIAL No.

R EPORT NO. CCQE TYPE

@ a(sy,,po gn EVENT YEAR g I 71 71 1-1 1 11 01 61 26 1/1 27 I6l3l 23 29 ILI 30 l-1 31 W

32

_ 21 22 23 24 S8 i PoR 8. SUPP ER MA UPA RER O P T ME hours N AC CN

@lzj@ l Zi@ l26Zl@ l 01 01 01 01 I41 Yl@ l42N ]@ y@ l44ZI Zl Zl Zl@ 47 37 40 43 34 35 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS on the I

i;o[lThe cause of this occurrence has been attributed to "calionine cnnam *n-="

b r o n tr o-, 4, *% i i, ,ij l transmission line which caused a trio of two 345 KV air circuit

---n I

,,#21lsvitchvard. The Load Dispatcher opened the n4* b e a ,1- wd*ck ,na -or i m aa - %

i

, #3j l 345 KV air circuit breakers which re-energized "K" Bus from the Toledo Edison I

I iii4l l Company Bay Shore Line. 80 1 a o OTHER STATUS IS Y DISCOVERY DESCRIPTION

' STA  % POV,ER l

li is 1 I E l@ 10 la 10 '2l@l "NA l l A[g[ NA 'o

" *

  • l

'Jnv,Ty C#TtNT LOCATION oP RELEASE utEASEo cP RELEASE - AucuNT cP ACTiviry @ l lNA . l li is l8 I9 Z l @ IZ 7 10 l@l NA 11 44 45 30 PERSONNEL EXPCSURES NUMBER TYPE CESCRIPTICN lIlIl 1 PER$0NNEL INJURIES NUM9ER DESCRIPTION l

li la 8l 1010101@l 7 9 11 NA 12 oSS OP OR DacAGE TO PACILITY

! E DESCRIPTION NA l

l d 9 Zl@l10 60 l 7 PU8UCITY .

NRC USE ONLY oESCRiPTic~ O,p, l

iSSut0 8 o o e o 4 c699 ] l!llll!!lI!!!!

l2lollNl$al NA l

68 69 40 3 F 8 9 10 Tom Beeler (419) 259-5000, Ext. 253)

PHONE: 3 DVR 178-1 & IS@YE OF FREPARER . l l

TOLEDO EDISON COMPANY p' DAVIS-BESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-106

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l DATE OF EVENT: December 6 and 7, 1977  ;

FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Loss of 02 Startup Transformer due to fault on the Ohio Edison Beaver Line ,

Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 1100 and Load (MWE) = 365. i Description of Occurrence: At 1741 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.624505e-4 months <br /> on December 6, 1977 and 0237 hours0.00274 days <br />0.0658 hours <br />3.918651e-4 weeks <br />9.01785e-5 months <br /> on December 7,1977, two 345 KV air circuit breakers on "K" Bus tripped due to a fault on the Ohio Edison Beaver Line. This de-energized 02 Startup Transformer and placed the unit into the Action Statement of Technical Specification 3.8.1.I since one of the 345/13.8 KV Startup Transformers was de-energized. .

Designation of Apparent Cause of Occurrence: The cause of this occurrence has been attributed to " galloping conductors" on the transmission line. "Calloping

. conductors" is a movement of transmission lines caused by high winds and ice U uildup b on the transmission lines. This caused the protective relaying scheme to trip two 345 KV air circuit breakers in the switchyard.

Analysis of Occurrence: There was no danger to the health *and safety of the public or to unit personnel.. At the time of the occurrence, the unit was on the Auxiliary Transformer, and not on the Startup Transformers. Also, there was two 345 KV trans-mission linen, one 345/13.8 KV Startup Transformers and two 13.8 KV Buses operable with two independent diesel generators to provide AC power.

Corrective Action: At 1742 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.62831e-4 months <br /> on December 6,1977 and 0237 hours0.00274 days <br />0.0658 hours <br />3.918651e-4 weeks <br />9.01785e-5 months <br /> on December 7, 1977, the Load Dispatcher opened the air break switch which cleared the Beaver Line from "K" Bus and at 1743 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.632115e-4 months <br /> on December 6, 1977 and 0238 hours0.00275 days <br />0.0661 hours <br />3.935185e-4 weeks <br />9.0559e-5 months <br /> on Decem-ber 7, 1977, reclosed the two 345 KV air circuit breakers which re-energized "K" Bus from the Toledo Edison Company Bay Shore Line. This removed the unit from the Action Statement of Technical Specification 3.8.1.1. The Transaission and Substation Engineering Division is continuing to study and test proposed resolu-tions to the " galloping conductors" problem.

Failure Data: No previous similar events have occurred.

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