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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES  
                            NUCLEAR REGULATORY COMMISSION
NUCLEAR REGULATORY COMMISSION  
                                              REGION III
REGION III  
                                2443 WARRENVILLE ROAD, SUITE 210
2443 WARRENVILLE ROAD, SUITE 210  
                                          LISLE, IL 60532-4352
LISLE, IL 60532-4352  
                                            January 27, 2010
Mr. Charles G. Pardee
Senior Vice President, Exelon Generation Company, LLC
January 27, 2010  
President and Chief Nuclear Officer (CNO), Exelon Nuclear
4300 Winfield Road
Warrenville, IL 60555
SUBJECT:       QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2
Mr. Charles G. Pardee  
                NRC INTEGRATED INSPECTION REPORT 05000254/2009005;
Senior Vice President, Exelon Generation Company, LLC  
                05000265/2009005
President and Chief Nuclear Officer (CNO), Exelon Nuclear  
Dear Mr. Pardee:
4300 Winfield Road  
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
Warrenville, IL 60555  
integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed
report documents the inspection findings, which were discussed on January 5, 2010, with
SUBJECT:  
Mr. T. Tulon and other members of your staff.
QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2  
The inspection examined activities conducted under your license as they relate to safety and
NRC INTEGRATED INSPECTION REPORT 05000254/2009005;  
compliance with the Commissions rules and regulations and with the conditions of your license.
05000265/2009005  
The inspectors reviewed selected procedures and records, observed activities, and interviewed
Dear Mr. Pardee:  
personnel.
On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an  
Based on the results of this inspection, three self-revealed findings of very low safety
integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed  
significance were identified. Two of the findings involved a violation of NRC requirements.
report documents the inspection findings, which were discussed on January 5, 2010, with  
However, because of their very low safety significance, and because the issues were entered
Mr. T. Tulon and other members of your staff.  
into your corrective action program, the NRC is treating the issues as non-cited violations
The inspection examined activities conducted under your license as they relate to safety and  
(NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally,
compliance with the Commissions rules and regulations and with the conditions of your license.
a licensee-identified violation is listed in Section 4OA7 of this report.
The inspectors reviewed selected procedures and records, observed activities, and interviewed  
If you contest the subject or severity of an NCV, you should provide a response within 30 days
personnel.  
of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear
Based on the results of this inspection, three self-revealed findings of very low safety  
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a
significance were identified. Two of the findings involved a violation of NRC requirements.
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,
However, because of their very low safety significance, and because the issues were entered  
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,
into your corrective action program, the NRC is treating the issues as non-cited violations  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector
(NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally,  
Office at the Quad Cities Nuclear Power Station. In addition, if you disagree with the
a licensee-identified violation is listed in Section 4OA7 of this report.  
characterization of any finding in this report, you should provide a response within 30 days of
If you contest the subject or severity of an NCV, you should provide a response within 30 days  
the date of this inspection report, with the basis for your disagreement, to the Regional
of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear  
Administrator, Region III, and the NRC Resident Inspector at the Quad Cities Nuclear Power
Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a  
Station. The information that you provide will be considered in accordance with Inspection
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,  
Manual Chapter 0305.
2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,  
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector  
Office at the Quad Cities Nuclear Power Station. In addition, if you disagree with the  
characterization of any finding in this report, you should provide a response within 30 days of  
the date of this inspection report, with the basis for your disagreement, to the Regional  
Administrator, Region III, and the NRC Resident Inspector at the Quad Cities Nuclear Power  
Station. The information that you provide will be considered in accordance with Inspection  
Manual Chapter 0305.


C. Pardee                                   -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter
and its enclosure will be made available electronically for public inspection in the
C. Pardee  
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                            Sincerely,
                                            /RA/
-2-  
                                            Mark A. Ring, Chief
                                            Branch 1
                                            Division of Reactor Projects
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter  
Docket Nos. 50-254; 50-265
and its enclosure will be made available electronically for public inspection in the  
License Nos. DPR-29; DPR-30
NRC Public Document Room or from the Publicly Available Records (PARS) component of  
Enclosure:     Inspection Report 05000254/2009005; 05000265/2009005
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at  
                w/Attachment: Supplemental Information
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
cc w/encl:     Distribution via ListServ
Sincerely,  
/RA/  
Mark A. Ring, Chief  
Branch 1  
Division of Reactor Projects  
Docket Nos. 50-254; 50-265  
License Nos. DPR-29; DPR-30  
Enclosure:  
Inspection Report 05000254/2009005; 05000265/2009005  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  


          U.S. NUCLEAR REGULATORY COMMISSION
                          REGION III
Enclosure
Docket Nos:         50-254, 50-265
U.S. NUCLEAR REGULATORY COMMISSION  
License Nos:       DPR-29, DPR-30
REGION III  
Report No:         05000254/2009005 and 05000265/2009005
Docket Nos:  
Licensee:           Exelon Nuclear
50-254, 50-265  
Facility:           Quad Cities Nuclear Power Station, Units 1 and 2
License Nos:  
Location:           Cordova, IL
DPR-29, DPR-30  
Dates:             October 1 through December 31, 2009
Report No:  
Inspectors:         J. McGhee, Senior Resident Inspector
05000254/2009005 and 05000265/2009005  
                    B. Cushman, Resident Inspector
Licensee:  
                    R. Orlikowski, Senior Resident Inspector - Duane Arnold
Exelon Nuclear  
                    M. Bielby, Senior Operations Engineer
Facility:  
                    C. Moore, Operations Engineer
Quad Cities Nuclear Power Station, Units 1 and 2  
                    M. Mitchell, Senior Radiation Protection Inspector
Location:  
                    R. Jickling, Senior Emergency Preparedness Inspector
Cordova, IL  
                    C. Mathews, Illinois Emergency Management Agency
Dates:  
Approved by:       M. Ring, Chief
October 1 through December 31, 2009  
                    Branch 1
Inspectors:  
                    Division of Reactor Projects
J. McGhee, Senior Resident Inspector  
                                                                      Enclosure
B. Cushman, Resident Inspector  
R. Orlikowski, Senior Resident Inspector - Duane Arnold  
M. Bielby, Senior Operations Engineer  
C. Moore, Operations Engineer  
M. Mitchell, Senior Radiation Protection Inspector  
R. Jickling, Senior Emergency Preparedness Inspector  
C. Mathews, Illinois Emergency Management Agency  
Approved by:  
M. Ring, Chief  
Branch 1  
Division of Reactor Projects  


                                          TABLE OF CONTENTS
SUMMARY OF FINDINGS ...........................................................................................................1
Enclosure
REPORT DETAILS .......................................................................................................................4
TABLE OF CONTENTS  
Summary of Plant Status...........................................................................................................4
SUMMARY OF FINDINGS ...........................................................................................................1  
  1.   REACTOR SAFETY .......................................................................................................4
REPORT DETAILS.......................................................................................................................4  
      1R01     Adverse Weather Protection (71111.01)..............................................................4
Summary of Plant Status...........................................................................................................4  
      1R04     Equipment Alignment (71111.04) ........................................................................5
1.  
      1R05     Fire Protection (71111.05) ...................................................................................6
REACTOR SAFETY .......................................................................................................4  
      1R11     Licensed Operator Requalification Program (71111.11)......................................7
1R01  
      1R12     Maintenance Effectiveness (71111.12)..............................................................11
Adverse Weather Protection (71111.01)..............................................................4  
      1R13     Maintenance Risk Assessments and Emergent Work Control (71111.13) ........12
1R04  
      1R15     Operability Evaluations (71111.15) ....................................................................12
Equipment Alignment (71111.04) ........................................................................5  
      1R19     Post-Maintenance Testing (71111.19) ...............................................................13
1R05  
      1R22     Surveillance Testing (71111.22) ........................................................................14
Fire Protection (71111.05) ...................................................................................6  
      1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ................15
1R11  
      1EP6 Drill Evaluation (71114.06).................................................................................17
Licensed Operator Requalification Program (71111.11)......................................7  
  4.   OTHER ACTIVITIES.....................................................................................................18
1R12  
      4OA1 Performance Indicator Verification (71151) .......................................................18
Maintenance Effectiveness (71111.12)..............................................................11  
      4OA2 Identification and Resolution of Problems (71152) ............................................21
1R13  
      4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............27
Maintenance Risk Assessments and Emergent Work Control (71111.13) ........12  
      4OA5 Other Activities ...................................................................................................30
1R15  
      4OA6 Management Meetings ......................................................................................30
Operability Evaluations (71111.15)....................................................................12  
      4OA7 Licensee-Identified Violations ............................................................................31
1R19  
SUPPLEMENTAL INFORMATION ...............................................................................................1
Post-Maintenance Testing (71111.19)...............................................................13  
Key Points of Contact ................................................................................................................1
1R22  
List of Items Opened, Closed and Discussed............................................................................1
Surveillance Testing (71111.22) ........................................................................14  
List of Documents Reviewed .....................................................................................................2
1EP4  
List of Acronyms Used ..............................................................................................................8
Emergency Action Level and Emergency Plan Changes (71114.04) ................15  
                                                                                                                        Enclosure
1EP6  
Drill Evaluation (71114.06).................................................................................17  
4.  
OTHER ACTIVITIES.....................................................................................................18  
4OA1  
Performance Indicator Verification (71151) .......................................................18  
4OA2  
Identification and Resolution of Problems (71152) ............................................21  
4OA3  
Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............27  
4OA5  
Other Activities...................................................................................................30  
4OA6
Management Meetings ......................................................................................30  
4OA7  
Licensee-Identified Violations ............................................................................31  
SUPPLEMENTAL INFORMATION ...............................................................................................1  
Key Points of Contact................................................................................................................1  
List of Items Opened, Closed and Discussed............................................................................1  
List of Documents Reviewed.....................................................................................................2  
List of Acronyms Used ..............................................................................................................8  


                                      SUMMARY OF FINDINGS
IR 05000254/2009005, 05000265/2009005; 10/01/09 - 12/31/09; Quad Cities Nuclear Power
Station, Units 1 & 2; Other Activities.
1
This report covers a 3-month period of inspection by resident inspectors and announced
Enclosure
baseline inspections by regional inspectors. Three Green findings were identified by the
SUMMARY OF FINDINGS  
inspectors. Two of the findings were considered Non-Cited Violations (NCVs) of NRC
IR 05000254/2009005, 05000265/2009005; 10/01/09 - 12/31/09; Quad Cities Nuclear Power  
regulations. The significance of most findings is indicated by their color (Green, White, Yellow,
Station, Units 1 & 2; Other Activities.  
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process
This report covers a 3-month period of inspection by resident inspectors and announced  
(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity
baseline inspections by regional inspectors. Three Green findings were identified by the  
level after NRC management review. The NRCs program for overseeing the safe operation of
inspectors. Two of the findings were considered Non-Cited Violations (NCVs) of NRC  
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
regulations. The significance of most findings is indicated by their color (Green, White, Yellow,  
Revision 4, dated December 2006.
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process  
A.     NRC-Identified and Self-Revealed Findings
(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity  
        Cornerstone: Mitigating Systems
level after NRC management review. The NRCs program for overseeing the safe operation of  
    *   Green. A finding of very low safety significance and a NCV of 10 CFR 50 Appendix B,
commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,  
        Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the
Revision 4, dated December 2006.  
        installation of an inappropriate component into the Unit 2 emergency diesel generator
A.  
        coolant system. Specifically, the licensee failed to properly perform a part evaluation for
NRC-Identified and Self-Revealed Findings  
        a replacement temperature indicator (TI) designated as augmented quality. This
Cornerstone: Mitigating Systems  
        resulted in the TI probe shearing off in the coolant flow stream and causing foreign
*  
        material to enter the coolant system. Immediate corrective actions included the
Green. A finding of very low safety significance and a NCV of 10 CFR 50 Appendix B,  
        installation of an appropriately approved TI and recovery of foreign material from the
Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the  
        system.
installation of an inappropriate component into the Unit 2 emergency diesel generator  
        The same part evaluation process was used for risk-significant components independent
coolant system. Specifically, the licensee failed to properly perform a part evaluation for  
        of the system being worked. Therefore, this finding was more than minor because, if left
a replacement temperature indicator (TI) designated as augmented quality. This  
        uncorrected, this performance deficiency could lead to unplanned unavailability of
resulted in the TI probe shearing off in the coolant flow stream and causing foreign  
        safety-related or risk-significant equipment and would become a more significant safety
material to enter the coolant system. Immediate corrective actions included the  
        concern. The inspectors performed a Phase 1 SDP screening and concluded that the
installation of an appropriately approved TI and recovery of foreign material from the  
        issue was of very low safety significance (Green) because the failure of the TI did not
system.  
        result in unplanned inoperability or loss of function of the diesel generator. The
The same part evaluation process was used for risk-significant components independent  
        inspectors determined that this finding did not have a cross-cutting aspect. This
of the system being worked. Therefore, this finding was more than minor because, if left  
        performance deficiency is not indicative of current licensee performance. The decision
uncorrected, this performance deficiency could lead to unplanned unavailability of  
        to install this type of TI was made in October 2007. The process which allowed this
safety-related or risk-significant equipment and would become a more significant safety  
        performance deficiency was identified and corrected through procedure and policy
concern. The inspectors performed a Phase 1 SDP screening and concluded that the  
        revisions in February 2008. (Section 4OA2)
issue was of very low safety significance (Green) because the failure of the TI did not  
    *   Green: A finding of very low safety significance and a NCV of TS 3.6.2.4,
result in unplanned inoperability or loss of function of the diesel generator. The  
        Residual Heat Removal (RHR) Suppression Pool Spray, was self-revealed for the
inspectors determined that this finding did not have a cross-cutting aspect. This  
        licensees failure to meet the Technical Specification (TS) limiting conditions of operation
performance deficiency is not indicative of current licensee performance. The decision  
        (LCO) requirement prior to transitioning into an operating mode where the LCO was
to install this type of TI was made in October 2007. The process which allowed this  
        required to be satisfied. Specifically, Motor Operator (MO) 1-1001-37B for the Unit 1
performance deficiency was identified and corrected through procedure and policy  
        RHR torus (suppression pool) spray isolation valve was found to have been inoperable
revisions in February 2008. (Section 4OA2)  
        when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009.
*  
        The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the
Green: A finding of very low safety significance and a NCV of TS 3.6.2.4,  
        valve was not demonstrated operable by stroking the valve electrically after the actuator
Residual Heat Removal (RHR) Suppression Pool Spray, was self-revealed for the  
                                                  1                                      Enclosure
licensees failure to meet the Technical Specification (TS) limiting conditions of operation  
(LCO) requirement prior to transitioning into an operating mode where the LCO was  
required to be satisfied. Specifically, Motor Operator (MO) 1-1001-37B for the Unit 1  
RHR torus (suppression pool) spray isolation valve was found to have been inoperable  
when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009.
The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the  
valve was not demonstrated operable by stroking the valve electrically after the actuator  


  motor was declutched. Inspectors determined that the finding was cross-cutting in the
  area of Problem Identification and Resolution - Corrective Action (P.1(a)) because plant
  personnel failed to identify the physical contact with the valve actuator that resulted in
2
  the valve being declutched; therefore, operators incorrectly assessed the system
Enclosure
  condition as in compliance with TS 3.6.2.4. Immediate licensee corrective actions
motor was declutched. Inspectors determined that the finding was cross-cutting in the  
  included engagement of the motor and stroke testing of the valve.
area of Problem Identification and Resolution - Corrective Action (P.1(a)) because plant  
  The finding is more than minor because it was associated with the equipment
personnel failed to identify the physical contact with the valve actuator that resulted in  
  performance quality attribute of the Mitigating Systems Cornerstone and affected the
the valve being declutched; therefore, operators incorrectly assessed the system  
  objective of ensuring availability, reliability, and capability of systems that respond to
condition as in compliance with TS 3.6.2.4. Immediate licensee corrective actions  
  initiating events to prevent undesirable consequences. Specifically, failure to verify
included engagement of the motor and stroke testing of the valve.  
  system availability and capability prior to entering the required modes resulted in fewer
The finding is more than minor because it was associated with the equipment  
  available mitigating systems than assumed in the operating risk evaluations. The
performance quality attribute of the Mitigating Systems Cornerstone and affected the  
  inspectors determined the finding could be evaluated using the SDP in accordance with
objective of ensuring availability, reliability, and capability of systems that respond to  
  IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial
initiating events to prevent undesirable consequences. Specifically, failure to verify  
  Screening and Characterization of findings, Table 4a. Inspectors answered all of the
system availability and capability prior to entering the required modes resulted in fewer  
  questions for the Mitigating Systems Cornerstone No. Therefore, the finding screened
available mitigating systems than assumed in the operating risk evaluations. The  
  as Green or very low safety significance. (Section 4OA3)
inspectors determined the finding could be evaluated using the SDP in accordance with  
  Cornerstone: Barrier Integrity
IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial  
* Green. A finding of very low safety significance was self-revealed for the failure to
Screening and Characterization of findings, Table 4a. Inspectors answered all of the  
  perform maintenance that would ensure the portable emergency flooding pump (Darley
questions for the Mitigating Systems Cornerstone No. Therefore, the finding screened  
  pump) was in a standby condition and readily available to accomplish the requirements
as Green or very low safety significance. (Section 4OA3)  
  of QCOA 0010-16, Flood Emergency Procedure. Specifically, the failure to perform
Cornerstone: Barrier Integrity  
  adequate maintenance resulted in the need to replace the battery and gasoline for the
*  
  pump and, upon pump start, fuel sprayed out of the fuel pump. Although the staged
Green. A finding of very low safety significance was self-revealed for the failure to  
  portable pump would not have supported the external flooding emergency response
perform maintenance that would ensure the portable emergency flooding pump (Darley  
  procedure, no violation of regulatory requirements occurred. The inspectors did not
pump) was in a standby condition and readily available to accomplish the requirements  
  identify a cross-cutting aspect associated with this finding because the issue is not
of QCOA 0010-16, Flood Emergency Procedure. Specifically, the failure to perform  
  reflective of current licensee performance. Immediate corrective actions included
adequate maintenance resulted in the need to replace the battery and gasoline for the  
  replacement of the degraded battery and overhaul of the pumps fuel pump. Other
pump and, upon pump start, fuel sprayed out of the fuel pump. Although the staged  
  actions included identification of preventative maintenance tasks and establishing a
portable pump would not have supported the external flooding emergency response  
  program owner of the pump and support equipment.
procedure, no violation of regulatory requirements occurred. The inspectors did not  
  This issue was more than minor because it was associated with the Structures,
identify a cross-cutting aspect associated with this finding because the issue is not  
  Systems, and Components (SSC) Performance attribute of the Barrier Integrity
reflective of current licensee performance. Immediate corrective actions included  
  Cornerstone objective of maintaining the functionality of spent fuel pool cooling.
replacement of the degraded battery and overhaul of the pumps fuel pump. Other  
  The finding affected the cornerstone objective of providing assurance that physical
actions included identification of preventative maintenance tasks and establishing a  
  design barriers protect the public from radionuclide releases caused by events including
program owner of the pump and support equipment.  
  external flooding. Specifically, the pump could fail due to maintenance preventable
This issue was more than minor because it was associated with the Structures,  
  component failure resulting in inadequate or degraded makeup to the spent fuel pool
Systems, and Components (SSC) Performance attribute of the Barrier Integrity  
  during an external flooding event. The inspectors determined the finding could be
Cornerstone objective of maintaining the functionality of spent fuel pool cooling.
  evaluated using the SDP in accordance with IMC 0609, Significance Determination
The finding affected the cornerstone objective of providing assurance that physical  
  Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of
design barriers protect the public from radionuclide releases caused by events including  
  findings, Tables 4a and 4b. The inspectors determined that even though this equipment
external flooding. Specifically, the pump could fail due to maintenance preventable  
  is assumed to completely fail, the licensee could provide an alternate portable pump
component failure resulting in inadequate or degraded makeup to the spent fuel pool  
  already located on site and capable of performing the safety function during this slow
during an external flooding event. The inspectors determined the finding could be  
  developing event. Since alternate equipment was available and the delay in mobilizing
evaluated using the SDP in accordance with IMC 0609, Significance Determination  
  the alternate equipment would not have resulted in loss of capability to mitigate the
Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of  
                                              2                                      Enclosure
findings, Tables 4a and 4b. The inspectors determined that even though this equipment  
is assumed to completely fail, the licensee could provide an alternate portable pump  
already located on site and capable of performing the safety function during this slow  
developing event. Since alternate equipment was available and the delay in mobilizing  
the alternate equipment would not have resulted in loss of capability to mitigate the  


  impact of the flooding event, the issue is of very low safety significance or Green.
  (Section 4OA2)
B. Licensee-Identified Violations
3
  A violation of very low safety significance that was identified by the licensee was
Enclosure
  reviewed by inspectors. Corrective actions planned or taken by the licensee have been
impact of the flooding event, the issue is of very low safety significance or Green.
  entered into the licensees corrective action program. This violation and associated
(Section 4OA2)  
  corrective action tracking number are listed in Section 4OA7 of this report.
B.  
                                            3                                      Enclosure
Licensee-Identified Violations  
A violation of very low safety significance that was identified by the licensee was  
reviewed by inspectors. Corrective actions planned or taken by the licensee have been  
entered into the licensees corrective action program. This violation and associated  
corrective action tracking number are listed in Section 4OA7 of this report.  


                                          REPORT DETAILS
Summary of Plant Status
Unit 1
4
Unit 1 operated at 100 percent thermal power throughout the evaluated period from October 1
Enclosure
until December 31, 2009, with the exception of planned power reductions for routine
REPORT DETAILS  
surveillances, planned equipment repair, and control rod maneuvers.
Summary of Plant Status  
Unit 2
Unit 1  
Unit 2 operated at or near 100 percent thermal power from October 1 until December 16 with
Unit 1 operated at 100 percent thermal power throughout the evaluated period from October 1  
the exception of planned power reductions for routine surveillances and control rod maneuvers.
until December 31, 2009, with the exception of planned power reductions for routine  
On December 16, 2009, operators attempted to replace a light bulb in the indication circuit for
surveillances, planned equipment repair, and control rod maneuvers.  
the extraction steam check valve A on the 2D feedwater heaters. The light bulb separated with
Unit 2  
the base remaining in the socket. During the evolution the D heaters tripped, resulting in a
Unit 2 operated at or near 100 percent thermal power from October 1 until December 16 with  
partial loss of feedwater heating and a resulting change in reactor power. Operators lowered
the exception of planned power reductions for routine surveillances and control rod maneuvers.
power about 150 MWth (50 MWe) by inserting one high reactivity-worth control rod. Power
On December 16, 2009, operators attempted to replace a light bulb in the indication circuit for  
increased by 0.59 percent during the loss of feedwater heating transient. By 10:45 a.m. that
the extraction steam check valve A on the 2D feedwater heaters. The light bulb separated with  
same morning, feedwater heaters had been restored and the control rod was withdrawn to
the base remaining in the socket. During the evolution the D heaters tripped, resulting in a  
restore the unit to 100 percent thermal power. The unit remained at 100 percent power for the
partial loss of feedwater heating and a resulting change in reactor power. Operators lowered  
duration of the evaluated period.
power about 150 MWth (50 MWe) by inserting one high reactivity-worth control rod. Power  
1.       REACTOR SAFETY
increased by 0.59 percent during the loss of feedwater heating transient. By 10:45 a.m. that  
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
same morning, feedwater heaters had been restored and the control rod was withdrawn to  
1R01 Adverse Weather Protection (71111.01)
restore the unit to 100 percent thermal power. The unit remained at 100 percent power for the  
  .1     Winter Seasonal Readiness Preparations
duration of the evaluated period.  
    a.   Inspection Scope
1.  
        The inspectors conducted a review of the licensees preparations for winter conditions to
REACTOR SAFETY  
        verify that the plants design features and implementation of procedures were sufficient
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity  
        to protect mitigating systems from the effects of adverse weather. Documentation for
1R01 Adverse Weather Protection (71111.01)  
        selected risk-significant systems was reviewed to ensure that these systems would
.1  
        remain functional when challenged by inclement weather. During the inspection, the
Winter Seasonal Readiness Preparations  
        inspectors focused on plant-specific design features and the licensees procedures used
a.  
        to mitigate or respond to adverse weather conditions. Additionally, the inspectors
Inspection Scope  
        reviewed the Updated Final Safety Analysis Report (UFSAR) and performance
The inspectors conducted a review of the licensees preparations for winter conditions to  
        requirements for systems selected for inspection, and verified that operator actions were
verify that the plants design features and implementation of procedures were sufficient  
        appropriate as specified by plant-specific procedures. Cold weather protection, such as
to protect mitigating systems from the effects of adverse weather. Documentation for  
        heat tracing and area heaters, was verified to be in operation where applicable. The
selected risk-significant systems was reviewed to ensure that these systems would  
        inspectors also reviewed corrective action program (CAP) items to verify that the
remain functional when challenged by inclement weather. During the inspection, the  
        licensee was identifying adverse weather issues at an appropriate threshold and
inspectors focused on plant-specific design features and the licensees procedures used  
        entering them into the CAP in accordance with station corrective action procedures.
to mitigate or respond to adverse weather conditions. Additionally, the inspectors  
        Specific documents reviewed during this inspection are listed in the Attachment to this
reviewed the Updated Final Safety Analysis Report (UFSAR) and performance  
        report. The inspectors reviews focused specifically on the following plant systems due
requirements for systems selected for inspection, and verified that operator actions were  
        to their risk significance or susceptibility to cold weather issues:
appropriate as specified by plant-specific procedures. Cold weather protection, such as  
                                                      4                                  Enclosure
heat tracing and area heaters, was verified to be in operation where applicable. The  
inspectors also reviewed corrective action program (CAP) items to verify that the  
licensee was identifying adverse weather issues at an appropriate threshold and  
entering them into the CAP in accordance with station corrective action procedures.
Specific documents reviewed during this inspection are listed in the Attachment to this  
report. The inspectors reviews focused specifically on the following plant systems due  
to their risk significance or susceptibility to cold weather issues:  


      *       heating steam, and
      *       circulating water/de-icing valve.
      This inspection constituted one winter seasonal readiness preparations sample as
5
      defined in Inspection Procedure (IP) 71111.01-05.
Enclosure
  b. Findings
*  
      No findings of significance were identified.
heating steam, and  
1R04 Equipment Alignment (71111.04)
*  
.1   Quarterly Partial System Walkdowns
circulating water/de-icing valve.  
  a. Inspection Scope
This inspection constituted one winter seasonal readiness preparations sample as  
      The inspectors performed partial system walkdowns of the following risk-significant
defined in Inspection Procedure (IP) 71111.01-05.  
      systems:
b.  
      *       1/2 B diesel driven fire pump; and
Findings  
      *       Unit 1 emergency diesel generator and diesel generator cooling water pump.
No findings of significance were identified.  
      The inspectors selected these systems based on their risk significance relative to the
1R04 Equipment Alignment (71111.04)  
      Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted
.1  
      to identify any discrepancies that could impact the function of the system, and, therefore,
Quarterly Partial System Walkdowns  
      potentially increase risk. The inspectors reviewed applicable operating procedures,
a.  
      system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work
Inspection Scope  
      orders (WOs), condition reports, and the impact of ongoing work activities on redundant
The inspectors performed partial system walkdowns of the following risk-significant  
      trains of equipment in order to identify conditions that could have rendered the systems
systems:  
      incapable of performing their intended functions. The inspectors also walked down
*  
      accessible portions of the systems to verify system components and support equipment
1/2 B diesel driven fire pump; and  
      were aligned correctly and operable. The inspectors examined the material condition of
*  
      the components and observed operating parameters of equipment to verify that there
Unit 1 emergency diesel generator and diesel generator cooling water pump.  
      were no obvious deficiencies. The inspectors also verified that the licensee had properly
The inspectors selected these systems based on their risk significance relative to the  
      identified and resolved equipment alignment problems that could cause initiating events
Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted  
      or impact the capability of mitigating systems or barriers and entered them into the CAP
to identify any discrepancies that could impact the function of the system, and, therefore,  
      with the appropriate significance characterization. Documents reviewed are listed in the
potentially increase risk. The inspectors reviewed applicable operating procedures,  
      Attachment to this report.
system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work  
      These activities constituted two partial system walkdown samples as defined in
orders (WOs), condition reports, and the impact of ongoing work activities on redundant  
      IP 71111.04-05.
trains of equipment in order to identify conditions that could have rendered the systems  
  b. Findings
incapable of performing their intended functions. The inspectors also walked down  
      No findings of significance were identified.
accessible portions of the systems to verify system components and support equipment  
                                                5                                    Enclosure
were aligned correctly and operable. The inspectors examined the material condition of  
the components and observed operating parameters of equipment to verify that there  
were no obvious deficiencies. The inspectors also verified that the licensee had properly  
identified and resolved equipment alignment problems that could cause initiating events  
or impact the capability of mitigating systems or barriers and entered them into the CAP  
with the appropriate significance characterization. Documents reviewed are listed in the  
Attachment to this report.  
These activities constituted two partial system walkdown samples as defined in  
IP 71111.04-05.  
b.  
Findings  
No findings of significance were identified.  


  .2   Semi-Annual Complete System Walkdown
   
  a. Inspection Scope
      On November 5, 2009, the inspectors performed a complete system alignment
6
      inspection of the Unit 2 emergency diesel generator to verify the functional capability of
Enclosure
      the system. This system was selected because it was considered both safety significant
.2  
      and risk significant in the licensees probabilistic risk assessment. The inspectors
Semi-Annual Complete System Walkdown  
      walked down the system to review mechanical and electrical equipment lineups;
a.  
      electrical power availability; system pressure and temperature indications, as
Inspection Scope  
      appropriate; component labeling; component lubrication; component and equipment
On November 5, 2009, the inspectors performed a complete system alignment  
      cooling; hangers and supports; operability of support systems; and to ensure that
inspection of the Unit 2 emergency diesel generator to verify the functional capability of  
      ancillary equipment or debris did not interfere with equipment operation. A review of a
the system. This system was selected because it was considered both safety significant  
      sample of past and outstanding work orders was performed to determine whether any
and risk significant in the licensees probabilistic risk assessment. The inspectors  
      deficiencies significantly affected the system function. In addition, the inspectors
walked down the system to review mechanical and electrical equipment lineups;  
      reviewed the CAP database to ensure that system equipment alignment problems were
electrical power availability; system pressure and temperature indications, as  
      being identified and appropriately resolved. Documents reviewed are listed in the
appropriate; component labeling; component lubrication; component and equipment  
      Attachment to this report.
cooling; hangers and supports; operability of support systems; and to ensure that  
      These activities constituted one complete system walkdown sample as defined in
ancillary equipment or debris did not interfere with equipment operation. A review of a  
      IP 71111.04-05.
sample of past and outstanding work orders was performed to determine whether any  
  b. Findings
deficiencies significantly affected the system function. In addition, the inspectors  
      No findings of significance were identified.
reviewed the CAP database to ensure that system equipment alignment problems were  
1R05 Fire Protection (71111.05)
being identified and appropriately resolved. Documents reviewed are listed in the  
.1   Routine Resident Inspector Tours (71111.05Q)
Attachment to this report.  
  a. Inspection Scope
These activities constituted one complete system walkdown sample as defined in  
      The inspectors conducted fire protection walkdowns which were focused on availability,
IP 71111.04-05.  
      accessibility, and the condition of firefighting equipment in the following risk-significant
b.  
      plant areas:
Findings  
      *       Unit 2 Reactor Bldg. El. 5540, NW Corner Room - 2A Core Spray, Fire Zone
No findings of significance were identified.  
              11.3.3;
1R05 Fire Protection (71111.05)  
      *       Unit 1 Turbine Bldg. El. 5950, Diesel Generator, Fire Zone 9.1;
.1  
      *       Unit 1 Turbine Bldg. El. 5950, Reactor Feed Pumps, Fire Zone 8.2.6.A;
Routine Resident Inspector Tours (71111.05Q)  
      *       Crib House Bldg. El. 5598, Basement, Fire Zone 11.4.A; and
a.  
      *       Crib House Bldg. El. 5950, Ground Floor/Service Water Pumps, Fire Zone
Inspection Scope  
              11.4.B.
The inspectors conducted fire protection walkdowns which were focused on availability,  
      The inspectors reviewed areas to assess if the licensee had implemented a fire
accessibility, and the condition of firefighting equipment in the following risk-significant  
      protection program that adequately controlled combustibles and ignition sources within
plant areas:  
      the plant, effectively maintained fire detection and suppression capability, maintained
*  
      passive fire protection features in good material condition, and implemented adequate
Unit 2 Reactor Bldg. El. 5540, NW Corner Room - 2A Core Spray, Fire Zone  
      compensatory measures for out-of-service, degraded or inoperable fire protection
11.3.3;  
      equipment, systems, or features in accordance with the licensees fire plan.
*  
      The inspectors selected fire areas based on their overall contribution to internal fire risk
Unit 1 Turbine Bldg. El. 5950, Diesel Generator, Fire Zone 9.1;  
                                                  6                                      Enclosure
*  
Unit 1 Turbine Bldg. El. 5950, Reactor Feed Pumps, Fire Zone 8.2.6.A;  
*  
Crib House Bldg. El. 5598, Basement, Fire Zone 11.4.A; and  
*  
Crib House Bldg. El. 5950, Ground Floor/Service Water Pumps, Fire Zone  
11.4.B.  
The inspectors reviewed areas to assess if the licensee had implemented a fire  
protection program that adequately controlled combustibles and ignition sources within  
the plant, effectively maintained fire detection and suppression capability, maintained  
passive fire protection features in good material condition, and implemented adequate  
compensatory measures for out-of-service, degraded or inoperable fire protection  
equipment, systems, or features in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk  


      as documented in the plants Individual Plant Examination of External Events with later
      additional insights, their potential to impact equipment which could initiate or mitigate a
      plant transient, or their impact on the plants ability to respond to a security event.
7
      Using the documents listed in the Attachment to this report, the inspectors verified that
Enclosure
      fire hoses and extinguishers were in their designated locations and available for
as documented in the plants Individual Plant Examination of External Events with later  
      immediate use; that fire detectors and sprinklers were unobstructed; that transient
additional insights, their potential to impact equipment which could initiate or mitigate a  
      material loading was within the analyzed limits; and fire doors, dampers, and penetration
plant transient, or their impact on the plants ability to respond to a security event.
      seals appeared to be in satisfactory condition. The inspectors also verified that minor
Using the documents listed in the Attachment to this report, the inspectors verified that  
      issues identified during the inspection were entered into the licensees CAP.
fire hoses and extinguishers were in their designated locations and available for  
      Documents reviewed are listed in the Attachment to this report.
immediate use; that fire detectors and sprinklers were unobstructed; that transient  
      These activities constituted five quarterly fire protection inspection samples as defined in
material loading was within the analyzed limits; and fire doors, dampers, and penetration  
      IP 71111.05-05.
seals appeared to be in satisfactory condition. The inspectors also verified that minor  
  b. Findings
issues identified during the inspection were entered into the licensees CAP.
      No findings of significance were identified.
Documents reviewed are listed in the Attachment to this report.  
1R11 Licensed Operator Requalification Program (71111.11)
These activities constituted five quarterly fire protection inspection samples as defined in  
.1   Resident Inspector Quarterly Review (71111.11Q)
IP 71111.05-05.  
  a. Inspection Scope
b.  
      On November 4, 2009, the inspectors observed licensed operator continuing training to
Findings  
      verify that operator performance was adequate, evaluators were identifying and
No findings of significance were identified.  
      documenting crew performance problems, and training was being conducted in
1R11 Licensed Operator Requalification Program (71111.11)  
      accordance with licensee procedures. The inspectors evaluated the following areas:
.1  
      *       licensed operator performance;
Resident Inspector Quarterly Review (71111.11Q)  
      *       crews communications and accuracy of documentation;
a.  
      *       ability to take timely actions in the conservative direction;
Inspection Scope  
      *       correct use and implementation of abnormal and emergency procedures;
On November 4, 2009, the inspectors observed licensed operator continuing training to  
      *       control board manipulations;
verify that operator performance was adequate, evaluators were identifying and  
      *       oversight and direction from supervisors; and
documenting crew performance problems, and training was being conducted in  
      *       ability to identify and implement Emergency Plan actions and notifications.
accordance with licensee procedures. The inspectors evaluated the following areas:  
      The crews performance in these areas was compared to pre-established operator action
*  
      expectations and lesson objectives. Documents reviewed are listed in the Attachment to
licensed operator performance;  
      this report.
*  
      This inspection constituted one quarterly licensed operator requalification program
crews communications and accuracy of documentation;  
      sample as defined in IP 71111.11.
*  
  b. Findings
ability to take timely actions in the conservative direction;  
      No findings of significance were identified.
*  
                                                  7                                      Enclosure
correct use and implementation of abnormal and emergency procedures;  
*  
control board manipulations;  
*  
oversight and direction from supervisors; and  
*  
ability to identify and implement Emergency Plan actions and notifications.  
The crews performance in these areas was compared to pre-established operator action  
expectations and lesson objectives. Documents reviewed are listed in the Attachment to  
this report.  
This inspection constituted one quarterly licensed operator requalification program  
sample as defined in IP 71111.11.  
b.  
Findings  
No findings of significance were identified.  


.2   Facility Operating History (71111.11B)
  a. Inspection Scope
    The inspectors reviewed the plants operating history from January 2007 through
8
    September 2009 to identify operating experience that was expected to be addressed by
Enclosure
    the Licensed Operator Requalification Training (LORT) program. The inspectors verified
.2  
    that the identified operating experience had been addressed by the facility licensee in
Facility Operating History (71111.11B)  
    accordance with the stations approved Systems Approach to Training (SAT) program to
a.  
    satisfy the requirements of 10 CFR 55.59(c). The documents reviewed during this
Inspection Scope  
    inspection are listed in the Attachment to this report.
The inspectors reviewed the plants operating history from January 2007 through  
  b. Findings
September 2009 to identify operating experience that was expected to be addressed by  
    No findings of significance were identified.
the Licensed Operator Requalification Training (LORT) program. The inspectors verified  
.3   Licensee Requalification Examinations
that the identified operating experience had been addressed by the facility licensee in  
  a. Inspection Scope
accordance with the stations approved Systems Approach to Training (SAT) program to  
    The inspectors performed an inspection of the licensees LORT test/examination
satisfy the requirements of 10 CFR 55.59(c). The documents reviewed during this  
    program for compliance with the stations SAT program which would satisfy the
inspection are listed in the Attachment to this report.  
    requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material
b.  
    consisted of two operating tests, each containing two dynamic simulator scenarios and
Findings  
    five job performance measures (JPMs). The two biennial written examinations reviewed
No findings of significance were identified.  
    consisted of two parts. Each written examination contained 30 questions consisting of
.3  
    15 written exam questions and 15 static exam questions. The inspectors reviewed the
Licensee Requalification Examinations  
    annual requalification operating test and biennial written examination material to
a.  
    evaluate general quality, construction, and difficulty level. The inspectors assessed the
Inspection Scope  
    level of examination material duplication from week to week during the current year
The inspectors performed an inspection of the licensees LORT test/examination  
    operating test. The examiners assessed the amount of written examination material
program for compliance with the stations SAT program which would satisfy the  
    duplication from week to week for the biennial written examination administered in
requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material  
    calendar year 2009. The inspectors reviewed the methodology for developing the
consisted of two operating tests, each containing two dynamic simulator scenarios and  
    examinations, including the LORT program 2-year sample plan, probabilistic risk
five job performance measures (JPMs). The two biennial written examinations reviewed  
    assessment insights, previously identified operator performance deficiencies, and plant
consisted of two parts. Each written examination contained 30 questions consisting of  
    modifications. The documents reviewed during this inspection are listed in the
15 written exam questions and 15 static exam questions. The inspectors reviewed the  
    Attachment to this report.
annual requalification operating test and biennial written examination material to  
  b. Findings
evaluate general quality, construction, and difficulty level. The inspectors assessed the  
    No findings of significance were identified.
level of examination material duplication from week to week during the current year  
.4   Licensee Administration of Requalification Examinations
operating test. The examiners assessed the amount of written examination material  
  a. Inspection Scope
duplication from week to week for the biennial written examination administered in  
    The inspectors observed the administration of a requalification operating test to
calendar year 2009. The inspectors reviewed the methodology for developing the  
    assess the licensees effectiveness in conducting the test to ensure compliance with
examinations, including the LORT program 2-year sample plan, probabilistic risk  
    10 CRF 55.59(c)(4). The inspectors evaluated the performance of one operating crew in
assessment insights, previously identified operator performance deficiencies, and plant  
    parallel with the facility evaluators during four dynamic simulator scenarios and
modifications. The documents reviewed during this inspection are listed in the  
    evaluated various licensed crew members concurrently with facility evaluators during the
Attachment to this report.  
                                                8                                    Enclosure
b.  
Findings  
No findings of significance were identified.  
.4  
Licensee Administration of Requalification Examinations  
a.  
Inspection Scope  
The inspectors observed the administration of a requalification operating test to  
assess the licensees effectiveness in conducting the test to ensure compliance with  
10 CRF 55.59(c)(4). The inspectors evaluated the performance of one operating crew in  
parallel with the facility evaluators during four dynamic simulator scenarios and  
evaluated various licensed crew members concurrently with facility evaluators during the  


    administration of several JPMs. The inspectors assessed the facility evaluators ability
    to determine adequate crew and individual performance using objective, measurable
    standards. The inspectors observed the training staff personnel administer the operating
9
    test, including conducting pre-examination briefings, evaluations of operator
Enclosure
    performance, and individual and crew evaluations upon completion of the operating test.
administration of several JPMs. The inspectors assessed the facility evaluators ability  
    The inspectors evaluated the ability of the simulator to support the examinations.
to determine adequate crew and individual performance using objective, measurable  
  b. Findings
standards. The inspectors observed the training staff personnel administer the operating  
    No findings of significance were identified.
test, including conducting pre-examination briefings, evaluations of operator  
.5   Examination Security
performance, and individual and crew evaluations upon completion of the operating test.
  a. Inspection Scope
The inspectors evaluated the ability of the simulator to support the examinations.  
    The inspectors observed and reviewed the licensees overall licensed operator
b.  
    requalification examination security program related to examination physical security
Findings  
    (e.g., access restrictions and simulator considerations) and integrity (e.g., predictability
No findings of significance were identified.  
    and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.
.5  
    The inspectors also reviewed the facility licensees examination security procedure and
Examination Security  
    the implementation of security and integrity measures (e.g., security agreements,
a.  
    sampling criteria, bank use, and test item repetition) throughout the examination
Inspection Scope  
    process. No examination security compromises occurred during these observations.
The inspectors observed and reviewed the licensees overall licensed operator  
    The documents reviewed during this inspection are listed in the Attachment to this
requalification examination security program related to examination physical security  
    report.
(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability  
  b. Findings
and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.
    No findings of significance were identified.
The inspectors also reviewed the facility licensees examination security procedure and  
.6   Licensee Training Feedback System
the implementation of security and integrity measures (e.g., security agreements,  
  a. Inspection Scope
sampling criteria, bank use, and test item repetition) throughout the examination  
    The inspectors assessed the methods and effectiveness of the licensees processes for
process. No examination security compromises occurred during these observations.
    revising and maintaining its LORT program up-to-date, including the use of feedback
The documents reviewed during this inspection are listed in the Attachment to this  
    from plant events and industry experience information. The inspectors reviewed the
report.  
    licensees quality assurance oversight activities, including licensee training department
b.  
    self-assessment reports. The inspectors evaluated the licensees ability to assess the
Findings  
    effectiveness of its LORT program and their ability to implement appropriate corrective
No findings of significance were identified.  
    actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and
.6  
    the licensees SAT based program. The documents reviewed during this inspection are
Licensee Training Feedback System  
    listed in the Attachment to this report.
a.  
  b. Findings
Inspection Scope  
    No findings of significance were identified.
The inspectors assessed the methods and effectiveness of the licensees processes for  
                                              9                                        Enclosure
revising and maintaining its LORT program up-to-date, including the use of feedback  
from plant events and industry experience information. The inspectors reviewed the  
licensees quality assurance oversight activities, including licensee training department  
self-assessment reports. The inspectors evaluated the licensees ability to assess the  
effectiveness of its LORT program and their ability to implement appropriate corrective  
actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and  
the licensees SAT based program. The documents reviewed during this inspection are  
listed in the Attachment to this report.  
b.  
Findings  
No findings of significance were identified.  


.7   Licensee Remedial Training Program
  a. Inspection Scope
    The inspectors assessed the adequacy and effectiveness of the remedial training
10
    conducted since the previous biennial requalification examinations and the training from
Enclosure
    the current examination cycle to ensure that they addressed weaknesses in licensed
.7  
    operator or crew performance identified during training and plant operations. The
Licensee Remedial Training Program  
    inspectors reviewed remedial training procedures and individual remedial training plans.
a.  
    This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to
Inspection Scope  
    the licensees SAT based program. The documents reviewed during this inspection are
The inspectors assessed the adequacy and effectiveness of the remedial training  
    listed in the Attachment to this report.
conducted since the previous biennial requalification examinations and the training from  
  b. Findings
the current examination cycle to ensure that they addressed weaknesses in licensed  
    No findings of significance were identified.
operator or crew performance identified during training and plant operations. The  
.8   Conformance With Operator License Conditions
inspectors reviewed remedial training procedures and individual remedial training plans.
  a. Inspection Scope
This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to  
    The inspectors reviewed the facility and individual operator licensees' conformance with
the licensees SAT based program. The documents reviewed during this inspection are  
    the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's
listed in the Attachment to this report.  
    program for maintaining active operator licenses and to assess compliance with
b.  
    10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the
Findings  
    process for tracking on-shift hours for licensed operators and which control room
No findings of significance were identified.  
    positions were granted watch-standing credit for maintaining active operator licenses.
.8  
    The inspectors reviewed the facility licensee's LORT program to assess compliance with
Conformance With Operator License Conditions  
    the requalification program requirements as described by 10 CFR 55.59(c). Additionally,
a.  
    medical records for 10 licensed operators were reviewed for compliance with
Inspection Scope  
    10 CFR 55.53(I). The documents reviewed during this inspection are listed in the
The inspectors reviewed the facility and individual operator licensees' conformance with  
    Attachment to this report.
the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's  
  b. Findings
program for maintaining active operator licenses and to assess compliance with  
    No findings of significance were identified.
10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the  
.9   Annual Operating Test Results and Biennial Written Examination Results (71111.11B)
process for tracking on-shift hours for licensed operators and which control room  
  a. Inspection Scope
positions were granted watch-standing credit for maintaining active operator licenses.
    The inspectors reviewed the overall pass/fail results of the individual JPM operating
The inspectors reviewed the facility licensee's LORT program to assess compliance with  
    tests, the simulator operating tests, and the biennial written examination (required to be
the requalification program requirements as described by 10 CFR 55.59(c). Additionally,  
    given per 10 CFR 55.59(a)(2)) administered by the licensee from September 2009
medical records for 10 licensed operators were reviewed for compliance with  
    through November 2009 as part of the licensees operator licensing requalification cycle.
10 CFR 55.53(I). The documents reviewed during this inspection are listed in the  
    These results were compared to the thresholds established in Inspection Manual
Attachment to this report.  
    Chapter 0609, Appendix I, Licensed Operator Requalification Significance
b.  
    Determination Process (SDP)." The evaluations were also performed to determine if the
Findings  
    licensee effectively implemented operator requalification guidelines established in
No findings of significance were identified.  
    NUREG 1021, Operator Licensing Examination Standards for Power Reactors, and
.9  
                                              10                                      Enclosure
Annual Operating Test Results and Biennial Written Examination Results (71111.11B)  
a.  
Inspection Scope  
The inspectors reviewed the overall pass/fail results of the individual JPM operating  
tests, the simulator operating tests, and the biennial written examination (required to be  
given per 10 CFR 55.59(a)(2)) administered by the licensee from September 2009  
through November 2009 as part of the licensees operator licensing requalification cycle.
These results were compared to the thresholds established in Inspection Manual  
Chapter 0609, Appendix I, Licensed Operator Requalification Significance  
Determination Process (SDP)." The evaluations were also performed to determine if the  
licensee effectively implemented operator requalification guidelines established in  
NUREG 1021, Operator Licensing Examination Standards for Power Reactors, and  


      IP 71111.11, Licensed Operator Requalification Program. The documents reviewed
      during this inspection are listed in the Attachment to this report.
      This inspection constituted one inspection sample as defined in IP 71111.11.
11
  b. Findings
Enclosure
      No findings of significance were identified.
IP 71111.11, Licensed Operator Requalification Program. The documents reviewed  
1R12 Maintenance Effectiveness (71111.12)
during this inspection are listed in the Attachment to this report.  
.1   Routine Quarterly Evaluations (71111.12Q)
This inspection constituted one inspection sample as defined in IP 71111.11.  
  a. Inspection Scope
b.  
      The inspectors evaluated degraded performance issues involving the following
Findings  
      risk-significant systems:
No findings of significance were identified.  
      *       Z2900; Safe Shutdown Makeup Pump, and
1R12 Maintenance Effectiveness (71111.12)  
      *       Z4700; Instrument Air.
.1  
      The inspectors reviewed events such as where ineffective equipment maintenance had
Routine Quarterly Evaluations (71111.12Q)  
      resulted in valid or invalid automatic actuations of engineered safeguards systems and
a.  
      independently verified the licensee's actions to address system performance or condition
Inspection Scope  
      problems in terms of the following:
The inspectors evaluated degraded performance issues involving the following  
      *       implementing appropriate work practices;
risk-significant systems:  
      *       identifying and addressing common cause failures;
*  
      *       scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
Z2900; Safe Shutdown Makeup Pump, and  
      *       characterizing system reliability issues for performance;
*  
      *       charging unavailability for performance;
Z4700; Instrument Air.  
      *       trending key parameters for condition monitoring;
The inspectors reviewed events such as where ineffective equipment maintenance had  
      *       ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
resulted in valid or invalid automatic actuations of engineered safeguards systems and  
      *       verifying appropriate performance criteria for SSCs/functions classified as (a)(2)
independently verified the licensee's actions to address system performance or condition  
              or appropriate and adequate goals and corrective actions for systems classified
problems in terms of the following:  
              as (a)(1).
*  
      The inspectors assessed performance issues with respect to the reliability, availability,
implementing appropriate work practices;  
      and condition monitoring of the system. In addition, the inspectors verified maintenance
*  
      effectiveness issues were entered into the CAP with the appropriate significance
identifying and addressing common cause failures;  
      characterization. Documents reviewed are listed in the Attachment to this report.
*  
      This inspection constituted two quarterly maintenance effectiveness samples as defined
scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;  
      in IP 71111.12-05.
*  
  b. Findings
characterizing system reliability issues for performance;  
      No findings of significance were identified.
*  
                                                11                                      Enclosure
charging unavailability for performance;  
*  
trending key parameters for condition monitoring;  
*  
ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and  
*  
verifying appropriate performance criteria for SSCs/functions classified as (a)(2)  
or appropriate and adequate goals and corrective actions for systems classified  
as (a)(1).  
The inspectors assessed performance issues with respect to the reliability, availability,  
and condition monitoring of the system. In addition, the inspectors verified maintenance  
effectiveness issues were entered into the CAP with the appropriate significance  
characterization. Documents reviewed are listed in the Attachment to this report.  
This inspection constituted two quarterly maintenance effectiveness samples as defined  
in IP 71111.12-05.  
b.  
Findings  
No findings of significance were identified.  


1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
.1   Maintenance Risk Assessments and Emergent Work Control
  a. Inspection Scope
12
      The inspectors reviewed the licensee's evaluation and management of plant risk for the
Enclosure
      maintenance and emergent work activities affecting risk-significant and safety-related
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)  
      equipment listed below to verify that the appropriate risk assessments were performed
.1  
      prior to removing equipment for work:
Maintenance Risk Assessments and Emergent Work Control  
      *       Work Week 45 - 1A residual heat removal (RHR) room cooler, 1A RHR service
a.  
              water (RHRSW) loop, 1B RHR seal cooler, 1-1001-16A boroscope and Votes
Inspection Scope  
              testing, 1-1001-37A MOV equipment qualification inspection; and
The inspectors reviewed the licensee's evaluation and management of plant risk for the  
      *       Work Week 51 - Unit 1 250 Vdc battery reconfiguration using Unit 1 125 Vdc
maintenance and emergent work activities affecting risk-significant and safety-related  
              alternate battery with emergent Unit 2 125 Vdc battery low specific gravity
equipment listed below to verify that the appropriate risk assessments were performed  
              problems, 2A RHR loop and 2B RHRSW pump unavailability.
prior to removing equipment for work:  
      These activities were selected based on their potential risk significance relative to the
*  
      Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that
Work Week 45 - 1A residual heat removal (RHR) room cooler, 1A RHR service  
      risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate
water (RHRSW) loop, 1B RHR seal cooler, 1-1001-16A boroscope and Votes  
      and complete. When emergent work was performed, the inspectors verified that the
testing, 1-1001-37A MOV equipment qualification inspection; and  
      plant risk was promptly reassessed and managed. The inspectors reviewed the scope
*  
      of maintenance work, discussed the results of the assessment with the licensee's
Work Week 51 - Unit 1 250 Vdc battery reconfiguration using Unit 1 125 Vdc  
      probabilistic risk analyst or shift technical advisor, and verified plant conditions were
alternate battery with emergent Unit 2 125 Vdc battery low specific gravity  
      consistent with the risk assessment. The inspectors also reviewed TS requirements and
problems, 2A RHR loop and 2B RHRSW pump unavailability.  
      walked down portions of redundant safety systems, when applicable, to verify risk
These activities were selected based on their potential risk significance relative to the  
      analysis assumptions were valid and applicable requirements were met.
Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that  
      These maintenance risk assessments and emergent work control activities constituted
risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate  
      two samples as defined in IP 71111.13-05.
and complete. When emergent work was performed, the inspectors verified that the  
  b. Findings
plant risk was promptly reassessed and managed. The inspectors reviewed the scope  
      No findings of significance were identified.
of maintenance work, discussed the results of the assessment with the licensee's  
1R15 Operability Evaluations (71111.15)
probabilistic risk analyst or shift technical advisor, and verified plant conditions were  
.1   Operability Evaluations
consistent with the risk assessment. The inspectors also reviewed TS requirements and  
  a. Inspection Scope
walked down portions of redundant safety systems, when applicable, to verify risk  
      The inspectors reviewed the following issues:
analysis assumptions were valid and applicable requirements were met.  
      *       IR 987904: 1A RHR Room Cooler Tube Sheet Has Pitting, and
These maintenance risk assessments and emergent work control activities constituted  
      *       IR 994823: TS SR 3.8.4.8 Frequency Not Met.
two samples as defined in IP 71111.13-05.  
      The inspectors selected these potential operability issues based on the risk significance
b.  
      of the associated components and systems. The inspectors evaluated the technical
Findings  
      adequacy of the evaluations to ensure that TS operability was properly justified and the
No findings of significance were identified.  
      subject component or system remained available such that no unrecognized increase in
1R15 Operability Evaluations (71111.15)  
                                                12                                        Enclosure
.1  
Operability Evaluations  
a.  
Inspection Scope  
The inspectors reviewed the following issues:  
*  
IR 987904: 1A RHR Room Cooler Tube Sheet Has Pitting, and  
*  
IR 994823: TS SR 3.8.4.8 Frequency Not Met.  
The inspectors selected these potential operability issues based on the risk significance  
of the associated components and systems. The inspectors evaluated the technical  
adequacy of the evaluations to ensure that TS operability was properly justified and the  
subject component or system remained available such that no unrecognized increase in  


      risk occurred. The inspectors compared the operability and design criteria in the
      appropriate sections of the TS and UFSAR to the licensees evaluations to determine
      whether the components or systems were operable. Where compensatory measures
13
      were required to maintain operability, the inspectors determined whether the measures
Enclosure
      in place would function as intended and were properly controlled. The inspectors
risk occurred. The inspectors compared the operability and design criteria in the  
      determined, where appropriate, compliance with bounding limitations associated with the
appropriate sections of the TS and UFSAR to the licensees evaluations to determine  
      evaluations. Additionally, the inspectors also reviewed a sampling of corrective action
whether the components or systems were operable. Where compensatory measures  
      documents to verify that the licensee was identifying and correcting any deficiencies
were required to maintain operability, the inspectors determined whether the measures  
      associated with operability evaluations. Documents reviewed are listed in the
in place would function as intended and were properly controlled. The inspectors  
      Attachment to this report.
determined, where appropriate, compliance with bounding limitations associated with the  
      This operability inspection constituted two samples as defined in IP 71111.15-05.
evaluations. Additionally, the inspectors also reviewed a sampling of corrective action  
  b. Findings
documents to verify that the licensee was identifying and correcting any deficiencies  
      No findings of significance were identified.
associated with operability evaluations. Documents reviewed are listed in the  
1R19 Post-Maintenance Testing (71111.19)
Attachment to this report.  
.1   Post-Maintenance Testing
This operability inspection constituted two samples as defined in IP 71111.15-05.  
  a. Inspection Scope
b.  
      The inspectors reviewed the following post-maintenance activities to verify that
Findings  
      procedures and test activities were adequate to ensure system operability and functional
No findings of significance were identified.  
      capability:
1R19 Post-Maintenance Testing (71111.19)  
      *       WO 1121775, 250 Vdc Battery Charger #2 4-Hour Load Test;
.1  
      *       WO 1261246, Replace Battery Changeover Relay R12 EC 376690;
Post-Maintenance Testing  
      *       QCMMS 4100-33, 1/2-4101B Diesel Driven Fire Pump Annual Capacity Test;
a.  
      *       WO 1130535, OP PMT Filter B Train Control Room HVAC; and
Inspection Scope  
      *       WO1107582, Replace Unit 2 DGCWP Alternate Feed Contactor.
The inspectors reviewed the following post-maintenance activities to verify that  
      These activities were selected based upon the structure, system, or component's ability
procedures and test activities were adequate to ensure system operability and functional  
      to impact risk. The inspectors evaluated these activities for the following (as applicable):
capability:  
      the effect of testing on the plant had been adequately addressed; testing was adequate
*  
      for the maintenance performed; acceptance criteria were clear and demonstrated
WO 1121775, 250 Vdc Battery Charger #2 4-Hour Load Test;
      operational readiness; test instrumentation was appropriate; tests were performed as
*  
      written in accordance with properly reviewed and approved procedures; equipment was
WO 1261246, Replace Battery Changeover Relay R12 EC 376690;  
      returned to its operational status following testing (temporary modifications or jumpers
*  
      required for test performance were properly removed after test completion); and test
QCMMS 4100-33, 1/2-4101B Diesel Driven Fire Pump Annual Capacity Test;  
      documentation was properly evaluated. The inspectors evaluated the activities against
*  
      TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various
WO 1130535, OP PMT Filter B Train Control Room HVAC; and  
      NRC generic communications to ensure that the test results adequately ensured that the
*  
      equipment met the licensing basis and design requirements. In addition, the inspectors
WO1107582, Replace Unit 2 DGCWP Alternate Feed Contactor.  
      reviewed corrective action documents associated with post-maintenance tests to
These activities were selected based upon the structure, system, or component's ability  
      determine whether the licensee was identifying problems and entering them in the CAP
to impact risk. The inspectors evaluated these activities for the following (as applicable):  
      and that the problems were being corrected commensurate with their importance to
the effect of testing on the plant had been adequately addressed; testing was adequate  
      safety. Documents reviewed are listed in the Attachment to this report.
for the maintenance performed; acceptance criteria were clear and demonstrated  
                                                13                                      Enclosure
operational readiness; test instrumentation was appropriate; tests were performed as  
written in accordance with properly reviewed and approved procedures; equipment was  
returned to its operational status following testing (temporary modifications or jumpers  
required for test performance were properly removed after test completion); and test  
documentation was properly evaluated. The inspectors evaluated the activities against  
TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various  
NRC generic communications to ensure that the test results adequately ensured that the  
equipment met the licensing basis and design requirements. In addition, the inspectors  
reviewed corrective action documents associated with post-maintenance tests to  
determine whether the licensee was identifying problems and entering them in the CAP  
and that the problems were being corrected commensurate with their importance to  
safety. Documents reviewed are listed in the Attachment to this report.  


      This inspection constituted five post-maintenance testing samples as defined in
      IP 71111.19-05.
  b. Findings
14
      No findings of significance were identified.
Enclosure
1R22 Surveillance Testing (71111.22)
This inspection constituted five post-maintenance testing samples as defined in  
.1   Surveillance Testing
IP 71111.19-05.  
  a. Inspection Scope
b.  
      The inspectors reviewed the test results for the following activities to determine whether
Findings  
      risk-significant systems and equipment were capable of performing their intended safety
No findings of significance were identified.  
      function and to verify testing was conducted in accordance with applicable procedural
1R22 Surveillance Testing (71111.22)  
      and TS requirements:
.1  
      *       QCOS 1400-01, 2A Core Spray Pump Performance Test (IST);
Surveillance Testing  
      *       QCIS 0300-02, Unit 1 Division 1 Scram Discharge Volume Calibration and
a.  
              Functional Test (Routine);
Inspection Scope  
      *       QCOS 7500-05, 1/2 B Standby Gas Treatment Operability Test (Routine);
The inspectors reviewed the test results for the following activities to determine whether  
      *       QCOS 1600-07, Reactor Coolant Leakage in the Drywell (RCS);
risk-significant systems and equipment were capable of performing their intended safety  
      *       QCEMS 0230-11, Modified Performance Test of Unit 1(2) 125 Vdc Normal or
function and to verify testing was conducted in accordance with applicable procedural  
              Alternate Battery (Routine); and
and TS requirements:  
      *       QCOS 6900-14, Station Battery Allowable Value Verification Surveillance
*  
              (Routine).
QCOS 1400-01, 2A Core Spray Pump Performance Test (IST);  
      The inspectors observed in plant activities and reviewed procedures and associated
*  
      records to determine the following:
QCIS 0300-02, Unit 1 Division 1 Scram Discharge Volume Calibration and  
      *       did preconditioning occur;
Functional Test (Routine);  
      *       were the effects of the testing adequately addressed by control room personnel
*  
              or engineers prior to the commencement of the testing;
QCOS 7500-05, 1/2 B Standby Gas Treatment Operability Test (Routine);  
      *       were acceptance criteria clearly stated, demonstrated operational readiness, and
*  
              consistent with the system design basis;
QCOS 1600-07, Reactor Coolant Leakage in the Drywell (RCS);  
      *       plant equipment calibration was correct, accurate, and properly documented;
*  
      *       as-left setpoints were within required ranges, and the calibration frequency were
QCEMS 0230-11, Modified Performance Test of Unit 1(2) 125 Vdc Normal or  
              in accordance with TS, the UFSAR, procedures, and applicable commitments;
Alternate Battery (Routine); and
      *       measuring and test equipment calibration was current;
*  
      *       test equipment was used within the required range and accuracy, applicable
QCOS 6900-14, Station Battery Allowable Value Verification Surveillance  
              prerequisites described in the test procedures were satisfied;
(Routine).  
      *       test frequencies met TS requirements to demonstrate operability and reliability;
The inspectors observed in plant activities and reviewed procedures and associated  
              tests were performed in accordance with the test procedures and other
records to determine the following:  
              applicable procedures, jumpers and lifted leads were controlled and restored
*  
              where used;
did preconditioning occur;  
      *       test data and results were accurate, complete, within limits, and valid;
*  
      *       test equipment was removed after testing;
were the effects of the testing adequately addressed by control room personnel  
      *       where applicable for inservice testing activities, testing was performed in
or engineers prior to the commencement of the testing;  
              accordance with the applicable version of Section XI, American Society of
*  
                                              14                                      Enclosure
were acceptance criteria clearly stated, demonstrated operational readiness, and  
consistent with the system design basis;  
*  
plant equipment calibration was correct, accurate, and properly documented;  
*  
as-left setpoints were within required ranges, and the calibration frequency were  
in accordance with TS, the UFSAR, procedures, and applicable commitments;  
*  
measuring and test equipment calibration was current;  
*  
test equipment was used within the required range and accuracy, applicable  
prerequisites described in the test procedures were satisfied;  
*  
test frequencies met TS requirements to demonstrate operability and reliability;  
tests were performed in accordance with the test procedures and other  
applicable procedures, jumpers and lifted leads were controlled and restored  
where used;  
*  
test data and results were accurate, complete, within limits, and valid;  
*  
test equipment was removed after testing;  
*  
where applicable for inservice testing activities, testing was performed in  
accordance with the applicable version of Section XI, American Society of  


              Mechanical Engineers code, and reference values were consistent with the
              system design basis;
      *       where applicable, test results not meeting acceptance criteria were addressed
15
              with an adequate operability evaluation or the system or component was
Enclosure
              declared inoperable;
Mechanical Engineers code, and reference values were consistent with the  
      *       where applicable for safety-related instrument control surveillance tests,
system design basis;  
              reference setting data were accurately incorporated in the test procedure;
*  
      *       where applicable, actual conditions encountering high resistance electrical
where applicable, test results not meeting acceptance criteria were addressed  
              contacts were such that the intended safety function could still be accomplished;
with an adequate operability evaluation or the system or component was  
      *       prior procedure changes had not provided an opportunity to identify problems
declared inoperable;  
              encountered during the performance of the surveillance or calibration test;
*  
      *       equipment was returned to a position or status required to support the
where applicable for safety-related instrument control surveillance tests,  
              performance of its safety functions; and
reference setting data were accurately incorporated in the test procedure;  
      *       all problems identified during the testing were appropriately documented and
*  
              dispositioned in the CAP.
where applicable, actual conditions encountering high resistance electrical  
      Documents reviewed are listed in the Attachment to this report.
contacts were such that the intended safety function could still be accomplished;  
      This inspection constituted four routine surveillance testing samples, one inservice
*  
      testing sample, and one reactor coolant system leak detection inspection samples as
prior procedure changes had not provided an opportunity to identify problems  
      defined in IP 71111.22, Sections -02 and -05.
encountered during the performance of the surveillance or calibration test;  
  b. Findings
*  
      No findings of significance were identified.
equipment was returned to a position or status required to support the  
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
performance of its safety functions; and  
.1   Emergency Action Level and Emergency Plan Changes
*  
  a. Inspection Scope
all problems identified during the testing were appropriately documented and  
      Since the last NRC inspection of this program area, Emergency Plan Annex,
dispositioned in the CAP.  
      Revisions 26 and 27 were implemented based on the licensees determination, in
Documents reviewed are listed in the Attachment to this report.  
      accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in
This inspection constituted four routine surveillance testing samples, one inservice  
      effectiveness of the Plan, and that the revised Plan as changed continues to meet the
testing sample, and one reactor coolant system leak detection inspection samples as  
      requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors
defined in IP 71111.22, Sections -02 and -05.  
      conducted a sampling review of the Emergency Plan changes and a review of the
b.  
      Emergency Action Level (EAL) changes to evaluate for potential decreases in
Findings  
      effectiveness of the Plan. However, this review does not constitute formal NRC approval
No findings of significance were identified.  
      of the changes. Therefore, these changes remain subject to future NRC inspection in
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)  
      their entirety.
.1  
      This emergency action level and emergency plan changes inspection constituted one
Emergency Action Level and Emergency Plan Changes  
      sample as defined in IP 71114.04-05.
a.  
                                                15                                    Enclosure
Inspection Scope  
Since the last NRC inspection of this program area, Emergency Plan Annex,  
Revisions 26 and 27 were implemented based on the licensees determination, in  
accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in  
effectiveness of the Plan, and that the revised Plan as changed continues to meet the  
requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors  
conducted a sampling review of the Emergency Plan changes and a review of the  
Emergency Action Level (EAL) changes to evaluate for potential decreases in  
effectiveness of the Plan. However, this review does not constitute formal NRC approval  
of the changes. Therefore, these changes remain subject to future NRC inspection in  
their entirety.  
This emergency action level and emergency plan changes inspection constituted one  
sample as defined in IP 71114.04-05.  


b. Findings
(1) Unresolved Item (URI) 05000254/2009005-01: Changes to EAL HU6 Potentially
    Decrease the Effectiveness of the Plans without Prior NRC Approval
16
    Introduction: The inspectors reviewed changes implemented to the Quad Cities Station
Enclosure
    Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 26, the licensee
b.  
    changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection
Findings  
    within the protected area boundary, by adding two statements. The two changes added
(1) Unresolved Item (URI) 05000254/2009005-01: Changes to EAL HU6 Potentially  
    to the EAL basis stated that if the alarm could not be verified by redundant control room
Decrease the Effectiveness of the Plans without Prior NRC Approval  
    or nearby fire panel indications, notification from the field that a fire exists starts the
Introduction: The inspectors reviewed changes implemented to the Quad Cities Station  
    15-minute classification and fire extinguishment clocks. The second change stated the
Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 26, the licensee  
    15-minute period to extinguish the fire does not start until either the fire alarm is verified
changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection  
    to be valid by additional control room or nearby fire panel instrumentation, or upon
within the protected area boundary, by adding two statements. The two changes added  
    notification of a fire from the field. These statements conflict with the previous
to the EAL basis stated that if the alarm could not be verified by redundant control room  
    Quad Cities Station Annex, Revision 25, basis statements and potentially decrease the
or nearby fire panel indications, notification from the field that a fire exists starts the  
    effectiveness of the Plans.
15-minute classification and fire extinguishment clocks. The second change stated the  
    Description: Quad Cities Station Radiological Emergency Plan Annex, Revision 25,
15-minute period to extinguish the fire does not start until either the fire alarm is verified  
    EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of
to be valid by additional control room or nearby fire panel instrumentation, or upon  
    detection, or explosion, within the protected area boundary." The threshold values for
notification of a fire from the field. These statements conflict with the previous  
    HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of
Quad Cities Station Annex, Revision 25, basis statements and potentially decrease the  
    control room notification or verification of a control room alarm; or 2) Fire outside any
effectiveness of the Plans.  
    Table H2 area with the potential to damage safety systems in any Table H2 area not
Description: Quad Cities Station Radiological Emergency Plan Annex, Revision 25,  
    extinguished within 15 minutes of control room notification or verification of a control
EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of  
    room alarm. Table H2, Vital Areas, were identified as main control room, reactor
detection, or explosion, within the protected area boundary." The threshold values for  
    building, diesel generator rooms, 4 kilovolt switchgear area, battery rooms, B train
HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of  
    control room heating-ventilation and air conditioning, service water pumps, and turbine
control room notification or verification of a control room alarm; or 2) Fire outside any  
    building cable tunnel. The basis defined fire as "combustion characterized by heat and
Table H2 area with the potential to damage safety systems in any Table H2 area not  
    light. Sources of smoke such as slipping drive belts or overheated electrical equipment
extinguished within 15 minutes of control room notification or verification of a control  
    do not constitute fires. Observation of flame is preferred but is not required if large
room alarm. Table H2, Vital Areas, were identified as main control room, reactor  
    quantities of smoke and heat are observed."
building, diesel generator rooms, 4 kilovolt switchgear area, battery rooms, B train  
    The basis for Revision 25, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of
control room heating-ventilation and air conditioning, service water pumps, and turbine  
    this threshold is to address the magnitude and extent of fires that may be potentially
building cable tunnel. The basis defined fire as "combustion characterized by heat and  
    significant precursors to damage to safety systems. As used here, notification is visual
light. Sources of smoke such as slipping drive belts or overheated electrical equipment  
    observation and report by plant personnel or sensor alarm indication. The 15-minute
do not constitute fires. Observation of flame is preferred but is not required if large  
    period begins with a credible notification that a fire is occurring or indication of a valid fire
quantities of smoke and heat are observed."  
    detection system alarm. A verified alarm is assumed to be an indication of a fire unless
    personnel dispatched to the scene disprove the alarm within the 15-minute period.
The basis for Revision 25, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of  
    The report, however, shall not be required to verify the alarm. The intent of the
this threshold is to address the magnitude and extent of fires that may be potentially  
    15-minute period is to size the fire and discriminate against small fires that are readily
significant precursors to damage to safety systems. As used here, notification is visual  
    extinguished (e.g., smoldering waste paper basket, etc.).
observation and report by plant personnel or sensor alarm indication. The 15-minute  
    Revision 26 of the Quad Cities Station Radiological Emergency Plan Annex, changed
period begins with a credible notification that a fire is occurring or indication of a valid fire  
    the threshold basis for EAL HU6 by adding the following two statements: 1)"If the alarm
detection system alarm. A verified alarm is assumed to be an indication of a fire unless  
    cannot be verified by redundant control room or nearby fire panel indications, notification
personnel dispatched to the scene disprove the alarm within the 15-minute period.
    from the field that a fire exists starts the 15-minute classification and fire extinguishment
The report, however, shall not be required to verify the alarm. The intent of the  
    clocks," and 2) "The 15-minute period to extinguish the fire does not start until either the
15-minute period is to size the fire and discriminate against small fires that are readily  
    fire alarm is verified to be valid by utilization of additional control room or nearby fire
extinguished (e.g., smoldering waste paper basket, etc.).  
    panel instrumentation, or upon notification of a fire from the field."
                                                16                                        Enclosure
Revision 26 of the Quad Cities Station Radiological Emergency Plan Annex, changed  
the threshold basis for EAL HU6 by adding the following two statements: 1)"If the alarm  
cannot be verified by redundant control room or nearby fire panel indications, notification  
from the field that a fire exists starts the 15-minute classification and fire extinguishment  
clocks," and 2) "The 15-minute period to extinguish the fire does not start until either the  
fire alarm is verified to be valid by utilization of additional control room or nearby fire  
panel instrumentation, or upon notification of a fire from the field."  


      The two statements added to the basis in Revision 26 conflict with the Revision 25
      threshold basis and initiating condition. The changed threshold basis in Revision 26
      could add an indeterminate amount of time to declaring an actual emergency until a
17
      person responded to the area of the fire and made a notification to the control room of a
Enclosure
      fire in the event that redundant control room or nearby fire panel indications were not
The two statements added to the basis in Revision 26 conflict with the Revision 25  
      available.
threshold basis and initiating condition. The changed threshold basis in Revision 26  
      Pending further review and verification by the NRC to determine if the changes to EAL
could add an indeterminate amount of time to declaring an actual emergency until a  
      HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue was
person responded to the area of the fire and made a notification to the control room of a  
      considered an unresolved item (URI 05000254/2009005-01; 05000265/2009005-01).
fire in the event that redundant control room or nearby fire panel indications were not  
1EP6 Drill Evaluation (71114.06)
available.  
.1   Emergency Preparedness Drill Observation
  a. Inspection Scope
Pending further review and verification by the NRC to determine if the changes to EAL  
      The inspectors evaluated the conduct of an after-hours licensee emergency drill on
HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue was  
      November 11, 2009, to identify any weaknesses and deficiencies in classification,
considered an unresolved item (URI 05000254/2009005-01; 05000265/2009005-01).  
      notification, and protective action recommendation development activities. The
1EP6 Drill Evaluation (71114.06)  
      after-hours drill was preceded by an unannounced, after-hours drive-in drill.
.1  
      The inspectors observed emergency response operations in the Technical Support
Emergency Preparedness Drill Observation  
      Center to determine whether the event classification, notifications, and protective action
a.  
      recommendations were performed in accordance with procedures. The inspectors also
Inspection Scope  
      attended the licensee drill critique to compare any inspector-observed weakness with
The inspectors evaluated the conduct of an after-hours licensee emergency drill on  
      those identified by the licensee staff in order to evaluate the critique and to verify
November 11, 2009, to identify any weaknesses and deficiencies in classification,  
      whether the licensee staff was properly identifying weaknesses and entering them into
notification, and protective action recommendation development activities. The  
      the corrective action program. As part of the inspection, the inspectors reviewed the drill
after-hours drill was preceded by an unannounced, after-hours drive-in drill.
      package and other documents listed in the Attachment to this report.
The inspectors observed emergency response operations in the Technical Support  
      This emergency preparedness drill inspection constituted one sample as defined in
Center to determine whether the event classification, notifications, and protective action  
      IP 71114.06-05.
recommendations were performed in accordance with procedures. The inspectors also  
  b. Findings
attended the licensee drill critique to compare any inspector-observed weakness with  
      No findings of significance were identified.
those identified by the licensee staff in order to evaluate the critique and to verify  
.2   Emergency Preparedness Termination and Recovery Drill Observation
whether the licensee staff was properly identifying weaknesses and entering them into  
  a. Inspection Scope
the corrective action program. As part of the inspection, the inspectors reviewed the drill  
      The inspectors evaluated the conduct of an emergency preparedness termination and
package and other documents listed in the Attachment to this report.  
      recovery drill on December 2, 2009, to identify any weaknesses and deficiencies in the
This emergency preparedness drill inspection constituted one sample as defined in  
      conduct of the drill and to assess the licensees ability to assess performance via a
IP 71114.06-05.  
      formal critique process in order to identify and correct Emergency Preparedness
b.  
      weaknesses. The inspectors observed emergency response operations in the Technical
Findings  
      Support Center to determine whether the recovery and termination activities associated
No findings of significance were identified.  
      with the drill were performed in accordance with procedures. The inspectors also
.2  
      attended the licensee drill critique to compare any inspector-observed weakness with
Emergency Preparedness Termination and Recovery Drill Observation  
      those identified by the licensee staff in order to evaluate the critique and to verify
a.  
      whether the licensee staff was properly identifying weaknesses and entering them into
Inspection Scope  
                                                17                                        Enclosure
The inspectors evaluated the conduct of an emergency preparedness termination and  
recovery drill on December 2, 2009, to identify any weaknesses and deficiencies in the  
conduct of the drill and to assess the licensees ability to assess performance via a  
formal critique process in order to identify and correct Emergency Preparedness  
weaknesses. The inspectors observed emergency response operations in the Technical  
Support Center to determine whether the recovery and termination activities associated  
with the drill were performed in accordance with procedures. The inspectors also  
attended the licensee drill critique to compare any inspector-observed weakness with  
those identified by the licensee staff in order to evaluate the critique and to verify  
whether the licensee staff was properly identifying weaknesses and entering them into  


      the corrective action program. As part of the inspection, the inspectors reviewed the drill
      package and other documents listed in the Attachment to this report.
      This emergency preparedness drill inspection constituted one sample as defined in
18
      IP 71114.06-05.
Enclosure
  b. Findings
the corrective action program. As part of the inspection, the inspectors reviewed the drill  
      No findings of significance were identified.
package and other documents listed in the Attachment to this report.  
4.   OTHER ACTIVITIES
This emergency preparedness drill inspection constituted one sample as defined in  
4OA1 Performance Indicator Verification (71151)
IP 71114.06-05.  
.1   Mitigating Systems Performance Index - Emergency Alternating Current Power System
b.  
  a. Inspection Scope
Findings  
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
No findings of significance were identified.  
      Index (MSPI) - Emergency Alternating Current (AC) Power System performance
4.  
      indicator for Quad Cities Units 1 and 2 for the period from the 4th quarter 2008 through
OTHER ACTIVITIES  
      the 3rd quarter 2009. To determine the accuracy of the performance indicator (PI) data
4OA1 Performance Indicator Verification (71151)  
      reported during those periods, PI definitions and guidance contained in the Nuclear
.1  
      Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator
Mitigating Systems Performance Index - Emergency Alternating Current Power System  
      Guideline, Revision 6, were used. The inspectors reviewed the licensees operator
a.  
      narrative logs, MSPI derivation reports, issue reports, event reports and NRC integrated
Inspection Scope  
      inspection reports for the period of October 1, 2008, through September 30, 2009, to
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
      validate the accuracy of the submittals. The inspectors reviewed the MSPI component
Index (MSPI) - Emergency Alternating Current (AC) Power System performance  
      risk coefficient to determine if it had changed by more than 25 percent in value since the
indicator for Quad Cities Units 1 and 2 for the period from the 4th quarter 2008 through  
      previous inspection, and if so, that the change was in accordance with applicable
the 3rd quarter 2009. To determine the accuracy of the performance indicator (PI) data  
      guidance. The inspectors also reviewed the licensees issue report database to
reported during those periods, PI definitions and guidance contained in the Nuclear  
      determine if any problems had been identified with the PI data collected or transmitted
Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator  
      for this indicator, and none were identified. Documents reviewed are listed in the
Guideline, Revision 6, were used. The inspectors reviewed the licensees operator  
      Attachment to this report.
narrative logs, MSPI derivation reports, issue reports, event reports and NRC integrated  
      This inspection constituted two MSPI emergency AC power system samples as defined
inspection reports for the period of October 1, 2008, through September 30, 2009, to  
      in IP 71151-05.
validate the accuracy of the submittals. The inspectors reviewed the MSPI component  
  b. Findings
risk coefficient to determine if it had changed by more than 25 percent in value since the  
      No findings of significance were identified.
previous inspection, and if so, that the change was in accordance with applicable  
.2   Mitigating Systems Performance Index - High Pressure Injection Systems
guidance. The inspectors also reviewed the licensees issue report database to  
  a. Inspection Scope
determine if any problems had been identified with the PI data collected or transmitted  
      The inspectors sampled licensee submittals for the Mitigating Systems Performance
for this indicator, and none were identified. Documents reviewed are listed in the  
      Index - High Pressure Injection Systems performance indicator for Quad Cities Units 1
Attachment to this report.  
      and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To
This inspection constituted two MSPI emergency AC power system samples as defined  
      determine the accuracy of the PI data reported during those periods, PI definitions and
in IP 71151-05.  
      guidance contained in the NEI Document 99-02, Regulatory Assessment Performance
b.  
                                                18                                    Enclosure
Findings  
No findings of significance were identified.  
.2  
Mitigating Systems Performance Index - High Pressure Injection Systems  
a.  
Inspection Scope  
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
Index - High Pressure Injection Systems performance indicator for Quad Cities Units 1  
and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To  
determine the accuracy of the PI data reported during those periods, PI definitions and  
guidance contained in the NEI Document 99-02, Regulatory Assessment Performance  


    Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees
    operator narrative logs, issue reports, MSPI derivation reports, event reports and
    NRC integrated inspection reports for the period of October 1, 2008, through
19
    September 30, 2009, to validate the accuracy of the submittals. The inspectors
Enclosure
    reviewed the MSPI component risk coefficient to determine if it had changed by more
Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees  
    than 25 percent in value since the previous inspection, and if so, that the change was in
operator narrative logs, issue reports, MSPI derivation reports, event reports and  
    accordance with applicable guidance. The inspectors also reviewed the licensees issue
NRC integrated inspection reports for the period of October 1, 2008, through  
    report database to determine if any problems had been identified with the PI data
September 30, 2009, to validate the accuracy of the submittals. The inspectors  
    collected or transmitted for this indicator, and none were identified. Documents
reviewed the MSPI component risk coefficient to determine if it had changed by more  
    reviewed are listed in the Attachment to this report.
than 25 percent in value since the previous inspection, and if so, that the change was in  
    This inspection constituted two MSPI high pressure injection system samples as defined
accordance with applicable guidance. The inspectors also reviewed the licensees issue  
    in IP 71151-05.
report database to determine if any problems had been identified with the PI data  
  b. Findings
collected or transmitted for this indicator, and none were identified. Documents  
    No findings of significance were identified.
reviewed are listed in the Attachment to this report.  
.3   Mitigating Systems Performance Index - Heat Removal System
This inspection constituted two MSPI high pressure injection system samples as defined  
  a. Inspection Scope
in IP 71151-05.  
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
b.  
    Index - Heat Removal System performance indicator for Quad Cities Units 1 and 2 for
Findings  
    the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the
No findings of significance were identified.  
    accuracy of the PI data reported during those periods, PI definitions and guidance
.3  
    contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator
Mitigating Systems Performance Index - Heat Removal System  
    Guideline, Revision 6, were used. The inspectors reviewed the licensees operator
a.  
    narrative logs, issue reports, event reports, MSPI derivation reports, and NRC integrated
Inspection Scope  
    inspection reports for the period of October 1, 2008, through September 30, 2009, to
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
    validate the accuracy of the submittals. The inspectors reviewed the MSPI component
Index - Heat Removal System performance indicator for Quad Cities Units 1 and 2 for  
    risk coefficient to determine if it had changed by more than 25 percent in value since the
the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the  
    previous inspection, and if so, that the change was in accordance with applicable
accuracy of the PI data reported during those periods, PI definitions and guidance  
    guidance. The inspectors also reviewed the licensees issue report database to
contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator  
    determine if any problems had been identified with the PI data collected or transmitted
Guideline, Revision 6, were used. The inspectors reviewed the licensees operator  
    for this indicator, and none were identified. Documents reviewed are listed in the
narrative logs, issue reports, event reports, MSPI derivation reports, and NRC integrated  
    Attachment to this report.
inspection reports for the period of October 1, 2008, through September 30, 2009, to  
    This inspection constituted two MSPI heat removal system samples as defined in
validate the accuracy of the submittals. The inspectors reviewed the MSPI component  
    IP 71151-05.
risk coefficient to determine if it had changed by more than 25 percent in value since the  
  b. Findings
previous inspection, and if so, that the change was in accordance with applicable  
    No findings of significance were identified.
guidance. The inspectors also reviewed the licensees issue report database to  
.4   Mitigating Systems Performance Index - Residual Heat Removal System
determine if any problems had been identified with the PI data collected or transmitted  
  a. Inspection Scope
for this indicator, and none were identified. Documents reviewed are listed in the  
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
Attachment to this report.  
    Index - Residual Heat Removal System performance indicator for Quad Cities Units 1
This inspection constituted two MSPI heat removal system samples as defined in  
                                                19                                    Enclosure
IP 71151-05.  
b.  
Findings  
No findings of significance were identified.  
.4  
Mitigating Systems Performance Index - Residual Heat Removal System  
a.  
Inspection Scope  
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
Index - Residual Heat Removal System performance indicator for Quad Cities Units 1  


    and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To
    determine the accuracy of the PI data reported during those periods, the PI definitions
    and guidance contained in the NEI Document 99-02, Regulatory Assessment
20
    Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the
Enclosure
    licensees operator narrative logs, issue reports, MSPI derivation reports, event reports
and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To  
    and NRC integrated inspection reports for the period of October 1, 2008, through
determine the accuracy of the PI data reported during those periods, the PI definitions  
    September 30, 2009, to validate the accuracy of the submittals. The inspectors
and guidance contained in the NEI Document 99-02, Regulatory Assessment  
    reviewed the MSPI component risk coefficient to determine if it had changed by more
Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the  
    than 25 percent in value since the previous inspection, and if so, that the change was in
licensees operator narrative logs, issue reports, MSPI derivation reports, event reports  
    accordance with applicable guidance. The inspectors also reviewed the licensees issue
and NRC integrated inspection reports for the period of October 1, 2008, through  
    report database to determine if any problems had been identified with the PI data
September 30, 2009, to validate the accuracy of the submittals. The inspectors  
    collected or transmitted for this indicator, and none were identified. Documents
reviewed the MSPI component risk coefficient to determine if it had changed by more  
    reviewed are listed in the Attachment to this report.
than 25 percent in value since the previous inspection, and if so, that the change was in  
    This inspection constituted two MSPI residual heat removal system samples as defined
accordance with applicable guidance. The inspectors also reviewed the licensees issue  
    in IP 71151-05.
report database to determine if any problems had been identified with the PI data  
  b. Findings
collected or transmitted for this indicator, and none were identified. Documents  
    No findings of significance were identified.
reviewed are listed in the Attachment to this report.  
.5   Mitigating Systems Performance Index - Cooling Water Systems
This inspection constituted two MSPI residual heat removal system samples as defined  
  a. Inspection Scope
in IP 71151-05.  
    The inspectors sampled licensee submittals for the Mitigating Systems Performance
b.  
    Index - Cooling Water Systems performance indicator for Quad Cities Units 1 and 2 for
Findings  
    the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the
No findings of significance were identified.  
    accuracy of the PI data reported during those periods, PI definitions and guidance
.5  
    contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator
Mitigating Systems Performance Index - Cooling Water Systems  
    Guideline, Revision 6, were used. The inspectors reviewed the licensees operator
a.  
    narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated
Inspection Scope  
    inspection reports for the period of October 1, 2008, through September 30, 2009, to
The inspectors sampled licensee submittals for the Mitigating Systems Performance  
    validate the accuracy of the submittals. The inspectors reviewed the MSPI component
Index - Cooling Water Systems performance indicator for Quad Cities Units 1 and 2 for  
    risk coefficient to determine if it had changed by more than 25 percent in value since the
the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the  
    previous inspection, and if so, that the change was in accordance with applicable
accuracy of the PI data reported during those periods, PI definitions and guidance  
    guidance. The inspectors also reviewed the licensees issue report database to
contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator  
    determine if any problems had been identified with the PI data collected or transmitted
Guideline, Revision 6, were used. The inspectors reviewed the licensees operator  
    for this indicator, and none were identified. Documents reviewed are listed in the
narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated  
    Attachment to this report.
inspection reports for the period of October 1, 2008, through September 30, 2009, to  
    This inspection constituted two MSPI cooling water system samples as defined in
validate the accuracy of the submittals. The inspectors reviewed the MSPI component  
    IP 71151-05.
risk coefficient to determine if it had changed by more than 25 percent in value since the  
  b. Findings
previous inspection, and if so, that the change was in accordance with applicable  
    No findings of significance were identified.
guidance. The inspectors also reviewed the licensees issue report database to  
                                                20                                    Enclosure
determine if any problems had been identified with the PI data collected or transmitted  
for this indicator, and none were identified. Documents reviewed are listed in the  
Attachment to this report.  
This inspection constituted two MSPI cooling water system samples as defined in  
IP 71151-05.  
b.  
Findings  
No findings of significance were identified.  


  .6   Radiological Effluent Technical Specification/Offsite Dose Calculation Manual
   
      Radiological Effluent Occurrences
  a. Inspection Scope
21
      The inspectors sampled licensee submittals for the Radiological Effluent Technical
Enclosure
      Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent
.6  
      Occurrences performance indicator for the period of December 2008 through
Radiological Effluent Technical Specification/Offsite Dose Calculation Manual  
      November 2009. The inspectors used PI definitions and guidance contained in the
Radiological Effluent Occurrences  
      NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,
a.  
      Revision 6 to determine the accuracy of the PI data reported during those periods.
Inspection Scope  
      The inspectors reviewed the licensees issue report database and selected individual
The inspectors sampled licensee submittals for the Radiological Effluent Technical  
      reports generated since this indicator was last reviewed to identify any potential
Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent  
      occurrences such as unmonitored, uncontrolled, or improperly calculated effluent
Occurrences performance indicator for the period of December 2008 through  
      releases that may have impacted offsite dose. The inspectors reviewed gaseous
November 2009. The inspectors used PI definitions and guidance contained in the  
      effluent summary data and the results of associated offsite dose calculations for selected
NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,  
      dates between December 2008 and November 2009 to determine if indicator results
Revision 6 to determine the accuracy of the PI data reported during those periods.
      were accurately reported. The inspectors also reviewed the licensees methods for
The inspectors reviewed the licensees issue report database and selected individual  
      quantifying gaseous and liquid effluents and determining effluent dose. Documents
reports generated since this indicator was last reviewed to identify any potential  
      reviewed are listed in the Attachment to this report.
occurrences such as unmonitored, uncontrolled, or improperly calculated effluent  
      This inspection constituted one RETS/ODCM radiological effluent occurrences sample
releases that may have impacted offsite dose. The inspectors reviewed gaseous  
      as defined in IP 71151-05.
effluent summary data and the results of associated offsite dose calculations for selected  
  b. Findings
dates between December 2008 and November 2009 to determine if indicator results  
      No findings of significance were identified.
were accurately reported. The inspectors also reviewed the licensees methods for  
4OA2 Identification and Resolution of Problems (71152)
quantifying gaseous and liquid effluents and determining effluent dose. Documents  
      Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency
reviewed are listed in the Attachment to this report.  
      Preparedness, Public Radiation Safety, Occupational Radiation Safety, and
This inspection constituted one RETS/ODCM radiological effluent occurrences sample  
      Physical Protection
as defined in IP 71151-05.  
.1   Routine Review of Items Entered into the Corrective Action Program (CAP)
b.  
  a. Inspection Scope
Findings  
      As part of the various baseline inspection procedures discussed in previous sections of
No findings of significance were identified.  
      this report, the inspectors routinely reviewed issues during baseline inspection activities
4OA2 Identification and Resolution of Problems (71152)  
      and plant status reviews to verify that they were being entered into the licensees CAP at
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency  
      an appropriate threshold, that adequate attention was being given to timely corrective
Preparedness, Public Radiation Safety, Occupational Radiation Safety, and  
      actions, and that adverse trends were identified and addressed. Attributes reviewed
Physical Protection  
      included: the complete and accurate identification of the problem; that timeliness was
.1  
      commensurate with the safety significance; that evaluation and disposition of
Routine Review of Items Entered into the Corrective Action Program (CAP)  
      performance issues, generic implications, common causes, contributing factors, root
a.  
      causes, extent of condition reviews, and previous occurrences reviews were proper and
Inspection Scope  
      adequate; and that the classification, prioritization, focus, and timeliness of corrective
As part of the various baseline inspection procedures discussed in previous sections of  
      actions were commensurate with safety and sufficient to prevent recurrence of the issue.
this report, the inspectors routinely reviewed issues during baseline inspection activities  
      Minor issues entered into the licensees CAP as a result of the inspectors observations
and plant status reviews to verify that they were being entered into the licensees CAP at  
      are included in the attached List of Documents Reviewed.
an appropriate threshold, that adequate attention was being given to timely corrective  
                                                21                                        Enclosure
actions, and that adverse trends were identified and addressed. Attributes reviewed  
included: the complete and accurate identification of the problem; that timeliness was  
commensurate with the safety significance; that evaluation and disposition of  
performance issues, generic implications, common causes, contributing factors, root  
causes, extent of condition reviews, and previous occurrences reviews were proper and  
adequate; and that the classification, prioritization, focus, and timeliness of corrective  
actions were commensurate with safety and sufficient to prevent recurrence of the issue.
Minor issues entered into the licensees CAP as a result of the inspectors observations  
are included in the attached List of Documents Reviewed.  


    These routine reviews for the identification and resolution of problems did not constitute
    any additional inspection samples. Instead, by procedure they were considered an
    integral part of the inspections performed during the quarter and documented in
22
    Section 1 of this report.
Enclosure
  b. Findings
These routine reviews for the identification and resolution of problems did not constitute  
    No findings of significance were identified.
any additional inspection samples. Instead, by procedure they were considered an  
.2   Daily Corrective Action Program Reviews
integral part of the inspections performed during the quarter and documented in  
  a. Inspection Scope
Section 1 of this report.  
    In order to assist with the identification of repetitive equipment failures and specific
b.  
    human performance issues for followup, the inspectors performed a daily screening of
Findings  
    items entered into the licensees CAP. This review was accomplished through
No findings of significance were identified.  
    inspection of the stations daily condition report packages.
.2  
    These daily reviews were performed by procedure as part of the inspectors daily plant
Daily Corrective Action Program Reviews  
    status monitoring activities and, as such, did not constitute any separate inspection
a.  
    samples.
Inspection Scope  
  b. Findings
In order to assist with the identification of repetitive equipment failures and specific  
    No findings of significance were identified.
human performance issues for followup, the inspectors performed a daily screening of  
.3   Semi-Annual Trend Review
items entered into the licensees CAP. This review was accomplished through  
  a. Inspection Scope
inspection of the stations daily condition report packages.  
    The inspectors performed a review of the licensees CAP and associated documents to
These daily reviews were performed by procedure as part of the inspectors daily plant  
    identify trends that could indicate the existence of a more significant safety issue. The
status monitoring activities and, as such, did not constitute any separate inspection  
    inspectors review was focused on repetitive equipment issues and associated corrective
samples.  
    actions, but also considered the results of daily inspector CAP item screening discussed
b.  
    in Section 4OA2.2 above, licensee trending efforts, and licensee human performance
Findings  
    results. The inspectors review nominally considered the 6-month period of
No findings of significance were identified.  
    January 1, 2009, through June 30, 2009, although some examples expanded beyond
.3  
    those dates where the scope of the trend warranted.
Semi-Annual Trend Review  
    The review also included issues documented outside the normal CAP in major
a.  
    equipment problem lists, repetitive and/or rework maintenance lists, departmental
Inspection Scope  
    problem/challenges lists, system health reports, quality assurance audit/surveillance
The inspectors performed a review of the licensees CAP and associated documents to  
    reports, self assessment reports, and Maintenance Rule assessments. The inspectors
identify trends that could indicate the existence of a more significant safety issue. The  
    compared and contrasted their results with the results contained in the licensees
inspectors review was focused on repetitive equipment issues and associated corrective  
    CAP trending reports. Corrective actions associated with a sample of the issues
actions, but also considered the results of daily inspector CAP item screening discussed  
    identified in the licensees trending reports were reviewed for adequacy. Additionally,
in Section 4OA2.2 above, licensee trending efforts, and licensee human performance  
    the inspectors reviewed CAP open priority 1, 2, and 3 corrective actions for timeliness.
results. The inspectors review nominally considered the 6-month period of  
    In addition, all open priority 4 action tracking items (ACITs) were reviewed to ensure they
January 1, 2009, through June 30, 2009, although some examples expanded beyond  
    were properly categorized and that the justifications for extension were appropriate and
those dates where the scope of the trend warranted.  
    properly documented.
The review also included issues documented outside the normal CAP in major  
                                                22                                    Enclosure
equipment problem lists, repetitive and/or rework maintenance lists, departmental  
problem/challenges lists, system health reports, quality assurance audit/surveillance  
reports, self assessment reports, and Maintenance Rule assessments. The inspectors  
compared and contrasted their results with the results contained in the licensees  
CAP trending reports. Corrective actions associated with a sample of the issues  
identified in the licensees trending reports were reviewed for adequacy. Additionally,  
the inspectors reviewed CAP open priority 1, 2, and 3 corrective actions for timeliness.
In addition, all open priority 4 action tracking items (ACITs) were reviewed to ensure they  
were properly categorized and that the justifications for extension were appropriate and  
properly documented.  


    This review constituted a single semi-annual trend inspection sample as defined in
    IP 71152-05.
  b. Findings
23
    No findings of significance were identified.
Enclosure
.4   Selected Issue Followup Inspection: Issue Report 966501, Darley Pump Leaking
This review constituted a single semi-annual trend inspection sample as defined in  
    Gasoline from the Fuel Pump
IP 71152-05.  
  a. Inspection Scope
b.  
    During a review of items entered in the licensees CAP, the inspectors followed up on a
Findings  
    corrective action item documenting gasoline leaking from the fuel pump of the portable
No findings of significance were identified.  
    emergency flooding pump (Darley pump) on September 17, 2009, during preparations
.4  
    for a pump capacity demonstration run. The pump capacity demonstration was a new
Selected Issue Followup Inspection: Issue Report 966501, Darley Pump Leaking  
    procedure developed in response to a non-cited violation (NCV) documented in
Gasoline from the Fuel Pump  
    Inspection Report 05000254/2007005.
a.  
    This review constituted one in-depth problem identification and resolution sample as
Inspection Scope  
    defined in IP 71152-05.
During a review of items entered in the licensees CAP, the inspectors followed up on a  
  b. Findings
corrective action item documenting gasoline leaking from the fuel pump of the portable  
    Introduction: A finding of very low safety significance was self-revealed for the failure to
emergency flooding pump (Darley pump) on September 17, 2009, during preparations  
    maintain the portable emergency flooding pump and supporting equipment in a condition
for a pump capacity demonstration run. The pump capacity demonstration was a new  
    required to support implementation of QCOA 0010-16, Flood Emergency Procedure.
procedure developed in response to a non-cited violation (NCV) documented in  
    Description: In Inspection Report 05000254/2007005, inspectors documented a NCV of
Inspection Report 05000254/2007005.  
    TS 5.4.1 for the licensees failure to develop adequate surveillance procedures for
This review constituted one in-depth problem identification and resolution sample as  
    equipment used during an external flooding event. Corrective action for this issue
defined in IP 71152-05.  
    included revising the external flooding procedure and developing and implementing a
b.  
    procedure to test a portable pump used as the sole source of makeup water to the spent
Findings  
    fuel pool following an external flooding event. The action to develop and implement the
Introduction: A finding of very low safety significance was self-revealed for the failure to  
    pump test procedure was issued in May and stated, Develop test procedure and
maintain the portable emergency flooding pump and supporting equipment in a condition  
    conduct test to confirm flow of greater than or equal to 200 gpm by mid-July. Brief
required to support implementation of QCOA 0010-16, Flood Emergency Procedure.  
    NRC Resident as appropriate. The action was closed to an Engineering Change (EC)
Description: In Inspection Report 05000254/2007005, inspectors documented a NCV of  
    366481, on July 18, 2007, with no actual test performed. The documented justification
TS 5.4.1 for the licensees failure to develop adequate surveillance procedures for  
    for this closure stated that discussions with the NRC resident clarified the intent of the
equipment used during an external flooding event. Corrective action for this issue  
    action and no physical testing needed to be performed. Followup discussions with the
included revising the external flooding procedure and developing and implementing a  
    resident inspectors stationed at Quad Cities in July 2007 had no recollection of the
procedure to test a portable pump used as the sole source of makeup water to the spent  
    conversation and their understanding of the intended action remained unchanged from
fuel pool following an external flooding event. The action to develop and implement the  
    the original report.
pump test procedure was issued in May and stated, Develop test procedure and  
    Licensee staff generated Issue Report (IR) 738335 in February 2008 to document the
conduct test to confirm flow of greater than or equal to 200 gpm by mid-July. Brief  
    review of the NCV response and generate a closure package of all related IRs. The lack
NRC Resident as appropriate. The action was closed to an Engineering Change (EC)  
    of preventative maintenance (PM) testing was identified and an action tracking item was
366481, on July 18, 2007, with no actual test performed.   The documented justification  
    generated to Develop PM/testing requirements for the Darley pump associated with the
for this closure stated that discussions with the NRC resident clarified the intent of the  
    external flooding event. The original corrective action due date was July 16, 2008.
action and no physical testing needed to be performed. Followup discussions with the  
    The action was extended several times, and on May 18, 2009, during a review of
resident inspectors stationed at Quad Cities in July 2007 had no recollection of the  
    corrective actions for NRC-identified issues, the licensee staff identified that a CAP
conversation and their understanding of the intended action remained unchanged from  
                                              23                                      Enclosure
the original report.  
Licensee staff generated Issue Report (IR) 738335 in February 2008 to document the  
review of the NCV response and generate a closure package of all related IRs. The lack  
of preventative maintenance (PM) testing was identified and an action tracking item was  
generated to Develop PM/testing requirements for the Darley pump associated with the  
external flooding event. The original corrective action due date was July 16, 2008.
The action was extended several times, and on May 18, 2009, during a review of  
corrective actions for NRC-identified issues, the licensee staff identified that a CAP  


action item (ACIT 624645-03) had been inappropriately closed. In addition, the licensee
determined that ACIT 624645-03 was inappropriately tagged as an Action Tracking Item
(ACIT) and should have been a corrective action. Issue Report 921197 was generated
24
and ACIT 624645 was upgraded to a corrective action with a July 31, 2009, due date.
Enclosure
The test procedure was developed and the pump was scheduled to run on
action item (ACIT 624645-03) had been inappropriately closed. In addition, the licensee  
September 17, 2009.
determined that ACIT 624645-03 was inappropriately tagged as an Action Tracking Item  
The capacity test was implemented with WO 01247374. When mechanics pulled the
(ACIT) and should have been a corrective action.   Issue Report 921197 was generated  
pump and support components from the storage location, they found that the engine
and ACIT 624645 was upgraded to a corrective action with a July 31, 2009, due date.
battery had to be replaced and the gasoline stored with the motor had to be replaced.
The test procedure was developed and the pump was scheduled to run on  
Since the mechanics performing the test had never operated the pump, they decided to
September 17, 2009.  
run it in the weld shop before taking it down to the river. When the mechanics started
The capacity test was implemented with WO 01247374. When mechanics pulled the  
the pump, fuel was spraying out of the fuel pump. They immediately shut down the
pump and support components from the storage location, they found that the engine  
pump and contained the fuel leak (IR 966501).
battery had to be replaced and the gasoline stored with the motor had to be replaced.
The Darley pump fuel system was repaired and the capacity test was completed
Since the mechanics performing the test had never operated the pump, they decided to  
satisfactorily on September 25, 2009. Review of recent pump operating history and
run it in the weld shop before taking it down to the river. When the mechanics started  
PM tasks revealed that the pump had not been operated since the NCV was identified in
the pump, fuel was spraying out of the fuel pump. They immediately shut down the  
2007. The annual maintenance performed under PM 164250 in July of 2009 changed
pump and contained the fuel leak (IR 966501).  
the oil and inspected the filters and spark plugs with no post-maintenance operation
The Darley pump fuel system was repaired and the capacity test was completed  
required. The PM also failed to identify that the battery was beyond the expected life
satisfactorily on September 25, 2009. Review of recent pump operating history and  
and did not determine that the battery would maintain its charge.
PM tasks revealed that the pump had not been operated since the NCV was identified in  
Analysis: The inspectors determined that the failure to perform maintenance that would
2007. The annual maintenance performed under PM 164250 in July of 2009 changed  
ensure the pump was in a standby condition and readily available to accomplish the
the oil and inspected the filters and spark plugs with no post-maintenance operation  
requirements of QCOA 0010-16 was a performance deficiency fully within the licensees
required. The PM also failed to identify that the battery was beyond the expected life  
ability to control, and therefore a finding. This issue was more than minor because it
and did not determine that the battery would maintain its charge.  
was associated with the SSC Performance attribute of the Barrier Integrity Cornerstone
Analysis: The inspectors determined that the failure to perform maintenance that would  
element of maintaining the functionality of spent fuel pool cooling. The finding affected
ensure the pump was in a standby condition and readily available to accomplish the  
the cornerstone objective of providing assurance that physical design barriers protect the
requirements of QCOA 0010-16 was a performance deficiency fully within the licensees  
public from radionuclide releases caused by events including external flooding.
ability to control, and therefore a finding. This issue was more than minor because it  
Specifically, the pump could fail due to a maintenance preventable component failure
was associated with the SSC Performance attribute of the Barrier Integrity Cornerstone  
resulting in inadequate or degraded makeup to the spent fuel pool during an external
element of maintaining the functionality of spent fuel pool cooling. The finding affected  
flooding event. The inspectors did not identify a cross-cutting aspect associated with
the cornerstone objective of providing assurance that physical design barriers protect the  
this finding because the maintenance issue is a legacy issue and not reflective of current
public from radionuclide releases caused by events including external flooding.
licensee performance. The pump and PM tasks had been in place for several years.
Specifically, the pump could fail due to a maintenance preventable component failure  
Inspectors reviewed maintenance requirements for other temporary equipment staged in
resulting in inadequate or degraded makeup to the spent fuel pool during an external  
support of external events and emergency operating procedures, some of which was put
flooding event. The inspectors did not identify a cross-cutting aspect associated with  
in place after the Darley pump was staged, and did not identify any similar issues.
this finding because the maintenance issue is a legacy issue and not reflective of current  
The inspectors determined the finding could be evaluated using the SDP in accordance
licensee performance. The pump and PM tasks had been in place for several years.
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Inspectors reviewed maintenance requirements for other temporary equipment staged in  
Initial Screening and Characterization of findings, Tables 4a and 4b. The inspectors
support of external events and emergency operating procedures, some of which was put  
determined that even though this equipment is assumed to completely fail, the licensee
in place after the Darley pump was staged, and did not identify any similar issues.  
could provide an alternate portable pump already located on site and capable of
The inspectors determined the finding could be evaluated using the SDP in accordance  
performing the safety function during this slow developing event. The alternate pump
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
had maintenance and test procedures in place to provide a basis for reliability. Since
Initial Screening and Characterization of findings, Tables 4a and 4b. The inspectors  
alternate equipment was available and the delay in mobilizing the alternate equipment
determined that even though this equipment is assumed to completely fail, the licensee  
would not have resulted in loss of capability to mitigate the impact of the flooding event,
could provide an alternate portable pump already located on site and capable of  
the issue is of very low safety significance or Green.
performing the safety function during this slow developing event. The alternate pump  
                                          24                                      Enclosure
had maintenance and test procedures in place to provide a basis for reliability. Since  
alternate equipment was available and the delay in mobilizing the alternate equipment  
would not have resulted in loss of capability to mitigate the impact of the flooding event,  
the issue is of very low safety significance or Green.  


    Enforcement: Technical Specification 5.4.1 required that written procedures be
    established, implemented, and maintained for the items specified in Regulatory
    Guide 1.33, Quality Assurance Program Requirements. QCOA 0010-16,
25
    Flood Emergency Procedure, was the licensee procedure used to meet the
Enclosure
    Regulatory Guide 1.33 requirement for an emergency flooding event. The procedure
Enforcement: Technical Specification 5.4.1 required that written procedures be  
    specified that the portable pump staged in the protected area warehouse is to be used to
established, implemented, and maintained for the items specified in Regulatory  
    respond to the event. Although the regulatory guide did not specifically require
Guide 1.33, Quality Assurance Program Requirements. QCOA 0010-16,  
    maintenance procedures for portable equipment, failure to maintain the staged
Flood Emergency Procedure, was the licensee procedure used to meet the  
    equipment in a condition to be used to mitigate the event does not support timely
Regulatory Guide 1.33 requirement for an emergency flooding event. The procedure  
    implementation of the procedure to provide spent fuel pool makeup and is a finding.
specified that the portable pump staged in the protected area warehouse is to be used to  
    Enforcement action does not apply because the performance deficiency did not involve a
respond to the event. Although the regulatory guide did not specifically require  
    violation of a regulatory requirement. Because the finding does not involve a violation of
maintenance procedures for portable equipment, failure to maintain the staged  
    regulatory requirements and has a very low safety significance, it is identified as
equipment in a condition to be used to mitigate the event does not support timely  
    (FIN 05000254/2009005-02; 05000265/2009005-02). The issue was added to the
implementation of the procedure to provide spent fuel pool makeup and is a finding.  
    licensees CAP program as IR 966501 and IR 968809. Immediate corrective actions
Enforcement action does not apply because the performance deficiency did not involve a  
    included replacement of the degraded battery and overhaul of the pumps fuel pump.
violation of a regulatory requirement. Because the finding does not involve a violation of  
    Other actions included identification of preventative maintenance tasks and establishing
regulatory requirements and has a very low safety significance, it is identified as  
    a program owner of the pump.
(FIN 05000254/2009005-02; 05000265/2009005-02). The issue was added to the  
.5   Selected Issue Followup Inspection: Incident Report 984769, Temperature Indicating
licensees CAP program as IR 966501 and IR 968809. Immediate corrective actions  
    Probe Found Broken in the Unit 2 Diesel Generator Coolant System
included replacement of the degraded battery and overhaul of the pumps fuel pump.
  a. Inspection Scope
Other actions included identification of preventative maintenance tasks and establishing  
    During a review of items entered in the licensees CAP, the inspectors followed up on a
a program owner of the pump.  
    corrective action item documenting a failed temperature indicating probe (TI) in the
.5  
    Unit 2 diesel generator coolant system on October 27, 2009, during planned
Selected Issue Followup Inspection: Incident Report 984769, Temperature Indicating  
    maintenance on the Unit 2 emergency diesel generator (EDG).
Probe Found Broken in the Unit 2 Diesel Generator Coolant System  
    This review constituted one in-depth problem identification and resolution sample as
a.  
    defined in IP 71152-05.
Inspection Scope  
  b. Findings
During a review of items entered in the licensees CAP, the inspectors followed up on a  
    Introduction: A finding of very low safety significance and associated NCV were
corrective action item documenting a failed temperature indicating probe (TI) in the  
    self-revealed when a TI failed in the Unit 2 diesel generator coolant system.
Unit 2 diesel generator coolant system on October 27, 2009, during planned  
    Description: On October 27, 2009, while performing corrective maintenance on
maintenance on the Unit 2 emergency diesel generator (EDG).  
    TI 2-6641-8205, technicians noted that the tip had broken off the probe when comparing
This review constituted one in-depth problem identification and resolution sample as  
    it to the length of the new TI. This TI provides local indication of the jacket coolant water
defined in IP 71152-05.  
    temperature at the inlet to the diesel engine and provides no alarm function.
b.  
    The TI was scheduled for replacement in October 2008 when Operations identified the
Findings  
    TI reading abnormally at zero degrees. A work order was written and scheduled for
Introduction: A finding of very low safety significance and associated NCV were  
    October 2009. During the performance of the maintenance, it was noted that the new TI
self-revealed when a TI failed in the Unit 2 diesel generator coolant system.  
    was longer than the one recently removed. A new work order was written to retrieve any
Description: On October 27, 2009, while performing corrective maintenance on  
    foreign material from the system. The broken tip was recovered from the diesel
TI 2-6641-8205, technicians noted that the tip had broken off the probe when comparing  
    generator coolant system.
it to the length of the new TI. This TI provides local indication of the jacket coolant water  
                                              25                                        Enclosure
temperature at the inlet to the diesel engine and provides no alarm function.  
The TI was scheduled for replacement in October 2008 when Operations identified the  
TI reading abnormally at zero degrees. A work order was written and scheduled for  
October 2009. During the performance of the maintenance, it was noted that the new TI  
was longer than the one recently removed. A new work order was written to retrieve any  
foreign material from the system. The broken tip was recovered from the diesel  
generator coolant system.  


The licensee investigation discovered that the installation analysis for this TI was
approved under the non-safety below level of design detail (NSBLD) process in October
2007 under Revision 3 of SM-AA-300, Procurement Engineering Support Activities.
26
Using this provision, NSBLD changes must be documented and shall identify the
Enclosure
change with justification of the changes technical acceptability. The length of the probe
The licensee investigation discovered that the installation analysis for this TI was  
was the only difference to the previously installed TI. The TI was installed with a
approved under the non-safety below level of design detail (NSBLD) process in October  
3.25 inch probe, which was longer than the previous 2 inch probe. The added length
2007 under Revision 3 of SM-AA-300, Procurement Engineering Support Activities.
increased the shear force from the coolant flow and caused the probe to break off.
Using this provision, NSBLD changes must be documented and shall identify the  
An operating experience (OPEX) review would have revealed an event at another
change with justification of the changes technical acceptability. The length of the probe  
nuclear facility where the same make and model TI experienced the same failure
was the only difference to the previously installed TI. The TI was installed with a  
mechanism in a diesel generator coolant system. Under Revision 3 of SM-AA-300,
3.25 inch probe, which was longer than the previous 2 inch probe. The added length  
OPEX reviews for NSBLD were not required, nor were additional peer reviews required.
increased the shear force from the coolant flow and caused the probe to break off.  
The lack of an OPEX review was an identified vulnerability by the licensees corporate
An operating experience (OPEX) review would have revealed an event at another  
supply organization in a common cause analysis which was performed for a lack of
nuclear facility where the same make and model TI experienced the same failure  
technical rigor issued in February 2008. A corrective action from this common cause
mechanism in a diesel generator coolant system. Under Revision 3 of SM-AA-300,  
analysis was to implement Revision 4 of SM-AA-300 which limited NSBLD reviews to
OPEX reviews for NSBLD were not required, nor were additional peer reviews required.
non-safety host component applications. Revision 4 was implemented at Quad Cities in
The lack of an OPEX review was an identified vulnerability by the licensees corporate  
February 2008. Since this specific TI is classified as augmented quality, Revision 4
supply organization in a common cause analysis which was performed for a lack of  
would prevent use of the NSBLD process of a non-identical replacement. A full item
technical rigor issued in February 2008. A corrective action from this common cause  
equivalency evaluation would be required for any non-identical replacement.
analysis was to implement Revision 4 of SM-AA-300 which limited NSBLD reviews to  
An extent of condition review is scheduled to be performed at Quad Cities by
non-safety host component applications. Revision 4 was implemented at Quad Cities in  
Procurement Engineering for all NSBLD reviews that were performed under Revision 3
February 2008. Since this specific TI is classified as augmented quality, Revision 4  
of SM-AA-300 from August 2007 through February 2008.
would prevent use of the NSBLD process of a non-identical replacement. A full item  
Analysis: The inspectors determined that the approval of an inappropriate component
equivalency evaluation would be required for any non-identical replacement.  
designated as augmented quality was a performance deficiency and a finding. The
An extent of condition review is scheduled to be performed at Quad Cities by  
same parts evaluation process was used for risk-significant components independent of
Procurement Engineering for all NSBLD reviews that were performed under Revision 3  
the system being worked. Therefore, this finding was more than minor because, if left
of SM-AA-300 from August 2007 through February 2008.  
uncorrected, this performance deficiency could lead to unplanned unavailability of
Analysis: The inspectors determined that the approval of an inappropriate component  
safety-related or risk-significant equipment and would become a more significant safety
designated as augmented quality was a performance deficiency and a finding. The  
concern. This performance deficiency challenged the Mitigating Systems Cornerstone
same parts evaluation process was used for risk-significant components independent of  
attribute of Equipment Performance by challenging equipment availability and reliability.
the system being worked. Therefore, this finding was more than minor because, if left  
The inspectors performed a Phase 1 SDP screening and concluded that the issue was
uncorrected, this performance deficiency could lead to unplanned unavailability of  
of very low safety significance (Green) because the failure of the TI did not result in
safety-related or risk-significant equipment and would become a more significant safety  
unplanned inoperability or loss of function of the diesel generator. The inspectors
concern. This performance deficiency challenged the Mitigating Systems Cornerstone  
determined that this finding did not have a cross-cutting aspect. This performance
attribute of Equipment Performance by challenging equipment availability and reliability.  
deficiency is not indicative of current licensee performance. The decision to install this
The inspectors performed a Phase 1 SDP screening and concluded that the issue was  
type of TI was made in October 2007. The process which allowed this performance
of very low safety significance (Green) because the failure of the TI did not result in  
deficiency was identified and corrected through procedure and policy revisions to
unplanned inoperability or loss of function of the diesel generator. The inspectors  
SM-AA-300 in February 2008.
determined that this finding did not have a cross-cutting aspect. This performance  
Enforcement: The TI was designated augmented quality in the licensees quality
deficiency is not indicative of current licensee performance. The decision to install this  
assurance program. The licensees quality assurance program applied controls
type of TI was made in October 2007. The process which allowed this performance  
equivalent to safety-related components for Class 1E equipment qualification to
deficiency was identified and corrected through procedure and policy revisions to  
augmented quality equipment and systems. This correlation is applicable to several
SM-AA-300 in February 2008.  
Appendix B criteria included in the program such as both Section 3 - Design Control,
Enforcement: The TI was designated augmented quality in the licensees quality  
and Section 5 - Instructions Procedures and Drawings, of the licensees Quality
assurance program. The licensees quality assurance program applied controls  
Assurance program for augmented quality.
equivalent to safety-related components for Class 1E equipment qualification to  
                                          26                                    Enclosure
augmented quality equipment and systems. This correlation is applicable to several  
Appendix B criteria included in the program such as both Section 3 - Design Control,  
and Section 5 - Instructions Procedures and Drawings, of the licensees Quality  
Assurance program for augmented quality.  


      Title 10 CFR 50, Appendix B, Criterion V states in part that activities affecting quality
      shall be prescribed by instructions and procedures of a type appropriate to the
      circumstances and shall be accomplished in accordance with these instructions or
27
      procedures.
Enclosure
      Contrary to the above, on October 30, 2007, SM-AA-300 was not appropriate to the
Title 10 CFR 50, Appendix B, Criterion V states in part that activities affecting quality  
      circumstances in that it did not require an approval process with technical rigor
shall be prescribed by instructions and procedures of a type appropriate to the  
      equivalent to the process used for safety-related components when a non-identical
circumstances and shall be accomplished in accordance with these instructions or  
      temperature indicating probe designated augmented quality was approved for use.
procedures.  
      That part was approved for use through a NSBLD review per Revision 3 of SM-AA-300
Contrary to the above, on October 30, 2007, SM-AA-300 was not appropriate to the  
      instead of undergoing a full item equivalency evaluation, and the part subsequently
circumstances in that it did not require an approval process with technical rigor  
      failed resulting in foreign material in the diesel generator coolant system. The foreign
equivalent to the process used for safety-related components when a non-identical  
      material did not cause any adverse consequences in this instance.
temperature indicating probe designated augmented quality was approved for use.
      Because this issue is of very low safety significance, and this issue has been entered
That part was approved for use through a NSBLD review per Revision 3 of SM-AA-300  
      into the licensees corrective action program as Issue Report 984769, this issue is being
instead of undergoing a full item equivalency evaluation, and the part subsequently  
      treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy
failed resulting in foreign material in the diesel generator coolant system. The foreign  
      (NCV 05000265/2009005-03).
material did not cause any adverse consequences in this instance.  
      Corrective actions for this event included replacement of the TI with an appropriately
Because this issue is of very low safety significance, and this issue has been entered  
      approved TI. The licensee has also scheduled to perform an extent of condition review
into the licensees corrective action program as Issue Report 984769, this issue is being  
      of NSBLD reviews performed under Revision 3 of SM-AA-300 from August 2007 through
treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy  
      February 2008.
(NCV 05000265/2009005-03).  
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)
Corrective actions for this event included replacement of the TI with an appropriately  
.1   (Closed) Licensee Event Report 05000254/2009-003-00: Failure of RHR Torus Spray
approved TI. The licensee has also scheduled to perform an extent of condition review  
      Isolation Valve to Open Due to Declutch Mechanism Problems
of NSBLD reviews performed under Revision 3 of SM-AA-300 from August 2007 through  
  a. Inspection Scope
February 2008.  
      Inspectors reviewed the event, evaluation, and corrective actions for the motor operated
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)  
      valve failure reported in Licensee Event Report (LER) 05000254/2009-003. Documents
.1  
      reviewed as part of this inspection are listed in the Attachment to this report. This LER is
(Closed) Licensee Event Report 05000254/2009-003-00: Failure of RHR Torus Spray  
      closed.
Isolation Valve to Open Due to Declutch Mechanism Problems  
      This event follow-up review constituted one sample as defined in IP 71153-05.
a.  
  b. Findings
Inspection Scope  
      Introduction: A finding of very low safety significance and an NCV of Technical
Inspectors reviewed the event, evaluation, and corrective actions for the motor operated  
      Specification (TS) 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool Spray,
valve failure reported in Licensee Event Report (LER) 05000254/2009-003.   Documents  
      was self-revealed for the licensees failure to meet the TS limiting condition for operation
reviewed as part of this inspection are listed in the Attachment to this report. This LER is  
      (LCO) requirements prior to transitioning into an operating mode where the LCO was
closed.  
      required to be satisfied. Specifically, MO 1-1001-37B, motor operator for the Unit 1 RHR
This event follow-up review constituted one sample as defined in IP 71153-05.  
      torus (suppression pool) spray isolation valve, was found to have been inoperable when
b.  
      the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. The
Findings  
      valve actuator had been inadvertently declutched (i.e., motor disengaged) and the valve
Introduction: A finding of very low safety significance and an NCV of Technical  
      was not demonstrated operable by stroking the valve electrically after the actuator motor
Specification (TS) 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool Spray,  
      was declutched.
was self-revealed for the licensees failure to meet the TS limiting condition for operation  
                                                27                                      Enclosure
(LCO) requirements prior to transitioning into an operating mode where the LCO was  
required to be satisfied. Specifically, MO 1-1001-37B, motor operator for the Unit 1 RHR  
torus (suppression pool) spray isolation valve, was found to have been inoperable when  
the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. The  
valve actuator had been inadvertently declutched (i.e., motor disengaged) and the valve  
was not demonstrated operable by stroking the valve electrically after the actuator motor  
was declutched.  


Discussion: On June 4, 2009, with Unit 1 in Mode 1 at 100 percent power following
startup from a forced outage, MO 1-1001-37B, torus spray shutoff valve, was determined
to be inoperable because it would not open remotely using the control switch during
28
performance of the residual heat removal power operated valve test surveillance.
Enclosure
The torus spray valve had been closed using the motor and a clearance order had been
Discussion: On June 4, 2009, with Unit 1 in Mode 1 at 100 percent power following  
placed on the valve during the outage. Another motor operated valve in the residual
startup from a forced outage, MO 1-1001-37B, torus spray shutoff valve, was determined  
heat removal system on that same clearance, MO 1-1001-7C, RHR C torus suction line
to be inoperable because it would not open remotely using the control switch during  
isolation valve, had failed to open on May 28, 2009, when the clearance tag was
performance of the residual heat removal power operated valve test surveillance.  
removed and valve stroking was being performed to restore the component to a standby
The torus spray valve had been closed using the motor and a clearance order had been  
configuration. Operators reported manually declutching (disengaging the actuator
placed on the valve during the outage. Another motor operated valve in the residual  
motor) the 7C valve while placing the clearance tag in order to verify the valve was
heat removal system on that same clearance, MO 1-1001-7C, RHR C torus suction line  
closed. Inspectors identified that the action of manually verifying valve position was not
isolation valve, had failed to open on May 28, 2009, when the clearance tag was  
a normal practice as supported by OP-AA-103-105, Limitorque Motor-Operated Valve
removed and valve stroking was being performed to restore the component to a standby  
Operations, and Operations department management. Investigation into the 7C failure
configuration. Operators reported manually declutching (disengaging the actuator  
revealed that the actuator lubricant was degraded in the area of the clutch return spring
motor) the 7C valve while placing the clearance tag in order to verify the valve was  
preventing the motor from engaging when called upon from the control circuit. The
closed. Inspectors identified that the action of manually verifying valve position was not  
RHR C valve actuator was rebuilt using MOV Long Life grease, new tripper cams, new
a normal practice as supported by OP-AA-103-105, Limitorque Motor-Operated Valve  
trip lever assembly, and a new outer declutch arm snap ring. The rebuilt actuator was
Operations, and Operations department management. Investigation into the 7C failure  
verified to operate correctly in all modes and returned to service prior to unit restart on
revealed that the actuator lubricant was degraded in the area of the clutch return spring  
May 30, 2009.
preventing the motor from engaging when called upon from the control circuit. The  
Inspectors interviewed operating personnel regarding the positioning of MO 1-1001-37B
RHR C valve actuator was rebuilt using MOV Long Life grease, new tripper cams, new  
torus spray valve. Operators stated that they did not manually declutch the 37B valve
trip lever assembly, and a new outer declutch arm snap ring. The rebuilt actuator was  
since the valve was already closed (normal position) when they hung the tag. The
verified to operate correctly in all modes and returned to service prior to unit restart on  
licensees investigation attempted to identify both how the motor on the 37B valve was
May 30, 2009.  
declutched and why the actuator did not return to the motor mode of operation
Inspectors interviewed operating personnel regarding the positioning of MO 1-1001-37B  
automatically as designed. The licensee verified that the actuator was not able to
torus spray valve. Operators stated that they did not manually declutch the 37B valve  
transition from the motor mode to the manual mode without external (human)
since the valve was already closed (normal position) when they hung the tag. The  
intervention.
licensees investigation attempted to identify both how the motor on the 37B valve was  
Although the licensee could not identify how or when the valve actuator motor was
declutched and why the actuator did not return to the motor mode of operation  
declutched, the licensees investigators concluded that the declutch lever was most likely
automatically as designed. The licensee verified that the actuator was not able to  
bumped during work activities on top of the Torus during the recent outage with the unit
transition from the motor mode to the manual mode without external (human)  
in Mode 4. Investigation further determined that with the valve motor disengaged,
intervention.  
increased friction in the actuator caused by degraded lubricant in the area of the clutch
Although the licensee could not identify how or when the valve actuator motor was  
return spring prevented the engagement of the motor to open the valve. The actuator
declutched, the licensees investigators concluded that the declutch lever was most likely  
motor was engaged by manually manipulating the declutch lever and stroke testing the
bumped during work activities on top of the Torus during the recent outage with the unit  
valve.
in Mode 4. Investigation further determined that with the valve motor disengaged,  
Inspectors reviewed the grease sampling methodology and the preventative
increased friction in the actuator caused by degraded lubricant in the area of the clutch  
maintenance frequency for the SMP-00 type actuators and determined that both were
return spring prevented the engagement of the motor to open the valve. The actuator  
conducted in accordance with the industry standards for these type valves.
motor was engaged by manually manipulating the declutch lever and stroke testing the  
Analysis: The failure of plant personnel to demonstrate operability of MO 1-1001-37B by
valve.  
stroking the valve electrically prior to changing modes was a performance deficiency.
Inspectors reviewed the grease sampling methodology and the preventative  
The finding is more than minor because it was associated with the equipment
maintenance frequency for the SMP-00 type actuators and determined that both were  
performance quality attribute of the Mitigating Systems Cornerstone and affected the
conducted in accordance with the industry standards for these type valves.  
objective of ensuring availability, reliability and capability of systems that respond to
Analysis: The failure of plant personnel to demonstrate operability of MO 1-1001-37B by  
initiating events to prevent undesirable consequences. Specifically, failure to verify
stroking the valve electrically prior to changing modes was a performance deficiency.
system availability and capability prior to entering the required modes resulted in fewer
The finding is more than minor because it was associated with the equipment  
                                            28                                      Enclosure
performance quality attribute of the Mitigating Systems Cornerstone and affected the  
objective of ensuring availability, reliability and capability of systems that respond to  
initiating events to prevent undesirable consequences. Specifically, failure to verify  
system availability and capability prior to entering the required modes resulted in fewer  


available mitigating systems than assumed in the operating risk evaluations. Inspectors
determined that the finding was cross-cutting in the area of Problem Identification and
Resolution - Corrective Action because plant personnel failed to identify the valve
29
actuator contact that resulted in the valve being declutched; therefore, operators
Enclosure
incorrectly assessed the system condition as in compliance with TS 3.6.2.4 (P.1(a)).
available mitigating systems than assumed in the operating risk evaluations. Inspectors  
The inspectors determined the finding could be evaluated using the SDP in accordance
determined that the finding was cross-cutting in the area of Problem Identification and  
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -
Resolution - Corrective Action because plant personnel failed to identify the valve  
Initial Screening and Characterization of Findings, Table 4a. Inspectors answered all of
actuator contact that resulted in the valve being declutched; therefore, operators  
the questions for the Mitigating Systems Cornerstone No. Therefore, the finding
incorrectly assessed the system condition as in compliance with TS 3.6.2.4 (P.1(a)).  
screened as Green or very low safety significance.
The inspectors determined the finding could be evaluated using the SDP in accordance  
Enforcement: Technical Specification 3.0, Limiting Condition for Operation (LCO)
with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -  
Applicability, LCO 3.0.4 stated in part that when an LCO is not met, entry into a mode in
Initial Screening and Characterization of Findings, Table 4a. Inspectors answered all of  
the Applicability shall only be made:
the questions for the Mitigating Systems Cornerstone No. Therefore, the finding  
*       when the associated actions to be entered permit continued operation while in
screened as Green or very low safety significance.  
        the mode or other specified condition in the Applicability for an unlimited time;
Enforcement: Technical Specification 3.0, Limiting Condition for Operation (LCO)  
*       after performance of a risk assessment addressing inoperable systems and
Applicability, LCO 3.0.4 stated in part that when an LCO is not met, entry into a mode in  
        components, and acceptability of entering the mode; or
the Applicability shall only be made:  
*       when an allowance is stated in the specification.
*  
Technical Specification 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool
when the associated actions to be entered permit continued operation while in  
Spray, required two RHR suppression pool spray subsystems to be operable in
the mode or other specified condition in the Applicability for an unlimited time;  
Modes 1, 2 and 3.
*  
Contrary to the above, on May 30, 2009, the licensee changed operating modes from
after performance of a risk assessment addressing inoperable systems and  
Mode 4 to Mode 2 with the MO 1-1001-37B valve inoperable in violation of TS 3.6.2.4
components, and acceptability of entering the mode; or  
LCO conditions since only one RHR suppression pool (Torus) spray subsystem was
*  
operable. Specifically, TS 3.6.2.4 had no allowance provided to permit mode change
when an allowance is stated in the specification.  
with less than two subsystems operable, no prior risk assessment was performed, and
Technical Specification 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool  
the specification did not permit operation for an unlimited time, the mode change
Spray, required two RHR suppression pool spray subsystems to be operable in  
resulted in non-compliance with TS LCO 3.6.2.4.
Modes 1, 2 and 3.  
Because this finding is of very low safety significance, and this issue has been entered
Contrary to the above, on May 30, 2009, the licensee changed operating modes from  
into the licensees corrective action program as IR 928048, this violation is being treated
Mode 4 to Mode 2 with the MO 1-1001-37B valve inoperable in violation of TS 3.6.2.4  
as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy
LCO conditions since only one RHR suppression pool (Torus) spray subsystem was  
(NCV 05000254/2009005-04).
operable. Specifically, TS 3.6.2.4 had no allowance provided to permit mode change  
Immediate corrective actions for this event included engagement of the actuator motor
with less than two subsystems operable, no prior risk assessment was performed, and  
by manually manipulating the declutch lever and stroke testing the valve. Since the
the specification did not permit operation for an unlimited time, the mode change  
hardened grease in this area of the actuator assembly was only an issue if the actuator
resulted in non-compliance with TS LCO 3.6.2.4.  
was manually declutched, the valve was left in standby, and overhaul of the valve
Because this finding is of very low safety significance, and this issue has been entered  
actuator was scheduled for the next refueling outage.
into the licensees corrective action program as IR 928048, this violation is being treated  
                                          29                                        Enclosure
as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy  
(NCV 05000254/2009005-04).  
Immediate corrective actions for this event included engagement of the actuator motor  
by manually manipulating the declutch lever and stroke testing the valve. Since the  
hardened grease in this area of the actuator assembly was only an issue if the actuator  
was manually declutched, the valve was left in standby, and overhaul of the valve  
actuator was scheduled for the next refueling outage.  


4OA5 Other Activities
.1   World Association of Nuclear Operators Plant Assessment Report Review
  a. Inspection Scope
30
      The inspectors reviewed the final report for the World Association of Nuclear Operators
Enclosure
      plant assessment conducted in February 2009. The inspectors reviewed the report to
4OA5 Other Activities  
      ensure that issues identified were consistent with the NRC perspectives of licensee
.1  
      performance and to verify if any significant safety issues were identified that required
World Association of Nuclear Operators Plant Assessment Report Review  
      further NRC followup.
a.  
  b. Findings
Inspection Scope  
      No findings of significance were identified.
The inspectors reviewed the final report for the World Association of Nuclear Operators  
.2   Quarterly Resident Inspector Observations of Security Personnel and Activities
plant assessment conducted in February 2009. The inspectors reviewed the report to  
  a. Inspection Scope
ensure that issues identified were consistent with the NRC perspectives of licensee  
      During the inspection period, the inspectors conducted observations of security force
performance and to verify if any significant safety issues were identified that required  
      personnel and activities to ensure that the activities were consistent with licensee
further NRC followup.  
      security procedures and regulatory requirements relating to nuclear plant security.
b.  
      These observations took place during both normal and off-normal plant working hours.
Findings  
      These quarterly resident inspector observations of security force personnel and activities
No findings of significance were identified.  
      did not constitute any additional inspection samples. Rather, they were considered an
.2  
      integral part of the inspectors' normal plant status review and inspection activities.
Quarterly Resident Inspector Observations of Security Personnel and Activities  
  b. Findings
a.  
      No findings of significance were identified.
Inspection Scope  
4OA6 Management Meetings
During the inspection period, the inspectors conducted observations of security force  
.1   Exit Meeting Summary
personnel and activities to ensure that the activities were consistent with licensee  
      On January 5, 2010, the inspectors presented the inspection results to T. Tulon and
security procedures and regulatory requirements relating to nuclear plant security.
      other members of the licensee staff. The licensee acknowledged the issues presented.
These observations took place during both normal and off-normal plant working hours.  
      The inspectors confirmed that none of the potential report input discussed was
These quarterly resident inspector observations of security force personnel and activities  
      considered proprietary.
did not constitute any additional inspection samples. Rather, they were considered an  
.2   Interim Exit Meetings
integral part of the inspectors' normal plant status review and inspection activities.  
      Interim exits were conducted for:
b.  
      *       The results of the licensed operator requalification training program inspection
Findings  
              and with the site vice president, Mr. T. Tulon, on October 2, 2009.
No findings of significance were identified.  
      *       The licensed operator requalification training biennial written examination and
4OA6 Management Meetings  
              annual operating test examination materials were discussed with the training
.1  
              manager, Mr. K. Moser, on November 12, 2009.
Exit Meeting Summary  
                                                30                                      Enclosure
On January 5, 2010, the inspectors presented the inspection results to T. Tulon and  
other members of the licensee staff. The licensee acknowledged the issues presented.
The inspectors confirmed that none of the potential report input discussed was  
considered proprietary.  
.2  
Interim Exit Meetings  
Interim exits were conducted for:  
*  
The results of the licensed operator requalification training program inspection  
and with the site vice president, Mr. T. Tulon, on October 2, 2009.  
*  
The licensed operator requalification training biennial written examination and  
annual operating test examination materials were discussed with the training  
manager, Mr. K. Moser, on November 12, 2009.  


    *       The licensed operator requalification training program annual inspection results
              with operations training manager, Mr. D. Snook, on November 20, 2009, via
              telephone.
31
    *       The results of the Radiological Effluent TS/Offsite Dose Calculation Manual
Enclosure
              Radiological Effluent Occurrences performance indicator verification program
*  
              inspection with the plant manager, Mr. R. Gideon, on December 16, 2009.
The licensed operator requalification training program annual inspection results  
    *       The annual review of Emergency Action Level and Emergency Plan changes
with operations training manager, Mr. D. Snook, on November 20, 2009, via  
              with the licensee's emergency preparedness coordinator, Mr. F. Swan, via
telephone.  
              telephone on December 21, 2009.
*  
    The inspectors confirmed that none of the potential report input discussed was
The results of the Radiological Effluent TS/Offsite Dose Calculation Manual  
    considered proprietary. Proprietary material received during the inspection was returned
Radiological Effluent Occurrences performance indicator verification program  
    to the licensee.
inspection with the plant manager, Mr. R. Gideon, on December 16, 2009.  
4OA7 Licensee-Identified Violations
*  
    The following violation of very low significance (Green) was identified by the licensee
The annual review of Emergency Action Level and Emergency Plan changes  
    and is a violation of NRC requirements which meets the criteria of Section VI of the
with the licensee's emergency preparedness coordinator, Mr. F. Swan, via  
    NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.
telephone on December 21, 2009.  
    *       Technical Specification 5.5.1 requires implementation of the Offsite Dose
The inspectors confirmed that none of the potential report input discussed was  
              Calculation Manual. Offsite Dose Calculation Manual, Revision 8, Part 12.2.1,
considered proprietary. Proprietary material received during the inspection was returned  
              Radioactive Liquid Effluent Monitoring Instrumentation, Section C requires that
to the licensee.  
              when the service water effluent gross activity monitor is operated with less than
4OA7 Licensee-Identified Violations  
              the minimum number of operable channels, the licensee shall collect and analyze
The following violation of very low significance (Green) was identified by the licensee  
              grab samples for beta or gamma activity once per 12 hours. Contrary to the
and is a violation of NRC requirements which meets the criteria of Section VI of the  
              above, grab samples were not collected while the Unit 1 service water effluent
NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.  
              gross activity monitor was inoperable from June 2-20, 2009. Specifically,
*  
              following fuse replacement, the licensee failed to recognize that the instrument
Technical Specification 5.5.1 requires implementation of the Offsite Dose  
              remained uninitialized; therefore, that compensatory samples were required. The
Calculation Manual. Offsite Dose Calculation Manual, Revision 8, Part 12.2.1,  
              finding was documented in the licensees corrective action program as
Radioactive Liquid Effluent Monitoring Instrumentation, Section C requires that  
              IR 933472. Corrective actions included returning the monitor to service and
when the service water effluent gross activity monitor is operated with less than  
              reviewing captured monitor data from June 2-20, 2009, to ensure that no release
the minimum number of operable channels, the licensee shall collect and analyze  
              events occurred during the monitor outage, revising the monitor repair and
grab samples for beta or gamma activity once per 12 hours. Contrary to the  
              maintenance procedures to clear direct communication with the Chemistry
above, grab samples were not collected while the Unit 1 service water effluent  
              Department subject matter experts during work on the system, and reinforcing
gross activity monitor was inoperable from June 2-20, 2009. Specifically,  
              the expectation that control room operators turn over all abnormal indications to
following fuse replacement, the licensee failed to recognize that the instrument  
              supervisors each shift. The finding was determined to be of very low safety
remained uninitialized; therefore, that compensatory samples were required. The  
              significance because, although the finding related to the effluent release
finding was documented in the licensees corrective action program as  
              program, it was not a failure to implement the effluent program or an event that
IR 933472. Corrective actions included returning the monitor to service and  
              resulted in a dose to the public in excess of Appendix I criterion or
reviewing captured monitor data from June 2-20, 2009, to ensure that no release  
              10 CFR 20.1301(e).
events occurred during the monitor outage, revising the monitor repair and  
ATTACHMENT: SUPPLEMENTAL INFORMATION
maintenance procedures to clear direct communication with the Chemistry  
                                                31                                      Enclosure
Department subject matter experts during work on the system, and reinforcing  
the expectation that control room operators turn over all abnormal indications to  
supervisors each shift. The finding was determined to be of very low safety  
significance because, although the finding related to the effluent release  
program, it was not a failure to implement the effluent program or an event that  
resulted in a dose to the public in excess of Appendix I criterion or  
10 CFR 20.1301(e).  
ATTACHMENT: SUPPLEMENTAL INFORMATION  


                              SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee
1
T. Tulon, Site Vice President
Attachment
R. Gideon, Plant Manager
SUPPLEMENTAL INFORMATION  
D. Kimler, Shift Operations Superintendent
KEY POINTS OF CONTACT  
S. Darin, Engineering Manager
Licensee  
W. Beck, Regulatory Assurance Manager
T. Tulon, Site Vice President  
J. Burkhead, Nuclear Oversight Manager
R. Gideon, Plant Manager  
J. Garrity, Work Control Manager
D. Kimler, Shift Operations Superintendent  
K. Moser, Training Manager
S. Darin, Engineering Manager  
V. Neels, Chemistry/Environ/Radwaste Manager
W. Beck, Regulatory Assurance Manager  
D. Collins, Radiation Protection Manager
J. Burkhead, Nuclear Oversight Manager  
D. Thompson, Security Manager
J. Garrity, Work Control Manager  
Nuclear Regulatory Commission
K. Moser, Training Manager  
M. Ring, Chief, Reactor Projects Branch 1
V. Neels, Chemistry/Environ/Radwaste Manager  
Illinois Emergency Management Agency
D. Collins, Radiation Protection Manager  
R. Zuffa, Unit Supervisor, Resident Inspector Section
D. Thompson, Security Manager  
                    LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
Opened
Nuclear Regulatory Commission  
05000254/2009005-01;       URI   Changes to EAL HU6 Potentially Decrease the Effectiveness
05000265/2009005-01              of the Plans without Prior NRC Approval
M. Ring, Chief, Reactor Projects Branch 1  
05000254/2009005-02;       FIN   Darley Pump Leaking Gasoline from the Fuel Pump
05000265/2009005-02
Illinois Emergency Management Agency
05000265/2009005-03        NCV   Temperature Indicating Probe Found Broken in the Unit 2
                                  Diesel Generator Coolant System
R. Zuffa, Unit Supervisor, Resident Inspector Section  
05000254/2009005-04       NCV   Failure of RHR Torus Spray Isolation Valve to Open Due to
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED  
                                  Declutch Mechanism Problems
Opened  
Closed
05000254/2009005-01;  
05000254/2009005-02;       FIN   Darley Pump Leaking Gasoline from the Fuel Pump
05000265/2009005-01
05000265/2009005-02
URI  
05000265/2009005-03        NCV   Temperature Indicating Probe Found Broken in the Unit 2
Changes to EAL HU6 Potentially Decrease the Effectiveness  
                                  Diesel Generator Coolant System
of the Plans without Prior NRC Approval  
05000254/2009005-04       NCV   Failure of RHR Torus Spray Isolation Valve to Open Due to
05000254/2009005-02;  
                                  Declutch Mechanism Problems
05000265/2009005-02
05000254/2009003-00       LER   Failure of RHR Torus Spray Isolation Valve to Open Due to
FIN  
                                  Declutch Mechanism Problems
Darley Pump Leaking Gasoline from the Fuel Pump  
                                                1                                  Attachment
05000265/2009005-03
NCV  
Temperature Indicating Probe Found Broken in the Unit 2  
Diesel Generator Coolant System  
05000254/2009005-04  
NCV  
Failure of RHR Torus Spray Isolation Valve to Open Due to  
Declutch Mechanism Problems  
Closed  
05000254/2009005-02;  
05000265/2009005-02
FIN  
Darley Pump Leaking Gasoline from the Fuel Pump  
05000265/2009005-03
NCV  
Temperature Indicating Probe Found Broken in the Unit 2  
Diesel Generator Coolant System  
05000254/2009005-04  
NCV  
Failure of RHR Torus Spray Isolation Valve to Open Due to  
Declutch Mechanism Problems  
05000254/2009003-00  
LER  
Failure of RHR Torus Spray Isolation Valve to Open Due to  
Declutch Mechanism Problems  


                                  LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that
2
selected sections of portions of the documents were evaluated as part of the overall inspection
Attachment
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
LIST OF DOCUMENTS REVIEWED  
any part of it, unless this is stated in the body of the inspection report.
The following is a list of documents reviewed during the inspection. Inclusion on this list does  
Section 1R01
not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that  
- QCOP 0010-01; Winterizing Checklist; Revision 48
selected sections of portions of the documents were evaluated as part of the overall inspection  
- QCOP 0010-02; Required Cold Weather Routines; Revision 28
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or  
- WC-AA-107; Seasonal Readiness; Revision 06
any part of it, unless this is stated in the body of the inspection report.  
- IR 99493; U-2 FW Heater LCV Response to Lowering Circulating Water Inlet Temp
Section 1R01  
- WO 1183498; Cycle CW De-Ice Valve
- QCOP 0010-01; Winterizing Checklist; Revision 48  
- WO 1282535; Ice Melt Valve Stuck Shut
- QCOP 0010-02; Required Cold Weather Routines; Revision 28  
- QCOP 4400-06; Circulating Water System De-icing; Revision 14
- WC-AA-107; Seasonal Readiness; Revision 06  
- ECR 59777; Design Alternate Method for Operation of Ice Melt Valve
- IR 99493; U-2 FW Heater LCV Response to Lowering Circulating Water Inlet Temp  
- IR 993018; Wire Rope Rating on Ice Melt Valve
- WO 1183498; Cycle CW De-Ice Valve  
- IR 986355; Ice Melt Valve Stuck Shut
- WO 1282535; Ice Melt Valve Stuck Shut  
- WO 01194645; MM Union Leaking Inside U1 Cond Demin Vault (HTG STM)
- QCOP 4400-06; Circulating Water System De-icing; Revision 14  
- WO 01215488; MM Repair Piping Leak Underground Next to Cribhouse
- ECR 59777; Design Alternate Method for Operation of Ice Melt Valve  
- WO 01242820; MM Seal Cracks in Ceiling Above Bus 23-1
- IR 993018; Wire Rope Rating on Ice Melt Valve  
Section 1R04
- IR 986355; Ice Melt Valve Stuck Shut  
- QCOP 4100-01; Firewater System Lineup for Standby Operation; Revision 4
- WO 01194645; MM Union Leaking Inside U1 Cond Demin Vault (HTG STM)  
- QCOP 6600-01: Diesel Generator 1(2) Preparation For Standby Operation; Revision 38
- WO 01215488; MM Repair Piping Leak Underground Next to Cribhouse  
- WO #01272234; EM Change RMS-9 Setting at SWGR 19 CUB 5D Per EC 377092
- WO 01242820; MM Seal Cracks in Ceiling Above Bus 23-1  
- WO #01107582; EM Replace U2 DGCWP Alternate Feed Contactor
Section 1R04  
- WO #920850; IM CAL DG HX 2-6661B Cooling Water Inlet PI 2-3941-67A
- QCOP 4100-01; Firewater System Lineup for Standby Operation; Revision 4  
- WO #945963; IM CAL DG HX 2-6661B Cooling Water Outlet PI 2-3941-67B
- QCOP 6600-01: Diesel Generator 1(2) Preparation For Standby Operation; Revision 38  
- WO #01107581; EM Replace U2 DGCWP Normal Feed Contactor
- WO #01272234; EM Change RMS-9 Setting at SWGR 19 CUB 5D Per EC 377092  
- WO #01245102; EM Support OP QCOS 6600-17 U2 DGCW Pump Alternate Feed Test
- WO #01107582; EM Replace U2 DGCWP Alternate Feed Contactor  
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for
- WO #920850; IM CAL DG HX 2-6661B Cooling Water Inlet PI 2-3941-67A  
  Appendix R; Revision 15
- WO #945963; IM CAL DG HX 2-6661B Cooling Water Outlet PI 2-3941-67B  
- EC 360507; Unit 2 EDG Voltage Regulator (Place EDG in Droop Mode Prior to
- WO #01107581; EM Replace U2 DGCWP Normal Feed Contactor  
  Synchronization to the Grid)
- WO #01245102; EM Support OP QCOS 6600-17 U2 DGCW Pump Alternate Feed Test  
- EC 377665; TMOD to Bypass Faulty SSES Switch Local/Remote Contact at U2 Diesel
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for  
  Generator
Appendix R; Revision 15  
Section 1R05
- EC 360507; Unit 2 EDG Voltage Regulator (Place EDG in Droop Mode Prior to  
- OP-AA-201-008; Pre-fire Plan Manual Index - Pre-Plan RB-16; Revision 2
Synchronization to the Grid)  
- Pre-plan TB-74; Fire Zone 9.1, Unit 1 Turbine Bldg. El. 595-0, Diesel Generator; Revision 24
- EC 377665; TMOD to Bypass Faulty SSES Switch Local/Remote Contact at U2 Diesel  
- Pre-plan TB-73; Fire Zone 8.2.6.A, Unit 1 Turbine Bldg. El. 595-0, Reactor Feed Pumps;
Generator  
  Revision 24
Section 1R05  
- Pre-plan CH-44; Fire Zone 11.4.A, Crib House Bldg. El. 559-8 Basement; Revision 0
- OP-AA-201-008; Pre-fire Plan Manual Index - Pre-Plan RB-16; Revision 2  
- Pre-plan CH-45; Fire Zone 11.4.B, Ground Floor/Service Water Pumps; Revision 22
- Pre-plan TB-74; Fire Zone 9.1, Unit 1 Turbine Bldg. El. 595-0, Diesel Generator; Revision 24  
                                                    2                                  Attachment
- Pre-plan TB-73; Fire Zone 8.2.6.A, Unit 1 Turbine Bldg. El. 595-0, Reactor Feed Pumps;  
Revision 24  
- Pre-plan CH-44; Fire Zone 11.4.A, Crib House Bldg. El. 559-8 Basement; Revision 0  
- Pre-plan CH-45; Fire Zone 11.4.B, Ground Floor/Service Water Pumps; Revision 22  


Section 1R11
- SY-AA-101-132; Assessment and Response to Suspicious Activity and Security Threats;
  Revision 14
3
- QCOA 0010-20; Security Event; Revision 25
Attachment
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27
Section 1R11  
- Requalification Examination Results/Calendar Year 2009
- SY-AA-101-132; Assessment and Response to Suspicious Activity and Security Threats;  
- Quad Cities, Units 1 and 2 NRC Integrated Inspection Reports; dated various from
Revision 14  
  January 2007 through September 2009
- QCOA 0010-20; Security Event; Revision 25  
- OP-AA-105-102; Attachment 1; Active License Tracking Log (for 1st & 2nd Quarters of 2009);
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27  
  Revision 9
- Requalification Examination Results/Calendar Year 2009  
- OP-AA-105-102; Attachment 2, Reactivation of License Log (2 for LSRO, 2 RO); Revision 9
- Quad Cities, Units 1 and 2 NRC Integrated Inspection Reports; dated various from  
- Quad Cities Classroom Sample Plan for Training Years 2008 and 2009; 6/18/2009
January 2007 through September 2009  
- Quad Cities Simulator Sample Plan for Training Years 2008 and 2009
- OP-AA-105-102; Attachment 1; Active License Tracking Log (for 1st & 2nd Quarters of 2009);  
- 71111.11 Appendix C Responses/Justifications; 9/28/2009
Revision 9  
- TQ-AA-224-F070; Evaluation Feedback Summary, LORT Cycle 08-1 through 08-5; LORT
- OP-AA-105-102; Attachment 2, Reactivation of License Log (2 for LSRO, 2 RO); Revision 9  
  Cycle 09-1 through 09-4
- Quad Cities Classroom Sample Plan for Training Years 2008 and 2009; 6/18/2009  
- TQ-AA-1002; Attachment 3; LORT Quarterly Curriculum Review Committee Meeting Minutes;
- Quad Cities Simulator Sample Plan for Training Years 2008 and 2009  
  all of 2008 and first two quarters of 2009
- 71111.11 Appendix C Responses/Justifications; 9/28/2009  
- Special LORT CRC Meeting Minutes; 1/23/2009
- TQ-AA-224-F070; Evaluation Feedback Summary, LORT Cycle 08-1 through 08-5; LORT  
- TQ-AA-150; Operator Training Programs; Revision 2
Cycle 09-1 through 09-4  
- TQ-AA-150-F07; Simulator Evaluation Form - STA or IA
- TQ-AA-1002; Attachment 3; LORT Quarterly Curriculum Review Committee Meeting Minutes;  
- TQ-AA-150-F08; Simulator Evaluation Form - Individual
all of 2008 and first two quarters of 2009  
- TQ-AA-150-F09; Simulator Evaluation Form - Crew
- Special LORT CRC Meeting Minutes; 1/23/2009  
- TQ-AA-210-5101; Training Observation Forms; dated various
- TQ-AA-150; Operator Training Programs; Revision 2  
- TQ-AA-306; Simulator Management
- TQ-AA-150-F07; Simulator Evaluation Form - STA or IA  
- TQ-AA-306-F06; BWR Critical Condition for Cold Startup; Revision 0
- TQ-AA-150-F08; Simulator Evaluation Form - Individual  
- TQ-AA-306-F07; BWR Power Coefficient of Reactivity and Control Rod Worth; Revision 0
- TQ-AA-150-F09; Simulator Evaluation Form - Crew  
- TQ-AA-306-F08; BWR Xenon Worth; Revision 0
- TQ-AA-210-5101; Training Observation Forms; dated various  
- TQ-AA-306-F06; BWR Site Specific Shutdown Margin and Reactivity Anomaly Tests
- TQ-AA-306; Simulator Management  
- TQ-AA-306-JA-02; Simulator Testing Report Update
- TQ-AA-306-F06; BWR Critical Condition for Cold Startup; Revision 0  
- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 14;
- TQ-AA-306-F07; BWR Power Coefficient of Reactivity and Control Rod Worth; Revision 0  
  7/17/09
- TQ-AA-306-F08; BWR Xenon Worth; Revision 0  
- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 15;
- TQ-AA-306-F06; BWR Site Specific Shutdown Margin and Reactivity Anomaly Tests  
  9/29/09
- TQ-AA-306-JA-02; Simulator Testing Report Update  
- LS-AA-126-1005; Attachment 2; Check-In Self-Assessment Report Template
- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 14;  
- LS-AA-126-1001; Attachment 2; FASA Self-Assessment Report
7/17/09  
- Simulator Malfunction Test Procedure, Grid Frequency Disturbance (ED16)
- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 15;  
- Simulator Malfunction Test Procedure, Reactor Building Instrument Air System (IA02)
9/29/09  
- Simulator Malfunction Test Procedure, Main Steam Isolation Valve Closure (MS01)
- LS-AA-126-1005; Attachment 2; Check-In Self-Assessment Report Template  
- Quad Cities Simulator Malfunction Testing Schedule; Revision 8; 5/5/2008
- LS-AA-126-1001; Attachment 2; FASA Self-Assessment Report  
- Simulator Transient Tests; dated various
- Simulator Malfunction Test Procedure, Grid Frequency Disturbance (ED16)  
- Safety System Functional Failure, Rolling Twelve Months Unit 1 and Unit 2; 9/28/09
- Simulator Malfunction Test Procedure, Reactor Building Instrument Air System (IA02)  
- Action Request Reports; various dates for LORT 2009
- Simulator Malfunction Test Procedure, Main Steam Isolation Valve Closure (MS01)  
- LORT Attendance Sheets; 2009
- Quad Cities Simulator Malfunction Testing Schedule; Revision 8; 5/5/2008  
                                              3                                    Attachment
- Simulator Transient Tests; dated various  
- Safety System Functional Failure, Rolling Twelve Months Unit 1 and Unit 2; 9/28/09
- Action Request Reports; various dates for LORT 2009  
- LORT Attendance Sheets; 2009  


Section 1R12
- Enterprise Maintenance Rule Production Database for the following systems:
      *     Z2900; Safe Shutdown Makeup Pump
4
      *     Z4700; Instrument Air
Attachment
- System Engineer Notebook and Accountability Logs for the following systems:
Section 1R12  
      *     Safe Shutdown Makeup Pump
- Enterprise Maintenance Rule Production Database for the following systems:  
      *     Instrument Air
*  
- IR 712670; Safe shutdown makeup pump failed surveillance; 12/17/07
Z2900; Safe Shutdown Makeup Pump  
- IR 713041; Broken SSMP part not found during repairs; 12/18/07
*  
- IR 711934; SSMP Suction line did not fill during fill; 12/14/07
Z4700; Instrument Air  
- IR 712059; SSMP fails to sustain flow and pressure; 12/15/07
- System Engineer Notebook and Accountability Logs for the following systems:  
- IR 731013; SSMP Sparking on Startup; 2/4/08
*  
- IR 729984; SSMP failed operability test per TIC-1982; 2/1/08
Safe Shutdown Makeup Pump  
- IR 729951; SSMP Local FIC failed PMT; 1/31/08
*  
- IR 734472; MRULE A-1 determination for SSMP required; 2/11/08
Instrument Air  
- IR 741838; SSMP feed breaker problems during system restoration; 2/27/08
- IR 712670; Safe shutdown makeup pump failed surveillance; 12/17/07  
- IR 787063; Local SSMP flow controller not reading correctly; 6/16/08
- IR 713041; Broken SSMP part not found during repairs; 12/18/07  
- IR 890904; SSMP controller connector degraded; 3/10/09
- IR 711934; SSMP Suction line did not fill during fill; 12/14/07  
- IR 930013; Historical FME identified in SSMP piping inspection; 6/10/09
- IR 712059; SSMP fails to sustain flow and pressure; 12/15/07  
- IR 956294; SSMP FIC Valve position discrepancy with local valve indication; 8/21/09
- IR 731013; SSMP Sparking on Startup; 2/4/08  
- IR 947201; FPI - SSMP Breaker and fuse coordination for CT-2; 7/29/08
- IR 729984; SSMP failed operability test per TIC-1982; 2/1/08  
- IR 1003024; SSMP Draws a vacuum when starting for PMT; 12/09/09
- IR 729951; SSMP Local FIC failed PMT; 1/31/08  
- IR 1002036; Drain valve for SSMP room cooler may be blocked; 12/06/09
- IR 734472; MRULE A-1 determination for SSMP required; 2/11/08  
- IR 991490; NCV 09-006-02 Closure package - SSMP Breaker coordination 11/10/09
- IR 741838; SSMP feed breaker problems during system restoration; 2/27/08  
- IR 673268; 1B Instrument Air Compressor Excessive Leakage; 9/20/07
- IR 787063; Local SSMP flow controller not reading correctly; 6/16/08  
- IR 762652; 1A Instrument Air Compressor Trip; 04/12/08
- IR 890904; SSMP controller connector degraded; 3/10/09  
- IR 856509; Red Trend Code for 1/2B Instrument Air Compressor - EC 364602
- IR 930013; Historical FME identified in SSMP piping inspection; 6/10/09  
- IR 871161; 1A Instrument Air Compressor Trip; 01/24/09
- IR 956294; SSMP FIC Valve position discrepancy with local valve indication; 8/21/09  
- IR 871939; 1A Instrument Air Compressor Trip; 01/26/09
- IR 947201; FPI - SSMP Breaker and fuse coordination for CT-2; 7/29/08  
- IR 977823; 1A Instrument Air Compressor Tripped Due to Low Oil Pressure; 2/7/09
- IR 1003024; SSMP Draws a vacuum when starting for PMT; 12/09/09  
- IR 936122; Compressor does not auto start; 6/27/09
- IR 1002036; Drain valve for SSMP room cooler may be blocked; 12/06/09  
Section 1R13
- IR 991490; NCV 09-006-02 Closure package - SSMP Breaker coordination 11/10/09  
- WO #01075655; EM Perform Boroscope INSP of MO 1-1001-16A MOV
- IR 673268; 1B Instrument Air Compressor Excessive Leakage; 9/20/07  
- WO #01120751; EM MOV 1-1001-37A MOV EQ Inspection
- IR 762652; 1A Instrument Air Compressor Trip; 04/12/08  
- WO #01123089; MM Inspect/Clean 1B RHR Pump Seal Cooler
- IR 856509; Red Trend Code for 1/2B Instrument Air Compressor - EC 364602  
- WO #01131318; EM Votes Test MOV 1-1001-16A
- IR 871161; 1A Instrument Air Compressor Trip; 01/24/09  
- WO #01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
- IR 871939; 1A Instrument Air Compressor Trip; 01/26/09  
Section 1R15
- IR 977823; 1A Instrument Air Compressor Tripped Due to Low Oil Pressure; 2/7/09  
- IR 849245; 1B RHR Room Cooler Heat Exchanger Has Tube Sheet Pitting
- IR 936122; Compressor does not auto start; 6/27/09  
- WO 862709; 1B RHR Air/Water Side Room CLR CLN/INSP
Section 1R13  
- IR 987904; 1A RHR Room Cooler Heat Exchanger Tube Sheet Has Pitting
- WO #01075655; EM Perform Boroscope INSP of MO 1-1001-16A MOV  
- WO 01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
- WO #01120751; EM MOV 1-1001-37A MOV EQ Inspection  
                                                4                                  Attachment
- WO #01123089; MM Inspect/Clean 1B RHR Pump Seal Cooler  
- WO #01131318; EM Votes Test MOV 1-1001-16A  
- WO #01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect
Section 1R15  
- IR 849245; 1B RHR Room Cooler Heat Exchanger Has Tube Sheet Pitting  
- WO 862709; 1B RHR Air/Water Side Room CLR CLN/INSP  
- IR 987904; 1A RHR Room Cooler Heat Exchanger Tube Sheet Has Pitting  
- WO 01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect  


- IR 849681; 1B RHR Room Cooler Reassembled at Risk
- EC 373177; Determination of Minimum Wall Thickness of Tubesheet for RHR Room
  Cooler 1-574B
5
- IR 994823; TS SR 3.8.4.8 Frequency Not Met
Attachment
- QC-SURV-01; Risk Assessment for Missed Surveillance for U2 125 Vdc Battery
- IR 849681; 1B RHR Room Cooler Reassembled at Risk  
Section 1R19
- EC 373177; Determination of Minimum Wall Thickness of Tubesheet for RHR Room  
- QCMMS 4100-32; 1/2 -4101A Diesel Driven Fire Pump Annual Capacity Test; Revision 24
Cooler 1-574B  
- WO 1261246; Replace Battery Changeover Relay R12 EC 376690
- IR 994823; TS SR 3.8.4.8 Frequency Not Met  
- EC 376690; 1/2 A Fire Pump Controller Replace Battery Changeover Relay R12; Revision 1
- QC-SURV-01; Risk Assessment for Missed Surveillance for U2 125 Vdc Battery  
- QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 28
Section 1R19  
- QCOP 4100-03; Diesel Fire Pump Operation; Revision 17
- QCMMS 4100-32; 1/2 -4101A Diesel Driven Fire Pump Annual Capacity Test; Revision 24  
- QCMMS 4100-33; 1/2 - 4101B Diesel Driven Fire Pump Annual Capacity Test; Revision 24
- WO 1261246; Replace Battery Changeover Relay R12 EC 376690  
- WO 1121775; 250 Vdc Battery Charger #2 4 Hour Load Test
- EC 376690; 1/2 A Fire Pump Controller Replace Battery Changeover Relay R12; Revision 1  
- WO 1130534; Control RM HVAC Air Filter Unit In Place DOP LK Test
- QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 28  
- QCOS 5750-02; Control Room Emergency Filter System Test; Revision 45
- QCOP 4100-03; Diesel Fire Pump Operation; Revision 17  
- QCIS 5700-04; Main Control Room Air Filter Unit DOP-Freon Test; Revision 0
- QCMMS 4100-33; 1/2 - 4101B Diesel Driven Fire Pump Annual Capacity Test; Revision 24  
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for
- WO 1121775; 250 Vdc Battery Charger #2 4 Hour Load Test  
  Appendix R; Revision 15
- WO 1130534; Control RM HVAC Air Filter Unit In Place DOP LK Test  
- QCEPM 0400-15; Emergency Diesel Generator Transfer Panel Inspection; Revision 9
- QCOS 5750-02; Control Room Emergency Filter System Test; Revision 45  
- WO 01107582; Replace Unit 2 DGCWP Alternate Feed Contactor
- QCIS 5700-04; Main Control Room Air Filter Unit DOP-Freon Test; Revision 0  
Section 1R22
- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for  
- QCOS 1400-01; Quarterly Core Spray System Flow Rate Test; Revision 38
Appendix R; Revision 15  
- QCOS 1400-07; Core Spray Pump Performance Test; Revision 10
- QCEPM 0400-15; Emergency Diesel Generator Transfer Panel Inspection; Revision 9  
- QCOS 7500-05; Standby Gas Treatment System Monthly Operability Test; Revision 30
- WO 01107582; Replace Unit 2 DGCWP Alternate Feed Contactor  
- QCIS 0300-02; Unit 1 Division 1 Scram Discharge Volume Rochester Instruments Calibration
Section 1R22  
  and Functional Test; Revision 09
- QCOS 1400-01; Quarterly Core Spray System Flow Rate Test; Revision 38  
- QCOS 1600-07, Revision 027; Reactor Coolant Leakage in the Drywell
- QCOS 1400-07; Core Spray Pump Performance Test; Revision 10  
- QCEMS 0230-11; Modified Performance Test of Unit 1(2) 125 Vdc Normal or Alternate
- QCOS 7500-05; Standby Gas Treatment System Monthly Operability Test; Revision 30  
  Battery; Revision 0
- QCIS 0300-02; Unit 1 Division 1 Scram Discharge Volume Rochester Instruments Calibration  
- QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 33
and Functional Test; Revision 09  
- QCOP 6900-24; Transfer of Unit 2 125 Vdc Battery Bus Between Normal and Alternate
- QCOS 1600-07, Revision 027; Reactor Coolant Leakage in the Drywell  
  Battery; Revision 12
- QCEMS 0230-11; Modified Performance Test of Unit 1(2) 125 Vdc Normal or Alternate  
- QCOS 6900-14; Station Battery Allowable Value Verification Surveillance; Revision 13
Battery; Revision 0  
Section 1EP4
- QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 33  
- Quad Cities Station Radiological Emergency Plan Annex; Revisions 25, 26, and 27
- QCOP 6900-24; Transfer of Unit 2 125 Vdc Battery Bus Between Normal and Alternate  
Section 1EP6
Battery; Revision 12  
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27
- QCOS 6900-14; Station Battery Allowable Value Verification Surveillance; Revision 13  
- Quad Cities Generating Station 2009 Termination and Recovery Drill Briefing Package;
Section 1EP4  
  December 2, 2009
- Quad Cities Station Radiological Emergency Plan Annex; Revisions 25, 26, and 27  
- EP-AA-115; Termination and Recovery; Revision 7
Section 1EP6  
- EP-AA-111-F-01; Termination/Recovery Checklist; Revision A
- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27  
                                              5                                    Attachment
- Quad Cities Generating Station 2009 Termination and Recovery Drill Briefing Package;  
December 2, 2009  
- EP-AA-115; Termination and Recovery; Revision 7  
- EP-AA-111-F-01; Termination/Recovery Checklist; Revision A  


Section 4OA1
- CY-QC-120-724; Continuous Liquid Effluent Analysis; Revision 1
- CY-QC-120, 723; Allocation of Radioactive Liquid Discharges; Revision 0
6
- CY-QC-120-720; Plant Effluent Dose Calculations; Revision 4
Attachment
- CY-QC-120-725; Gaseous Release of Tritium Calculation; Revision 1
Section 4OA1  
- Cy-QC-120-726; Fe-55, Sr-89, Sr-90 and Gaseous Alpha Release; Revision 3
- CY-QC-120-724; Continuous Liquid Effluent Analysis; Revision 1  
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline, Revision 6
- CY-QC-120, 723; Allocation of Radioactive Liquid Discharges; Revision 0  
- Enterprise Maintenance Rule Production Database for the following systems:
- CY-QC-120-720; Plant Effluent Dose Calculations; Revision 4  
      *       Z2300; High Pressure Coolant Injection System
- CY-QC-120-725; Gaseous Release of Tritium Calculation; Revision 1  
      *       Z1000; Residual Heat Removal System
- Cy-QC-120-726; Fe-55, Sr-89, Sr-90 and Gaseous Alpha Release; Revision 3  
      *       Z6600; Diesel Generator System
- NEI 99-02; Regulatory Assessment Performance Indicator Guideline, Revision 6  
      *       Z1300; Reactor Core Isolation Cooling System
- Enterprise Maintenance Rule Production Database for the following systems:  
      *       Z9700; 345 kV Switchyard
*  
- System Engineer Notebook and Accountability Logs for the following systems:
Z2300; High Pressure Coolant Injection System  
      *       Residual Heat Removal
*  
      *       RHR Service Water
Z1000; Residual Heat Removal System  
      *       Reactor Core Isolation Cooling
*  
      *       HPCI
Z6600; Diesel Generator System  
      *       Emergency Diesel Generators
*  
Section 4OA2Q
Z1300; Reactor Core Isolation Cooling System  
- IR 984769; Well Broke Off TI in Diesel Generator Coolant System
*  
- WO 1198663; U-2 EDG Eng Temp Indicator TI-2-6641-8205 Not Working
Z9700; 345 kV Switchyard  
- WO 1280197; Well Broke Off TI In U2 Diesel Generator Coolant System
- System Engineer Notebook and Accountability Logs for the following systems:  
- SM-AA-300; Procurement Engineering Support Activities; Revision 5
*  
- IR 624645; Flood Emergency Pump Testing Documentation; 05/02/07
Residual Heat Removal  
- IR 638004; Clarify UFSAR 3.4.1.1 Required Flow Rate to SFP During Flood; 06/07/07
*  
- IR 738335; NCV 07-005-02 GR NCV & X-cutting WRT External Flooding Event; 02/19/08
RHR Service Water  
- IR 921197; Inappropriate ACIT Closure of Darley Pump NCV; 05/18/09
*  
- IR 927463; Request For Darley Pump Testing in On-line Schedule; 06/03/09
Reactor Core Isolation Cooling  
- IR 966501; Darley Pump Leaking Gasoline from the Fuel Pump; 09/17/09
*  
- IR 968809; Adequacy of Preventative Maintenance on Darley Pump; 09/22/09
HPCI  
- WO 01247374; Darley Pump Baseline Testing; 9/17/09
*  
- QCOA 0010-16; Flood Emergency Procedure; Revision 12
Emergency Diesel Generators  
- QCMMS 1500-12; Portable Emergency Flood Pump Capacity Test; Revision 0
Section 4OA2Q  
- QCOP 4100-19; Emergency Portable Pump Operations; Revision 7
- IR 984769; Well Broke Off TI in Diesel Generator Coolant System  
- PMID/RQ 164250; Perform Maintenance on the External Portable Pump; 09/17/09
- WO 1198663; U-2 EDG Eng Temp Indicator TI-2-6641-8205 Not Working  
Section 4OA3
- WO 1280197; Well Broke Off TI In U2 Diesel Generator Coolant System  
- 10 Medical Files for Licensed Operators; Various Dates
- SM-AA-300; Procurement Engineering Support Activities; Revision 5  
- Licensee Event Report 254/09-003; Failure of RHR Torus Spray Isolation Valve Due to
- IR 624645; Flood Emergency Pump Testing Documentation; 05/02/07  
  Declutch Mechanism Problems; 8/3/09
- IR 638004; Clarify UFSAR 3.4.1.1 Required Flow Rate to SFP During Flood; 06/07/07  
- IR 928048; MO 1-1001-37B Failed to Open During QCOS 1000-09; 6/4/09
- IR 738335; NCV 07-005-02 GR NCV & X-cutting WRT External Flooding Event; 02/19/08  
- IR 924666; 1-1001-7C Will Not Open; 5/28/09
- IR 921197; Inappropriate ACIT Closure of Darley Pump NCV; 05/18/09  
- OP-AA-103-105; Limitorque Motor-operated Valve Operations; Revision 1
- IR 927463; Request For Darley Pump Testing in On-line Schedule; 06/03/09  
                                                6                                Attachment
- IR 966501; Darley Pump Leaking Gasoline from the Fuel Pump; 09/17/09  
- IR 968809; Adequacy of Preventative Maintenance on Darley Pump; 09/22/09  
- WO 01247374; Darley Pump Baseline Testing; 9/17/09  
- QCOA 0010-16; Flood Emergency Procedure; Revision 12  
- QCMMS 1500-12; Portable Emergency Flood Pump Capacity Test; Revision 0  
- QCOP 4100-19; Emergency Portable Pump Operations; Revision 7  
- PMID/RQ 164250; Perform Maintenance on the External Portable Pump; 09/17/09  
Section 4OA3  
- 10 Medical Files for Licensed Operators; Various Dates  
- Licensee Event Report 254/09-003; Failure of RHR Torus Spray Isolation Valve Due to  
Declutch Mechanism Problems; 8/3/09  
- IR 928048; MO 1-1001-37B Failed to Open During QCOS 1000-09; 6/4/09  
- IR 924666; 1-1001-7C Will Not Open; 5/28/09  
- OP-AA-103-105; Limitorque Motor-operated Valve Operations; Revision 1  


Section 4OA7
- AR 933472, Service Water Effluent Radiation Monitor Inoperable; 6/20/09
                                              7                          Attachment
7
Attachment
Section 4OA7  
- AR 933472, Service Water Effluent Radiation Monitor Inoperable; 6/20/09  


                          LIST OF ACRONYMS USED
AC   Alternating Current
ADAMS Agencywide Document Access Management System
8
ACIT Action Tracking Item
Attachment
CAP   Corrective Action Program
LIST OF ACRONYMS USED
CFR   Code of Federal Regulations
AC  
DGCWP Diesel Generator Cooling Water Pump
Alternating Current  
EAL   Emergency Action Level
ADAMS  
EC   Engineering Change
Agencywide Document Access Management System  
EDG   Emergency Diesel Generator
ACIT  
IMC   Inspection Manual Chapter
Action Tracking Item  
IP   Inspection Procedure
CAP  
IR   Issue Report
Corrective Action Program  
IST   Inservice Test
CFR  
JPM   Job Performance Measure
Code of Federal Regulations  
LCO   Limiting Condition for Operation
DGCWP  
LER   Licensee Event Report
Diesel Generator Cooling Water Pump  
LORT Licensed Operator Requalification Training
EAL  
MO   Motor Operator
Emergency Action Level  
MOV   Motor Operated Valve
EC  
MSPI Mitigating System Performance Index
Engineering Change  
NCV   Non-Cited Violation
EDG  
NEI   Nuclear Energy Institute
Emergency Diesel Generator  
NRC   U.S. Nuclear Regulatory Commission
IMC  
NSBLD Non-Safety Below Level of Design Detail
Inspection Manual Chapter  
OP   Operations
IP  
OPEX Operating Experience
Inspection Procedure  
ODCM Offsite Dose Calculation Manual
IR  
PARS Publicly Available Records
Issue Report  
PI   Performance Indicator
IST  
PM   Planned or Preventative Maintenance
Inservice Test  
PMT   Post Maintenance Test
JPM  
RCS   Reactor Coolant System
Job Performance Measure  
RETS Radiological Effluent Technical Specification
LCO  
RHR   Residual Heat Removal
Limiting Condition for Operation  
RHRSW Residual Heat Removal Service Water
LER  
SAT   Systems Approach to Training
Licensee Event Report  
SDP   Significance Determination Process
LORT  
SSC   Systems, Structures, and Components
Licensed Operator Requalification Training  
TI   Temperature Indicator
MO  
TS   Technical Specification
Motor Operator  
UFSAR Updated Final Safety Analysis Report
MOV  
URI   Unresolved Item
Motor Operated Valve  
Vdc   Volt direct current
MSPI  
WO   Work Order
Mitigating System Performance Index  
                                      8            Attachment
NCV  
Non-Cited Violation  
NEI  
Nuclear Energy Institute  
NRC  
U.S. Nuclear Regulatory Commission  
NSBLD  
Non-Safety Below Level of Design Detail  
OP  
Operations  
OPEX  
Operating Experience  
ODCM  
Offsite Dose Calculation Manual  
PARS  
Publicly Available Records  
PI  
Performance Indicator  
PM  
Planned or Preventative Maintenance  
PMT  
Post Maintenance Test  
RCS  
Reactor Coolant System  
RETS  
Radiological Effluent Technical Specification  
RHR  
Residual Heat Removal  
RHRSW  
Residual Heat Removal Service Water  
SAT  
Systems Approach to Training  
SDP  
Significance Determination Process  
SSC  
Systems, Structures, and Components  
TI  
Temperature Indicator  
TS  
Technical Specification  
UFSAR  
Updated Final Safety Analysis Report  
URI  
Unresolved Item  
Vdc  
Volt direct current  
WO  
Work Order  


C. Pardee                                           -2-
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter
and its enclosure will be made available electronically for public inspection in the
C. Pardee  
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
                                                    Sincerely,
                                                    /RA/
-2-  
                                                    Mark A. Ring, Chief
                                                    Branch 1
                                                    Division of Reactor Projects
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter  
Docket Nos. 50-254; 50-265
and its enclosure will be made available electronically for public inspection in the  
License Nos. DPR-29; DPR-30
NRC Public Document Room or from the Publicly Available Records (PARS) component of  
Enclosure:         Inspection Report 05000254/2009005; 05000265/2009005
NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at  
                    w/Attachment: Supplemental Information
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
cc w/encl:         Distribution via ListServ
DOCUMENT NAME: G:\1-Secy\1-Work In Progress\QUA 2009005.doc
  Publicly Available           Non-Publicly Available       Sensitive   Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl
"E" = Copy with attach/encl "N" = No copy
OFFICE           RIII           E RIII
  NAME             MRing:cms
  DATE             01/27/2010
Sincerely,  
                                          OFFICIAL RECORD COPY
/RA/  
Mark A. Ring, Chief  
Branch 1  
Division of Reactor Projects  
Docket Nos. 50-254; 50-265  
License Nos. DPR-29; DPR-30  
Enclosure:  
Inspection Report 05000254/2009005; 05000265/2009005  
  w/Attachment: Supplemental Information  
cc w/encl:  
Distribution via ListServ  
DOCUMENT NAME: G:\\1-Secy\\1-Work In Progress\\QUA 2009005.doc  
  Publicly Available  
Non-Publicly Available  
Sensitive  
Non-Sensitive  
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl  
"E" = Copy with attach/encl "N" = No copy  
OFFICE  
RIII  
E RIII  
 
   
NAME  
MRing:cms  
   
DATE  
01/27/2010  
OFFICIAL RECORD COPY  


Letter to C. Pardee from M. Ring dated January 27, 2010
SUBJECT:       QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 INTEGRATED
              INSPECTION REPORT 05000254/2009005; 05000265/2009005
Letter to C. Pardee from M. Ring dated January 27, 2010  
DISTRIBUTION:
Susan Bagley
SUBJECT:  
RidsNrrDorlLpl3-2 Resource
QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 INTEGRATED  
RidsNrrPMQuad Cities
INSPECTION REPORT 05000254/2009005; 05000265/2009005  
RidsNrrDirsIrib Resource
DISTRIBUTION:  
Cynthia Pederson
Susan Bagley  
Steven Orth
RidsNrrDorlLpl3-2 Resource  
Jared Heck
RidsNrrPMQuad Cities  
Allan Barker
RidsNrrDirsIrib Resource  
Carole Ariano
Cynthia Pederson  
Linda Linn
Steven Orth  
DRPIII
Jared Heck  
DRSIII
Allan Barker  
Patricia Buckley
Carole Ariano  
Tammy Tomczak
Linda Linn  
DRPIII  
DRSIII  
Patricia Buckley  
Tammy Tomczak  
ROPreports Resource
ROPreports Resource
}}
}}

Latest revision as of 06:58, 14 January 2025

IR 05000254-09-005 and 05000265-09-005 on 10/01/09 - 12/31/09 for Quad Cities Nuclear Power Station, Units 1 & 2
ML100271264
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 01/27/2010
From: Ring M
NRC/RGN-III/DRP/B1
To: Pardee C
Exelon Generation Co, Exelon Nuclear
References
FOIA/PA-2010-0209 IR-09-005
Download: ML100271264 (45)


See also: IR 05000254/2009005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

January 27, 2010

Mr. Charles G. Pardee

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer (CNO), Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 05000254/2009005;

05000265/2009005

Dear Mr. Pardee:

On December 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed

report documents the inspection findings, which were discussed on January 5, 2010, with

Mr. T. Tulon and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, three self-revealed findings of very low safety

significance were identified. Two of the findings involved a violation of NRC requirements.

However, because of their very low safety significance, and because the issues were entered

into your corrective action program, the NRC is treating the issues as non-cited violations

(NCVs) in accordance with Section VI.A.1 of the NRC Enforcement Policy. Additionally,

a licensee-identified violation is listed in Section 4OA7 of this report.

If you contest the subject or severity of an NCV, you should provide a response within 30 days

of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Quad Cities Nuclear Power Station. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region III, and the NRC Resident Inspector at the Quad Cities Nuclear Power

Station. The information that you provide will be considered in accordance with Inspection

Manual Chapter 0305.

C. Pardee

-2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter

and its enclosure will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Enclosure:

Inspection Report 05000254/2009005; 05000265/2009005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-254, 50-265

License Nos:

DPR-29, DPR-30

Report No:

05000254/2009005 and 05000265/2009005

Licensee:

Exelon Nuclear

Facility:

Quad Cities Nuclear Power Station, Units 1 and 2

Location:

Cordova, IL

Dates:

October 1 through December 31, 2009

Inspectors:

J. McGhee, Senior Resident Inspector

B. Cushman, Resident Inspector

R. Orlikowski, Senior Resident Inspector - Duane Arnold

M. Bielby, Senior Operations Engineer

C. Moore, Operations Engineer

M. Mitchell, Senior Radiation Protection Inspector

R. Jickling, Senior Emergency Preparedness Inspector

C. Mathews, Illinois Emergency Management Agency

Approved by:

M. Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ...........................................................................................................1

REPORT DETAILS.......................................................................................................................4

Summary of Plant Status...........................................................................................................4

1.

REACTOR SAFETY .......................................................................................................4

1R01

Adverse Weather Protection (71111.01)..............................................................4

1R04

Equipment Alignment (71111.04) ........................................................................5

1R05

Fire Protection (71111.05) ...................................................................................6

1R11

Licensed Operator Requalification Program (71111.11)......................................7

1R12

Maintenance Effectiveness (71111.12)..............................................................11

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13) ........12

1R15

Operability Evaluations (71111.15)....................................................................12

1R19

Post-Maintenance Testing (71111.19)...............................................................13

1R22

Surveillance Testing (71111.22) ........................................................................14

1EP4

Emergency Action Level and Emergency Plan Changes (71114.04) ................15

1EP6

Drill Evaluation (71114.06).................................................................................17

4.

OTHER ACTIVITIES.....................................................................................................18

4OA1

Performance Indicator Verification (71151) .......................................................18

4OA2

Identification and Resolution of Problems (71152) ............................................21

4OA3

Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............27

4OA5

Other Activities...................................................................................................30

4OA6

Management Meetings ......................................................................................30

4OA7

Licensee-Identified Violations ............................................................................31

SUPPLEMENTAL INFORMATION ...............................................................................................1

Key Points of Contact................................................................................................................1

List of Items Opened, Closed and Discussed............................................................................1

List of Documents Reviewed.....................................................................................................2

List of Acronyms Used ..............................................................................................................8

1

Enclosure

SUMMARY OF FINDINGS

IR 05000254/2009005, 05000265/2009005; 10/01/09 - 12/31/09; Quad Cities Nuclear Power

Station, Units 1 & 2; Other Activities.

This report covers a 3-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Three Green findings were identified by the

inspectors. Two of the findings were considered Non-Cited Violations (NCVs) of NRC

regulations. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity

level after NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 4, dated December 2006.

A.

NRC-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green. A finding of very low safety significance and a NCV of 10 CFR 50 Appendix B,

Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the

installation of an inappropriate component into the Unit 2 emergency diesel generator

coolant system. Specifically, the licensee failed to properly perform a part evaluation for

a replacement temperature indicator (TI) designated as augmented quality. This

resulted in the TI probe shearing off in the coolant flow stream and causing foreign

material to enter the coolant system. Immediate corrective actions included the

installation of an appropriately approved TI and recovery of foreign material from the

system.

The same part evaluation process was used for risk-significant components independent

of the system being worked. Therefore, this finding was more than minor because, if left

uncorrected, this performance deficiency could lead to unplanned unavailability of

safety-related or risk-significant equipment and would become a more significant safety

concern. The inspectors performed a Phase 1 SDP screening and concluded that the

issue was of very low safety significance (Green) because the failure of the TI did not

result in unplanned inoperability or loss of function of the diesel generator. The

inspectors determined that this finding did not have a cross-cutting aspect. This

performance deficiency is not indicative of current licensee performance. The decision

to install this type of TI was made in October 2007. The process which allowed this

performance deficiency was identified and corrected through procedure and policy

revisions in February 2008. (Section 4OA2)

Green: A finding of very low safety significance and a NCV of TS 3.6.2.4,

Residual Heat Removal (RHR) Suppression Pool Spray, was self-revealed for the

licensees failure to meet the Technical Specification (TS) limiting conditions of operation

(LCO) requirement prior to transitioning into an operating mode where the LCO was

required to be satisfied. Specifically, Motor Operator (MO) 1-1001-37B for the Unit 1

RHR torus (suppression pool) spray isolation valve was found to have been inoperable

when the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009.

The valve actuator had been inadvertently declutched (i.e., motor disengaged) and the

valve was not demonstrated operable by stroking the valve electrically after the actuator

2

Enclosure

motor was declutched. Inspectors determined that the finding was cross-cutting in the

area of Problem Identification and Resolution - Corrective Action (P.1(a)) because plant

personnel failed to identify the physical contact with the valve actuator that resulted in

the valve being declutched; therefore, operators incorrectly assessed the system

condition as in compliance with TS 3.6.2.4. Immediate licensee corrective actions

included engagement of the motor and stroke testing of the valve.

The finding is more than minor because it was associated with the equipment

performance quality attribute of the Mitigating Systems Cornerstone and affected the

objective of ensuring availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, failure to verify

system availability and capability prior to entering the required modes resulted in fewer

available mitigating systems than assumed in the operating risk evaluations. The

inspectors determined the finding could be evaluated using the SDP in accordance with

IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 - Initial

Screening and Characterization of findings, Table 4a. Inspectors answered all of the

questions for the Mitigating Systems Cornerstone No. Therefore, the finding screened

as Green or very low safety significance. (Section 4OA3)

Cornerstone: Barrier Integrity

Green. A finding of very low safety significance was self-revealed for the failure to

perform maintenance that would ensure the portable emergency flooding pump (Darley

pump) was in a standby condition and readily available to accomplish the requirements

of QCOA 0010-16, Flood Emergency Procedure. Specifically, the failure to perform

adequate maintenance resulted in the need to replace the battery and gasoline for the

pump and, upon pump start, fuel sprayed out of the fuel pump. Although the staged

portable pump would not have supported the external flooding emergency response

procedure, no violation of regulatory requirements occurred. The inspectors did not

identify a cross-cutting aspect associated with this finding because the issue is not

reflective of current licensee performance. Immediate corrective actions included

replacement of the degraded battery and overhaul of the pumps fuel pump. Other

actions included identification of preventative maintenance tasks and establishing a

program owner of the pump and support equipment.

This issue was more than minor because it was associated with the Structures,

Systems, and Components (SSC) Performance attribute of the Barrier Integrity

Cornerstone objective of maintaining the functionality of spent fuel pool cooling.

The finding affected the cornerstone objective of providing assurance that physical

design barriers protect the public from radionuclide releases caused by events including

external flooding. Specifically, the pump could fail due to maintenance preventable

component failure resulting in inadequate or degraded makeup to the spent fuel pool

during an external flooding event. The inspectors determined the finding could be

evaluated using the SDP in accordance with IMC 0609, Significance Determination

Process, Attachment 0609.04, Phase 1 - Initial Screening and Characterization of

findings, Tables 4a and 4b. The inspectors determined that even though this equipment

is assumed to completely fail, the licensee could provide an alternate portable pump

already located on site and capable of performing the safety function during this slow

developing event. Since alternate equipment was available and the delay in mobilizing

the alternate equipment would not have resulted in loss of capability to mitigate the

3

Enclosure

impact of the flooding event, the issue is of very low safety significance or Green.

(Section 4OA2)

B.

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee was

reviewed by inspectors. Corrective actions planned or taken by the licensee have been

entered into the licensees corrective action program. This violation and associated

corrective action tracking number are listed in Section 4OA7 of this report.

4

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1

Unit 1 operated at 100 percent thermal power throughout the evaluated period from October 1

until December 31, 2009, with the exception of planned power reductions for routine

surveillances, planned equipment repair, and control rod maneuvers.

Unit 2

Unit 2 operated at or near 100 percent thermal power from October 1 until December 16 with

the exception of planned power reductions for routine surveillances and control rod maneuvers.

On December 16, 2009, operators attempted to replace a light bulb in the indication circuit for

the extraction steam check valve A on the 2D feedwater heaters. The light bulb separated with

the base remaining in the socket. During the evolution the D heaters tripped, resulting in a

partial loss of feedwater heating and a resulting change in reactor power. Operators lowered

power about 150 MWth (50 MWe) by inserting one high reactivity-worth control rod. Power

increased by 0.59 percent during the loss of feedwater heating transient. By 10:45 a.m. that

same morning, feedwater heaters had been restored and the control rod was withdrawn to

restore the unit to 100 percent thermal power. The unit remained at 100 percent power for the

duration of the evaluated period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1

Winter Seasonal Readiness Preparations

a.

Inspection Scope

The inspectors conducted a review of the licensees preparations for winter conditions to

verify that the plants design features and implementation of procedures were sufficient

to protect mitigating systems from the effects of adverse weather. Documentation for

selected risk-significant systems was reviewed to ensure that these systems would

remain functional when challenged by inclement weather. During the inspection, the

inspectors focused on plant-specific design features and the licensees procedures used

to mitigate or respond to adverse weather conditions. Additionally, the inspectors

reviewed the Updated Final Safety Analysis Report (UFSAR) and performance

requirements for systems selected for inspection, and verified that operator actions were

appropriate as specified by plant-specific procedures. Cold weather protection, such as

heat tracing and area heaters, was verified to be in operation where applicable. The

inspectors also reviewed corrective action program (CAP) items to verify that the

licensee was identifying adverse weather issues at an appropriate threshold and

entering them into the CAP in accordance with station corrective action procedures.

Specific documents reviewed during this inspection are listed in the Attachment to this

report. The inspectors reviews focused specifically on the following plant systems due

to their risk significance or susceptibility to cold weather issues:

5

Enclosure

heating steam, and

circulating water/de-icing valve.

This inspection constituted one winter seasonal readiness preparations sample as

defined in Inspection Procedure (IP) 71111.01-05.

b.

Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a.

Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

1/2 B diesel driven fire pump; and

Unit 1 emergency diesel generator and diesel generator cooling water pump.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstone at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders (WOs), condition reports, and the impact of ongoing work activities on redundant

trains of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment to this report.

These activities constituted two partial system walkdown samples as defined in

IP 71111.04-05.

b.

Findings

No findings of significance were identified.

6

Enclosure

.2

Semi-Annual Complete System Walkdown

a.

Inspection Scope

On November 5, 2009, the inspectors performed a complete system alignment

inspection of the Unit 2 emergency diesel generator to verify the functional capability of

the system. This system was selected because it was considered both safety significant

and risk significant in the licensees probabilistic risk assessment. The inspectors

walked down the system to review mechanical and electrical equipment lineups;

electrical power availability; system pressure and temperature indications, as

appropriate; component labeling; component lubrication; component and equipment

cooling; hangers and supports; operability of support systems; and to ensure that

ancillary equipment or debris did not interfere with equipment operation. A review of a

sample of past and outstanding work orders was performed to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the CAP database to ensure that system equipment alignment problems were

being identified and appropriately resolved. Documents reviewed are listed in the

Attachment to this report.

These activities constituted one complete system walkdown sample as defined in

IP 71111.04-05.

b.

Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a.

Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

Unit 2 Reactor Bldg. El. 5540, NW Corner Room - 2A Core Spray, Fire Zone

11.3.3;

Unit 1 Turbine Bldg. El. 5950, Diesel Generator, Fire Zone 9.1;

Unit 1 Turbine Bldg. El. 5950, Reactor Feed Pumps, Fire Zone 8.2.6.A;

Crib House Bldg. El. 5598, Basement, Fire Zone 11.4.A; and

Crib House Bldg. El. 5950, Ground Floor/Service Water Pumps, Fire Zone

11.4.B.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

7

Enclosure

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in

IP 71111.05-05.

b.

Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1

Resident Inspector Quarterly Review (71111.11Q)

a.

Inspection Scope

On November 4, 2009, the inspectors observed licensed operator continuing training to

verify that operator performance was adequate, evaluators were identifying and

documenting crew performance problems, and training was being conducted in

accordance with licensee procedures. The inspectors evaluated the following areas:

licensed operator performance;

crews communications and accuracy of documentation;

ability to take timely actions in the conservative direction;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and lesson objectives. Documents reviewed are listed in the Attachment to

this report.

This inspection constituted one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b.

Findings

No findings of significance were identified.

8

Enclosure

.2

Facility Operating History (71111.11B)

a.

Inspection Scope

The inspectors reviewed the plants operating history from January 2007 through

September 2009 to identify operating experience that was expected to be addressed by

the Licensed Operator Requalification Training (LORT) program. The inspectors verified

that the identified operating experience had been addressed by the facility licensee in

accordance with the stations approved Systems Approach to Training (SAT) program to

satisfy the requirements of 10 CFR 55.59(c). The documents reviewed during this

inspection are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

.3

Licensee Requalification Examinations

a.

Inspection Scope

The inspectors performed an inspection of the licensees LORT test/examination

program for compliance with the stations SAT program which would satisfy the

requirements of 10 CFR 55.59(c)(4). The reviewed operating examination material

consisted of two operating tests, each containing two dynamic simulator scenarios and

five job performance measures (JPMs). The two biennial written examinations reviewed

consisted of two parts. Each written examination contained 30 questions consisting of

15 written exam questions and 15 static exam questions. The inspectors reviewed the

annual requalification operating test and biennial written examination material to

evaluate general quality, construction, and difficulty level. The inspectors assessed the

level of examination material duplication from week to week during the current year

operating test. The examiners assessed the amount of written examination material

duplication from week to week for the biennial written examination administered in

calendar year 2009. The inspectors reviewed the methodology for developing the

examinations, including the LORT program 2-year sample plan, probabilistic risk

assessment insights, previously identified operator performance deficiencies, and plant

modifications. The documents reviewed during this inspection are listed in the

Attachment to this report.

b.

Findings

No findings of significance were identified.

.4

Licensee Administration of Requalification Examinations

a.

Inspection Scope

The inspectors observed the administration of a requalification operating test to

assess the licensees effectiveness in conducting the test to ensure compliance with

10 CRF 55.59(c)(4). The inspectors evaluated the performance of one operating crew in

parallel with the facility evaluators during four dynamic simulator scenarios and

evaluated various licensed crew members concurrently with facility evaluators during the

9

Enclosure

administration of several JPMs. The inspectors assessed the facility evaluators ability

to determine adequate crew and individual performance using objective, measurable

standards. The inspectors observed the training staff personnel administer the operating

test, including conducting pre-examination briefings, evaluations of operator

performance, and individual and crew evaluations upon completion of the operating test.

The inspectors evaluated the ability of the simulator to support the examinations.

b.

Findings

No findings of significance were identified.

.5

Examination Security

a.

Inspection Scope

The inspectors observed and reviewed the licensees overall licensed operator

requalification examination security program related to examination physical security

(e.g., access restrictions and simulator considerations) and integrity (e.g., predictability

and bias) to verify compliance with 10 CFR 55.49, Integrity of Examinations and Tests.

The inspectors also reviewed the facility licensees examination security procedure and

the implementation of security and integrity measures (e.g., security agreements,

sampling criteria, bank use, and test item repetition) throughout the examination

process. No examination security compromises occurred during these observations.

The documents reviewed during this inspection are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

.6

Licensee Training Feedback System

a.

Inspection Scope

The inspectors assessed the methods and effectiveness of the licensees processes for

revising and maintaining its LORT program up-to-date, including the use of feedback

from plant events and industry experience information. The inspectors reviewed the

licensees quality assurance oversight activities, including licensee training department

self-assessment reports. The inspectors evaluated the licensees ability to assess the

effectiveness of its LORT program and their ability to implement appropriate corrective

actions. This evaluation was performed to verify compliance with 10 CFR 55.59(c) and

the licensees SAT based program. The documents reviewed during this inspection are

listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

10

Enclosure

.7

Licensee Remedial Training Program

a.

Inspection Scope

The inspectors assessed the adequacy and effectiveness of the remedial training

conducted since the previous biennial requalification examinations and the training from

the current examination cycle to ensure that they addressed weaknesses in licensed

operator or crew performance identified during training and plant operations. The

inspectors reviewed remedial training procedures and individual remedial training plans.

This evaluation was performed in accordance with 10 CFR 55.59(c) and with respect to

the licensees SAT based program. The documents reviewed during this inspection are

listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

.8

Conformance With Operator License Conditions

a.

Inspection Scope

The inspectors reviewed the facility and individual operator licensees' conformance with

the requirements of 10 CFR Part 55. The inspectors reviewed the facility licensee's

program for maintaining active operator licenses and to assess compliance with

10 CFR 55.53(e) and (f). The inspectors reviewed the procedural guidance and the

process for tracking on-shift hours for licensed operators and which control room

positions were granted watch-standing credit for maintaining active operator licenses.

The inspectors reviewed the facility licensee's LORT program to assess compliance with

the requalification program requirements as described by 10 CFR 55.59(c). Additionally,

medical records for 10 licensed operators were reviewed for compliance with

10 CFR 55.53(I). The documents reviewed during this inspection are listed in the

Attachment to this report.

b.

Findings

No findings of significance were identified.

.9

Annual Operating Test Results and Biennial Written Examination Results (71111.11B)

a.

Inspection Scope

The inspectors reviewed the overall pass/fail results of the individual JPM operating

tests, the simulator operating tests, and the biennial written examination (required to be

given per 10 CFR 55.59(a)(2)) administered by the licensee from September 2009

through November 2009 as part of the licensees operator licensing requalification cycle.

These results were compared to the thresholds established in Inspection Manual

Chapter 0609, Appendix I, Licensed Operator Requalification Significance

Determination Process (SDP)." The evaluations were also performed to determine if the

licensee effectively implemented operator requalification guidelines established in

NUREG 1021, Operator Licensing Examination Standards for Power Reactors, and

11

Enclosure

IP 71111.11, Licensed Operator Requalification Program. The documents reviewed

during this inspection are listed in the Attachment to this report.

This inspection constituted one inspection sample as defined in IP 71111.11.

b.

Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1

Routine Quarterly Evaluations (71111.12Q)

a.

Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

Z2900; Safe Shutdown Makeup Pump, and

Z4700; Instrument Air.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for SSCs/functions classified as (a)(2)

or appropriate and adequate goals and corrective actions for systems classified

as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b.

Findings

No findings of significance were identified.

12

Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1

Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

Work Week 45 - 1A residual heat removal (RHR) room cooler, 1A RHR service

water (RHRSW) loop, 1B RHR seal cooler, 1-1001-16A boroscope and Votes

testing, 1-1001-37A MOV equipment qualification inspection; and

Work Week 51 - Unit 1 250 Vdc battery reconfiguration using Unit 1 125 Vdc

alternate battery with emergent Unit 2 125 Vdc battery low specific gravity

problems, 2A RHR loop and 2B RHRSW pump unavailability.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted

two samples as defined in IP 71111.13-05.

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following issues:

IR 987904: 1A RHR Room Cooler Tube Sheet Has Pitting, and

IR 994823: TS SR 3.8.4.8 Frequency Not Met.

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

13

Enclosure

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment to this report.

This operability inspection constituted two samples as defined in IP 71111.15-05.

b.

Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (71111.19)

.1

Post-Maintenance Testing

a.

Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

WO 1121775, 250 Vdc Battery Charger #2 4-Hour Load Test;

WO 1261246, Replace Battery Changeover Relay R12 EC 376690;

QCMMS 4100-33, 1/2-4101B Diesel Driven Fire Pump Annual Capacity Test;

WO 1130535, OP PMT Filter B Train Control Room HVAC; and

WO1107582, Replace Unit 2 DGCWP Alternate Feed Contactor.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment to this report.

14

Enclosure

This inspection constituted five post-maintenance testing samples as defined in

IP 71111.19-05.

b.

Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

.1

Surveillance Testing

a.

Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

QCOS 1400-01, 2A Core Spray Pump Performance Test (IST);

QCIS 0300-02, Unit 1 Division 1 Scram Discharge Volume Calibration and

Functional Test (Routine);

QCOS 7500-05, 1/2 B Standby Gas Treatment Operability Test (Routine);

QCOS 1600-07, Reactor Coolant Leakage in the Drywell (RCS);

QCEMS 0230-11, Modified Performance Test of Unit 1(2) 125 Vdc Normal or

Alternate Battery (Routine); and

QCOS 6900-14, Station Battery Allowable Value Verification Surveillance

(Routine).

The inspectors observed in plant activities and reviewed procedures and associated

records to determine the following:

did preconditioning occur;

were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges, and the calibration frequency were

in accordance with TS, the UFSAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy, applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures, jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

15

Enclosure

Mechanical Engineers code, and reference values were consistent with the

system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted four routine surveillance testing samples, one inservice

testing sample, and one reactor coolant system leak detection inspection samples as

defined in IP 71111.22, Sections -02 and -05.

b.

Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

.1

Emergency Action Level and Emergency Plan Changes

a.

Inspection Scope

Since the last NRC inspection of this program area, Emergency Plan Annex,

Revisions 26 and 27 were implemented based on the licensees determination, in

accordance with 10 CFR 50.54(q), that the changes resulted in no decrease in

effectiveness of the Plan, and that the revised Plan as changed continues to meet the

requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors

conducted a sampling review of the Emergency Plan changes and a review of the

Emergency Action Level (EAL) changes to evaluate for potential decreases in

effectiveness of the Plan. However, this review does not constitute formal NRC approval

of the changes. Therefore, these changes remain subject to future NRC inspection in

their entirety.

This emergency action level and emergency plan changes inspection constituted one

sample as defined in IP 71114.04-05.

16

Enclosure

b.

Findings

(1) Unresolved Item (URI) 05000254/2009005-01: Changes to EAL HU6 Potentially

Decrease the Effectiveness of the Plans without Prior NRC Approval

Introduction: The inspectors reviewed changes implemented to the Quad Cities Station

Radiological Emergency Plan Annex EALs and EAL Basis. In Revision 26, the licensee

changed the basis of EAL HU6, "Fire not extinguished within 15 minutes of detection

within the protected area boundary, by adding two statements. The two changes added

to the EAL basis stated that if the alarm could not be verified by redundant control room

or nearby fire panel indications, notification from the field that a fire exists starts the

15-minute classification and fire extinguishment clocks. The second change stated the

15-minute period to extinguish the fire does not start until either the fire alarm is verified

to be valid by additional control room or nearby fire panel instrumentation, or upon

notification of a fire from the field. These statements conflict with the previous

Quad Cities Station Annex, Revision 25, basis statements and potentially decrease the

effectiveness of the Plans.

Description: Quad Cities Station Radiological Emergency Plan Annex, Revision 25,

EAL HU6, initiating condition stated, "Fire not extinguished within 15 minutes of

detection, or explosion, within the protected area boundary." The threshold values for

HU6 were, in part: 1) Fire in any Table H2 area not extinguished within 15 minutes of

control room notification or verification of a control room alarm; or 2) Fire outside any

Table H2 area with the potential to damage safety systems in any Table H2 area not

extinguished within 15 minutes of control room notification or verification of a control

room alarm. Table H2, Vital Areas, were identified as main control room, reactor

building, diesel generator rooms, 4 kilovolt switchgear area, battery rooms, B train

control room heating-ventilation and air conditioning, service water pumps, and turbine

building cable tunnel. The basis defined fire as "combustion characterized by heat and

light. Sources of smoke such as slipping drive belts or overheated electrical equipment

do not constitute fires. Observation of flame is preferred but is not required if large

quantities of smoke and heat are observed."

The basis for Revision 25, EAL HU6 thresholds 1 and 2 stated, in part, the purpose of

this threshold is to address the magnitude and extent of fires that may be potentially

significant precursors to damage to safety systems. As used here, notification is visual

observation and report by plant personnel or sensor alarm indication. The 15-minute

period begins with a credible notification that a fire is occurring or indication of a valid fire

detection system alarm. A verified alarm is assumed to be an indication of a fire unless

personnel dispatched to the scene disprove the alarm within the 15-minute period.

The report, however, shall not be required to verify the alarm. The intent of the

15-minute period is to size the fire and discriminate against small fires that are readily

extinguished (e.g., smoldering waste paper basket, etc.).

Revision 26 of the Quad Cities Station Radiological Emergency Plan Annex, changed

the threshold basis for EAL HU6 by adding the following two statements: 1)"If the alarm

cannot be verified by redundant control room or nearby fire panel indications, notification

from the field that a fire exists starts the 15-minute classification and fire extinguishment

clocks," and 2) "The 15-minute period to extinguish the fire does not start until either the

fire alarm is verified to be valid by utilization of additional control room or nearby fire

panel instrumentation, or upon notification of a fire from the field."

17

Enclosure

The two statements added to the basis in Revision 26 conflict with the Revision 25

threshold basis and initiating condition. The changed threshold basis in Revision 26

could add an indeterminate amount of time to declaring an actual emergency until a

person responded to the area of the fire and made a notification to the control room of a

fire in the event that redundant control room or nearby fire panel indications were not

available.

Pending further review and verification by the NRC to determine if the changes to EAL

HU6 threshold basis potentially decreased the effectiveness of the Plans, this issue was

considered an unresolved item (URI 05000254/2009005-01; 05000265/2009005-01).

1EP6 Drill Evaluation (71114.06)

.1

Emergency Preparedness Drill Observation

a.

Inspection Scope

The inspectors evaluated the conduct of an after-hours licensee emergency drill on

November 11, 2009, to identify any weaknesses and deficiencies in classification,

notification, and protective action recommendation development activities. The

after-hours drill was preceded by an unannounced, after-hours drive-in drill.

The inspectors observed emergency response operations in the Technical Support

Center to determine whether the event classification, notifications, and protective action

recommendations were performed in accordance with procedures. The inspectors also

attended the licensee drill critique to compare any inspector-observed weakness with

those identified by the licensee staff in order to evaluate the critique and to verify

whether the licensee staff was properly identifying weaknesses and entering them into

the corrective action program. As part of the inspection, the inspectors reviewed the drill

package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b.

Findings

No findings of significance were identified.

.2

Emergency Preparedness Termination and Recovery Drill Observation

a.

Inspection Scope

The inspectors evaluated the conduct of an emergency preparedness termination and

recovery drill on December 2, 2009, to identify any weaknesses and deficiencies in the

conduct of the drill and to assess the licensees ability to assess performance via a

formal critique process in order to identify and correct Emergency Preparedness

weaknesses. The inspectors observed emergency response operations in the Technical

Support Center to determine whether the recovery and termination activities associated

with the drill were performed in accordance with procedures. The inspectors also

attended the licensee drill critique to compare any inspector-observed weakness with

those identified by the licensee staff in order to evaluate the critique and to verify

whether the licensee staff was properly identifying weaknesses and entering them into

18

Enclosure

the corrective action program. As part of the inspection, the inspectors reviewed the drill

package and other documents listed in the Attachment to this report.

This emergency preparedness drill inspection constituted one sample as defined in

IP 71114.06-05.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Mitigating Systems Performance Index - Emergency Alternating Current Power System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Emergency Alternating Current (AC) Power System performance

indicator for Quad Cities Units 1 and 2 for the period from the 4th quarter 2008 through

the 3rd quarter 2009. To determine the accuracy of the performance indicator (PI) data

reported during those periods, PI definitions and guidance contained in the Nuclear

Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, were used. The inspectors reviewed the licensees operator

narrative logs, MSPI derivation reports, issue reports, event reports and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator, and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI emergency AC power system samples as defined

in IP 71151-05.

b.

Findings

No findings of significance were identified.

.2

Mitigating Systems Performance Index - High Pressure Injection Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - High Pressure Injection Systems performance indicator for Quad Cities Units 1

and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To

determine the accuracy of the PI data reported during those periods, PI definitions and

guidance contained in the NEI Document 99-02, Regulatory Assessment Performance

19

Enclosure

Indicator Guideline, Revision 6, were used. The inspectors reviewed the licensees

operator narrative logs, issue reports, MSPI derivation reports, event reports and

NRC integrated inspection reports for the period of October 1, 2008, through

September 30, 2009, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable guidance. The inspectors also reviewed the licensees issue

report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator, and none were identified. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI high pressure injection system samples as defined

in IP 71151-05.

b.

Findings

No findings of significance were identified.

.3

Mitigating Systems Performance Index - Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Heat Removal System performance indicator for Quad Cities Units 1 and 2 for

the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, were used. The inspectors reviewed the licensees operator

narrative logs, issue reports, event reports, MSPI derivation reports, and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator, and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI heat removal system samples as defined in

IP 71151-05.

b.

Findings

No findings of significance were identified.

.4

Mitigating Systems Performance Index - Residual Heat Removal System

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Residual Heat Removal System performance indicator for Quad Cities Units 1

20

Enclosure

and 2 for the period from the 4th quarter 2008 through the 3rd quarter 2009. To

determine the accuracy of the PI data reported during those periods, the PI definitions

and guidance contained in the NEI Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 6, were used. The inspectors reviewed the

licensees operator narrative logs, issue reports, MSPI derivation reports, event reports

and NRC integrated inspection reports for the period of October 1, 2008, through

September 30, 2009, to validate the accuracy of the submittals. The inspectors

reviewed the MSPI component risk coefficient to determine if it had changed by more

than 25 percent in value since the previous inspection, and if so, that the change was in

accordance with applicable guidance. The inspectors also reviewed the licensees issue

report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator, and none were identified. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted two MSPI residual heat removal system samples as defined

in IP 71151-05.

b.

Findings

No findings of significance were identified.

.5

Mitigating Systems Performance Index - Cooling Water Systems

a.

Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index - Cooling Water Systems performance indicator for Quad Cities Units 1 and 2 for

the period from the 4th quarter 2008 through the 3rd quarter 2009. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator

Guideline, Revision 6, were used. The inspectors reviewed the licensees operator

narrative logs, issue reports, MSPI derivation reports, event reports and NRC integrated

inspection reports for the period of October 1, 2008, through September 30, 2009, to

validate the accuracy of the submittals. The inspectors reviewed the MSPI component

risk coefficient to determine if it had changed by more than 25 percent in value since the

previous inspection, and if so, that the change was in accordance with applicable

guidance. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator, and none were identified. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted two MSPI cooling water system samples as defined in

IP 71151-05.

b.

Findings

No findings of significance were identified.

21

Enclosure

.6

Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences

a.

Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent Technical

Specifications (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent

Occurrences performance indicator for the period of December 2008 through

November 2009. The inspectors used PI definitions and guidance contained in the

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6 to determine the accuracy of the PI data reported during those periods.

The inspectors reviewed the licensees issue report database and selected individual

reports generated since this indicator was last reviewed to identify any potential

occurrences such as unmonitored, uncontrolled, or improperly calculated effluent

releases that may have impacted offsite dose. The inspectors reviewed gaseous

effluent summary data and the results of associated offsite dose calculations for selected

dates between December 2008 and November 2009 to determine if indicator results

were accurately reported. The inspectors also reviewed the licensees methods for

quantifying gaseous and liquid effluents and determining effluent dose. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample

as defined in IP 71151-05.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

.1

Routine Review of Items Entered into the Corrective Action Program (CAP)

a.

Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

22

Enclosure

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b.

Findings

No findings of significance were identified.

.2

Daily Corrective Action Program Reviews

a.

Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for followup, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b.

Findings

No findings of significance were identified.

.3

Semi-Annual Trend Review

a.

Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues and associated corrective

actions, but also considered the results of daily inspector CAP item screening discussed

in Section 4OA2.2 above, licensee trending efforts, and licensee human performance

results. The inspectors review nominally considered the 6-month period of

January 1, 2009, through June 30, 2009, although some examples expanded beyond

those dates where the scope of the trend warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy. Additionally,

the inspectors reviewed CAP open priority 1, 2, and 3 corrective actions for timeliness.

In addition, all open priority 4 action tracking items (ACITs) were reviewed to ensure they

were properly categorized and that the justifications for extension were appropriate and

properly documented.

23

Enclosure

This review constituted a single semi-annual trend inspection sample as defined in

IP 71152-05.

b.

Findings

No findings of significance were identified.

.4

Selected Issue Followup Inspection: Issue Report 966501, Darley Pump Leaking

Gasoline from the Fuel Pump

a.

Inspection Scope

During a review of items entered in the licensees CAP, the inspectors followed up on a

corrective action item documenting gasoline leaking from the fuel pump of the portable

emergency flooding pump (Darley pump) on September 17, 2009, during preparations

for a pump capacity demonstration run. The pump capacity demonstration was a new

procedure developed in response to a non-cited violation (NCV) documented in

Inspection Report 05000254/2007005.

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b.

Findings

Introduction: A finding of very low safety significance was self-revealed for the failure to

maintain the portable emergency flooding pump and supporting equipment in a condition

required to support implementation of QCOA 0010-16, Flood Emergency Procedure.

Description: In Inspection Report 05000254/2007005, inspectors documented a NCV of

TS 5.4.1 for the licensees failure to develop adequate surveillance procedures for

equipment used during an external flooding event. Corrective action for this issue

included revising the external flooding procedure and developing and implementing a

procedure to test a portable pump used as the sole source of makeup water to the spent

fuel pool following an external flooding event. The action to develop and implement the

pump test procedure was issued in May and stated, Develop test procedure and

conduct test to confirm flow of greater than or equal to 200 gpm by mid-July. Brief

NRC Resident as appropriate. The action was closed to an Engineering Change (EC) 366481, on July 18, 2007, with no actual test performed. The documented justification

for this closure stated that discussions with the NRC resident clarified the intent of the

action and no physical testing needed to be performed. Followup discussions with the

resident inspectors stationed at Quad Cities in July 2007 had no recollection of the

conversation and their understanding of the intended action remained unchanged from

the original report.

Licensee staff generated Issue Report (IR) 738335 in February 2008 to document the

review of the NCV response and generate a closure package of all related IRs. The lack

of preventative maintenance (PM) testing was identified and an action tracking item was

generated to Develop PM/testing requirements for the Darley pump associated with the

external flooding event. The original corrective action due date was July 16, 2008.

The action was extended several times, and on May 18, 2009, during a review of

corrective actions for NRC-identified issues, the licensee staff identified that a CAP

24

Enclosure

action item (ACIT 624645-03) had been inappropriately closed. In addition, the licensee

determined that ACIT 624645-03 was inappropriately tagged as an Action Tracking Item

(ACIT) and should have been a corrective action. Issue Report 921197 was generated

and ACIT 624645 was upgraded to a corrective action with a July 31, 2009, due date.

The test procedure was developed and the pump was scheduled to run on

September 17, 2009.

The capacity test was implemented with WO 01247374. When mechanics pulled the

pump and support components from the storage location, they found that the engine

battery had to be replaced and the gasoline stored with the motor had to be replaced.

Since the mechanics performing the test had never operated the pump, they decided to

run it in the weld shop before taking it down to the river. When the mechanics started

the pump, fuel was spraying out of the fuel pump. They immediately shut down the

pump and contained the fuel leak (IR 966501).

The Darley pump fuel system was repaired and the capacity test was completed

satisfactorily on September 25, 2009. Review of recent pump operating history and

PM tasks revealed that the pump had not been operated since the NCV was identified in

2007. The annual maintenance performed under PM 164250 in July of 2009 changed

the oil and inspected the filters and spark plugs with no post-maintenance operation

required. The PM also failed to identify that the battery was beyond the expected life

and did not determine that the battery would maintain its charge.

Analysis: The inspectors determined that the failure to perform maintenance that would

ensure the pump was in a standby condition and readily available to accomplish the

requirements of QCOA 0010-16 was a performance deficiency fully within the licensees

ability to control, and therefore a finding. This issue was more than minor because it

was associated with the SSC Performance attribute of the Barrier Integrity Cornerstone

element of maintaining the functionality of spent fuel pool cooling. The finding affected

the cornerstone objective of providing assurance that physical design barriers protect the

public from radionuclide releases caused by events including external flooding.

Specifically, the pump could fail due to a maintenance preventable component failure

resulting in inadequate or degraded makeup to the spent fuel pool during an external

flooding event. The inspectors did not identify a cross-cutting aspect associated with

this finding because the maintenance issue is a legacy issue and not reflective of current

licensee performance. The pump and PM tasks had been in place for several years.

Inspectors reviewed maintenance requirements for other temporary equipment staged in

support of external events and emergency operating procedures, some of which was put

in place after the Darley pump was staged, and did not identify any similar issues.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of findings, Tables 4a and 4b. The inspectors

determined that even though this equipment is assumed to completely fail, the licensee

could provide an alternate portable pump already located on site and capable of

performing the safety function during this slow developing event. The alternate pump

had maintenance and test procedures in place to provide a basis for reliability. Since

alternate equipment was available and the delay in mobilizing the alternate equipment

would not have resulted in loss of capability to mitigate the impact of the flooding event,

the issue is of very low safety significance or Green.

25

Enclosure

Enforcement: Technical Specification 5.4.1 required that written procedures be

established, implemented, and maintained for the items specified in Regulatory

Guide 1.33, Quality Assurance Program Requirements. QCOA 0010-16,

Flood Emergency Procedure, was the licensee procedure used to meet the

Regulatory Guide 1.33 requirement for an emergency flooding event. The procedure

specified that the portable pump staged in the protected area warehouse is to be used to

respond to the event. Although the regulatory guide did not specifically require

maintenance procedures for portable equipment, failure to maintain the staged

equipment in a condition to be used to mitigate the event does not support timely

implementation of the procedure to provide spent fuel pool makeup and is a finding.

Enforcement action does not apply because the performance deficiency did not involve a

violation of a regulatory requirement. Because the finding does not involve a violation of

regulatory requirements and has a very low safety significance, it is identified as

(FIN 05000254/2009005-02; 05000265/2009005-02). The issue was added to the

licensees CAP program as IR 966501 and IR 968809. Immediate corrective actions

included replacement of the degraded battery and overhaul of the pumps fuel pump.

Other actions included identification of preventative maintenance tasks and establishing

a program owner of the pump.

.5

Selected Issue Followup Inspection: Incident Report 984769, Temperature Indicating

Probe Found Broken in the Unit 2 Diesel Generator Coolant System

a.

Inspection Scope

During a review of items entered in the licensees CAP, the inspectors followed up on a

corrective action item documenting a failed temperature indicating probe (TI) in the

Unit 2 diesel generator coolant system on October 27, 2009, during planned

maintenance on the Unit 2 emergency diesel generator (EDG).

This review constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b.

Findings

Introduction: A finding of very low safety significance and associated NCV were

self-revealed when a TI failed in the Unit 2 diesel generator coolant system.

Description: On October 27, 2009, while performing corrective maintenance on

TI 2-6641-8205, technicians noted that the tip had broken off the probe when comparing

it to the length of the new TI. This TI provides local indication of the jacket coolant water

temperature at the inlet to the diesel engine and provides no alarm function.

The TI was scheduled for replacement in October 2008 when Operations identified the

TI reading abnormally at zero degrees. A work order was written and scheduled for

October 2009. During the performance of the maintenance, it was noted that the new TI

was longer than the one recently removed. A new work order was written to retrieve any

foreign material from the system. The broken tip was recovered from the diesel

generator coolant system.

26

Enclosure

The licensee investigation discovered that the installation analysis for this TI was

approved under the non-safety below level of design detail (NSBLD) process in October

2007 under Revision 3 of SM-AA-300, Procurement Engineering Support Activities.

Using this provision, NSBLD changes must be documented and shall identify the

change with justification of the changes technical acceptability. The length of the probe

was the only difference to the previously installed TI. The TI was installed with a

3.25 inch probe, which was longer than the previous 2 inch probe. The added length

increased the shear force from the coolant flow and caused the probe to break off.

An operating experience (OPEX) review would have revealed an event at another

nuclear facility where the same make and model TI experienced the same failure

mechanism in a diesel generator coolant system. Under Revision 3 of SM-AA-300,

OPEX reviews for NSBLD were not required, nor were additional peer reviews required.

The lack of an OPEX review was an identified vulnerability by the licensees corporate

supply organization in a common cause analysis which was performed for a lack of

technical rigor issued in February 2008. A corrective action from this common cause

analysis was to implement Revision 4 of SM-AA-300 which limited NSBLD reviews to

non-safety host component applications. Revision 4 was implemented at Quad Cities in

February 2008. Since this specific TI is classified as augmented quality, Revision 4

would prevent use of the NSBLD process of a non-identical replacement. A full item

equivalency evaluation would be required for any non-identical replacement.

An extent of condition review is scheduled to be performed at Quad Cities by

Procurement Engineering for all NSBLD reviews that were performed under Revision 3

of SM-AA-300 from August 2007 through February 2008.

Analysis: The inspectors determined that the approval of an inappropriate component

designated as augmented quality was a performance deficiency and a finding. The

same parts evaluation process was used for risk-significant components independent of

the system being worked. Therefore, this finding was more than minor because, if left

uncorrected, this performance deficiency could lead to unplanned unavailability of

safety-related or risk-significant equipment and would become a more significant safety

concern. This performance deficiency challenged the Mitigating Systems Cornerstone

attribute of Equipment Performance by challenging equipment availability and reliability.

The inspectors performed a Phase 1 SDP screening and concluded that the issue was

of very low safety significance (Green) because the failure of the TI did not result in

unplanned inoperability or loss of function of the diesel generator. The inspectors

determined that this finding did not have a cross-cutting aspect. This performance

deficiency is not indicative of current licensee performance. The decision to install this

type of TI was made in October 2007. The process which allowed this performance

deficiency was identified and corrected through procedure and policy revisions to

SM-AA-300 in February 2008.

Enforcement: The TI was designated augmented quality in the licensees quality

assurance program. The licensees quality assurance program applied controls

equivalent to safety-related components for Class 1E equipment qualification to

augmented quality equipment and systems. This correlation is applicable to several

Appendix B criteria included in the program such as both Section 3 - Design Control,

and Section 5 - Instructions Procedures and Drawings, of the licensees Quality

Assurance program for augmented quality.

27

Enclosure

Title 10 CFR 50, Appendix B, Criterion V states in part that activities affecting quality

shall be prescribed by instructions and procedures of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions or

procedures.

Contrary to the above, on October 30, 2007, SM-AA-300 was not appropriate to the

circumstances in that it did not require an approval process with technical rigor

equivalent to the process used for safety-related components when a non-identical

temperature indicating probe designated augmented quality was approved for use.

That part was approved for use through a NSBLD review per Revision 3 of SM-AA-300

instead of undergoing a full item equivalency evaluation, and the part subsequently

failed resulting in foreign material in the diesel generator coolant system. The foreign

material did not cause any adverse consequences in this instance.

Because this issue is of very low safety significance, and this issue has been entered

into the licensees corrective action program as Issue Report 984769, this issue is being

treated as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(NCV 05000265/2009005-03).

Corrective actions for this event included replacement of the TI with an appropriately

approved TI. The licensee has also scheduled to perform an extent of condition review

of NSBLD reviews performed under Revision 3 of SM-AA-300 from August 2007 through

February 2008.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1

(Closed) Licensee Event Report 05000254/2009-003-00: Failure of RHR Torus Spray

Isolation Valve to Open Due to Declutch Mechanism Problems

a.

Inspection Scope

Inspectors reviewed the event, evaluation, and corrective actions for the motor operated

valve failure reported in Licensee Event Report (LER) 05000254/2009-003. Documents

reviewed as part of this inspection are listed in the Attachment to this report. This LER is

closed.

This event follow-up review constituted one sample as defined in IP 71153-05.

b.

Findings

Introduction: A finding of very low safety significance and an NCV of Technical

Specification (TS) 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool Spray,

was self-revealed for the licensees failure to meet the TS limiting condition for operation

(LCO) requirements prior to transitioning into an operating mode where the LCO was

required to be satisfied. Specifically, MO 1-1001-37B, motor operator for the Unit 1 RHR

torus (suppression pool) spray isolation valve, was found to have been inoperable when

the operating crew transitioned Unit 1 from Mode 4 to Mode 2 on May 30, 2009. The

valve actuator had been inadvertently declutched (i.e., motor disengaged) and the valve

was not demonstrated operable by stroking the valve electrically after the actuator motor

was declutched.

28

Enclosure

Discussion: On June 4, 2009, with Unit 1 in Mode 1 at 100 percent power following

startup from a forced outage, MO 1-1001-37B, torus spray shutoff valve, was determined

to be inoperable because it would not open remotely using the control switch during

performance of the residual heat removal power operated valve test surveillance.

The torus spray valve had been closed using the motor and a clearance order had been

placed on the valve during the outage. Another motor operated valve in the residual

heat removal system on that same clearance, MO 1-1001-7C, RHR C torus suction line

isolation valve, had failed to open on May 28, 2009, when the clearance tag was

removed and valve stroking was being performed to restore the component to a standby

configuration. Operators reported manually declutching (disengaging the actuator

motor) the 7C valve while placing the clearance tag in order to verify the valve was

closed. Inspectors identified that the action of manually verifying valve position was not

a normal practice as supported by OP-AA-103-105, Limitorque Motor-Operated Valve

Operations, and Operations department management. Investigation into the 7C failure

revealed that the actuator lubricant was degraded in the area of the clutch return spring

preventing the motor from engaging when called upon from the control circuit. The

RHR C valve actuator was rebuilt using MOV Long Life grease, new tripper cams, new

trip lever assembly, and a new outer declutch arm snap ring. The rebuilt actuator was

verified to operate correctly in all modes and returned to service prior to unit restart on

May 30, 2009.

Inspectors interviewed operating personnel regarding the positioning of MO 1-1001-37B

torus spray valve. Operators stated that they did not manually declutch the 37B valve

since the valve was already closed (normal position) when they hung the tag. The

licensees investigation attempted to identify both how the motor on the 37B valve was

declutched and why the actuator did not return to the motor mode of operation

automatically as designed. The licensee verified that the actuator was not able to

transition from the motor mode to the manual mode without external (human)

intervention.

Although the licensee could not identify how or when the valve actuator motor was

declutched, the licensees investigators concluded that the declutch lever was most likely

bumped during work activities on top of the Torus during the recent outage with the unit

in Mode 4. Investigation further determined that with the valve motor disengaged,

increased friction in the actuator caused by degraded lubricant in the area of the clutch

return spring prevented the engagement of the motor to open the valve. The actuator

motor was engaged by manually manipulating the declutch lever and stroke testing the

valve.

Inspectors reviewed the grease sampling methodology and the preventative

maintenance frequency for the SMP-00 type actuators and determined that both were

conducted in accordance with the industry standards for these type valves.

Analysis: The failure of plant personnel to demonstrate operability of MO 1-1001-37B by

stroking the valve electrically prior to changing modes was a performance deficiency.

The finding is more than minor because it was associated with the equipment

performance quality attribute of the Mitigating Systems Cornerstone and affected the

objective of ensuring availability, reliability and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, failure to verify

system availability and capability prior to entering the required modes resulted in fewer

29

Enclosure

available mitigating systems than assumed in the operating risk evaluations. Inspectors

determined that the finding was cross-cutting in the area of Problem Identification and

Resolution - Corrective Action because plant personnel failed to identify the valve

actuator contact that resulted in the valve being declutched; therefore, operators

incorrectly assessed the system condition as in compliance with TS 3.6.2.4 (P.1(a)).

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of Findings, Table 4a. Inspectors answered all of

the questions for the Mitigating Systems Cornerstone No. Therefore, the finding

screened as Green or very low safety significance.

Enforcement: Technical Specification 3.0, Limiting Condition for Operation (LCO)

Applicability, LCO 3.0.4 stated in part that when an LCO is not met, entry into a mode in

the Applicability shall only be made:

when the associated actions to be entered permit continued operation while in

the mode or other specified condition in the Applicability for an unlimited time;

after performance of a risk assessment addressing inoperable systems and

components, and acceptability of entering the mode; or

when an allowance is stated in the specification.

Technical Specification 3.6.2.4, Residual Heat Removal (RHR) Suppression Pool

Spray, required two RHR suppression pool spray subsystems to be operable in

Modes 1, 2 and 3.

Contrary to the above, on May 30, 2009, the licensee changed operating modes from

Mode 4 to Mode 2 with the MO 1-1001-37B valve inoperable in violation of TS 3.6.2.4

LCO conditions since only one RHR suppression pool (Torus) spray subsystem was

operable. Specifically, TS 3.6.2.4 had no allowance provided to permit mode change

with less than two subsystems operable, no prior risk assessment was performed, and

the specification did not permit operation for an unlimited time, the mode change

resulted in non-compliance with TS LCO 3.6.2.4.

Because this finding is of very low safety significance, and this issue has been entered

into the licensees corrective action program as IR 928048, this violation is being treated

as an NCV consistent with Section VI.A.1 of the NRC Enforcement Policy

(NCV 05000254/2009005-04).

Immediate corrective actions for this event included engagement of the actuator motor

by manually manipulating the declutch lever and stroke testing the valve. Since the

hardened grease in this area of the actuator assembly was only an issue if the actuator

was manually declutched, the valve was left in standby, and overhaul of the valve

actuator was scheduled for the next refueling outage.

30

Enclosure

4OA5 Other Activities

.1

World Association of Nuclear Operators Plant Assessment Report Review

a.

Inspection Scope

The inspectors reviewed the final report for the World Association of Nuclear Operators

plant assessment conducted in February 2009. The inspectors reviewed the report to

ensure that issues identified were consistent with the NRC perspectives of licensee

performance and to verify if any significant safety issues were identified that required

further NRC followup.

b.

Findings

No findings of significance were identified.

.2

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

b.

Findings

No findings of significance were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On January 5, 2010, the inspectors presented the inspection results to T. Tulon and

other members of the licensee staff. The licensee acknowledged the issues presented.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary.

.2

Interim Exit Meetings

Interim exits were conducted for:

The results of the licensed operator requalification training program inspection

and with the site vice president, Mr. T. Tulon, on October 2, 2009.

The licensed operator requalification training biennial written examination and

annual operating test examination materials were discussed with the training

manager, Mr. K. Moser, on November 12, 2009.

31

Enclosure

The licensed operator requalification training program annual inspection results

with operations training manager, Mr. D. Snook, on November 20, 2009, via

telephone.

The results of the Radiological Effluent TS/Offsite Dose Calculation Manual

Radiological Effluent Occurrences performance indicator verification program

inspection with the plant manager, Mr. R. Gideon, on December 16, 2009.

The annual review of Emergency Action Level and Emergency Plan changes

with the licensee's emergency preparedness coordinator, Mr. F. Swan, via

telephone on December 21, 2009.

The inspectors confirmed that none of the potential report input discussed was

considered proprietary. Proprietary material received during the inspection was returned

to the licensee.

4OA7 Licensee-Identified Violations

The following violation of very low significance (Green) was identified by the licensee

and is a violation of NRC requirements which meets the criteria of Section VI of the

NRC Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

Technical Specification 5.5.1 requires implementation of the Offsite Dose

Calculation Manual. Offsite Dose Calculation Manual, Revision 8, Part 12.2.1,

Radioactive Liquid Effluent Monitoring Instrumentation, Section C requires that

when the service water effluent gross activity monitor is operated with less than

the minimum number of operable channels, the licensee shall collect and analyze

grab samples for beta or gamma activity once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to the

above, grab samples were not collected while the Unit 1 service water effluent

gross activity monitor was inoperable from June 2-20, 2009. Specifically,

following fuse replacement, the licensee failed to recognize that the instrument

remained uninitialized; therefore, that compensatory samples were required. The

finding was documented in the licensees corrective action program as

IR 933472. Corrective actions included returning the monitor to service and

reviewing captured monitor data from June 2-20, 2009, to ensure that no release

events occurred during the monitor outage, revising the monitor repair and

maintenance procedures to clear direct communication with the Chemistry

Department subject matter experts during work on the system, and reinforcing

the expectation that control room operators turn over all abnormal indications to

supervisors each shift. The finding was determined to be of very low safety

significance because, although the finding related to the effluent release

program, it was not a failure to implement the effluent program or an event that

resulted in a dose to the public in excess of Appendix I criterion or

10 CFR 20.1301(e).

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Tulon, Site Vice President

R. Gideon, Plant Manager

D. Kimler, Shift Operations Superintendent

S. Darin, Engineering Manager

W. Beck, Regulatory Assurance Manager

J. Burkhead, Nuclear Oversight Manager

J. Garrity, Work Control Manager

K. Moser, Training Manager

V. Neels, Chemistry/Environ/Radwaste Manager

D. Collins, Radiation Protection Manager

D. Thompson, Security Manager

Nuclear Regulatory Commission

M. Ring, Chief, Reactor Projects Branch 1

Illinois Emergency Management Agency

R. Zuffa, Unit Supervisor, Resident Inspector Section

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened 05000254/2009005-01; 05000265/2009005-01

URI

Changes to EAL HU6 Potentially Decrease the Effectiveness

of the Plans without Prior NRC Approval 05000254/2009005-02; 05000265/2009005-02

FIN

Darley Pump Leaking Gasoline from the Fuel Pump 05000265/2009005-03

NCV

Temperature Indicating Probe Found Broken in the Unit 2

Diesel Generator Coolant System 05000254/2009005-04

NCV

Failure of RHR Torus Spray Isolation Valve to Open Due to

Declutch Mechanism Problems

Closed 05000254/2009005-02; 05000265/2009005-02

FIN

Darley Pump Leaking Gasoline from the Fuel Pump 05000265/2009005-03

NCV

Temperature Indicating Probe Found Broken in the Unit 2

Diesel Generator Coolant System 05000254/2009005-04

NCV

Failure of RHR Torus Spray Isolation Valve to Open Due to

Declutch Mechanism Problems05000254/2009003-00

LER

Failure of RHR Torus Spray Isolation Valve to Open Due to

Declutch Mechanism Problems

2

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01

- QCOP 0010-01; Winterizing Checklist; Revision 48

- QCOP 0010-02; Required Cold Weather Routines; Revision 28

- WC-AA-107; Seasonal Readiness; Revision 06

- IR 99493; U-2 FW Heater LCV Response to Lowering Circulating Water Inlet Temp

- WO 1183498; Cycle CW De-Ice Valve

- WO 1282535; Ice Melt Valve Stuck Shut

- QCOP 4400-06; Circulating Water System De-icing; Revision 14

- ECR 59777; Design Alternate Method for Operation of Ice Melt Valve

- IR 993018; Wire Rope Rating on Ice Melt Valve

- IR 986355; Ice Melt Valve Stuck Shut

- WO 01194645; MM Union Leaking Inside U1 Cond Demin Vault (HTG STM)

- WO 01215488; MM Repair Piping Leak Underground Next to Cribhouse

- WO 01242820; MM Seal Cracks in Ceiling Above Bus 23-1

Section 1R04

- QCOP 4100-01; Firewater System Lineup for Standby Operation; Revision 4

- QCOP 6600-01: Diesel Generator 1(2) Preparation For Standby Operation; Revision 38

- WO #01272234; EM Change RMS-9 Setting at SWGR 19 CUB 5D Per EC 377092

- WO #01107582; EM Replace U2 DGCWP Alternate Feed Contactor

- WO #920850; IM CAL DG HX 2-6661B Cooling Water Inlet PI 2-3941-67A

- WO #945963; IM CAL DG HX 2-6661B Cooling Water Outlet PI 2-3941-67B

- WO #01107581; EM Replace U2 DGCWP Normal Feed Contactor

- WO #01245102; EM Support OP QCOS 6600-17 U2 DGCW Pump Alternate Feed Test

- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for

Appendix R; Revision 15

- EC 360507; Unit 2 EDG Voltage Regulator (Place EDG in Droop Mode Prior to

Synchronization to the Grid)

- EC 377665; TMOD to Bypass Faulty SSES Switch Local/Remote Contact at U2 Diesel

Generator

Section 1R05

- OP-AA-201-008; Pre-fire Plan Manual Index - Pre-Plan RB-16; Revision 2

- Pre-plan TB-74; Fire Zone 9.1, Unit 1 Turbine Bldg. El. 595-0, Diesel Generator; Revision 24

- Pre-plan TB-73; Fire Zone 8.2.6.A, Unit 1 Turbine Bldg. El. 595-0, Reactor Feed Pumps;

Revision 24

- Pre-plan CH-44; Fire Zone 11.4.A, Crib House Bldg. El. 559-8 Basement; Revision 0

- Pre-plan CH-45; Fire Zone 11.4.B, Ground Floor/Service Water Pumps; Revision 22

3

Attachment

Section 1R11

- SY-AA-101-132; Assessment and Response to Suspicious Activity and Security Threats;

Revision 14

- QCOA 0010-20; Security Event; Revision 25

- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27

- Requalification Examination Results/Calendar Year 2009

- Quad Cities, Units 1 and 2 NRC Integrated Inspection Reports; dated various from

January 2007 through September 2009

- OP-AA-105-102; Attachment 1; Active License Tracking Log (for 1st & 2nd Quarters of 2009);

Revision 9

- OP-AA-105-102; Attachment 2, Reactivation of License Log (2 for LSRO, 2 RO); Revision 9

- Quad Cities Classroom Sample Plan for Training Years 2008 and 2009; 6/18/2009

- Quad Cities Simulator Sample Plan for Training Years 2008 and 2009

- 71111.11 Appendix C Responses/Justifications; 9/28/2009

- TQ-AA-224-F070; Evaluation Feedback Summary, LORT Cycle 08-1 through 08-5; LORT

Cycle 09-1 through 09-4

- TQ-AA-1002; Attachment 3; LORT Quarterly Curriculum Review Committee Meeting Minutes;

all of 2008 and first two quarters of 2009

- Special LORT CRC Meeting Minutes; 1/23/2009

- TQ-AA-150; Operator Training Programs; Revision 2

- TQ-AA-150-F07; Simulator Evaluation Form - STA or IA

- TQ-AA-150-F08; Simulator Evaluation Form - Individual

- TQ-AA-150-F09; Simulator Evaluation Form - Crew

- TQ-AA-210-5101; Training Observation Forms; dated various

- TQ-AA-306; Simulator Management

- TQ-AA-306-F06; BWR Critical Condition for Cold Startup; Revision 0

- TQ-AA-306-F07; BWR Power Coefficient of Reactivity and Control Rod Worth; Revision 0

- TQ-AA-306-F08; BWR Xenon Worth; Revision 0

- TQ-AA-306-F06; BWR Site Specific Shutdown Margin and Reactivity Anomaly Tests

- TQ-AA-306-JA-02; Simulator Testing Report Update

- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 14;

7/17/09

- Differences between the Quad Cities Simulator and Quad Cities U-1 & U-2; Revision 15;

9/29/09

- LS-AA-126-1005; Attachment 2; Check-In Self-Assessment Report Template

- LS-AA-126-1001; Attachment 2; FASA Self-Assessment Report

- Simulator Malfunction Test Procedure, Grid Frequency Disturbance (ED16)

- Simulator Malfunction Test Procedure, Reactor Building Instrument Air System (IA02)

- Simulator Malfunction Test Procedure, Main Steam Isolation Valve Closure (MS01)

- Quad Cities Simulator Malfunction Testing Schedule; Revision 8; 5/5/2008

- Simulator Transient Tests; dated various

- Safety System Functional Failure, Rolling Twelve Months Unit 1 and Unit 2; 9/28/09

- Action Request Reports; various dates for LORT 2009

- LORT Attendance Sheets; 2009

4

Attachment

Section 1R12

- Enterprise Maintenance Rule Production Database for the following systems:

Z2900; Safe Shutdown Makeup Pump

Z4700; Instrument Air

- System Engineer Notebook and Accountability Logs for the following systems:

Safe Shutdown Makeup Pump

Instrument Air

- IR 712670; Safe shutdown makeup pump failed surveillance; 12/17/07

- IR 713041; Broken SSMP part not found during repairs; 12/18/07

- IR 711934; SSMP Suction line did not fill during fill; 12/14/07

- IR 712059; SSMP fails to sustain flow and pressure; 12/15/07

- IR 731013; SSMP Sparking on Startup; 2/4/08

- IR 729984; SSMP failed operability test per TIC-1982; 2/1/08

- IR 729951; SSMP Local FIC failed PMT; 1/31/08

- IR 734472; MRULE A-1 determination for SSMP required; 2/11/08

- IR 741838; SSMP feed breaker problems during system restoration; 2/27/08

- IR 787063; Local SSMP flow controller not reading correctly; 6/16/08

- IR 890904; SSMP controller connector degraded; 3/10/09

- IR 930013; Historical FME identified in SSMP piping inspection; 6/10/09

- IR 956294; SSMP FIC Valve position discrepancy with local valve indication; 8/21/09

- IR 947201; FPI - SSMP Breaker and fuse coordination for CT-2; 7/29/08

- IR 1003024; SSMP Draws a vacuum when starting for PMT; 12/09/09

- IR 1002036; Drain valve for SSMP room cooler may be blocked; 12/06/09

- IR 991490; NCV 09-006-02 Closure package - SSMP Breaker coordination 11/10/09

- IR 673268; 1B Instrument Air Compressor Excessive Leakage; 9/20/07

- IR 762652; 1A Instrument Air Compressor Trip; 04/12/08

- IR 856509; Red Trend Code for 1/2B Instrument Air Compressor - EC 364602

- IR 871161; 1A Instrument Air Compressor Trip; 01/24/09

- IR 871939; 1A Instrument Air Compressor Trip; 01/26/09

- IR 977823; 1A Instrument Air Compressor Tripped Due to Low Oil Pressure; 2/7/09

- IR 936122; Compressor does not auto start; 6/27/09

Section 1R13

- WO #01075655; EM Perform Boroscope INSP of MO 1-1001-16A MOV

- WO #01120751; EM MOV 1-1001-37A MOV EQ Inspection

- WO #01123089; MM Inspect/Clean 1B RHR Pump Seal Cooler

- WO #01131318; EM Votes Test MOV 1-1001-16A

- WO #01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect

Section 1R15

- IR 849245; 1B RHR Room Cooler Heat Exchanger Has Tube Sheet Pitting

- WO 862709; 1B RHR Air/Water Side Room CLR CLN/INSP

- IR 987904; 1A RHR Room Cooler Heat Exchanger Tube Sheet Has Pitting

- WO 01190642; MM U-1A RHR HX Room Cooler Air/Water Side Clean Inspect

5

Attachment

- IR 849681; 1B RHR Room Cooler Reassembled at Risk

- EC 373177; Determination of Minimum Wall Thickness of Tubesheet for RHR Room

Cooler 1-574B

- IR 994823; TS SR 3.8.4.8 Frequency Not Met

- QC-SURV-01; Risk Assessment for Missed Surveillance for U2 125 Vdc Battery

Section 1R19

- QCMMS 4100-32; 1/2 -4101A Diesel Driven Fire Pump Annual Capacity Test; Revision 24

- WO 1261246; Replace Battery Changeover Relay R12 EC 376690

- EC 376690; 1/2 A Fire Pump Controller Replace Battery Changeover Relay R12; Revision 1

- QCOS 4100-01; Monthly Diesel Fire Pump Test; Revision 28

- QCOP 4100-03; Diesel Fire Pump Operation; Revision 17

- QCMMS 4100-33; 1/2 - 4101B Diesel Driven Fire Pump Annual Capacity Test; Revision 24

- WO 1121775; 250 Vdc Battery Charger #2 4 Hour Load Test

- WO 1130534; Control RM HVAC Air Filter Unit In Place DOP LK Test

- QCOS 5750-02; Control Room Emergency Filter System Test; Revision 45

- QCIS 5700-04; Main Control Room Air Filter Unit DOP-Freon Test; Revision 0

- QCOS 6600-17; Operating Cycle Diesel Cooling Water Pump Alternate Power Feed Test for

Appendix R; Revision 15

- QCEPM 0400-15; Emergency Diesel Generator Transfer Panel Inspection; Revision 9

- WO 01107582; Replace Unit 2 DGCWP Alternate Feed Contactor

Section 1R22

- QCOS 1400-01; Quarterly Core Spray System Flow Rate Test; Revision 38

- QCOS 1400-07; Core Spray Pump Performance Test; Revision 10

- QCOS 7500-05; Standby Gas Treatment System Monthly Operability Test; Revision 30

- QCIS 0300-02; Unit 1 Division 1 Scram Discharge Volume Rochester Instruments Calibration

and Functional Test; Revision 09

- QCOS 1600-07, Revision 027; Reactor Coolant Leakage in the Drywell

- QCEMS 0230-11; Modified Performance Test of Unit 1(2) 125 Vdc Normal or Alternate

Battery; Revision 0

- QCOS 6900-02; Station Safety Related Battery Quarterly Surveillance; Revision 33

- QCOP 6900-24; Transfer of Unit 2 125 Vdc Battery Bus Between Normal and Alternate

Battery; Revision 12

- QCOS 6900-14; Station Battery Allowable Value Verification Surveillance; Revision 13

Section 1EP4

- Quad Cities Station Radiological Emergency Plan Annex; Revisions 25, 26, and 27

Section 1EP6

- EP-AA-1006; Radiological Emergency Plan Annex for Quad Cities Station; Revision 27

- Quad Cities Generating Station 2009 Termination and Recovery Drill Briefing Package;

December 2, 2009

- EP-AA-115; Termination and Recovery; Revision 7

- EP-AA-111-F-01; Termination/Recovery Checklist; Revision A

6

Attachment

Section 4OA1

- CY-QC-120-724; Continuous Liquid Effluent Analysis; Revision 1

- CY-QC-120, 723; Allocation of Radioactive Liquid Discharges; Revision 0

- CY-QC-120-720; Plant Effluent Dose Calculations; Revision 4

- CY-QC-120-725; Gaseous Release of Tritium Calculation; Revision 1

- Cy-QC-120-726; Fe-55, Sr-89, Sr-90 and Gaseous Alpha Release; Revision 3

- NEI 99-02; Regulatory Assessment Performance Indicator Guideline, Revision 6

- Enterprise Maintenance Rule Production Database for the following systems:

Z2300; High Pressure Coolant Injection System

Z1000; Residual Heat Removal System

Z6600; Diesel Generator System

Z1300; Reactor Core Isolation Cooling System

Z9700; 345 kV Switchyard

- System Engineer Notebook and Accountability Logs for the following systems:

Residual Heat Removal

RHR Service Water

Reactor Core Isolation Cooling

HPCI

Emergency Diesel Generators

Section 4OA2Q

- IR 984769; Well Broke Off TI in Diesel Generator Coolant System

- WO 1198663; U-2 EDG Eng Temp Indicator TI-2-6641-8205 Not Working

- WO 1280197; Well Broke Off TI In U2 Diesel Generator Coolant System

- SM-AA-300; Procurement Engineering Support Activities; Revision 5

- IR 624645; Flood Emergency Pump Testing Documentation; 05/02/07

- IR 638004; Clarify UFSAR 3.4.1.1 Required Flow Rate to SFP During Flood; 06/07/07

- IR 738335; NCV 07-005-02 GR NCV & X-cutting WRT External Flooding Event; 02/19/08

- IR 921197; Inappropriate ACIT Closure of Darley Pump NCV; 05/18/09

- IR 927463; Request For Darley Pump Testing in On-line Schedule; 06/03/09

- IR 966501; Darley Pump Leaking Gasoline from the Fuel Pump; 09/17/09

- IR 968809; Adequacy of Preventative Maintenance on Darley Pump; 09/22/09

- WO 01247374; Darley Pump Baseline Testing; 9/17/09

- QCOA 0010-16; Flood Emergency Procedure; Revision 12

- QCMMS 1500-12; Portable Emergency Flood Pump Capacity Test; Revision 0

- QCOP 4100-19; Emergency Portable Pump Operations; Revision 7

- PMID/RQ 164250; Perform Maintenance on the External Portable Pump; 09/17/09

Section 4OA3

- 10 Medical Files for Licensed Operators; Various Dates

- Licensee Event Report 254/09-003; Failure of RHR Torus Spray Isolation Valve Due to

Declutch Mechanism Problems; 8/3/09

- IR 928048; MO 1-1001-37B Failed to Open During QCOS 1000-09; 6/4/09

- IR 924666; 1-1001-7C Will Not Open; 5/28/09

- OP-AA-103-105; Limitorque Motor-operated Valve Operations; Revision 1

7

Attachment

Section 4OA7

- AR 933472933472 Service Water Effluent Radiation Monitor Inoperable; 6/20/09

8

Attachment

LIST OF ACRONYMS USED

AC

Alternating Current

ADAMS

Agencywide Document Access Management System

ACIT

Action Tracking Item

CAP

Corrective Action Program

CFR

Code of Federal Regulations

DGCWP

Diesel Generator Cooling Water Pump

EAL

Emergency Action Level

EC

Engineering Change

EDG

Emergency Diesel Generator

IMC

Inspection Manual Chapter

IP

Inspection Procedure

IR

Issue Report

IST

Inservice Test

JPM

Job Performance Measure

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LORT

Licensed Operator Requalification Training

MO

Motor Operator

MOV

Motor Operated Valve

MSPI

Mitigating System Performance Index

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NRC

U.S. Nuclear Regulatory Commission

NSBLD

Non-Safety Below Level of Design Detail

OP

Operations

OPEX

Operating Experience

ODCM

Offsite Dose Calculation Manual

PARS

Publicly Available Records

PI

Performance Indicator

PM

Planned or Preventative Maintenance

PMT

Post Maintenance Test

RCS

Reactor Coolant System

RETS

Radiological Effluent Technical Specification

RHR

Residual Heat Removal

RHRSW

Residual Heat Removal Service Water

SAT

Systems Approach to Training

SDP

Significance Determination Process

SSC

Systems, Structures, and Components

TI

Temperature Indicator

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

Vdc

Volt direct current

WO

Work Order

C. Pardee

-2-

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter

and its enclosure will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Enclosure:

Inspection Report 05000254/2009005; 05000265/2009005

w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

DOCUMENT NAME: G:\\1-Secy\\1-Work In Progress\\QUA 2009005.doc

Publicly Available

Non-Publicly Available

Sensitive

Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl

"E" = Copy with attach/encl "N" = No copy

OFFICE

RIII

E RIII

NAME

MRing:cms

DATE

01/27/2010

OFFICIAL RECORD COPY

Letter to C. Pardee from M. Ring dated January 27, 2010

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2 INTEGRATED

INSPECTION REPORT 05000254/2009005; 05000265/2009005

DISTRIBUTION:

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