IR 05000445/2018003: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(StriderTol Bot change)
 
(2 intermediate revisions by the same user not shown)
Line 18: Line 18:


=Text=
=Text=
{{#Wiki_filter:ber 31, 2018
{{#Wiki_filter:October 31, 2018


==SUBJECT:==
==SUBJECT:==
Line 33: Line 33:


Sincerely,
Sincerely,
/RA/
/RA/  
Mark S. Haire, Chief Project Branch A Division of Reactor Projects Docket Nos. 50-445 and 50-446 License Nos. NPF-87 and NPF-89 Enclosure:
 
Mark S. Haire, Chief Project Branch A Division of Reactor Projects  
 
Docket Nos. 50-445 and 50-446 License Nos. NPF-87 and NPF-89  
 
Enclosure:
Inspection Report 05000445/2018003 and 05000446/2018003 w/ Attachments:
Inspection Report 05000445/2018003 and 05000446/2018003 w/ Attachments:
1. Documents Reviewed 2. Detailed Risk Evaluation
1. Documents Reviewed 2. Detailed Risk Evaluation  


U.S. NUCLEAR REGULATORY COMMISSION
Enclosure
 
U.S. NUCLEAR REGULATORY COMMISSION  


==Inspection Report==
==Inspection Report==
Docket Number(s): 05000445 and 05000446 License Number(s): NPF-87 and NPF-89 Report Number(s): 05000445/2018003 and 05000446/2018003 Enterprise Identifier: I-2018-003-0011 Licensee: Vistra Operations Company, LLC Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2 Location: Glen Rose, Texas Inspection Dates: July 1, 2018 to September 30, 2018 Inspectors: J. Josey, Senior Resident Inspector R. Kumana, Resident Inspector H. Freeman, Senior Reactor Inspector Approved By: Mark S. Haire Chief, Project Branch A Division of Reactor Projects Enclosure
Docket Number(s):
05000445 and 05000446  
 
License Number(s):
NPF-87 and NPF-89  
 
Report Number(s):
05000445/2018003 and 05000446/2018003  
 
Enterprise Identifier: I-2018-003-0011  
 
Licensee:
Vistra Operations Company, LLC  
 
Facility:
Comanche Peak Nuclear Power Plant, Units 1 and 2  
 
Location:
Glen Rose, Texas  
 
Inspection Dates:
July 1, 2018 to September 30, 2018  
 
Inspectors:
J. Josey, Senior Resident Inspector  
 
R. Kumana, Resident Inspector  
 
H. Freeman, Senior Reactor Inspector  
 
Approved By:
Mark S. Haire  
 
Chief, Project Branch A  
 
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
Line 49: Line 91:
NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations are documented in the Inspection Results at the end of this report.
NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations are documented in the Inspection Results at the end of this report.


List of Findings and Violations Failure to Maintain the Ability to Withstand a Station Blackout Cornerstone       Significance                                     Cross-cutting   Inspection Aspect          Procedure Mitigating       Green                                             None            71152 -
===List of Findings and Violations===
Systems          NCV 05000445/2018003-01;                                         Problem 05000446/2018003-01                                               Identification Closed                                                            and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50.63 for the licensees failure to maintain the ability to withstand and recover from a station blackout. Specifically, the licensees approved coping analysis for each unit required the availability of equipment on the non-blacked-out unit, and the licensee failed to maintain the required equipment available.
Failure to Maintain the Ability to Withstand a Station Blackout Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000445/2018003-01; 05000446/2018003-01 Closed None 71152 -
Problem Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50.63 for the licensees failure to maintain the ability to withstand and recover from a station blackout. Specifically, the licensees approved coping analysis for each unit required the availability of equipment on the non-blacked-out unit, and the licensee failed to maintain the required equipment available.


The licensee entered this violation into their corrective action program as condition report CR-2017-011090.
The licensee entered this violation into their corrective action program as condition report CR-2017-011090.


Failure to Establish Adequate Procedural Guidance for Processing Technical Changes Performed by a Vendor on Installed Plant Equipment Cornerstone Significance                                           Cross-cutting Report Aspect          Section Mitigating     Green                                               None            71152 -
Failure to Establish Adequate Procedural Guidance for Processing Technical Changes Performed by a Vendor on Installed Plant Equipment Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018003-02; 5000446/2018003-02 Closed None 71152 -
Systems        NCV 05000445/2018003-02;                                           Problem 5000446/2018003-02                                                 Identification Closed                                                              and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to establish an adequate procedure for controlling and processing vendor documents and vendor technical information. This resulted in the licensees failure to properly evaluate changes made by vendors to plant equipment. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes. The licensee entered this issue into the corrective action program as Condition Reports CR-2018-004485 and CR-2018-004605.
Problem Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to establish an adequate procedure for controlling and processing vendor documents and vendor technical information. This resulted in the licensees failure to properly evaluate changes made by vendors to plant equipment. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes. The licensee entered this issue into the corrective action program as Condition Reports CR-2018-004485 and CR-2018-004605.


Additional Tracking Items Type Issue number           Title                   Inspection Status Procedure VIO 05000445/2017010-01;   Failure to Update Final 92702      Closed 05000446/2017010-01   Safety Analysis Report Section 8.3.1.1.11
===Additional Tracking Items===
Type Issue number Title Inspection Procedure Status VIO 05000445/2017010-01; 05000446/2017010-01 Failure to Update Final Safety Analysis Report Section 8.3.1.1.11 92702 Closed


=PLANT STATUS=
=PLANT STATUS=
Line 69: Line 113:


==REACTOR SAFETY==
==REACTOR SAFETY==
 
===71111.01Adverse Weather Protection Seasonal Extreme Weather===
===71111.01Adverse Weather Protection Seasonal Extreme Weather ===
{{IP sample|IP=IP 71111.01|count=1}}
{{IP sample|IP=IP 71111.01|count=1}}
The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal hot temperatures.
The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal hot temperatures.


===71111.04Equipment Alignment Partial Walkdown ===
===71111.04Equipment Alignment Partial Walkdown===
{{IP sample|IP=IP 71111.04|count=4}}
{{IP sample|IP=IP 71111.04|count=4}}
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
Line 80: Line 123:
: (2) Unit 2 residual heat removal pump 2-02 on September 5, 2018
: (2) Unit 2 residual heat removal pump 2-02 on September 5, 2018
: (3) Unit 2 turbine driven auxiliary feedwater pump on September 12, 2018
: (3) Unit 2 turbine driven auxiliary feedwater pump on September 12, 2018
: (4) Unit 2 instrument air system on September 14, 2018
: (4) Unit 2 instrument air system on September 14, 2018  


===Complete Walkdown (1 Sample)===
===Complete Walkdown (1 Sample)===
The inspectors evaluated system configurations during a complete walkdown of the uninterruptible power supply (UPS) heating ventilation and air conditioning system on September 25, 2018.
The inspectors evaluated system configurations during a complete walkdown of the uninterruptible power supply (UPS) heating ventilation and air conditioning system on September 25, 2018.


===71111.05AQFire Protection Annual/Quarterly Quarterly Inspection ===
===71111.05AQFire Protection Annual/Quarterly Quarterly Inspection===
{{IP sample|IP=IP 71111.05|count=4}}
{{IP sample|IP=IP 71111.05|count=4}}
The inspectors evaluated fire protection program implementation in the following selected areas:
The inspectors evaluated fire protection program implementation in the following selected areas:
Line 91: Line 134:
: (2) Fire zone ER150, UPS Chiller X-02 on September 17, 2018
: (2) Fire zone ER150, UPS Chiller X-02 on September 17, 2018
: (3) Fire zone EH52 and EH53, train A UPS rooms on September 21, 2018
: (3) Fire zone EH52 and EH53, train A UPS rooms on September 21, 2018
: (4) Fire zone EC50 and EC51, train B UPS rooms on September 21, 2018
: (4) Fire zone EC50 and EC51, train B UPS rooms on September 21, 2018  


===71111.06Flood Protection Measures Internal Flooding ===
===71111.06Flood Protection Measures Internal Flooding===
{{IP sample|IP=IP 71111.06|count=1}}
{{IP sample|IP=IP 71111.06|count=1}}
The inspectors evaluated internal flooding mitigation protections in the UPS chiller rooms on August 29, 2018.
The inspectors evaluated internal flooding mitigation protections in the UPS chiller rooms on August 29, 2018.


===71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification ===
===71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification===
{{IP sample|IP=IP 71111.11|count=1}}
{{IP sample|IP=IP 71111.11|count=1}}
The inspectors observed and evaluated a crew during an evaluated simulator scenario on
The inspectors observed and evaluated a crew during an evaluated simulator scenario on September 5, 2018.


===September 5, 2018.
===Operator Performance (1 Sample)===
 
Operator Performance (1 Sample)===
The inspectors observed and evaluated Unit 2 control room operators during post trip response on August 13, 2018, and Unit 2 startup activities on August 15, 2018.
The inspectors observed and evaluated Unit 2 control room operators during post trip response on August 13, 2018, and Unit 2 startup activities on August 15, 2018.


===71111.12Maintenance Effectiveness Routine Maintenance Effectiveness ===
===71111.12Maintenance Effectiveness Routine Maintenance Effectiveness===
{{IP sample|IP=IP 71111.12|count=1}}
{{IP sample|IP=IP 71111.12|count=1}}
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:
: (1) Units 1 and 2 UPS chillers on August 22, 2018
: (1) Units 1 and 2 UPS chillers on August 22, 2018  


===71111.13Maintenance Risk Assessments and Emergent Work Control ===
===71111.13Maintenance Risk Assessments and Emergent Work Control===
{{IP sample|IP=IP 71111.13|count=5}}
{{IP sample|IP=IP 71111.13|count=5}}
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
Line 118: Line 159:
: (3) Units 1 and 2, breach of control room envelope on August 24, 2018
: (3) Units 1 and 2, breach of control room envelope on August 24, 2018
: (4) Units 1 and 2, repair of auxiliary feedwater pump flow control valves on August 28, 2018
: (4) Units 1 and 2, repair of auxiliary feedwater pump flow control valves on August 28, 2018
: (5) Units 1 and 2, measurement of silt level in station service water intake bay on July 25, 2018
: (5) Units 1 and 2, measurement of silt level in station service water intake bay on July 25, 2018  


===71111.15Operability Determinations and Functionality Assessments ===
===71111.15Operability Determinations and Functionality Assessments===
{{IP sample|IP=IP 71111.15|count=5}}
{{IP sample|IP=IP 71111.15|count=5}}
The inspectors evaluated the following operability determinations and functionality assessments:
The inspectors evaluated the following operability determinations and functionality assessments:
: (1) Unit 2, containment isolation valve leakage, on July 9 , 2018
: (1) Unit 2, containment isolation valve leakage, on July 9, 2018
: (2) Unit 1, failure of battery cell on battery 1ED2, on July 2, 2018
: (2) Unit 1, failure of battery cell on battery 1ED2, on July 2, 2018
: (3) Units 1 and 2, inadequate procedure for makeup to component cooling water system, on July 16, 2018
: (3) Units 1 and 2, inadequate procedure for makeup to component cooling water system, on July 16, 2018
: (4) Unit 2, safety injection accumulator 2-01 high pressure, on July 26, 2018
: (4) Unit 2, safety injection accumulator 2-01 high pressure, on July 26, 2018
: (5) Unit 1, incorrect fuses removed from 480V bus 1EB1, on September 24, 2018
: (5) Unit 1, incorrect fuses removed from 480V bus 1EB1, on September 24, 2018  


===71111.18Plant Modifications ===
===71111.18Plant Modifications===
{{IP sample|IP=IP 71111.18|count=1}}
{{IP sample|IP=IP 71111.18|count=1}}
The inspectors evaluated the following temporary or permanent modifications:
The inspectors evaluated the following temporary or permanent modifications:
: (1) Removal of cell 27 from battery 1ED2 after the cell was discovered cracked on July 2, 2018
: (1) Removal of cell 27 from battery 1ED2 after the cell was discovered cracked on July 2, 2018  


===71111.19Post Maintenance Testing ===
===71111.19Post Maintenance Testing===
{{IP sample|IP=IP 71111.19|count=7}}
{{IP sample|IP=IP 71111.19|count=7}}
The inspectors evaluated the following post maintenance tests:
The inspectors evaluated the following post maintenance tests:
Line 143: Line 184:
: (5) Unit 2, diesel generator 2-02 following replacement of master drive, on August 27, 2018
: (5) Unit 2, diesel generator 2-02 following replacement of master drive, on August 27, 2018
: (6) Unit 1, drip pot drain isolation valve 1-LV-2373 following repair, on August 29, 2018
: (6) Unit 1, drip pot drain isolation valve 1-LV-2373 following repair, on August 29, 2018
: (7) Unit 1, battery charger 1ED1-1 following card replacement, on September 26, 2018
: (7) Unit 1, battery charger 1ED1-1 following card replacement, on September 26, 2018  


===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:
===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:
Routine ===
Routine===
{{IP sample|IP=IP 71111.22|count=3}}
{{IP sample|IP=IP 71111.22|count=3}}
: (1) Unit 1, OPT-447A, train A reactor trip breaker test, on August 1, 2018
: (1) Unit 1, OPT-447A, train A reactor trip breaker test, on August 1, 2018
: (2) Units 1 and 2, OPT-220, fire pump X-06 test, on August 30, 2018
: (2) Units 1 and 2, OPT-220, fire pump X-06 test, on August 30, 2018
: (3) Unit 1, OPT-206A, turbine driven auxiliary feedwater pump test, on September 7, 2018
: (3) Unit 1, OPT-206A, turbine driven auxiliary feedwater pump test, on September 7, 2018  


===In-service (2 Samples)===
===In-service (2 Samples)===
: (1) Unit 2, OPT-837, 2-HV-5545, air particulate, iodine and gas detector sample isolation valve leak test, on July 10, 2018
: (1) Unit 2, OPT-837, 2-HV-5545, air particulate, iodine and gas detector sample isolation valve leak test, on July 10, 2018
: (2) Unit 1, OPT-208A, component cooling water pump 1-01 discharge valve test, on August 29, 2018
: (2) Unit 1, OPT-208A, component cooling water pump 1-01 discharge valve test, on August 29, 2018  


===71114.06Drill Evaluation Drill/Training Evolution ===
===71114.06Drill Evaluation Drill/Training Evolution===
{{IP sample|IP=IP 71114.06|count=1}}
{{IP sample|IP=IP 71114.06|count=1}}
The inspectors evaluated an emergency preparedness drill on July 11,
The inspectors evaluated an emergency preparedness drill on July 11,


==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
 
===71151Performance Indicator Verification===
===71151Performance Indicator Verification ===
{{IP sample|IP=IP 71151|count=6}}
{{IP sample|IP=IP 71151|count=6}}
The inspectors verified licensee performance indicators submittals listed below:
The inspectors verified licensee performance indicators submittals listed below:
: (1) MS06: Emergency AC Power Systems (07/01/2017-06/30/2018)
: (1) MS06: Emergency AC Power Systems (07/01/2017-06/30/2018)
: (2) MS07: High Pressure Injection Systems (07/01/2017-06/30/2018)
: (2) MS07: High Pressure Injection Systems (07/01/2017-06/30/2018)
: (3) MS08: Heat Removal Systems (07/01/2017-06/30/2018)
: (3) MS08: Heat Removal Systems (07/01/2017-06/30/2018)  


===71152Problem Identification and Resolution Annual Follow-up of Selected Issues ===
===71152Problem Identification and Resolution Annual Follow-up of Selected Issues===
{{IP sample|IP=IP 71152|count=2}}
{{IP sample|IP=IP 71152|count=2}}
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
: (1) Failure to meet station blackout coping requirements during adjacent unit refueling outages
: (1) Failure to meet station blackout coping requirements during adjacent unit refueling outages
: (2) Failure to perform a 50.59 evaluation for a vendor change to a component cooling water pump
: (2) Failure to perform a 50.59 evaluation for a vendor change to a component cooling water pump  


===71153Follow-up of Events and Notices of Enforcement Discretion Personnel Performance ===
===71153Follow-up of Events and Notices of Enforcement Discretion Personnel Performance===
{{IP sample|IP=IP 71153|count=1}}
{{IP sample|IP=IP 71153|count=1}}
The inspectors evaluated a Unit 2 reactor trip and licensees performance on August 13,
The inspectors evaluated a Unit 2 reactor trip and licensees performance on August 13,


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 92702Follow-up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution Confirmatory Orders The inspectors reviewed the licensees response to Notice of Violation (NOV) 05000445/2017010-01; 05000446/2017010-01 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance will be achieved for this violation are adequately addressed and captured on the docket.
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL  
 
92702Follow-up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution Confirmatory Orders  
 
The inspectors reviewed the licensees response to Notice of Violation (NOV) 05000445/2017010-01; 05000446/2017010-01 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance will be achieved for this violation are adequately addressed and captured on the docket.


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Failure to Maintain the Ability to Withstand a Station Blackout Cornerstone       Significance                                   Cross-cutting   Inspection Aspect          Procedure Mitigating         Green                                          None
Failure to Maintain the Ability to Withstand a Station Blackout Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems


==71152 - Systems==
Green NCV 05000445/2018003-01; 05000446/2018003-01 Closed None
NCV 05000445/2018003-01;                                         Problem 05000446/2018003-01                                             Identification Closed                                                          and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50.63 for the licensees failure to maintain the ability to withstand and recover from a station blackout. Specifically, the licensees approved coping analysis for each unit required the availability of equipment on the non-blacked-out unit, and the licensee failed to maintain the required equipment available.
 
==71152 - Problem==
Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50.63 for the licensees failure to maintain the ability to withstand and recover from a station blackout. Specifically, the licensees approved coping analysis for each unit required the availability of equipment on the non-blacked-out unit, and the licensee failed to maintain the required equipment available.


=====Description:=====
=====Description:=====
Line 199: Line 245:
Corrective Action(s): The licensee entered this violation into their corrective action program.
Corrective Action(s): The licensee entered this violation into their corrective action program.


Corrective Action Reference: CR-2017-011090
Corrective Action Reference: CR-2017-011090  


=====Performance Assessment:=====
=====Performance Assessment:=====
Line 219: Line 265:
Enforcement Action: This violation is being treated as a non-cited violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy.
Enforcement Action: This violation is being treated as a non-cited violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy.


Failure to Establish Adequate Procedural Guidance for Processing Technical Changes Performed by A Vendor on Installed Plant Equipment Cornerstone             Significance                             Cross-cutting     Report Aspect            Section Mitigating             Green                                     None
Failure to Establish Adequate Procedural Guidance for Processing Technical Changes Performed by A Vendor on Installed Plant Equipment Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018003-02; 5000446/2018003-02 Closed None


==71152 - Systems==
==71152 - Problem==
NCV 05000445/2018003-02;                                    Problem 5000446/2018003-02                                          Identification Closed                                                      and Resolution The inspectors identified a Green, NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to establish an adequate procedure for controlling and processing vendor documents and vendor technical information. This resulted in the licensees failure to properly evaluate changes made by vendors to plant equipment. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes.
Identification and Resolution The inspectors identified a Green, NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to establish an adequate procedure for controlling and processing vendor documents and vendor technical information. This resulted in the licensees failure to properly evaluate changes made by vendors to plant equipment. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes.


=====Description:=====
=====Description:=====
Line 237: Line 283:
Corrective Action(s): The licensee performed operability determinations that established a reasonable expectation of operability pending development of additional corrective actions.
Corrective Action(s): The licensee performed operability determinations that established a reasonable expectation of operability pending development of additional corrective actions.


Corrective Action References: CR-2018-004485 and CR-2018-004605
Corrective Action References: CR-2018-004485 and CR-2018-004605  


=====Performance Assessment:=====
=====Performance Assessment:=====
Line 266: Line 312:
71152Problem Identification and Resolution
71152Problem Identification and Resolution
Condition Reports
Condition Reports
CR-2017-011090         TR-2017-011125         CR-2018-004485           CR-2018-004605
CR-2017-011090
CR-2018-001530         CR-2018-001532         CR-2018-003476           CR-2018-000941
TR-2017-011125
CR-2018-004485
CR-2018-004605
CR-2018-001530
CR-2018-001532
CR-2018-003476
CR-2018-000941
Procedures
Procedures
Number           Title                                                     Revision
Number
STA-206           Review of Vendor Documents and Vendor Technical           20
Title
Manuals
Revision
STA-206
Review of Vendor Documents and Vendor Technical
Manuals  
 
Miscellaneous
Miscellaneous
Documents                                                                   Revision
Documents
Number           Title                                                     or Date
Number  
DBD-EE-043       118V AC Uninterruptible Power System                       14
 
DBD-ME-026       Station Blackout                                           12
Title
TXX-92447         Response to Station Blackout (SBO) Rule                   October 1, 1992
Revision
LDCR SA-2000-     Update/Clarify SBO Coping as Described on Pages 2         October 25,
or Date
049              Through 6                                                  2000
DBD-EE-043
DBD-ME-313       Uninterruptible Power Supply HVAC System                   12
118V AC Uninterruptible Power System
TXX-96475         Additional Information for License Amendment 96-004       October 1, 1996
DBD-ME-026
Station Blackout
TXX-92447
Response to Station Blackout (SBO) Rule
October 1, 1992
LDCR SA-2000-
049
Update/Clarify SBO Coping as Described on Pages 2
Through 6
October 25,
2000
DBD-ME-313
Uninterruptible Power Supply HVAC System
TXX-96475
Additional Information for License Amendment 96-004
Uninterruptible Power Supplies (UPS) HVAC System
Uninterruptible Power Supplies (UPS) HVAC System
Addition of Fan Coil Units to Technical Specifications
Addition of Fan Coil Units to Technical Specifications
October 1, 1996
Engineering
Engineering
Reports Number   Title                                                     Revision
Reports Number
ER-ME-011         Unit 1 & Unit 2 Station Blackout Assessment               2
Title
Revision
ER-ME-011
Unit 1 & Unit 2 Station Blackout Assessment  
 
Calculations
Calculations
Number             Title                                                           Revision
Number
3-D-2-027           Temperature Transient Study for Station Blackout                 0
Title
RXE-LA-CPX/0-099 Station Blackout Coping Analysis for CPSES Units 1& 2 at           0
Revision
3-D-2-027
Temperature Transient Study for Station Blackout
RXE-LA-CPX/0-099 Station Blackout Coping Analysis for CPSES Units 1& 2 at
3634 MW
3634 MW
3-D-2-025           UPS Room Temperature Transients During Sta. Blkot &             0
3-D-2-025
UPS Room Temperature Transients During Sta. Blkot &
FSSD
FSSD
ME-CA-0313-4079 UPS Inverter Rooms Temperature Transient following Station           2
ME-CA-0313-4079
Blackout with one Room Cooler in Operation
UPS Inverter Rooms Temperature Transient following Station
Blackout with one Room Cooler in Operation  
 
2702 Follow-up on Traditional Enforcement Actions Including Violations, Deviations,
2702 Follow-up on Traditional Enforcement Actions Including Violations, Deviations,
Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution
Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution
Line 301: Line 382:
Miscellaneous
Miscellaneous
Documents
Documents
Number           Title                                                     Date
Number  
CP-201800120     Comanche Peak Nuclear Power Plant Docket                   March 22, 2018
 
TXX-18012        Nos. 05000445 and 05000446 Reply to a Notice of
Title  
 
Date
CP-201800120
TXX-18012
Comanche Peak Nuclear Power Plant Docket
Nos. 05000445 and 05000446 Reply to a Notice of
Violation
Violation
March 22, 2018
Comanche Peak Station Blackout Issue
Comanche Peak Station Blackout Issue
NCV 05000445/2018003-01; 05000446/2018003-01
NCV 05000445/2018003-01; 05000446/2018003-01
Line 311: Line 400:
the finding was of very low safety significance (Green) by determining a bounding estimate of
the finding was of very low safety significance (Green) by determining a bounding estimate of
the increase in core damage frequency of 3.5E-9/year.
the increase in core damage frequency of 3.5E-9/year.
To establish this bounding estimate the analyst assumed:
To establish this bounding estimate the analyst assumed:  
    * The exposure time was 138 hours based on the longest time the vulnerability was in
*
place.
The exposure time was 138 hours based on the longest time the vulnerability was in
    * The initiating event frequency for losses of offsite power was 3.24E-2 per year. This
place.  
*
The initiating event frequency for losses of offsite power was 3.24E-2 per year. This
frequency was obtained from the current Comanche Peak SPAR model. This includes
frequency was obtained from the current Comanche Peak SPAR model. This includes
losses of offsite power from grid-related, plant-centered, switchyard-centered, and
losses of offsite power from grid-related, plant-centered, switchyard-centered, and
weather-related causes.
weather-related causes.  
    * Losses of offsite power from external events (e.g., tornados, earthquakes) occurred at
*
Losses of offsite power from external events (e.g., tornados, earthquakes) occurred at
very low frequencies and were insignificant contributors to the increase in core damage
very low frequencies and were insignificant contributors to the increase in core damage
frequency.
frequency.  
    * The probability of a loss of emergency diesel generator electrical output to its respective
*
The probability of a loss of emergency diesel generator electrical output to its respective
electrical bus was:
electrical bus was:
o Emergency Diesel 1 to Bus 1EA1: 7.13E-2
o Emergency Diesel 1 to Bus 1EA1:
o Emergency Diesel 2 to Bus 1EA2: 7.14E-2
7.13E-2
o Emergency Diesel 2 to Bus 1EA2:
7.14E-2
These values were obtained by solving sub-fault trees ACP-1EA1-3 and ACP-1EA2-5 in
These values were obtained by solving sub-fault trees ACP-1EA1-3 and ACP-1EA2-5 in
the current Comanche Peak SPAR model.
the current Comanche Peak SPAR model.  
    * The probability of a fault on either bus 1EA1 or bus 1EA2 was 2.29E-5. This value was
*
obtained from the current Comanche Peak SPAR model.
The probability of a fault on either bus 1EA1 or bus 1EA2 was 2.29E-5. This value was
    * All mitigating equipment would fail as a result of the performance deficiency yielding a
obtained from the current Comanche Peak SPAR model.  
*
All mitigating equipment would fail as a result of the performance deficiency yielding a
conditional core damage probability of 1.0. This assumption was conservative as
conditional core damage probability of 1.0. This assumption was conservative as
complete failure of all mitigating equipment was not realistically expected.
complete failure of all mitigating equipment was not realistically expected.
Line 338: Line 435:
Recovery of the emergency diesel generators was available for mitigation of the dominant
Recovery of the emergency diesel generators was available for mitigation of the dominant
sequences. The analyst solved fault trees and obtained data from the Comanche Peak SPAR
sequences. The analyst solved fault trees and obtained data from the Comanche Peak SPAR
model, Revision 8.55, on SAPHIRE, Version 8.1.8, using a cutset truncation of 1.0E-12.
model, Revision 8.55, on SAPHIRE, Version 8.1.8, using a cutset truncation of 1.0E-12.  
 
COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT
05000445/2018003 AND 05000446/2018003 - October 31, 2018
DISTRIBUTION
KKennedy, RA
SMorris, DRA
AVegel, DRP
MHay, DRP
MShaffer, DRS
RLantz, DRS
DCylkowski, RC
JJosey, DRP
RKumana, DRP
MHaire, DRP
RAlexander, DRP
AAthar, DRP
LNewman, DRP
LReyna, DRP
CCook, RIV/OEDO
VDricks, ORA
JWeil, OCA
MOBanion, NRR
AMoreno, RIV/CAO
BMaier, RSLO
GMiller, IPAT
PJayroe, DRP/IPAT
MHerrera, DRMA
R4Enforcement
ROP Reports
Electronic Distribution for Comanche Peak Nuclear Power Plant
 
OFFICIAL RECORD COPY
ADAMS ACCESSION NUMBER: ML18304A318
SUNSI Review
By: MSH
ADAMS
Yes No
Non-Sensitive
Sensitive
Publicly Available Keyword:
Non-Publicly Available NRC-002
OFFICE
SRI:DRP/A
RI:DRP/A
SPE:DRP/A
BC:EB1
BC:EB2
BC:OB
NAME
JJosey
RKumana
RAlexander
TFarnholtz
GWerner
VGaddy
SIGNATURE
JEJ
RJK
RDA
TRF
GEW
vgg
DATE
10/29/2018
10/22/2018
10/29/2018
10/22/2018
10/29/2018
10/23/18
OFFICE
BC:PSB2
TL-IPAT
BC:DRP/A
 
NAME
HGepford
GMiller
MHaire
 
SIGNATURE
hjg
GBM
MSH


ML18304A318
DATE
SUNSI Review          ADAMS            Non-Sensitive  Publicly Available          Keyword:
10/22/18
By: MSH                  Yes  No      Sensitive      Non-Publicly Available      NRC-002
10/22/18
OFFICE        SRI:DRP/A      RI:DRP/A      SPE:DRP/A    BC:EB1          BC:EB2    BC:OB
10/31/2018
NAME          JJosey        RKumana      RAlexander    TFarnholtz      GWerner    VGaddy
SIGNATURE JEJ                RJK          RDA          TRF              GEW        vgg
DATE          10/29/2018    10/22/2018    10/29/2018    10/22/2018      10/29/2018 10/23/18
OFFICE        BC:PSB2        TL-IPAT      BC:DRP/A
NAME          HGepford      GMiller      MHaire
SIGNATURE hjg                GBM          MSH
DATE          10/22/18       10/22/18      10/31/2018
}}
}}

Latest revision as of 10:00, 5 January 2025

NRC Integrated Inspection Report 05000445/2018003 and 05000446/2018003
ML18304A318
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 10/31/2018
From: Mark Haire
NRC/RGN-IV/DRP
To: Peters K
Vistra Operations Company
References
IR 2018003
Download: ML18304A318 (18)


Text

October 31, 2018

SUBJECT:

COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000445/2018003 AND 05000446/2018003

Dear Mr. Peters:

On September 30, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. On October 11, 2018, the NRC inspectors discussed the results of this inspection with Mr. Tom McCool, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

Both of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Comanche Peak Nuclear Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Mark S. Haire, Chief Project Branch A Division of Reactor Projects

Docket Nos. 50-445 and 50-446 License Nos. NPF-87 and NPF-89

Enclosure:

Inspection Report 05000445/2018003 and 05000446/2018003 w/ Attachments:

1. Documents Reviewed 2. Detailed Risk Evaluation

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number(s):

05000445 and 05000446

License Number(s):

NPF-87 and NPF-89

Report Number(s):

05000445/2018003 and 05000446/2018003

Enterprise Identifier: I-2018-003-0011

Licensee:

Vistra Operations Company, LLC

Facility:

Comanche Peak Nuclear Power Plant, Units 1 and 2

Location:

Glen Rose, Texas

Inspection Dates:

July 1, 2018 to September 30, 2018

Inspectors:

J. Josey, Senior Resident Inspector

R. Kumana, Resident Inspector

H. Freeman, Senior Reactor Inspector

Approved By:

Mark S. Haire

Chief, Project Branch A

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Comanche Peak Nuclear Power Plant,

Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

NRC-identified and self-revealed findings, violations, and additional items are summarized in the table below. Licensee-identified non-cited violations are documented in the Inspection Results at the end of this report.

List of Findings and Violations

Failure to Maintain the Ability to Withstand a Station Blackout Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000445/2018003-01; 05000446/2018003-01 Closed None 71152 -

Problem Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50.63 for the licensees failure to maintain the ability to withstand and recover from a station blackout. Specifically, the licensees approved coping analysis for each unit required the availability of equipment on the non-blacked-out unit, and the licensee failed to maintain the required equipment available.

The licensee entered this violation into their corrective action program as condition report CR-2017-011090.

Failure to Establish Adequate Procedural Guidance for Processing Technical Changes Performed by a Vendor on Installed Plant Equipment Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018003-02; 5000446/2018003-02 Closed None 71152 -

Problem Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to establish an adequate procedure for controlling and processing vendor documents and vendor technical information. This resulted in the licensees failure to properly evaluate changes made by vendors to plant equipment. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes. The licensee entered this issue into the corrective action program as Condition Reports CR-2018-004485 and CR-2018-004605.

Additional Tracking Items

Type Issue number Title Inspection Procedure Status VIO 05000445/2017010-01; 05000446/2017010-01 Failure to Update Final Safety Analysis Report Section 8.3.1.1.11 92702 Closed

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire inspection period.

Unit 2 began the inspection period at rated thermal power. On August 13, 2018, the unit tripped automatically due to a failure on the turbine generator voltage regulator. The unit was restarted on August 15, 2018. The unit was returned to rated thermal power on August 17, 2018, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515 Appendix D, Plant Status and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01Adverse Weather Protection Seasonal Extreme Weather

The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal hot temperatures.

71111.04Equipment Alignment Partial Walkdown

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 batteries 1ED1 and 1ED3 on July 26, 2018
(2) Unit 2 residual heat removal pump 2-02 on September 5, 2018
(3) Unit 2 turbine driven auxiliary feedwater pump on September 12, 2018
(4) Unit 2 instrument air system on September 14, 2018

Complete Walkdown (1 Sample)

The inspectors evaluated system configurations during a complete walkdown of the uninterruptible power supply (UPS) heating ventilation and air conditioning system on September 25, 2018.

71111.05AQFire Protection Annual/Quarterly Quarterly Inspection

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Fire zone EQ149, UPS Chiller X-01 on September 17, 2018
(2) Fire zone ER150, UPS Chiller X-02 on September 17, 2018
(3) Fire zone EH52 and EH53, train A UPS rooms on September 21, 2018
(4) Fire zone EC50 and EC51, train B UPS rooms on September 21, 2018

71111.06Flood Protection Measures Internal Flooding

The inspectors evaluated internal flooding mitigation protections in the UPS chiller rooms on August 29, 2018.

71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed and evaluated a crew during an evaluated simulator scenario on September 5, 2018.

Operator Performance (1 Sample)

The inspectors observed and evaluated Unit 2 control room operators during post trip response on August 13, 2018, and Unit 2 startup activities on August 15, 2018.

71111.12Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety significant functions:

(1) Units 1 and 2 UPS chillers on August 22, 2018

71111.13Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 2, repair of containment pressure relief valve on July 9, 2018
(2) Unit 2, trip and repair of emergency diesel generator 2-02 on August 22, 2018
(3) Units 1 and 2, breach of control room envelope on August 24, 2018
(4) Units 1 and 2, repair of auxiliary feedwater pump flow control valves on August 28, 2018
(5) Units 1 and 2, measurement of silt level in station service water intake bay on July 25, 2018

71111.15Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2, containment isolation valve leakage, on July 9, 2018
(2) Unit 1, failure of battery cell on battery 1ED2, on July 2, 2018
(3) Units 1 and 2, inadequate procedure for makeup to component cooling water system, on July 16, 2018
(4) Unit 2, safety injection accumulator 2-01 high pressure, on July 26, 2018
(5) Unit 1, incorrect fuses removed from 480V bus 1EB1, on September 24, 2018

71111.18Plant Modifications

The inspectors evaluated the following temporary or permanent modifications:

(1) Removal of cell 27 from battery 1ED2 after the cell was discovered cracked on July 2, 2018

71111.19Post Maintenance Testing

The inspectors evaluated the following post maintenance tests:

(1) Unit 2, containment pressure relief valve 2-HV-5549 following repair, on July 19, 2018
(2) Unit 1, battery 1ED2 following installation of cell jumper, on July 27, 2018
(3) Unit 2, reactor trip breaker following replacement of auxiliary switches, on August 16, 2018
(4) Unit 2, steam generator feedwater leading edge flow monitor following probe replacement, on August 20, 2018
(5) Unit 2, diesel generator 2-02 following replacement of master drive, on August 27, 2018
(6) Unit 1, drip pot drain isolation valve 1-LV-2373 following repair, on August 29, 2018
(7) Unit 1, battery charger 1ED1-1 following card replacement, on September 26, 2018

===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:

Routine===

(1) Unit 1, OPT-447A, train A reactor trip breaker test, on August 1, 2018
(2) Units 1 and 2, OPT-220, fire pump X-06 test, on August 30, 2018
(3) Unit 1, OPT-206A, turbine driven auxiliary feedwater pump test, on September 7, 2018

In-service (2 Samples)

(1) Unit 2, OPT-837, 2-HV-5545, air particulate, iodine and gas detector sample isolation valve leak test, on July 10, 2018
(2) Unit 1, OPT-208A, component cooling water pump 1-01 discharge valve test, on August 29, 2018

71114.06Drill Evaluation Drill/Training Evolution

The inspectors evaluated an emergency preparedness drill on July 11,

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

(1) MS06: Emergency AC Power Systems (07/01/2017-06/30/2018)
(2) MS07: High Pressure Injection Systems (07/01/2017-06/30/2018)
(3) MS08: Heat Removal Systems (07/01/2017-06/30/2018)

71152Problem Identification and Resolution Annual Follow-up of Selected Issues

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Failure to meet station blackout coping requirements during adjacent unit refueling outages
(2) Failure to perform a 50.59 evaluation for a vendor change to a component cooling water pump

71153Follow-up of Events and Notices of Enforcement Discretion Personnel Performance

The inspectors evaluated a Unit 2 reactor trip and licensees performance on August 13,

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

92702Follow-up on Traditional Enforcement Actions Including Violations, Deviations, Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution Confirmatory Orders

The inspectors reviewed the licensees response to Notice of Violation (NOV)05000445/2017010-01; 05000446/2017010-01 and determined that the reason, corrective actions taken and planned to address recurrence, and the date when full compliance will be achieved for this violation are adequately addressed and captured on the docket.

INSPECTION RESULTS

Failure to Maintain the Ability to Withstand a Station Blackout Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems

Green NCV 05000445/2018003-01; 05000446/2018003-01 Closed None

71152 - Problem

Identification and Resolution The inspectors identified a Green, non-cited violation of 10 CFR Part 50.63 for the licensees failure to maintain the ability to withstand and recover from a station blackout. Specifically, the licensees approved coping analysis for each unit required the availability of equipment on the non-blacked-out unit, and the licensee failed to maintain the required equipment available.

Description:

During the inspectors review of the outage schedule for Unit 1 refueling outage 1RF19, the inspectors noted that the licensee planned to remove both diesel generators from service while Unit 1 was defueled. The inspectors asked the licensee whether they would be able to comply with their station blackout coping analysis for Unit 2 with both Unit 1 diesel generators out of service. The licensee revised their outage schedule to ensure one diesel generator would be available while the inspectors continued to inspect the issue.

The inspectors determined that the licensees coping analysis for station blackout assumed the ability to cope for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> without AC power to the blackout unit by crediting one onsite AC source from the non-blacked-out unit supplying power to shared equipment. This was approved by the NRC because the station blackout rule (10 CFR 50.63) applies to each unit individually. The coping analysis assumes that the non-blacked-out unit has one diesel generator available to mitigate the concurrent loss of offsite power and unit trip on the non-blacked-out unit, provide ventilation and air conditioning to the common control room and uninterruptible power supply (UPS) rooms, and provide power to shared onsite communication systems. In order for the strategy documented in the analysis to succeed, the licensee requires the non-blacked-out unit to be able to start and run one emergency diesel generator, one station service water pump, one control room air conditioning unit, one UPS supply fan, and one component cooling water pump. Subsequently, the licensee credited an additional fan coil unit in each UPS room for cooling, assuming one fan coil unit and one safety chiller would start and run. These loads normally automatically start on a loss of voltage to the associated safety bus.

In 1999, the licensee planned for both Unit 1 diesel generators and both Unit 1 component cooling water pumps to be out of service concurrently during refueling outage 1RF07. The licensee identified the impact of this activity to the station blackout coping analysis, but assumed the activity could be performed as long as actions were taken to mitigate the risk of a station blackout on the operating unit. Following that outage, the licensee incorporated the decision to perform maintenance by disabling the ability to cope with a station blackout into the Final Safety Analysis Report and implemented this strategy during multiple subsequent refueling outages on both units.

The inspectors determined that the licensee had, on multiple occasions, removed equipment from service that was necessary to allow the operating unit to withstand and recover from a station blackout. The inspectors determined that this practice was not correct and was a violation of the station blackout rule (10 CFR 50.63). The inspectors determined that the licensees decision to take this equipment out of service during outages was made in 1999 and was not reflective of present performance.

Corrective Action(s): The licensee entered this violation into their corrective action program.

Corrective Action Reference: CR-2017-011090

Performance Assessment:

Performance Deficiency: The licensees failure to maintain the ability to implement their approved station blackout coping strategy was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it is associated with the configuration control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensees failure to ensure equipment relied upon to implement their approved station blackout coping analysis was available resulted in multiple periods of time where the station blackout coping analysis could not be met.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, and determined the finding required a detailed risk evaluation because the finding represented a loss of system and/or function.

A region-based senior reactor analyst performed a detailed risk evaluation and determined that the finding was of very low safety significance (Green) based on a bounding estimate of the increase in core damage frequency of 3.5E-9 per year. The bounding estimate was based on an exposure time of 138 hours0.0016 days <br />0.0383 hours <br />2.281746e-4 weeks <br />5.2509e-5 months <br /> (i.e., the longest time the vulnerability existed during prior refueling outages), and initiating event and Class 1E electrical system failure probabilities obtained from the current Standardized Plant Analysis Risk (SPAR) model for Comanche Peak. Losses of offsite power comprised the most dominant core damage sequences. (Additional details regarding the evaluation are contained in the attachment to this report.)

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the finding was not indicative of present performance.

Enforcement:

Violation: Title 10 CFR 50.63 Loss of All Alternating Current Power, requires, in part, that each light-water-cooled nuclear power plant licensed to operate under this part must be able to withstand for a specified duration and recover from a station blackout as defined in § 50.2, and that the capability for coping with a station blackout of specified duration shall be determined by an appropriate coping analysis. In the coping analysis approved by the agency in NUREG-0797 Supplement 26 for Units 1 and 2, the licensee credits the availability of an emergency diesel generator in the non-blacked-out unit for the operation of selected systems necessary to cope with a station blackout.

Contrary to the above, from approximately 1999 until 2017, the licensee failed to maintain the ability of each unit to withstand and recover from a station blackout during outages of the adjacent unit. Specifically, the licensee, on multiple occasions, removed both diesel generators from service on the non-blacked-out unit resulting in an inability to implement the approved coping analysis.

Enforcement Action: This violation is being treated as a non-cited violation (NCV), consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Establish Adequate Procedural Guidance for Processing Technical Changes Performed by A Vendor on Installed Plant Equipment Cornerstone Significance Cross-cutting Aspect Report Section Mitigating Systems Green NCV 05000445/2018003-02; 5000446/2018003-02 Closed None

71152 - Problem

Identification and Resolution The inspectors identified a Green, NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, associated with the licensees failure to establish an adequate procedure for controlling and processing vendor documents and vendor technical information. This resulted in the licensees failure to properly evaluate changes made by vendors to plant equipment. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes.

Description:

While reviewing vendor refurbishment records supplied to the licensee for a component cooling water pump shaft and main steam isolation valve actuators, the inspectors noted that the vendors had performed physical changes to these components during refurbishment. (These records were from activities that occurred in 2002.) The inspectors noted that the licensees paperwork did not contain documentation of how these changes were evaluated for adverse impacts since these items were subsequently installed in the facility.

The inspectors asked the licensee for the documents that evaluated these changes. The licensee informed the inspectors that there were no evaluations performed at the time. The inspectors questioned this and were told by the licensee that station procedure STA-206, Review of Vendor Documents and Vendor Technical Manuals, Revision 20 (procedure in effect at the time), did not require a review because these changes were maintenance activities and therefore did not require evaluation.

The inspectors determined that this guidance was not correct and resulted in the licensee allowing vendors to make unevaluated physical changes to installed plant equipment.

Specifically, the licensee implemented guidance contained in EPRI/NSAC-125, Guidelines for 10 CFR 50.59 Safety Evaluations, in STA-206, Revision 20, when the determination was made in 2002 that the changes to the components were maintenance activities, and therefore did not require an evaluation. However, the guidance in NSAC-125 has never been reviewed and endorsed by the NRC; rather, NEI 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, had been reviewed and endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments (issued in late 1999 and late 2000, respectively). The endorsed guidance in NEI 96-07 specifically noted that for those situations where a plant component is not restored to its original condition following completion of maintenance activities (which may have been controlled by the requirements of 10 CFR 50.65(a)(4) [i.e., the Maintenance Rule]), the requirements of 10 CFR 50.59 (including the completion of an evaluation for adverse impact) would be applied to the permanent change to the plant component.

The inspectors determined that these issues occurred in 2002 and the procedure guidance that allowed the licensee to incorrectly control vendor information has since been revised in 2010; therefore this was not reflective of present performance.

Corrective Action(s): The licensee performed operability determinations that established a reasonable expectation of operability pending development of additional corrective actions.

Corrective Action References: CR-2018-004485 and CR-2018-004605

Performance Assessment:

Performance Deficiency: The licensees failure to establish adequate procedural guidance for processing technical changes performed by a vendor on installed plant equipment was a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee allowed vendors to make physical changes to a component cooling water pump shaft and main steam isolation valve actuators without evaluating these changes.

Significance: The inspectors assessed the significance of the finding using Inspection Manual Chapter 0609, Attachment 04, Initial Characterization of Findings, dated October 7, 2016, and Inspection Manual Chapter 0609, Appendix A, Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined the finding was of very low safety significance (Green)because:

(1) it was not a design deficiency;
(2) it did not represent a loss of system and/or function;
(3) it did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
(4) it did not result in the loss of a high safety significant non-technical specification train.

Cross-cutting Aspect: The finding was not assigned a cross-cutting aspect because the finding was not indicative of current performance.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, and drawings.

Contrary to the above, from 2002 until 2010, activities affecting quality that were not prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances. Specifically, Station Procedure STA-206, Review of Vendor Documents and Vendor Technical Manuals, Revision 20, provided inadequate guidance for processing technical changes performed by a vendor on installed plant equipment.

Enforcement Action: This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

On October 11, 2018, the inspectors presented the quarterly resident inspection results to Mr. Tom McCool, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.

DOCUMENTS REVIEWED

71152Problem Identification and Resolution

Condition Reports

CR-2017-011090

TR-2017-011125

CR-2018-004485

CR-2018-004605

CR-2018-001530

CR-2018-001532

CR-2018-003476

CR-2018-000941

Procedures

Number

Title

Revision

STA-206

Review of Vendor Documents and Vendor Technical

Manuals

Miscellaneous

Documents

Number

Title

Revision

or Date

DBD-EE-043

118V AC Uninterruptible Power System

DBD-ME-026

Station Blackout

TXX-92447

Response to Station Blackout (SBO) Rule

October 1, 1992

LDCR SA-2000-

049

Update/Clarify SBO Coping as Described on Pages 2

Through 6

October 25,

2000

DBD-ME-313

Uninterruptible Power Supply HVAC System

TXX-96475

Additional Information for License Amendment 96-004

Uninterruptible Power Supplies (UPS) HVAC System

Addition of Fan Coil Units to Technical Specifications

October 1, 1996

Engineering

Reports Number

Title

Revision

ER-ME-011

Unit 1 & Unit 2 Station Blackout Assessment

Calculations

Number

Title

Revision

3-D-2-027

Temperature Transient Study for Station Blackout

RXE-LA-CPX/0-099 Station Blackout Coping Analysis for CPSES Units 1& 2 at

3634 MW

3-D-2-025

UPS Room Temperature Transients During Sta. Blkot &

FSSD

ME-CA-0313-4079

UPS Inverter Rooms Temperature Transient following Station

Blackout with one Room Cooler in Operation

2702 Follow-up on Traditional Enforcement Actions Including Violations, Deviations,

Confirmatory Action Letters, Confirmatory Orders, and Alternative Dispute Resolution

Confirmatory Orders

Miscellaneous

Documents

Number

Title

Date

CP-201800120

TXX-18012

Comanche Peak Nuclear Power Plant Docket

Nos. 05000445 and 05000446 Reply to a Notice of

Violation

March 22, 2018

Comanche Peak Station Blackout Issue

NCV 05000445/2018003-01; 05000446/2018003-01

Detailed Risk Evaluation

A region-based senior reactor analyst performed a detailed risk evaluation and determined that

the finding was of very low safety significance (Green) by determining a bounding estimate of

the increase in core damage frequency of 3.5E-9/year.

To establish this bounding estimate the analyst assumed:

The exposure time was 138 hours0.0016 days <br />0.0383 hours <br />2.281746e-4 weeks <br />5.2509e-5 months <br /> based on the longest time the vulnerability was in

place.

The initiating event frequency for losses of offsite power was 3.24E-2 per year. This

frequency was obtained from the current Comanche Peak SPAR model. This includes

losses of offsite power from grid-related, plant-centered, switchyard-centered, and

weather-related causes.

Losses of offsite power from external events (e.g., tornados, earthquakes) occurred at

very low frequencies and were insignificant contributors to the increase in core damage

frequency.

The probability of a loss of emergency diesel generator electrical output to its respective

electrical bus was:

o Emergency Diesel 1 to Bus 1EA1:

7.13E-2

o Emergency Diesel 2 to Bus 1EA2:

7.14E-2

These values were obtained by solving sub-fault trees ACP-1EA1-3 and ACP-1EA2-5 in

the current Comanche Peak SPAR model.

The probability of a fault on either bus 1EA1 or bus 1EA2 was 2.29E-5. This value was

obtained from the current Comanche Peak SPAR model.

All mitigating equipment would fail as a result of the performance deficiency yielding a

conditional core damage probability of 1.0. This assumption was conservative as

complete failure of all mitigating equipment was not realistically expected.

A detailed estimate of the increase in large early release frequency was not performed because

the increase in core damage frequency was so low that even if the containment failed

completely, the maximum increase in large early release frequency would have been 3.5E-

9/year (Green). Losses of offsite power comprised the most dominant core damage sequences.

Recovery of the emergency diesel generators was available for mitigation of the dominant

sequences. The analyst solved fault trees and obtained data from the Comanche Peak SPAR

model, Revision 8.55, on SAPHIRE, Version 8.1.8, using a cutset truncation of 1.0E-12.

COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT

05000445/2018003 AND 05000446/2018003 - October 31, 2018

DISTRIBUTION

KKennedy, RA

SMorris, DRA

AVegel, DRP

MHay, DRP

MShaffer, DRS

RLantz, DRS

DCylkowski, RC

JJosey, DRP

RKumana, DRP

MHaire, DRP

RAlexander, DRP

AAthar, DRP

LNewman, DRP

LReyna, DRP

CCook, RIV/OEDO

VDricks, ORA

JWeil, OCA

MOBanion, NRR

AMoreno, RIV/CAO

BMaier, RSLO

GMiller, IPAT

PJayroe, DRP/IPAT

MHerrera, DRMA

R4Enforcement

ROP Reports

Electronic Distribution for Comanche Peak Nuclear Power Plant

OFFICIAL RECORD COPY

ADAMS ACCESSION NUMBER: ML18304A318

SUNSI Review

By: MSH

ADAMS

Yes No

Non-Sensitive

Sensitive

Publicly Available Keyword:

Non-Publicly Available NRC-002

OFFICE

SRI:DRP/A

RI:DRP/A

SPE:DRP/A

BC:EB1

BC:EB2

BC:OB

NAME

JJosey

RKumana

RAlexander

TFarnholtz

GWerner

VGaddy

SIGNATURE

JEJ

RJK

RDA

TRF

GEW

vgg

DATE

10/29/2018

10/22/2018

10/29/2018

10/22/2018

10/29/2018

10/23/18

OFFICE

BC:PSB2

TL-IPAT

BC:DRP/A

NAME

HGepford

GMiller

MHaire

SIGNATURE

hjg

GBM

MSH

DATE

10/22/18

10/22/18

10/31/2018