PNO-I-15-001, Pilgrim: Shutdown Greater than 72 Hours Due to Reactor Scram Following a Partial Loss of Offsite Power: Difference between revisions

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{{#Wiki_filter:Date: January 29, 2015  
{{#Wiki_filter:Date: January 29, 2015 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-I-15-001 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated by the Region I staff.
 
Facility                                               Licensee Emergency Classification Entergy Nuclear Operations, Inc.                       __ Notification of Unusual Event Pilgrim Nuclear Power Station                           ___ Alert Plymouth, MA                                           ___ Site Area Emergency Docket No.       50-293                                 ___ General Emergency License No. DPR-35                                       X Not Applicable
PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE
  - PNO-I-15-001 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated by the Region I staff.
 
Facility       Licensee Emergency Classification Entergy Nuclear Operations, Inc. __   Notification of Unusual Event Pilgrim Nuclear Power Station   ___ Alert Plymouth, MA       ___ Site Area Emergency   Docket No. 50-293     ___ General Emergency License No. DPR-35     X     Not Applicable


==SUBJECT:==
==SUBJECT:==
PILGRIM NUCLEAR POWER STATION: SHUTDOWN GREATER THAN 72 HOURS DUE TO REACTOR SCRAM FOLLOWING A PARTIAL LOSS OF OFFSITE POWER
PILGRIM NUCLEAR POWER STATION: SHUTDOWN GREATER THAN 72 HOURS DUE TO REACTOR SCRAM FOLLOWING A PARTIAL LOSS OF OFFSITE POWER On January 27, 2015, Pilgrim Nuclear Power Station experienced an automatic scram following a turbine trip due to a partial loss of offsite power. The station was experiencing high winds and heavy snowfall during a severe winter storm when the station began experiencing degrading switchyard conditions. The station had already transferred the emergency busses onto their respective emergency diesel generators and was downpowering to 20% power to take the turbine offline. At 4:02 a.m. with the reactor at 52% power, the second offsite line was lost and the station experienced a load reject.
 
On January 27, 2015, Pilgrim Nuclear Power Station experienced an automatic scram following a turbine trip due to a partial loss of offsite power. The station was experiencing high winds and heavy snowfall during a severe winter storm when the station began experiencing degrading switchyard conditions. The station had already transferred the emergency busses onto their respective emergency diesel generators and was downpowering to 20% power to take the turbine offline. At 4:02 a.m. with the reactor at 52% power, the second offsite line was lost and the station experienced a load reject.  
 
The station experienced equipment issues while cooling down after the scram including: the station diesel air compressor failed to start, one of four safety relief valves could not be operated manually from the control room, and high pressure coolant injection had to be secured due to failure of the gland seal motor.
The station experienced equipment issues while cooling down after the scram including: the station diesel air compressor failed to start, one of four safety relief valves could not be operated manually from the control room, and high pressure coolant injection had to be secured due to failure of the gland seal motor.
The station is currently in cold shutdown, the safety buses are being powered by their respective emergency diesel generators, and all safety-related equipment required for safe plant shutdown are available. The licensee is working on restoring their 345kV lines.  
The station is currently in cold shutdown, the safety buses are being powered by their respective emergency diesel generators, and all safety-related equipment required for safe plant shutdown are available. The licensee is working on restoring their 345kV lines.
 
Resident inspectors and region-based inspectors are providing oversight and performing follow-up inspections.
Resident inspectors and region-based inspectors are providing oversight and performing follow-up inspections.  
This preliminary notification is issued for information only.
 
The information presented herein has been discussed with the licensee and is current as of 1:00 p.m. on January 29, 2015. Commonwealth of Massachusetts officials have been kept informed.
This preliminary notification is issued for information only.  
ADAMS Accession Number: ML15029A433 CONTACT:         Raymond McKinley, Projects Branch 5 (610) 337-5150 Raymond.McKinley@nrc.gov
 
The information presented herein has been discussed with the licensee and is current as of 1:00 p.m. on January 29, 2015. Commonwealth of Massachusetts officials have been kept  
 
informed.
ADAMS Accession Number: ML15029A433 CONTACT: Raymond McKinley, Projects Branch 5 (610) 337-5150 Raymond.McKinley@nrc.gov


ML15029A433 SUNSI Review Non-Sensitive Sensitive Publicly Available Non-Publicly Available OFFICE RI/DRP RI/DRP RI/PAO RI/SLO RI/ORA NAME     RMcKinley/RRM HNieh/HKN DScrenci/DS NMcNamara/NM DLew/DCL DATE 1/29/15 1/29/15 1/29/15 1/29/15 1/29/15}}
ML15029A433 Non-Sensitive                     Publicly Available SUNSI Review Sensitive                        Non-Publicly Available OFFICE     RI/DRP           RI/DRP           RI/PAO           RI/SLO                 RI/ORA NAME       RMcKinley/RRM     HNieh/HKN         DScrenci/DS       NMcNamara/NM           DLew/DCL DATE       1/29/15           1/29/15           1/29/15         1/29/15                 1/29/15}}


{{PNO-Nav|region=I}}
{{PNO-Nav|region=I}}

Latest revision as of 17:29, 31 October 2019

PNO-I-15-001 - Pilgrim: Shutdown Greater than 72 Hours Due to Reactor Scram Following a Partial Loss of Offsite Power
ML15029A433
Person / Time
Site: Pilgrim
Issue date: 01/29/2015
From: Raymond Mckinley
NRC/RGN-I/DRP/PB5
To:
McKinley R
References
PNO-I-15-001
Download: ML15029A433 (2)


Date: January 29, 2015 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE - PNO-I-15-001 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. Some of the information may not yet be fully verified or evaluated by the Region I staff.

Facility Licensee Emergency Classification Entergy Nuclear Operations, Inc. __ Notification of Unusual Event Pilgrim Nuclear Power Station ___ Alert Plymouth, MA ___ Site Area Emergency Docket No. 50-293 ___ General Emergency License No. DPR-35 X Not Applicable

SUBJECT:

PILGRIM NUCLEAR POWER STATION: SHUTDOWN GREATER THAN 72 HOURS DUE TO REACTOR SCRAM FOLLOWING A PARTIAL LOSS OF OFFSITE POWER On January 27, 2015, Pilgrim Nuclear Power Station experienced an automatic scram following a turbine trip due to a partial loss of offsite power. The station was experiencing high winds and heavy snowfall during a severe winter storm when the station began experiencing degrading switchyard conditions. The station had already transferred the emergency busses onto their respective emergency diesel generators and was downpowering to 20% power to take the turbine offline. At 4:02 a.m. with the reactor at 52% power, the second offsite line was lost and the station experienced a load reject.

The station experienced equipment issues while cooling down after the scram including: the station diesel air compressor failed to start, one of four safety relief valves could not be operated manually from the control room, and high pressure coolant injection had to be secured due to failure of the gland seal motor.

The station is currently in cold shutdown, the safety buses are being powered by their respective emergency diesel generators, and all safety-related equipment required for safe plant shutdown are available. The licensee is working on restoring their 345kV lines.

Resident inspectors and region-based inspectors are providing oversight and performing follow-up inspections.

This preliminary notification is issued for information only.

The information presented herein has been discussed with the licensee and is current as of 1:00 p.m. on January 29, 2015. Commonwealth of Massachusetts officials have been kept informed.

ADAMS Accession Number: ML15029A433 CONTACT: Raymond McKinley, Projects Branch 5 (610) 337-5150 Raymond.McKinley@nrc.gov

ML15029A433 Non-Sensitive Publicly Available SUNSI Review Sensitive Non-Publicly Available OFFICE RI/DRP RI/DRP RI/PAO RI/SLO RI/ORA NAME RMcKinley/RRM HNieh/HKN DScrenci/DS NMcNamara/NM DLew/DCL DATE 1/29/15 1/29/15 1/29/15 1/29/15 1/29/15