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{{#Wiki_filter:CATEGORY 1 REGULATO     INFORMATIOh DISTRIBUTION SYSTEM (RIDS)
{{#Wiki_filter:CATEGORY 1 REGULATO INFORMATIOh DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9801050374           DOC.DATE: 97/12/24 NOTARIZED: NO                     DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTHOR AFFILIATION AUTH. NAME FITZPATRICK,E.
ACCESSION NBR:9801050374 DOC.DATE: 97/12/24 NOTARIZED: NO DOCKET FACIL:50-315 Donald C.
RECIP.NAME American Electric Power Co., Inc.
Cook Nuclear Power Plant, Unit 1, Indiana M
RECIPIENT AFFILIATION
05000315 50-316 Donald C.
                                                                                    +    gp2 Document Control Branch (Document Control Desk)
Cook Nuclear Power Plant, Unit 2, Indiana M
05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.
American Electric Power Co., Inc.
+ gp2 RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
I.
I.


==SUBJECT:==
==SUBJECT:==
Documents       info re three specific issues discussed at             971222 meeting. Attachment 1 to       ltr   contains root cause analysis short term assessment program development.
Documents info re three specific issues discussed at 971222 C
                                                                                        &
meeting. Attachment 1 to ltr contains root cause analysis short term assessment program development.
C A
A DISTRIBUTION CODE:
DISTRIBUTION CODE: IE36D         COPIES RECEIVED:LTR TITLE: Immediate/Confirmatory Action             Ltr i ENCL I SIZE:        0  l (50 Dkt-Other Than Emergency Prepar NOTES:                                                                                             E RECIPIENT           COPIES              RECXPIENT            COPIES ID CODE/NAME         LTTR ENCL          XD CODE/NAME        LTTR ENCL PD3-3 PD                   1     1       HICKMAN,J                1     1 INTERNA  . FILE CENTER      1       1     1       NRR/DRPM/PECB             1     1 1     1 EXTERNAL: NOAC                        1     1       NRC PDR                  1    .1 D
IE36D COPIES RECEIVED:LTR i
ENCL I
SIZE: 0 l TITLE: Immediate/Confirmatory Action Ltr (50 Dkt-Other Than Emergency Prepar E
NOTES:
RECIPIENT ID CODE/NAME PD3-3 PD INTERNA
. FILE CENTER 1
EXTERNAL: NOAC COPIES LTTR ENCL 1
1 1
1 1
1 1
1 RECXPIENT XD CODE/NAME HICKMAN,J NRR/DRPM/PECB NRC PDR COPIES LTTR ENCL 1
1 1
1 1
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U E
U E
N NOTE TO ALL "RIDS" RECIPIENTS:
N NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR               7   ENCL     7
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ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED:
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44 Indiana Michigan Power Company 500 Circle Drive Buchanan, Ml 491071395 IItIOIANA MICHIGAN IrQBfM December 24, 1997                                               AEP:NRC:1260G4 Docket Nos.:         50-315 50-316 U.S. Nuclear Regulatory Commission ATTN:     Document Control Desk Mail Stop 0-Pl-17 Washington,       DC 20555-0001 Gentlemen:
44 Indiana Michigan Power Company 500 Circle Drive Buchanan, Ml 491071395 IItIOIANA MICHIGAN IrQBfM December 24, 1997 AEP:NRC:1260G4 Docket Nos.:
Donald C. Cook Nuclear Plant Units 1 and 2 CONFIRMATORY ACTION LETTER (CAL) SUPPLEMENTAL RESPONSE On December       16, 1997, a public meeting was held with the NRC to discuss issues associated with the NRC's confirmatory action letter dated September 19, 1997.             Subsequent to the meeting, we were informed that further information regarding three specific issues was needed.           These issues were the root cause analyses we performed for the architect engineering (AE) inspection items and the development of our short term assessment                   program, our 10 CFR 50.59 program, and calculations reviewed as part of the short term assessment program.               These issues were discussed with the NRC staff at a meeting held in Lisle, Illinois on December 22, 1997.
50-315 50-316 U.S. Nuclear Regulatory Commission ATTN:
At that meeting, we agreed to perform additional reviews of design changes, procedure changes, and 10 CFR 50.59 screenings to review for the types of problems identified during the AE inspection. The results of this review will be forwarded to the NRC under separate correspondence.
Document Control Desk Mail Stop 0-Pl-17 Washington, DC 20555-0001 Gentlemen:
While the additional 10           CFR   50.59 reviews and our short               term assessment       represent   specific actions taken to ensure that the types of problems found during the AE design =inspection do not affect the operability of other safety systems, we also recognize that operability and maintenance of design basis are continuous processes.       As a licensee, we must continually assess plant and external conditions to assure ourselves that systems remain within their licensing and design bases, and where instances of degradation         or non-conformance       are   identified, we must expeditiously evaluate operability of potentially affected equipment.
Donald C.
A   questioning attitude by our staff ensures that safety reviews, calculations, and procedures are challenged. As an example, at least,131 condition reports by five different plant organizations have been issued, since the AE design inspection, to document potential discrepancies of a type similar to those identified during the inspection. This includes discrepancies found in the i Jvv.
Cook Nuclear Plant Units 1 and 2
ra AQUA UFSAR.        Additionally, condition reports open at the time of the inspection were reviewed with increased awareness of the design and licensing basis.           'hose 'ondition reports that documented conditions having the potential to adversely impact the design or licensing bases or operability were identified and flagged for resolution prior to entry into a mode where the condition is applicable.
CONFIRMATORY ACTION LETTER (CAL) SUPPLEMENTAL RESPONSE On December 16,
980%050374 971224                                             IIIIIIIIIIIIIIII,llllilllilllllllllill PDR   ADQCK   050003i5 P                     PDRQ
: 1997, a public meeting was held with the NRC to discuss issues associated with the NRC's confirmatory action {{letter dated|date=September 19, 1997|text=letter dated September 19, 1997}}.
Subsequent to the
: meeting, we were informed that further information regarding three specific issues was needed.
These issues were the root cause analyses we performed for the architect engineering (AE) inspection items and the development of our short term assessment
: program, our 10 CFR 50.59
: program, and calculations reviewed as part of the short term assessment program.
These issues were discussed with the NRC staff at a
meeting held in Lisle, Illinois on December 22, 1997.
ra AQUA i Jvv.
At that meeting, we agreed to perform additional reviews of design
: changes, procedure
: changes, and 10 CFR 50.59 screenings to review for the types of problems identified during the AE inspection.
The results of this review will be forwarded to the NRC under separate correspondence.
While the additional 10 CFR 50.59 reviews and our short term assessment represent specific actions taken to ensure that the types of problems found during the AE design =inspection do not affect the operability of other safety systems, we also recognize that operability and maintenance of design basis are continuous processes.
As a licensee, we must continually assess plant and external conditions to assure ourselves that systems remain within their licensing and design
: bases, and where instances of degradation or non-conformance are identified, we must expeditiously evaluate operability of potentially affected equipment.
A questioning attitude by our staff ensures that safety reviews, calculations, and procedures are challenged.
As an example, at least,131 condition reports by five different plant organizations have been
: issued, since the AE design inspection, to document potential discrepancies of a
type similar to those identified during the inspection.
This includes discrepancies found in the UFSAR.
Additionally, condition reports open at the time of the inspection were reviewed with increased awareness of the design and licensing basis.
'hose 'ondition reports that documented conditions having the potential to adversely impact the design or licensing bases or operability were identified and flagged for resolution prior to entry into a mode where the condition is applicable.
980%050374 971224 PDR ADQCK 050003i5 P
PDRQ IIIIIIIIIIIIIIII,llllilllilllllllllill


U.S. Nuclear Regulatory Commission                   AEP: NRC: 1260G4 Page 2 This letter dockets the information related to the three specific issues discussed at the December 22, 1997, meeting. Attachment 1 to this letter contains the root cause analysis and short term assessment   program development. Attachment 2 contains our 10 CFR 50.59 program.     Attachment 3 contains the calculation review program. Attachment 4 documents the presentation materials for our response to the confirmatory action letter issues that were provided during the December 16, 1997, public meeting.
U.S. Nuclear Regulatory Commission Page 2
Sincerely, g- Q4 E. E. Fitzpatrick Vice President
AEP: NRC: 1260G4 This letter dockets the information related to the three specific issues discussed at the December 22,
/vlb Attachments A. A. Blind A. B. Beach MDEQ - DW & RPD NRC Resident inspector J. A. Abramson
: 1997, meeting.
Attachment 1
to this letter contains the root cause analysis and short term assessment program development.
Attachment 2
contains our 10 CFR 50.59 program.
Attachment 3
contains the calculation review program.
Attachment 4 documents the presentation materials for our response to the confirmatory action letter issues that were provided during the December 16, 1997, public meeting.
Sincerely, g-Q4 E.
E. Fitzpatrick Vice President
/vlb Attachments A. A. Blind A. B. Beach MDEQ -
DW & RPD NRC Resident inspector J.
A. Abramson


ATTACHMENT 1 TO AEP:NRC: 1260G4 ROOT CAUSE ANALSYIS AND SHORT TERM ASSESSMENT PROGRAM DEVELOPMENT
ATTACHMENT 1 TO AEP:NRC: 1260G4 ROOT CAUSE ANALSYIS AND SHORT TERM ASSESSMENT PROGRAM DEVELOPMENT


Short Term Assessment Program Introduction In Confirmatory Action Letter No. RIII-97-011, the NRC Region III Administrator stated, "Lastly, given the limited scope of our inspection and its substantial findings, it is necessary   to determine the extent of problems and their potential impact on other systems. It is my understanding, in the short term, you will perform an assessment to determine whether these types of engineering problems exist in other safety related.
Short Term Assessment Program Introduction In Confirmatory Action Letter No. RIII-97-011, the NRC Region III Administrator stated, "Lastly, given the limited scope ofour inspection and its substantial findings, it is necessary to determine the extent of problems and their potential impact on other systems.
It is my understanding, in the short term, you will perform an assessment to determine whether these types of engineering problems exist in other safety related.
systems and whether they affect system operability."
systems and whether they affect system operability."
This paper documents the approach taken to develop the short-term assessment program.
This paper documents the approach taken to develop the short-term assessment program.
In particular, it captures the process used to identify the engineering issues to be addressed and provides rationale for selecting specific short-term actions for each engineering issue.
In particular, it captures the process used to identify the engineering issues to be addressed and provides rationale for selecting specific short-term actions for each engineering issue.
In keeping with the guidance of the CAL, the short-term assessment is intentionally focused on operability of systems within the guidelines of'Generic Letter 91-18, Revision 1 and its attachments     and references.       Some root causes identified during the investigation   of design inspection findings     are not relevant to the operability of safety systems, and were therefore excluded from the short-term assessment program. The arguments used to exclude some root causes are not intended to downplay the significance of nonconforming conditions found during the design inspection. We are committed to addressing these important issues in longer-term programs to assure these kinds of engineering problems are promptly identified, thoroughly evaluated, and resolved.
In keeping with the guidance of the CAL, the short-term assessment is intentionally focused on operability ofsystems within the guidelines of'Generic Letter 91-18, Revision 1
and its attachments and references.
Some root causes identified during the investigation of design inspection findings are not relevant to the operability of safety
: systems, and were therefore excluded from the short-term assessment program.
The arguments used to exclude some root causes are not intended to downplay the significance of nonconforming conditions found during the design inspection.
We are committed to addressing these important issues in longer-term programs to assure these kinds of engineering problems are promptly identified, thoroughly evaluated, and resolved.
Development Approach Development of the short-term assessment program is shown in Figure 1. The first task in developing the assessment program was to determine what constituted "these types of engineering problems." This task was accomplished in three steps.
Development Approach Development of the short-term assessment program is shown in Figure 1. The first task in developing the assessment program was to determine what constituted "these types of engineering problems." This task was accomplished in three steps.
: 1. Root causes of issues identified during the design inspection were identified.
1.
Independent teams comprised of AEP and contractor personnel conducted root cause evaluations of the eight individual CAL items.
Root causes ofissues identified during the design inspection were identified.
Root causes of other concerns identified during the design inspection, but not addressed in the CAL, were determined within the standard framework of our corrective action'system. They were independently reviewed.
Independent teams comprised ofAEP and contractor personnel conducted root cause evaluations ofthe eight individual CAL items.
Root causes ofother concerns identified during the design inspection, but not addressed in the CAL,were determined within the standard framework ofour corrective action'system.
They were independently reviewed.
Additionally, senior industry peers reviewed all root cause investigation reports.
Additionally, senior industry peers reviewed all root cause investigation reports.
: 2. The root causes were reviewed by a group of senior managers and staff in several working sessions. Implications of the various root causes were identified and Page   1 of 13
2.
The root causes were reviewed by a group ofsenior managers and staff in several working sessions.
Implications of the various root causes were identified and Page 1 of 13


Short Term Assessment Program Rev. 2 discussed,   with particular attention given to causes with potentially broader implications.
Short Term Assessment Program Rev. 2 discussed, with particular attention given to causes with potentially broader implications.
: 3. The   final step involved evaluating and identifying engineering issues that have the potential to impact operability of other safety systems. A total of five issues were identified.
3.
The next task was to identify specific actions necessary to determine whether these five issues were present in other safety systems, and if they were, whether operability of the systems was affected. Action plans were endorsed by senior management and staff and were approved by the Nuclear Safety and Design Review Committee.
The final step involved evaluating and identifying engineering issues that have the potential to impact operability ofother safety systems.
Identification of "These Types of Engineering Problems" Ste s   1 and 2- Root Cause Determination and Consideration   of Im lications Root cause determination (Step 1) and consideration of the implications (Step 2) are described in Appendix A for each of the eight CAL items and other design inspection concerns. Results are summarized in Tables 1 and 2.
A total offive issues were identified.
A total of     15 design inspection issues were included in the formal root cause determination (Table 1, Column 1). Although this is less than the number of findings presented in the NRC's design inspection report, in some cases the issues included in our root cause evaluation encompassed multiple findings.
The next task was to identify specific actions necessary to determine whether these five issues were present in other safety systems, and ifthey were, whether operability of the systems was affected.
Twenty-two separate root causes or significant contributors were identified (Table 1, Column 2. (Although there are 24 entries in the column, two are duplicates and in one case the root cause team did not determine a cause.) Comparing these causes against a simplified diagram of our change processes, represented in Figure 2, reveals that five processes     or sub-processes were involved:         design development, configuration management, design documentation, procedure development, and 10 CFR 50.59 safety reviews (Table 1, Column 3).
Action plans were endorsed by senior management and staff and were approved by the Nuclear Safety and Design Review Committee.
Ste   3 Identification of Relevant En ineerin Issues The process or sub-process associated with each cause was broken down further into a descriptive category to identify where or how the process failed (Table 1, Column 4). Of the 22 causes identified, 13 were considered as potentially affecting operability of other safety systems (Table 1, Column 5).
Identification of"These Types ofEngineering Problems" Ste s
Of interest is the fact that eight of the causes that did not potentially affect operability of other safety systems fell under the category of "failure to consider UFSAR as top-tier design basis." These causes were associated with several processes or sub-processes.
1 and 2-Root Cause Determination and Consideration ofIm lications Root cause determination (Step
Although not specifically included in short-term assessment actions, our failure to recognize UFSAR information as design basis will be a focus of our longer-term program.
: 1) and consideration of the implications (Step 2) are described in Appendix A for each of the eight CAL items and other design inspection concerns.
Results are summarized in Tables 1 and 2.
A total of 15 design inspection issues were included in the formal root cause determination (Table 1, Column 1).
Although this is less than the number of findings presented in the NRC's design inspection report, in some cases the issues included in our root cause evaluation encompassed multiple findings.
Twenty-two separate root causes or significant contributors were identified (Table 1,
Column 2. (Although there are 24 entries in the column, two are duplicates and in one case the root cause team did not determine a cause.)
Comparing these causes against a simplified diagram of our change processes, represented in Figure 2, reveals that five processes or sub-processes were involved:
design development, configuration management, design documentation, procedure development, and 10 CFR 50.59 safety reviews (Table 1, Column 3).
Ste 3 Identification ofRelevant En ineerin Issues The process or sub-process associated with each cause was broken down further into a descriptive category to identify where or how the process failed (Table 1, Column 4). Of the 22 causes identified, 13 were considered as potentially affecting operability of other safety systems (Table 1, Column 5).
Ofinterest is the fact that eight ofthe causes that did not potentially affect operability of other safety systems fell under the category of "failure to consider UFSAR as top-tier design basis."
These causes were associated with several processes or sub-processes.
Although not specifically included in short-term assessment
: actions, our failure to recognize UFSAR information as design basis will be a focus of our longer-term program.
The 13 causes potentially affecting operability were then grouped under their common category (Columns 1 and 2, Table 2). The five broad engineering issues were:
The 13 causes potentially affecting operability were then grouped under their common category (Columns 1 and 2, Table 2). The five broad engineering issues were:
Page 2 of 13
Page 2 of 13


Short Term Assessment Program Rev. 2
Short Term Assessment Program Rev. 2 1.
: 1. Calculation deficiencies
Calculation deficiencies 2.
: 2. Adverse effects   of non-safety related systems     on safety related systems
Adverse effects ofnon-safety related systems on safety related systems 3.
: 3. Improper consideration of instrument bias
Improper consideration ofinstrument bias 4.
: 4. Failure to consider and preserve multiple functional design requirements
Failure to consider and preserve multiple functional design requirements 5.
: 5. Failure to properly apply single failure criteria Identification of Specific Assessment Actions The five broad issues, ifconsidered in the absence of existing knowledge, could generate an extensive list of follow-up items to ensure that they did not render safety systems at Cook Plant inoperable. For most of these items, however, substantial documentation or other rationale already existed that provided confidence that these potential follow-up items did not significantly impact other systems. For example, the failure to consider the Bernoulli effect on RWST level measurement suggested that instrument biases in general might be a concern. However, this concern was dispelled by a review of instrument calculation procedures and instrument calculations that provides confidence that other biases are recognized and are routinely applied. Therefore, the scope of new actions to undertake prior to restart was focused on assessing the Bernoulli effect on process measurement. Some issues, such as improper application of single failure criteria could not be limited.
Failure to properly apply single failure criteria Identification ofSpecific Assessment Actions The five broad issues, ifconsidered in the absence ofexisting knowledge, could generate an extensive list of follow-up items to ensure that they did not render safety systems at Cook Plant inoperable.
The implications and factors affecting the potential significance and scope of problems associated with each cause were determined (Column 3, Table 2). Consideration of these factors allowed the issues to be focused (Column 4, Table 2).
For most of these items, however, substantial documentation or other rationale already existed that provided confidence that these potential follow-up items did not significantly impact other systems.
The final statement of each issue approved by the NSDRC is as follows:
For example, the failure to consider the Bernoulli effect on RWST level measurement suggested that instrument biases in general might be a concern.
: 1. Some AEP/Westinghouse analyses were found to contain errors.
However, this concern was dispelled by a review of instrument calculation procedures and instrument calculations that provides confidence that other biases are recognized and are routinely applied.
: 2. Lack   of consideration of a credible failure mode     on a non-safety related systems interfacing with safety related systems
Therefore, the scope of new actions to undertake prior to restart was focused on assessing the Bernoulli effect on process measurement.
: 3. Lack   of consideration of level instrument   bias due to Bernoulli effect
Some issues, such as improper application of single failure criteria could not be limited.
: 4. Some containment attributes such as those related to sump performance have not been adequately preserved
The implications and factors affecting the potential significance and scope of problems associated with each cause were determined (Column 3, Table 2). Consideration ofthese factors allowed the issues to be focused (Column 4, Table 2).
: 5. Improper application   of single failure criteria Short-term assessment actions identified and approved for each engineering issue are summarized in Table 3.
The final statement ofeach issue approved by the NSDRC is as follows:
Page 3 of 13
1.
Some AEP/Westinghouse analyses were found to contain errors.
2.
Lack of consideration of a credible failure mode on a non-safety related systems interfacing with safety related systems 3.
Lack ofconsideration oflevel instrument bias due to Bernoulli effect 4.
Some containment attributes such as those related to sump performance have not been adequately preserved 5.
Improper application ofsingle failure criteria Short-term assessment actions identified and approved for each engineering issue are summarized in Table 3.
Page 3 of 13


Short Term Assessment Program Rev. 2 Summary Development of the short-term assessment program was thorough and rigorous. Root causes of the CAL items and other issues identified during the design inspection were evaluated. Substantial documentation or other rationale existed in many cases to limit the additional actions required prior to restart, and some of the root causes are more appropriately addressed in the longer-term programs aimed at assuring that these kinds of engineering problems are promptly identified, thoroughly evaluated, and resolved.
Short Term Assessment Program Rev. 2 Summary Development of the short-term assessment program was thorough and rigorous.
This latter group includes human performance deficiencies and organizational weaknesses that were recognized to some extent in all of the issues, but were not germane to determining the scope and impact of identified problems on the operability of other safety systems.
Root causes of the CAL items and other issues identified during the design inspection were evaluated.
Satisfactory completion of the short-term assessment actions, coupled. with the existing information used to determine the scope of the assessment, provides reasonable assurance that the kinds of engineering problems found during the design inspection do not affect the operability of other safety systems.
Substantial documentation or other rationale existed in many cases to limitthe additional actions required prior to restart, and some of the root causes are more appropriately addressed in the longer-term programs aimed at assuring that these kinds of engineering problems are promptly identified, thoroughly evaluated, and resolved.
This latter group includes human performance deficiencies and organizational weaknesses that were recognized to some extent in all ofthe issues, but were not germane to determining the scope and impact of identified problems on the operability of other safety systems.
Satisfactory completion of the short-term assessment actions, coupled. with the existing information used to determine the scope ofthe assessment, provides reasonable assurance that the kinds of engineering problems found during the design inspection do not affect the operability ofother safety systems.
Page 4 of 13
Page 4 of 13


Figure 1 Short-Term Assessment Program Development Design inspection Root causes Root causes             that could impact findings operability Existing knowledge (SSFI, surveillances, procedures, etc.)
Figure 1
Issue 1           Issue 2         Issue 3 Issue 4             Issue 5 Short-term assessment actions Short Term Assessment Program Rev. 2 Page 5 of 13
Short-Term Assessment Program Development Design inspection findings Root causes Root causes that could impact operability Existing knowledge (SSFI, surveillances, procedures, etc.)
Issue 1
Issue 2 Issue 3 Issue 4 Issue 5 Short-term assessment actions Short Term Assessment Program Rev. 2 Page 5 of 13


Figure 2 - Simplified                     nge Iden        rk activity                                Perform work Process Design Basis Design Is it a change'                     Work control                                         Licensing Basis           Documenfafion Engineering Basis Yes Physical change Type of change                     Operational change           Typical change process                                       Select tools and Gather information methods Technical change                                                                     Analyze and develop Select solution alternative solutions Administrative change Design or Procedure Oevelopmenf
Iden rk activity Perform work Figure 2 - Simplified nge Process Is it a change' Work control Design Basis Licensing Basis Engineering Basis Design Documenfafion Yes Physical change Type of change Operational change Typical change process Gather information Select tools and methods Technical change Select solution Analyze and develop alternative solutions Administrative change Design or Procedure Oevelopmenf
                                          -10 CFR 50.59 Review Potential Is the change                    Submit under regulatory         ~~Yes Is USQD req'd'?       Yes                                                                   Obtain NRC approval a USQ?                       10 CFR 50.92 impact No                               No Configuration Implement change Short Term Assessment Program                                                                       control Rev. 2 Page 6 of 13                                                                                           -
-10 CFR 50.59 Review Potential regulatory impact
Configuration Managemenf
~~Yes Is USQD req'd'?
* Short Term Assessment Program Rev. 2 Table  I - Summary      and Initial Categorization of Root Causes Design Inspection      Idcntificd Root Cause        Related Process      Category                    Operability Finding            or Contributor            or Sub-proccss                                    Implications CAL Item I:          Lack of thorough              Design            Calculation                      Yes Recirculation        engineering review          development        deficiencies sump inventory Inadequate design control    Design            Failure to consider              Yes during initial plant design  development        multiple functional requirements Improper implementation      Configuration     Failure to preserve              Yes of well defined  design      management        multiple functional expectations                                    requirements CAL Item 2:          Foreign material              Design            Failure to consider              Yes Recirculation        exclusion (FME)              development        multiple functional sump cover          protection not installed                                            'equirements venting Design change not            Design            Failure to consider              Yes properly incorporated        documentation    multiple functional into design                                    requirements documentation Design and licensing          Design            Failure to consider              No basis information not        documentation    UFSAR as top-tier retrieved in a timely                          design basis manner CAL Item 3: 36-      Design parameters for all    Design            Failure to consider              No hour cooldown        system conditions were        documentation    UFSAR as top-tier not described in the                            design basis UFSAR Analysis used an              Design            Calculation                      Yes unverified (and incorrect)    development      deficiency assumption ofheat exchangertype CAL Item 4:          Lack of consideration of      Design            Improper                          Yes Switchover from      Bernoulli effect on level    development      consideration of injection to        instrumentation                                instrument bias recirculation Incorrect application  of    Design            Failure to properly              Yes single failure criteria        development      apply single failure criteria CAL Item 5:        Failure to identify a non-    Design            Adverse effects of                Yes Compressed air      safety system failure          development      non-safety related overpressure        mode that could impact                          systems on safety safety system                                    related systems components Page 7  of 13
Yes Is the change a USQ?
Submit under 10 CFR 50.92 Obtain NRC approval No No Short Term Assessment Program Rev. 2 Page 6 of 13 Configuration control Implement change
- Configuration Managemenf


Short Term Assessment Program Rev. 2 Table I Summary       and Initial Categorization of Root Causes (cont'd)
Short Term Assessment Program Rev. 2 Table I - Summary and InitialCategorization ofRoot Causes Design Inspection Finding Idcntificd Root Cause or Contributor Related Process or Sub-proccss Category Operability Implications CALItem I:
Design Inspection     Identified Root Cause           Related Process     Category        Operability Finding              or Contributor              or Sub-process                    Implications
Recirculation sump inventory CALItem 2:
                                                                                                  'p CALItem6: RHR        Processes in place (at the      Procedure        Failure to consider Literally suction valve        time) did not emphasize          development      UFSAR as top-tier  inoperable interlock            the UFSAR, resulting in                          design basis        per T/S, but an inadequate safety                                                  no effect on review                                                                functionality Design change                    Procedure        Configuration       No accomplished via                development     management procedure revision CAL Item 7:        Lack of procedures for            Configuration    Failure to preserve Yes Fibrous material in  implementing an                  management      multiple functional containment          insulation specification                          design requirements Failure to address sump-        Design            Failure to consider Yes plugging potential of            development      multiple functional fibrous insulation                                design material installed in                              requirements containment CAL Item 8: Leak    Failure to ensure that          Design            Calculation        Yes back to RWST        plant equipment met              development      deficiencies during              assumptions incorporated recirculation        in licensing basis calculations Lake temperature    Failure to recognize              10 CFR 50.59    Failure to consider No design basis                  value as a design a'FSAR safety reviews    UFSAR as top-tier discrepancies        basis parameter                                    design basis Failure to recognize inter-      10 CFR 50.59    Failure to consider No (see relationships between a          safety reviews    UFSAR as top-tier   discussion Iil UFSAR value and other                              design basis       Appendix A) design aspects Unit 2 full core    10 CFR 50.59 reviews              10 CFR 50.59    Failure to consider No (see off-load with        may be inadequate                safety reviews    UFSAR as top-tier   discussion in concurrent CCW                                                          design basis       Appendix A) dual train outage Restriction of       10 CFR 50.59 reviews            10 CFR 50.59      Failure to consider No (see CCW temperature      may be inadequate                safety reviews    UFSAR as top-tier  discussion in during Unit 2 full,                                                    design basis        Appendix A) core off-load Page of 13
Recirculation sump cover venting CALItem 3: 36-hour cooldown CALItem 4:
Switchover from injection to recirculation CALItem 5:
Compressed air overpressure Lack ofthorough engineering review Inadequate design control during initial plant design Improper implementation ofwell defined design expectations Foreign material exclusion (FME) protection not installed Design change not properly incorporated into design documentation Design and licensing basis information not retrieved in a timely manner Design parameters for all system conditions were not described in the UFSAR Analysis used an unverified (and incorrect) assumption ofheat exchangertype Lack ofconsideration of Bernoulli effect on level instrumentation Incorrect application of single failure criteria Failure to identify a non-safety system failure mode that could impact safety system components Design development Design development Configuration management Design development Design documentation Design documentation Design documentation Design development Design development Design development Design development Calculation deficiencies Failure to consider multiple functional requirements Failure to preserve multiple functional requirements Failure to consider multiple functional
'equirements Failure to consider multiple functional requirements Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Calculation deficiency Improper consideration of instrument bias Failure to properly apply single failure criteria Adverse effects of non-safety related systems on safety related systems Yes Yes Yes Yes Yes No No Yes Yes Yes Yes Page 7 of 13


Short Term Assessment Program Rev. 2 Table   1- Summary      and Initial Categorization of Root Causes (cont'tl)
Short Term Assessment Program Rev. 2 Table ISummary and InitialCategorization ofRoot Causes (cont'd)
Design Inspection     Identified Root Cause       Related Process     Category        Operability Finding              or Contributor            or Sub-process                     Implications
Design Inspection Finding Identified Root Cause or Contributor Related Process or Sub-process Category Operability Implications
                                                                                              'P RWST minimum        Misinterpretation of T/S      Design           Calculation        Yes volume for           resulted in failure to       development      deficiencies Appendix R          translate calculation assumptions and results into operating procedures 2-CD battery cell    N/A no cause                N/A              N/A                No (see left on charge for  determined by root cause                                          discussion ill an extended period  team                                                              Appendix A)
'p CALItem6: RHR suction valve interlock CALItem 7:
Code discrepancy    Failure to translate design   Procedure       Configuration       No in CCW system        requirements into            development     management safety valves        operating procedures Procedures          Failure to translate          Procedure        Failure to consider No allowing both        UFSAR requirements            development      UFSAR as top-tier RHR pumps to run    into operating procedures                      design basis with the RCS vented Page of 13
Fibrous material in containment CALItem 8: Leak back to RWST during recirculation Lake temperature design basis discrepancies Unit 2 fullcore off-load with concurrent CCW dual train outage Restriction of CCW temperature during Unit 2 full, core off-load Processes in place (at the time) did not emphasize the UFSAR, resulting in an inadequate safety review Design change accomplished via procedure revision Lack ofprocedures for implementing an insulation specification Failure to address sump-plugging potential of fibrous insulation material installed in containment Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Failure to recognize a'FSAR value as a design basis parameter Failure to recognize inter-relationships between a UFSAR value and other design aspects 10 CFR 50.59 reviews may be inadequate 10 CFR 50.59 reviews may be inadequate Procedure development Procedure development Configuration management Design development Design development 10 CFR 50.59 safety reviews 10 CFR 50.59 safety reviews 10 CFR 50.59 safety reviews 10 CFR 50.59 safety reviews Failure to consider UFSAR as top-tier design basis Configuration management Failure to preserve multiple functional design requirements Failure to consider multiple functional design requirements Calculation deficiencies Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Literally inoperable per T/S, but no effect on functionality No Yes Yes Yes No No (see discussion Iil Appendix A)
No (see discussion in Appendix A)
No (see discussion in Appendix A)
Page 8 of 13


Short Term Assessment Program Rev. 2 Table   2- Implications of Root Causes           Potentially Affecting Operability Broad Category          IdcntiTicd Root Cause (or       Implications and Factors          Enginccring Issue Contributor)            Affecting Scope of Review Calculation deficiencies    Lack of thorough                ~  Involved Westinghouse-     Some AEP/Westinghouse engineering review                  AEP interface              analyses were found to
Short Term Assessment Program Rev. 2 Table 1-Summary and InitialCategorization ofRoot Causes (cont'tl)
                                                              ~  Systems could not be        contain errors.
Design Inspection Finding Identified Root Cause or Contributor Related Process or Sub-process Category Operability Implications
(From CAL Item 1) functionally tested
'P RWST minimum volume for Appendix R 2-CD battery cell left on charge for an extended period Code discrepancy in CCW system safety valves Procedures allowing both RHR pumps to run with the RCS vented Misinterpretation ofT/S resulted in failure to translate calculation assumptions and results into operating procedures N/Ano cause determined by root cause team Failure to translate design requirements into operating procedures Failure to translate UFSAR requirements into operating procedures Design development N/A Procedure development Procedure development Calculation deficiencies N/A Configuration management Failure to consider UFSAR as top-tier design basis Yes No (see discussion ill Appendix A)
                                                              ~  First-of-a-kind design
No No Page 9 of 13
                                                              ~  Error occurred almost 30 years ago Analysis used an unverified    ~  Involved Westinghouse-(and incorrect) assumption          AEP interface of heat exchanger type          ~  Original error occurred almost 30 years ago (From CAL Item 3)
Failure to ensure that plant    ~  Controls need to be in equipment met                      place to assure that assumptions incorporated            assumptions remain valid in licensing basis calculations (From CAL Item 8)
Misinterpretation of T/S       ~  End use of calculation resulted in failure to             needs to be understood translate calculation           ~  Controls need to be in assumptions and results             place to assure that into operating procedures           assumptions remain valid (from RWST minimum volume for Appendix R)
Adverse effects of non-      Failure to identify a non-      ~  Vulnerability is limited to Lack of consideration of a safety related systems on    safety system failure mode          non-safety related          credible failure mode on a safety related systems      that could impact safety            systems that interface      non-safety related system system components                  with safety systems        interfacing with safety related systems (From CAL Item 5)
Improper consideration    of Lack of consideration of        ~  I&C procedure includes      Lack of consideration of instrument bias              Bernoulli effect on level          other bias terms but not    level instrument bias due to instrumentation                    velocity effects            Bernoulli effect
                                                            ~  Calculation review (From CAL Item 4) confirmed that other biases are considered
                                                            ~  1993 system-based I&C inspection addressed bias Page   10 of 13


Short Term Assessment Program Rev. 2 Table   2- Implications of Root Causes         Potentially Affecting Operability (cont'd)
Short Term Assessment Program Rev. 2 Table 2-Implications ofRoot Causes Potentially Affecting Operability Broad Category Calculation deficiencies Adverse effects ofnon-safety related systems on safety related systems Improper consideration of instrument bias IdcntiTicd Root Cause (or Contributor)
Broad Category       Identified Root Cause (or       Implications and Factors             Engineering Issue Contributor)            Affecting Scope of Review Failure to consider and    Inadequate design control      ~   Involved Westinghouse-       Some containment preserve multiple         during initial plant design        AEP interface                attributes such as those functional design                                             Considered unique case      related to sump requirements (From CAL Item    I),         ~
Lack ofthorough engineering review (From CALItem 1)
Sump cannot be tested,   performance have not been but relies on analysis   adequately preserved for demonstrating adequacy Unlike typical cases where analysis is the only tool, this relies on totally plant-specific assumptions and calculations
Analysis used an unverified (and incorrect) assumption ofheat exchanger type (From CALItem 3)
                                                          ~   Error occurred almost 30 years ago Improper implementation        ~ Design feature is not of well-defined design              functionally tested expectations (From CAL Item    I)
Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations (From CALItem 8)
Design change not properly    ~   Minor aspect of a larger incorporated into design          design change documentation                  ~   Design function was negligible, with no (From CAL Item 2) impact on operability
Misinterpretation of T/S resulted in failure to translate calculation assumptions and results into operating procedures (from RWST minimum volume for Appendix R)
                                                          ~ Feature was functioning outside its discipline (structural feature performing mechanical function)
Failure to identify a non-safety system failure mode that could impact safety system components (From CALItem 5)
                                                          ~ Feature was not tested or part of inspection program
Lack ofconsideration of Bernoulli effect on level instrumentation (From CAL Item 4)
                                                          ~ Other structures with mechanical functions are typically controlled, e.g.
Implications and Factors Affecting Scope ofReview
~ Involved Westinghouse-AEP interface
~ Systems could not be functionally tested
~ First-of-a-kind design
~ Error occurred almost 30 years ago
~ Involved Westinghouse-AEP interface
~ Original error occurred almost 30 years ago
~ Controls need to be in place to assure that assumptions remain valid
~ End use ofcalculation needs to be understood
~ Controls need to be in place to assure that assumptions remain valid
~ Vulnerability is limited to non-safety related systems that interface with safety systems
~ I&Cprocedure includes other bias terms but not velocity effects
~ Calculation review confirmed that other biases are considered
~ 1993 system-based I&C inspection addressed bias Enginccring Issue Some AEP/Westinghouse analyses were found to contain errors.
Lack ofconsideration ofa credible failure mode on a non-safety related system interfacing with safety related systems Lack ofconsideration of level instrument bias due to Bernoulli effect Page 10 of 13
 
Short Term Assessment Program Rev. 2 Table 2-Implications ofRoot Causes Potentially Affecting Operability (cont'd)
Broad Category Failure to consider and preserve multiple functional design requirements Identified Root Cause (or Contributor)
Inadequate design control during initialplant design (From CALItem I),
Improper implementation ofwell-defined design expectations (From CALItem I)
Design change not properly incorporated into design documentation (From CALItem 2)
Implications and Factors Affecting Scope ofReview
~ Involved Westinghouse-AEP interface
~ Considered unique case Sump cannot be tested, but relies on analysis for demonstrating adequacy Unlike typical cases where analysis is the only tool, this relies on totally plant-specific assumptions and calculations
~ Error occurred almost 30 years ago
~ Design feature is not functionally tested
~ Minoraspect ofa larger design change
~ Design function was negligible, with no impact on operability
~ Feature was functioning outside its discipline (structural feature performing mechanical function)
~ Feature was not tested or part ofinspection program
~ Other structures with mechanical functions are typically controlled, e.g.
doors acting as HELB barriers
doors acting as HELB barriers
                                                          ~ Containment is the most notable example of a system that cannot be functionally tested in its accident response mode
~ Containment is the most notable example ofa system that cannot be functionally tested in its accident response mode
                                                          ~ Search of maintenance work system provides assurance that plant mods are not made via work orders; controls exist to prevent unauthorized mods Page I I of 13
~ Search ofmaintenance work system provides assurance that plant mods are not made via work orders; controls exist to prevent unauthorized mods Engineering Issue Some containment attributes such as those related to sump performance have not been adequately preserved Page I I of 13


Short Term Assessment Program Rev. 2 Table   2- Implications of Root Causes         Potentially Affecting Operability (cont'd)
Short Term Assessment Program Rev. 2 Table 2-Implications ofRoot Causes Potentially Affecting Operability (cont'd)
Broad Category         Idcntificd Root Cause (or       Implications and Factors        Engineering Issue Contributor)           Affecting Scope of Review Cont'd from previous page  Foreign material exclusion     ~  Unprotected vent holes  Cont'd from previous page Failure to consider and (FME) protection not               were found by NRC Some containment installed                          resident during a preserve multiple                                                                      attributes such as those containment walkdown functional design          (From CAL Item 2)                                          related to sump
Broad Category Cont'd from previous page Failure to consider and preserve multiple functional design requirements Failure to properly apply single failure criteria Idcntificd Root Cause (or Contributor)
                                                            ~ Recent focus on FME has requirements                                                                            performance have not been led to better controls adequately preserved since this problem was identified in 1996 Lack of procedures for          ~ Contractor work was not implementing an insulation        closely supervised by specification                      AEP
Foreign material exclusion (FME) protection not installed (From CALItem 2)
                                                            ~ Engineering involvement (From CAL Item 7) was minimal Failure to address sump-        ~ This problem was found plugging potential of              by NRC inspector during fibrous insulation material        a containment walkdown installed in containment (From CAL Item 7)
Lack ofprocedures for implementing an insulation specification (From CALItem 7)
Failure to properly apply  Incorrect application of        ~ Interpretation of active Improper application    of single failure criteria    single failure criteria            failure definition may   single failure criteria have led to error (From CAL Item 4)              ~ Systems with crosstie capabilities between trains or units are susceptible Page 12 of 13.
Failure to address sump-plugging potential of fibrous insulation material installed in containment (From CAL Item 7)
Incorrect application of single failure criteria (From CALItem 4)
Implications and Factors Affecting Scope ofReview
~ Unprotected vent holes were found by NRC resident during a containment walkdown
~ Recent focus on FME has led to better controls since this problem was identified in 1996
~ Contractor work was not closely supervised by AEP
~ Engineering involvement was minimal
~ This problem was found by NRC inspector during a containment walkdown
~ Interpretation ofactive failure definition may have led to error
~ Systems with crosstie capabilities between trains or units are susceptible Engineering Issue Cont'd from previous page Some containment attributes such as those related to sump performance have not been adequately preserved Improper application of single failure criteria Page 12 of 13.


Table 3 - Short               Assessment Plan
Table 3 - Short Assessment Plan


==Purpose:==
==Purpose:==
To determine whether these issues exist in other safety related systems and     ifso, whether they affect system operability Engineering Issue                                       Short Term Scope                             Deliverables             Owner   Date
To determine whether these issues exist in other safety related systems and ifso, whether they affect system operability Engineering Issue Short Term Scope Deliverables Owner Date 1.
: 1. Some AEP/Westinghouse analyses were               ~ Conduct assessment of Westinghouse analyses            ~ Assessment report found to contain errors.                         ~ Confirm that Westinghouse analyses accurately         ~ Assessment report depict the type of heat exchanger for CCW, RHR, and CTS systems
Some AEP/Westinghouse analyses were found to contain errors.
                                                      ~ Confirm that Holtec analyses accurately depict         ~ Letter from Holtec the type of heat exchanger for SFP cooling               with confirming system                                                   memo from Malin
2.
                                                      ~ Confirm that AEP internal analyses accurately         ~ CR 97-2316 depict the type of heat exchanger for these same systems
Lack ofconsideration ofa credible failure mode on a non-safety related systems interfacing with safety related systems 3.
                                                      ~ Perform peer review of calculations referenced         ~ Summary report in CR 97-2525, calculations performed in support of restart, and representative historic calculations from other safety systems
Lack ofconsideration oflevel instrument bias due to Bernoulli effect 4.
: 2. Lack of consideration of a credible failure      ~ Develop rationale for selecting other non-safety        ~ White paper mode on a non-safety related systems                related systems for further FMEA interfacing with safety related systems          ~ Perform FMEA of control air system                     ~ CR 97-2447
Some containment attributes such as those related to sump performance have not been adequately preserved 5.
                                                      ~ Confirm that FMEA on reactor control system             ~ White paper adequately covered failure modes
Improper application ofsingle failure criteria
                                                      ~ Perform FMEA of pressurizer heaters                     ~ White paper
~ Conduct assessment ofWestinghouse analyses
: 3. Lack of consideration of level instrument bias    ~ Review safety-related tank level indication             ~ White paper due to Bernoulli effect                          ~ Review mid-loop monitoring and RVLIS                   ~ White paper
~ Confirm that Westinghouse analyses accurately depict the type ofheat exchanger for CCW, RHR, and CTS systems
: 4. Some containment attributes such as those        ~ Perform containment walkdown, focusing on               ~ Walkdown report related to sump performance have not been            factors like those affecting sump performance, adequately preserved                                especially items which are not surveilled
~ Confirm that Holtec analyses accurately depict the type ofheat exchanger for SFP cooling system
                                                      ~ Resolve containment walkdown questions                 ~ Summary report
~ Confirm that AEP internal analyses accurately depict the type ofheat exchanger for these same systems
: 5. Improper application  of single failure criteria ~ Clarify definition of single failure and                ~ List procedures and incorporate into procedures                             revise
~ Perform peer review ofcalculations referenced in CR 97-2525, calculations performed in support ofrestart, and representative historic calculations from other safety systems
                                                      ~ Verify that "failure-to-run" was considered in         ~ White paper, with Westinghouse and AEP analyses                           Westinghouse letter
~ Develop rationale for selecting other non-safety related systems for further FMEA
                                                      ~ Verify that AFW, ESW, CVCS, 250 v. DC, and             ~ White paper, electrical distribution system crosstie capabilities     including selection have been properly evaluated for use in                 criteria procedures Scope Revision   1 Status Updated 11/5/97 9:30 AM Page13 of13
~ Perform FMEAofcontrol air system
~ Confirm that FMEA on reactor control system adequately covered failure modes
~ Perform FMEAofpressurizer heaters
~ Review safety-related tank level indication
~ Review mid-loop monitoring and RVLIS
~ Perform containment walkdown, focusing on factors like those affecting sump performance, especially items which are not surveilled
~ Resolve containment walkdown questions
~ Clarify definition ofsingle failure and incorporate into procedures
~ Verifythat "failure-to-run" was considered in Westinghouse and AEP analyses
~ Verifythat AFW, ESW, CVCS, 250 v. DC, and electrical distribution system crosstie capabilities have been properly evaluated for use in procedures
~ Assessment report
~ Assessment report
~ Letter from Holtec with confirming memo from Malin
~ CR 97-2316
~ Summary report
~ White paper
~ CR 97-2447
~ White paper
~ White paper
~ White paper
~ White paper
~ Walkdown report
~ Summary report
~ List procedures and revise
~ White paper, with Westinghouse letter
~ White paper, including selection criteria Scope Revision 1 Status Updated 11/5/97 9:30 AM Page13 of13


Short Term Assessment Program APPENDIX A Root Cause Determination and Consideration of Implications Page A-1
Short Term Assessment Program APPENDIXA Root Cause Determination and Consideration ofImplications Page A-1


Short Term Assessment Program Rev. 2 Appendix   A CAL Item 1: Recirculation Sump Inventory Ste   1 Root Cause Determination The problem was defined as "minimum required recirculation sump level to protect against pump vortexing could not be assured for all accident conditions." (Note - The inability to assure adequate sump level was due in part to potential RWST level instrument bias, which was addressed in another investigation.)
Short Term Assessment Program Rev. 2 Appendix A CALItem 1: Recirculation Sump Inventory Ste 1 Root Cause Determination The problem was defined as "minimum required recirculation sump level to protect against pump vortexing could not be assured for all accident conditions."
(Note - The inability to assure adequate sump level was due in part to potential RWST level instrument bias, which was addressed in another investigation.)
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
In late 1967, AEP deviated from Westinghouse's original containment spray system (CTS) design of "a four pump, four heat exchanger configuration per unit" and selected a design that utilized the residual heat removal (RHR) system to supplement CTS. The CTS design also included the addition of lower volume spray headers for iodine removal capability. Implications of the spray header additions with respect to system performance were not discussed in design memoranda.
In late 1967, AEP deviated from Westinghouse's original containment spray system (CTS) design of"a four pump, four heat exchanger configuration per unit" and selected a design that utilized the residual heat removal (RHR) system to supplement CTS.
~   A September     1968 document discussing containment drainage indicates that the annulus should be designed to exclude recirculation water. An October 1968 update to the document notes the need to install drains from the accumulator/fan rooms to the active sump. It also suggests an alternate discharge from the pipe annulus to the recirculation sump "for use during recirc mode in case of a leak in the safety system piping within the access tunnel." These documents reflect an incomplete understanding of the containment, design, as large amounts of recirculation water would be sprayed into the fan accumulator rooms and subsequently drain through the floor gaps and gratings into the pipe annulus.
The CTS design also included the addition of lower volume spray headers for iodine removal capability.
A Nuclear   Safeguards Design Memo from July 1971 addresses the subject of containment flood-up, including the sequence of flooding various containment compartments during a design basis accident. The memo mentions that 300 gpm flow will be diverted via the accumulator/fan rooms to the pipe annulus. The sequence described does not mention entry'of water into the accumulator/fan rooms or pipe annulus until after the lower containment (inside the crane wall),
Implications of the spray header additions with respect to system performance were not discussed in design memoranda.
lower reactor cavity, and seal table area are filled, at which time water spills into the accumulator/fan rooms. The section of the memo titled "Small Loss-of-Coolant Accident Flood-up" states that the flood-up sequence is the same as the design basis accident case. The review uses the design basis flood-up scheme to conclude that there will be sufficient NPSH to accomplish the switchover to recirculation phase when needed.
~
~   In Question 212.29 of FSAR Appendix Q, the NRC requested a detailed description of our calculations for the ECCS pumps during LOCA conditions.
A September 1968 document discussing containment drainage indicates that the annulus should be designed to exclude recirculation water.
An October 1968 update to the document notes the need to install drains from the accumulator/fan rooms to the active sump.
It also suggests an alternate discharge from the pipe annulus to the recirculation sump "foruse during recirc mode in case of a leak in the safety system piping within the access tunnel."
These documents reflect an incomplete understanding of the containment,
: design, as large amounts of recirculation water would be sprayed into the fan accumulator rooms and subsequently drain through the floor gaps and gratings into the pipe annulus.
A Nuclear Safeguards Design Memo from July 1971 addresses the subject of containment flood-up, including the sequence of flooding various containment compartments during a design basis accident.
The memo mentions that 300 gpm flow will be diverted via the accumulator/fan rooms to the pipe annulus.
The sequence described does not mention entry'of water into the accumulator/fan rooms or pipe annulus until after the lower containment (inside the crane wall),
lower reactor cavity, and seal table area are filled, at which time water spills into the accumulator/fan rooms.
The section of the memo titled "Small Loss-of-Coolant Accident Flood-up" states that the flood-up sequence is the same as the design basis accident case.
The review uses the design basis flood-up scheme to conclude that there will be sufficient NPSH to accomplish the switchover to recirculation phase when needed.
~
In Question 212.29 of FSAR Appendix Q, the NRC requested a detailed description of our calculations for the ECCS pumps during LOCA conditions.
The calculation provided assumes that the entire volume of the RWST from the minimum level to the low alarm level is transferred to the active sump, resulting in flood-up to elevation 602'-10" in containment.
The calculation provided assumes that the entire volume of the RWST from the minimum level to the low alarm level is transferred to the active sump, resulting in flood-up to elevation 602'-10" in containment.
Page A-2
Page A-2


Short Term Assessment Program Rev. 2 Appendix A
Short Term Assessment Program Rev. 2 Appendix A
  ~ 'The LOTIC computer analysis models the active sump as a fixed volume and the inactive sump as an "overflow" from the active sump. It does not consider inventory lost to the inactive sump during recirculation. The simplified modeling is an indication that the LOTIC code was not intended to evaluate containment sump performance.
~
This root cause determination employed the fault tree method. The root cause team used a variety of resources, including the original FSAR, early-revision drawings, condition reports, design basis documents and associated reference notebooks, design memoranda, and Westinghouse WCAP documents. AEP and Westinghouse personnel were consulted as needed.
'The LOTIC computer analysis models the active sump as a fixed volume and the inactive sump as an "overflow" from the active sump.
The team initially identified five contributors to this issue: 1) loss of inventory via CTS flow to accumulator/fan rooms, 2) loss of inventory via stairwells, 3) loss of inventory into the reactor cavity, 4) loss of inventory through unsealed penetrations in the crane wall, and 5) incomplete knowledge regarding the response of plant systems to events requiring operation in the recirculation mode.
It does not consider inventory lost to the inactive sump during recirculation.
The first contributor, loss of inventory via CTS flow to the accumulator/fan rooms, is a consequence of the original plant design. Awareness of CTS flow diversion is evident in early documents. However, the drains that were installed to return this diverted water from the accumulator/fan rooms to the active sump are elevated several inches above the floor, and are ineffective due to a competing flow path into the annulus through floor drains, floor grating, and structural gaps. The team questioned why these competing flow paths were not recognized during design. Similarly, the team questioned why additional scrutiny of small break LOCA response following the Three Mile Island accident did not address containment sump inventory questions, but rather focused only on core response.
The simplified modeling is an indication that the LOTIC code was not intended to evaluate containment sump performance.
Lack of thorough review was identified as a root cause of this contributor. Change control was also identified as a root cause, specifically with regard to the change from the original Westinghouse design that led to lack of thorough review.
This root cause determination employed the fault tree method.
The second contributor, loss of inventory via stairwells, was considered by the team to be analogous to the first contributor, and hence had the same cause.
The root cause team used a variety of resources, including the original FSAR, early-revision drawings, condition reports, design basis documents and associated reference notebooks, design memoranda, and Westinghouse WCAP documents.
Inventory loss to the reactor cavity was subsequently determined by the team not to be a contributor. Historically, this aspect of containment inventory has been dealt with appropriately.
AEP and Westinghouse personnel were consulted as needed.
Documentation shows that penetrations in the crane wall were intended to be sealed to restrict flow into the annulus. Failure to seal some of the penetrations resulted from improper implementation of the well-defined design expectations. The team considered this problem not directly related in terms of cause to the other inventory loss mechanisms under consideration. (Note Although the root cause team did not include "improper implementation of well-defined design expectations" in their summary of root causes, it was identified in their report. Management considered this a relevant root cause or contributor and included it in the discussions of root causes that could potentially affect operability of safety systems.)
The team initiallyidentified five contributors to this issue:
: 1) loss of inventory via CTS flow to accumulator/fan rooms, 2) loss of inventory via stairwells, 3) loss of inventory into the reactor cavity, 4) loss of inventory through unsealed penetrations in the crane wall, and 5) incomplete knowledge regarding the response of plant systems to events requiring operation in the recirculation mode.
The first contributor, loss of inventory via CTS flow to the accumulator/fan rooms, is a consequence ofthe original plant design.
Awareness of CTS flowdiversion is evident in early documents.
However, the drains that were installed to return this diverted water from the accumulator/fan rooms to the active sump are elevated several inches above the floor, and are ineffective due to a competing flow path into the annulus through floor drains, floor grating, and structural gaps.
The team questioned why these competing flow paths were not recognized during design.
Similarly, the team questioned why additional scrutiny ofsmall break LOCA response followingthe Three Mile Island accident did not address containment sump inventory questions, but rather focused only on core response.
Lack of thorough review was identified as a root cause of this contributor.
Change control was also identified as a root cause, specifically with regard to the change from the original Westinghouse design that led to lack ofthorough review.
The second contributor, loss ofinventory via stairwells, was considered by the team to be analogous to the first contributor, and hence had the same cause.
Inventory loss to the reactor cavity was subsequently determined by the team not to be a contributor.
Historically, this aspect of containment inventory has been dealt with appropriately.
Documentation shows that penetrations in the crane wall were intended to be sealed to restrict flow into the annulus.
Failure to seal some of the penetrations resulted from improper implementation ofthe well-defined design expectations.
The team considered this problem not directly related in terms ofcause to the other inventory loss mechanisms under consideration.
(Note Although the root cause team did not include "improper implementation ofwell-defined design expectations" in their summary of root causes, it was identified in their report.
Management considered this a relevant root cause or contributor and included it in the discussions of root causes that could potentially affect operability ofsafety systems.)
Page A-3
Page A-3


Short Term Assessment Program Rev. 2 Appendix A With regard to the fifth contributor, until recently there was incomplete knowledge pertaining to the effect of the inactive sump on recirculation sump inventory during accident scenarios. The team concluded that, while this condition warrants concern, the cause of this contributor is rooted in the lack of identification of the issue on a more fundamental level. Since the concern had never been identified, the operations and engineering staff could not be expected to be knowledgeable on the subject.
Short Term Assessment Program Rev. 2 Appendix A With regard to the fifth contributor, until recently there was incomplete knowledge pertaining to the effect of the inactive sump on recirculation sump inventory during accident scenarios.
The root causes associated with CAL Item    1 are:
The team concluded that, while this condition warrants concern, the cause of this contributor is rooted in the lack of identification of the issue on a more fundamental level.
Lack of thorough engineering review
Since the concern had never been identified, the operations and engineering staff could not be expected to be knowledgeable on the subject.
The root causes associated with CALItem 1 are:
Lack ofthorough engineering review
~ ~
Inadequate design control during initialplant design
~
~
    ~  Inadequate design control during initial plant design
Improper implementation ofwell defined design expectations Ste 2 - Consideration ofIm lications Lack ofthorough engineering review Design reviews addressing the recirculation sump incorporated simplifying assumptions that were considered bounding, but did not consider the entire range of conditions under which the equipment could be required to function.
    ~
For example, small break LOCA concerns were generally considered bounded by large break LOCA analysis.
Improper implementation   of well defined design expectations Ste 2 - Consideration of Im lications Lack ofthorough engineering review Design reviews addressing the recirculation sump incorporated simplifying assumptions that were considered bounding, but did not consider the entire range of conditions under which the equipment could be required to function. For example, small break LOCA concerns were generally considered bounded by large break LOCA analysis.
Assumptions were made that small break LOCA scenarios did not need to be reviewed with respect to recirculation sump performance and that additional evaluations were not needed to supplement the simplified methodology utilized in the LOTIC code to model containment performance for large break scenarios.
Assumptions were made that small break LOCA scenarios did not need to be reviewed with respect to recirculation sump performance and that additional evaluations were not needed to supplement the simplified methodology utilized in the LOTIC code to model containment performance for large break scenarios. Hence the true dynamic nature of recirculation sump level was never recognized. Lack of thoroughness in reviews of safety related equipment could result in systems being unable to perform their intended function. Short-term assessment actions were considered necessary to address this concern.
Hence the true dynamic nature of recirculation sump level was never recognized.
Inadequate design control during initialplant design This concern centered on failure of AEP and Westinghouse to ensure that all were met for a system that had shared engineering responsibility. This design'equirements
Lack of thoroughness in reviews of safety related equipment could result in systems being unable to perform their intended function.
  ,example is considered unique. First, the adequacy of containment sump inventory can not be functionally tested. Unlike other design aspects that rely solely on analyses to demonstrate their acceptability (e.g. evaluating core response during transients using industry-accepted assumptions and analysis techniques), the assumptions and analytical techniques needed to assess sump performance are plant-specific.           The ability to functionally test other interfacing systems and the use of industry-accepted methodologies on other important safety analyses were considered adequate to preclude this cause from affecting other safety systems. Although specific short-term actions were not identified for this root cause due to the uniqueness of the situation, this was considered another general example of failure to consider multiple functional design requirements of an SSC, which was addressed in the 'short-term assessment.
Short-term assessment actions were considered necessary to address this concern.
Inadequate design control during initialplant design This concern centered on failure of AEP and Westinghouse to ensure that all design'equirements were met for a system that had shared engineering responsibility.
This
,example is considered unique.
First, the adequacy of containment sump inventory can not be functionally tested.
Unlike other design aspects that rely solely on analyses to demonstrate their acceptability (e.g. evaluating core response during transients using industry-accepted assumptions and analysis techniques), the assumptions and analytical techniques needed to assess sump performance are plant-specific.
The ability to functionally test other interfacing systems and the use of industry-accepted methodologies on other important safety analyses were considered adequate to preclude this cause from affecting other safety systems.
Although specific short-term actions were not identified for this root cause due to the uniqueness of the situation, this was considered another general example of failure to consider multiple functional design requirements ofan SSC, which was addressed in the 'short-term assessment.
Page A-4
Page A-4


Short Term Assessment Program Rev. 2 Appendix A Improper implementation       ofmell defined design   expectations The expectations for crane wall penetration sealing were clearly defined, but were not implemented.       Although it was recently determined that sealing of the crane wall penetrations was not necessary to ensure adequate inventory, the implications of improperly implementing and maintaining design expectations on SSCs are significant.
Short Term Assessment Program Rev. 2 Appendix A Improper implementation ofmell defined design expectations The expectations for crane wall penetration sealing were clearly defined, but were not implemented.
Although it was recently determined that sealing of the crane wall penetrations was not necessary to ensure adequate inventory, the implications of improperly implementing and maintaining design expectations on SSCs are significant.
Short-term assessment actions were considered necessary to address this concern.
Short-term assessment actions were considered necessary to address this concern.
CAL Item 2: Recirculation Sump Cover Venting Ste   1 Root Cause Determination The problem was defined as "plant design was changed by plugging the holes in the roof of containment recirculation sump without considering the design and licensing bases for the holes."
CALItem 2: Recirculation Sump Cover Venting Ste 1 Root Cause Determination The problem was defined as "plant design was changed by plugging the holes in the roof ofcontainment recirculation sump without considering the design and licensing bases for the holes."
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
~   The design change, RFC 12-2361, contained a description and reason for boring the holes in the sump cover. Hole locations were accurately defined on a core bore request sketch in the field installation portion of the RFC.
~
~   The basis for the holes in the Units 1 and 2 sump cover is contained in submittal AEP:NRC:0110, which was a commitment from the FSAR questions and answers. This correspondence leads the Alden Lab sump model study report.
The design change, RFC 12-2361, contained a description and reason for boring the holes in the sump cover.
The vent holes were plugged under job orders in response to condition report investigations in 1996 and 1997. One of the job orders identified that the holes were assumed abandoned bolt holes.
Hole locations were accurately defined on a core bore request sketch in the field installation portion ofthe RFC.
~   RFC 12-2361 was inadequate in that:
~
Changes made were not fully reflected in design documents; the holes were shown on a structural drawing, but not on flow diagrams or system description.
The basis for the holes in the Units 1 and 2 sump cover is contained in submittal AEP:NRC:0110, which was a commitment from the FSAR questions and answers.
The foreign material exclusion (FME) zone for the sump was relocated upstream when the internal plate was removed and a fine mesh screen was added at the sump entrance. However, steps were not taken to assure particle retention criteria were maintained for other sump inlets (such as the sump cover vent holes).
This correspondence leads the Alden Lab sump model study report.
~   A   search of the computerized licensing database (using FOLIO) for "sump holes" provides an immediate link to AEP:NRC:0110. FOLIO was not available to system engineers until mid-1997.
The vent holes were plugged under job orders in response to condition report investigations in 1996 and 1997.
The root cause determination employed change analysis, barrier analysis, interviewing, and event and causal factor charting. The root cause team summarized their findings Page A-5
One of the job orders identified that the holes were assumed abandoned bolt holes.
~
RFC 12-2361 was inadequate in that:
Changes made were not fullyreflected in design documents; the holes were shown on a structural drawing, but not on flow diagrams or system description.
The foreign material exclusion (FME) zone for the sump was relocated upstream when the internal plate was removed and a fine mesh screen was added at the sump entrance.
However, steps were not taken to assure particle retention criteria were maintained for other sump inlets (such as the sump cover vent holes).
~
A search of the computerized licensing database (using FOLIO) for "sump holes" provides an immediate link to AEP:NRC:0110.
FOLIO was not available to system engineers until mid-1997.
The root cause determination employed change analysis, barrier analysis, interviewing, and event and causal factor charting.
The root cause team summarized their findings Page A-5


0 Short Term Assessment Program Rev. 2 Appendix A primarily in terms of human performance issues, but more direct causes can       be, derived from their investigation:
0
The relevant root causes associated with CAL Item 2 are:
 
~   FME protection not installed (considered as another example of "improper implementation of well-defined design expectations" noted in CAL Item 1)
Short Term Assessment Program Rev. 2 Appendix A primarily in terms of human performance issues, but more direct causes can be, derived from their investigation:
~   Design change not properly incorporated into design documentation
The relevant root causes associated with CALItem 2 are:
~
~
Design and licensing basis not retrieved in a timely manner Ste 2-ConsiderationofIm lications FMEprotection not installed Failure to consider FME requirements in this case occurred nearly 20 years ago. FME, particularly with regard to recirculation sump performance, has been a,focus area in recent years. In'act, heightened awareness of the importance of FME led to plugging the holes in the sump cover. No specific short-term efforts were considered necessary to address FME protection. However, this situation was considered an example of failing to implement design expectations and failing to preserve design requirements, which were considered necessary to address in the short-term assessment.
FME protection not installed (considered as another example of "improper implementation ofwell-defined design expectations" noted in CALItem 1)
Design change not properly incorporatedinto design documentation Although the root cause as stated could indicate a fundamental weakness in configuration management, there are reasons for limiting the scope of concern. First, this was a case where a minor aspect of a larger design change was overlooked in some portions of the documentation. Safety system operability was not threatened by this oversight. There is no basis for concluding from this example that functionally significant features have been omitted from design documentation. Second, this design feature was functioning outside its typical discipline; the holes were a structural feature that was performing a mechanical function. The structural drawings portrayed the holes, but their function (i.e., vent holes) was not indicated. They were not included on the mechanical flow diagrams. Finally, a third factor is that this design feature could not be tested and was not included in an inspection program. While the first point supports a conclusion that operability of safety systems is not threatened by design documentation deficiencies, it was concluded that some additional actions be included in the short-term assessment actions.
~
l Although it was not designated as a root cause or significant contributor by the investigating team, the management group also discussed the implications of plugging these holes under a maintenance action request. To provide assurance that there is not a programmatic weakness allowing modifications to be done under a work order, a search of the computerized maintenance work order system was conducted using various key words that could indicate modifications were being done. No maintenance action requests were found that improperly implemented modifications. The management group concluded that that appropriate programmatic controls to prevent unauthorized modifications are in place. In the case of the sump cover holes, the system engineer believed that plugging the holes was necessary to return the sump to its intended Page A-6
Design change not properly incorporated into design documentation
~
Design and licensing basis not retrieved in a timely manner Ste 2-ConsiderationofIm lications FMEprotection not installed Failure to consider FME requirements in this case occurred nearly 20 years ago.
: FME, particularly with regard to recirculation sump performance, has been a,focus area in recent years. In'act, heightened awareness ofthe importance ofFME led to plugging the holes in the sump cover.
No specific short-term efforts were considered necessary to address FME protection. However, this situation was considered an example offailing to implement design expectations and failing to preserve design requirements, which were considered necessary to address in the short-term assessment.
Design change notproperly incorporatedinto design documentation Although the root cause as stated could indicate a fundamental weakness in configuration management, there are reasons for limiting the scope of concern.
First, this was a case where a minor aspect of a larger design change was overlooked in some portions of the documentation.
Safety system operability was not threatened by this oversight.
There is no basis for concluding from this example that functionally significant features have been omitted from design documentation.
Second, this design feature was functioning outside its typical discipline; the holes were a structural feature that was performing a mechanical function. The structural drawings portrayed the holes, but their function (i.e., vent holes) was not indicated.
They were not included on the mechanical flow diagrams.
Finally, a third factor is that this design feature could not be tested and was not included in an inspection program.
While the first point supports a conclusion that operability of safety systems is not threatened by design documentation deficiencies, it was concluded that some additional actions be included in the short-term assessment actions.
l Although it was not designated as a root cause or significant contributor by the investigating team, the management group also discussed the implications of plugging these holes under a maintenance action request.
To provide assurance that there is not a programmatic weakness allowing modifications to be done under a work order, a search of the computerized maintenance work order system was conducted using various key words that could indicate modifications were being done.
No maintenance action requests were found that improperly implemented modifications. The management group concluded that that appropriate programmatic controls to prevent unauthorized modifications are in place.
In the case of the sump cover holes, the system engineer believed that plugging the holes was necessary to return the sump to its intended Page A-6


Short Term Assessment Program Rev. 2 Appendix A configuration and therefore made a conscious (but incorrect) decision that the work was not a modification.
Short Term Assessment Program Rev. 2 Appendix A configuration and therefore made a conscious (but incorrect) decision that the work was not a modification.
Design atid licensing basis information not retrieved in a timely manner Two facts help mitigate the implications of this cause. First, the design information in question was a minor aspect of the overall sump modification package and was not properly documented. Second, the system engineers now have access to FOLIO, which increases the efficiency with which obscure licensing information can be retrieved. No additional short-term assessment actions were considered necessary.
Design atid licensing basis information not retrieved in a timely manner Two facts help mitigate the implications of this cause.
Cal 3: 36-hour Cooldown Ste   1 Root Cause Determination The root cause investigation focused on two problems.             First, discrepancies were
First, the design information in question was a minor aspect of the overall sump modification package and was not properly documented.
'identified between the CCW system design temperature of 95' contained in the UFSAR and the procedural temperature allowance of 120'. Second, CCW heat exchanger modeling errors were discovered in the 36-hour cooldown analysis performed by Westinghouse.
Second, the system engineers now have access to FOLIO, which increases the efficiency with which obscure licensing information can be retrieved.
For the first problem area, the team found that as early as 1969, the Westinghouse design criteria and functional requirements for the CCW system (transmitted via Westinghouse letter AEW-640) has verbiage describing 95'         as the normal operating value, with allowance for operation at 120'       during cooldown of the plant. Review of other documentation and discussions with Westinghouse led the team to conclude that the design basis was intended to allow higher temperature operation during single train cooldown, but the UFSAR contained an incomplete description of the intended design basis.
No additional short-term assessment actions were considered necessary.
Cal 3: 36-hour Cooldown Ste 1 Root Cause Determination The root cause investigation focused on two problems.
First, discrepancies were
'identified between the CCW system design temperature of95' contained in the UFSAR and the procedural temperature allowance of 120'.
: Second, CCW heat exchanger modeling errors were discovered in the 36-hour cooldown analysis performed by Westinghouse.
For the first problem area, the team found that as early as 1969, the Westinghouse design criteria and functional requirements for the CCW system (transmitted via Westinghouse letter AEW-640) has verbiage describing 95' as the normal operating value, with allowance for operation at 120' during cooldown of the plant.
Review of other documentation and discussions with Westinghouse led the team to conclude that the design basis was intended to allow higher temperature operation during single train cooldown, but the UFSAR contained an incomplete description of the intended design basis.
'For the second problem area, the team found that the CCW heat exchanger, a TEMA-E type procured by AEP, was assumed by Westinghouse to be a counterflow type, which was consistent with CCW heat exchangers typically supplied by Westinghouse.
'For the second problem area, the team found that the CCW heat exchanger, a TEMA-E type procured by AEP, was assumed by Westinghouse to be a counterflow type, which was consistent with CCW heat exchangers typically supplied by Westinghouse.
The root causes associated with CAL Item 3 are:
The root causes associated with CALItem 3 are:
Design parameters for all system conditions were not described in the UFSAR
Design parameters for all system conditions were not described in the UFSAR
~   Analysis used an unverified (and incorrect) assumption   of heat exchanger type Ste   2-ConsiderationofIm lications Design parameters for all system conditions were not describedin       the UFSAR Failure to totally describe the intended design basis of the CCW system in the FSAR led to being outside the design basis by definition, but did not represent a threat to system function or operability. No short-term assessment actions were considered necessary.
~
Analysis used an unverified (and incorrect) assumption ofheat exchanger type Ste 2-ConsiderationofIm lications Design parameters forall system conditions were not describedin the UFSAR Failure to totally describe the intended design basis ofthe CCW system in the FSAR led to being outside the design basis by definition, but did not represent a threat to system function or operability. No short-term assessment actions were considered necessary.
Page A-7
Page A-7


Short Term Assessment Program Rev. 2 Appendix A Analysis used an unverified (and incorrect) assumption     ofheat exchanger type Using incorrect heat exchanger information in the analysis model could potentially result in a system being unable to perform its intended function. This instance could also be considered another example of "inadequate design control during initial plant design."
Short Term Assessment Program Rev. 2 Appendix A Analysis used an unverified (and incorrect) assumption ofheat exchanger type Using incorrect heat exchanger information in the analysis model could potentially result in a system being unable to perform its intended function.
This instance could also be considered another example of "inadequate design control during initial plant design."
Short-term assessment actions were considered necessary to address this concern.
Short-term assessment actions were considered necessary to address this concern.
                                                              '
CALItem 4: Switchover from Injection to Recirculation Ste 1-Root Cause Determination Two problems were investigated.
CAL Item 4: Switchover from Injection to Recirculation Ste   1- Root Cause   Determination Two problems were investigated. The first addressed refueling water storage tank (RWST) level instrumentation not reflecting actual RWST level. The second addressed a procedure-directed alignment where a single active failure of the west residual heat removal (RHR) pump could cause a loss of all high head safety injection pumps duririg transfer to cold leg recirculation.
The first addressed refueling water storage tank (RWST) level instrumentation not reflecting actual RWST level. The second addressed a
procedure-directed alignment where a single active failure of the west residual heat removal (RHR) pump could cause a loss of all high head safety injection pumps duririg transfer to cold leg recirculation.
Pertinent facts for the RWST level problem included:
Pertinent facts for the RWST level problem included:
~   Westinghouse originally designed the system with the level instrumentation located on the RWST. AEP moved the instrumentation from the tank to the ECCS pump suction piping.
~
~   Start-up tests did not identify the error introduced by the instrument location, although it should be noted that identification of such errors was not the purpose of the testing.
Westinghouse originally designed the system with the level instrumentation located on the RWST.
~   AEP did not recognize that relocation of the instruments from the RWST to the pipe introduced significant water velocity induced error in the level measurements, which are used by the operators and provide input to the automatic RHR pump trips.
AEP moved the instrumentation from the tank to the ECCS pump suction piping.
In 1993, the NRC identified that AEP calculations supporting relocation of the
~
* instrument tap had not considered the velocity-induced bias.
Start-up tests did not identify the error introduced by the instrument location, although it should be noted that identification of such errors was not the purpose ofthe testing.
~   AEP attempted to address the identified NRC concern. No changes were made to the instrumentation, but in the effort to resolve the issue, two errors occurred:
~
Only part of the velocity induced error was recognized. The friction losses associated with elbows and straight sections of pipe were addressed, but the entrance losses and the dynamic head losses were not addressed.
AEP did not recognize that relocation of the instruments from the RWST to the pipe introduced significant water velocity induced error in the level measurements, which are used by the operators and provide input to the automatic RHR pump trips.
Only the need to prevent pump damage that could result from operation at too low an RWST level was recognized. The need to assure that sufficient water was transferred &om the RWST to the active sump was not recognized. Therefore, it was concluded that since the friction error made the indicated water level in the RWST appear lower than actual, the error was conservative because it would trip the RHR pumps sooner, thereby Page A-8
In 1993, the NRC identified that AEP calculations supporting relocation of the instrument tap had not considered the velocity-induced bias.
~
AEP attempted to address the identified NRC concern. No changes were made to the instrumentation, but in the effort to resolve the issue, two errors occurred:
Only part of the velocity induced error was recognized.
The friction losses associated with elbows and straight sections ofpipe were addressed, but the entrance losses and the dynamic head losses were not addressed.
Only the need to prevent pump damage that could result from operation at too low an RWST level was recognized.
The need to assure that sufficient water was transferred
&om the RWST to the active sump was not recognized.
Therefore, it was concluded that since the friction error made the indicated water level in the RWST appear lower than actual, the error was conservative because it would trip the RHR pumps sooner, thereby Page A-8


Short Term Assessment Program Rev. 2 Appendix A providing even better protection for the RHR pumps.             It was not recognized that the same error was non-conservative with regard to the second purpose of the instrumentation, i.e., to transfer sufficient water from the RWST for long-term core cooling and containment protection.
Short Term Assessment Program Rev. 2 Appendix A providing even better protection for the RHR pumps.
It was not recognized that the same error was non-conservative with regard to the second purpose of the instrumentation, i.e., to transfer sufficient water from the RWST for long-term core cooling and containment protection.
In that case, the operator would believe more water had been transferred to the sump than actually had been transferred.
In that case, the operator would believe more water had been transferred to the sump than actually had been transferred.
  ~   It has since been determined that locating the level instrument on the process pipe is unacceptable. The instrumerit tap has been moved and the containment sump levels designated in procedure OHP-4023.ES-1.3 have been revised to provide for proper water levels to protect the pumps from vortexing and ensure adequate water inventory in the sump for long-term cooling.
~
This root cause determination was conducted using fault tree analysis methodology. The evaluation team used a variety of resources, including condition reports, design basis documents and notebooks, early-revision drawings, and interviews with AEP personnel.
It has since been determined that locating the level instrument on the process pipe is unacceptable.
The team identified four contributors to this problem: 1) using this type of instrumentation in a non-standard location, 2) failure to recognize the physics of the location, 3) incomplete understanding of the purposes of the instrumentation, and 4) lack of strong interdisciplinary reviews.
The instrumerit tap has been moved and the containment sump levels designated in procedure OHP-4023.ES-1.3 have been revised to provide for proper water levels to protect the pumps from vortexing and ensure adequate water inventory in the sump for long-term cooling.
The first contributor, use of an instrument in a non-standard location, resulted from AEP changing the location of the instrument tap from the tank to the ECCS pump suction piping during the original design of the plant. Although no documentation could be found describing why the position was changed, some AEP personnel indicated that they believe the instrument was moved to provide better protection from cold weather.
This root cause determination was conducted using fault tree analysis methodology.
The second contributor, failure to recognize the physics of the instrument location, resulted from relocation of the instrument. AEP personnel did not recognize that the pipe location introduced velocity effects not present in the original location. Therefore, the calculations that supported the relocation made no provisions for the velocity effects.
The evaluation team used a variety of resources, including condition reports, design basis documents and notebooks, early-revision drawings, and interviews with AEP personnel.
The plant remained in that condition until 1993 when an NRC inspection identified those velocity effects had not been considered. At that time,'EP revisited the calculations and addressed some, but not all the velocity induced effects The third contributor, incomplete understanding of the purposes of the instrumentation, resulted in some instrument bias not being included in the RWST level setpoint. Since the velocity friction losses that were identified tend to make the RWST level appear lower than actual, it was decided they were conservative because they would cause the RHR pumps to trip sooner and provide better protection of the RHR pumps from vortexing. The second, unrecognized purpose is to assure that adequate water is transferred from the RWST for long term cooling of the core and containment. No changes to the instrumentation or procedure were made. The plant remained in the same condition until the recent extensive reviews in 1997.
The team identified four contributors to this problem:
The fourth contributor was lack of a strong interdisciplinary review. Although the calculations were verified by I&C personnel, interdisciplinary reviews of the calculations were not conducted. Such reviews might have recognized the oversight.
1) using this type of instrumentation in a non-standard location, 2) failure to recognize the physics of the location, 3) incomplete understanding ofthe purposes ofthe instrumentation, and 4) lack ofstrong interdisciplinary reviews.
The first contributor, use of an instrument in a non-standard location, resulted from AEP changing the location of the instrument tap from the tank to the ECCS pump suction piping during the original design of the plant.
Although no documentation could be found describing why the position was changed, some AEP personnel indicated that they believe the instrument was moved to provide better protection from cold weather.
The second contributor, failure to recognize the physics of the instrument location, resulted from relocation ofthe instrument. AEP personnel did not recognize that the pipe location introduced velocity effects not present in the original location.
Therefore, the calculations that supported the relocation made no provisions for the velocity effects.
The plant remained in that condition until 1993 when an NRC inspection identified those velocity effects had not been considered.
Atthat time,'EP revisited the calculations and addressed some, but not all the velocity induced effects The third contributor, incomplete understanding of the purposes of the instrumentation, resulted in some instrument bias not being included in the RWST level setpoint.
Since the velocity friction losses that were identified tend to make the RWST level appear lower than actual, it was decided they were conservative because they would cause the RHR pumps to trip sooner and provide better protection of the RHR pumps from vortexing.
The second, unrecognized purpose is to assure that adequate water is transferred from the RWST for long term cooling of the core and containment.
No changes to the instrumentation or procedure were made.
The plant remained in the same condition until the recent extensive reviews in 1997.
The fourth contributor was lack of a strong interdisciplinary review.
Although the calculations were verified by I&Cpersonnel, interdisciplinary reviews ofthe calculations were not conducted.
Such reviews might have recognized the oversight.
Page A-9
Page A-9


Short Term Assessment Program Rev. 2 Appendix A Pertinent facts related to the problem of the procedure configuration where a single active failure of the west RHR pump could cause a loss of all high head safety injection pumps during transfer to cold leg recirculation include:
Short Term Assessment Program Rev. 2 Appendix A Pertinent facts related to the problem ofthe procedure configuration where a single active failure ofthe west RHR pump could cause a loss ofall high head safety injection pumps during transfer to cold leg recirculation include:
Procedure   OHP 4023.ES-1.3, Rev 1, provided an alignment sequence for switchover from ECCS injection to recirculation phase which established SI pump flow via the west RHR train and CCP flow via the east RHR train prior to isolation of the RWST as a suction source for the CCPs. This sequence does not establish dependence of all high head safety injection on either RHR pump and therefore precludes single failure vulnerability.
Procedure OHP 4023.ES-1.3, Rev 1, provided an alignment sequence for switchover from ECCS injection to recirculation phase which established SI pump flow via the west RHR train and CCP flow via the east RHR train prior to isolation ofthe RWST as a suction source for the CCPs.
~   ES-1.3, Rev 2, provided an alignment sequence for switchover from ECCS injection to recirculation which established both trains of safety injection (SI) pump flow and centrifugal charging pump (CCP) flow simultaneously from the west RHR train, with the RWST suction source for both the CCPs and SI pumps isolated. At this point, the suction source &om the east RHR train would not be available. This sequence established dependence of all high head safety injection pumps on the west RHR pump. The failure of the pump under these conditions could have resulted in the loss of all high head safety injection pumps.
This sequence does not establish dependence of all high head safety injection on either RHR pump and therefore precludes single failure vulnerability.
~   During the time frame of the preparation of ES-1.3, Rev 2 the sequence of             .
~
switchover from injection to recirculation mode of ECCS and CTS operation was described in Table 6.2-10 of the updated FSAR (pages 6.2-52 and 6.2-53). This sequence provides for establishment of the RHR suction source for the CCPs from the east RHR train prior to the isolation of the RWST suction supply. This sequence does not establish dependence of all high head safety injection on either RHR pump.
ES-1.3, Rev 2, provided an alignment sequence for switchover from ECCS injection to recirculation which established both trains of safety injection (SI) pump flow and centrifugal charging pump (CCP) flow simultaneously from the west RHR train, with the RWST suction source for both the CCPs and SI pumps isolated. At this point, the suction source &om the east RHR train would not be available.
~   The unreviewed safety question determination for ES-1.3, Rev 2 (for both units) is contained in a June 8, 1992 safety review memorandum. The review is more extensive than many such reviews and discusses a considerable number of open items, but it does not identify or discuss the switchover sequence which resulted in the dependency of all high head safety injection on the west RHR pump.
This sequence established dependence ofall high head safety injection pumps on the west RHR pump.
~   The definition   of "single active failure" contained in Section 6.2 of both the original FSAR and the updated FSAR in effect at the time of the generation of ES-1.3, Rev 2 states that active failure is the "inability of any single dynamic component or instrument to perform its design function when called upon to do so by the proper actuation signal." The FSAR/UFSAR also states, "Table 6.2-6 summarizes the results of the single failure analysis applied during the injection phase. All failures during this phase are assumed to be active failures. It is during this phase that the pumps are starting and automatic isolation valves are required to move. All credible active failures are considered." The failures described in Table 6.2-6 for RHR pumps in both the injection and recirculation phases are noted as "failure to start."
The failure of the pump under these conditions could have resulted in the loss ofall high head safety injection pumps.
This root cause analysis was performed using the fault tree method. During the root cause investigation of this event, the team consulted a variety of information resources, Page A-10
~
During the time frame of the preparation of ES-1.3, Rev 2 the sequence of switchover from injection to recirculation mode of ECCS and CTS operation was described in Table 6.2-10 ofthe updated FSAR (pages 6.2-52 and 6.2-53).
This sequence provides for establishment ofthe RHR suction source for the CCPs from the east RHR train prior to the isolation of the RWST suction supply.
This sequence does not establish dependence ofall high head safety injection on either RHR pump.
~
The unreviewed safety question determination for ES-1.3, Rev 2 (for both units) is contained in a June 8, 1992 safety review memorandum.
The review is more extensive than many such reviews and discusses a considerable number of open items, but it does not identify or discuss the switchover sequence which resulted in the dependency ofall high head safety injection on the west RHR pump.
~
The definition of "single active failure" contained in Section 6.2 of both the original FSAR and the updated FSAR in effect at the time of the generation of ES-1.3, Rev 2 states that active failure is the "inability of any single dynamic component or instrument to perform its design function when called upon to do so by the proper actuation signal."
The FSAR/UFSAR also states, "Table 6.2-6 summarizes the results of the single failure analysis applied during the injection phase.
All failures during this phase are assumed to be active failures.
It is during this phase that the pumps are starting and automatic isolation valves are required to move.
All credible active failures are considered."
The failures described in Table 6.2-6 for RHR pumps in both the injection and recirculation phases are noted as "failure to start."
This root cause analysis was performed using the fault tree method.
During the root cause investigation of this event, the team consulted a variety of information resources, Page A-10


Short Term Assessment Program Rev. 2 Appendix A including earlier revisions of ES-1.3 and associated safety screenings and safety reviews, condition reports, and the original FSAR, current UFSAR, and intermediate revisions of the UFSAR. AEP personnel were consulted as needed.
Short Term Assessment Program Rev. 2 Appendix A including earlier revisions of ES-1.3 and associated safety screenings and safety reviews, condition reports, and the original FSAR, current UFSAR, and intermediate revisions of the UFSAR. AEP personnel were consulted as needed.
The team identified three contributors for additional investigation: 1) definition of "single active failure", 2) development of the procedure revision which directed the improper equipment alignment, and 3) reviews of the procedure revision that failed to identify the problem.
The team identified three contributors for additional investigation:
The team considered the definition of "single active failure" with respect to ambiguity and lack of consistency between internal documents, within the UFSAR, and in regulatory documents. While contributing factors may lie in these areas, the primary consideration impacting the situation under review was the fact that the ECCS alignment of concern did not appear to be a "single active failure" requiring review under the criteria of the plant's design basis (original FSAR). Failure to recognize the correct definition contributed to the failure to identify and correct the unacceptable ECCS lineup.
: 1) definition of "single active failure", 2) development of the procedure revision which directed the improper equipment alignment, and 3) reviews of the procedure revision that failed to identify the problem.
To establish the point at which the unacceptable lineup first appeared, earlier revisions of the ES-1.3 for both units and the UFSAR were examined. The unacceptable lineup was incorporated into these procedures during revision 2. This revision was intended to make the procedures consistent with the sequence of steps specified in the FSAR for switching to the recirculation mode of ECCS and CTS operation as well as to provide for more inventory transfer from the RWST to the recirculation sump. The preparer was not able to provide any additional information to provide an understanding of the apparent inconsistency between his intention to incorporate the procedure specified in the FSAR into ES-1.3 and the fact that the procedure and the FSAR do not match. Proper incorporation of the FSAR steps would have precluded the single failure vulnerability introduced by revision 2.
The team considered the definition of "single active failure" with respect to ambiguity and lack of consistency between internal documents, within the UFSAR, and in regulatory documents.
The root causes associated with CAL Item 4 are:
While contributing factors may lie in these
~   Lack of consideration  of Bernoulli effect on level instrumentation
: areas, the primary consideration impacting the situation under review was the fact that the ECCS alignment of concern did not appear to be a "single active failure" requiring review under the criteria of the plant's design basis (original FSAR).
~   Incorrect application of single failure criteria Ste   2-Consideration ofIm lications Lack ofconsideration     ofBernoulli effect on level instrumentation Failing to consider potential biases on instrumentation could potentially result in a system unable to 'perform its intended function. Short-term assessment actions were       'eing considered necessary to address this concern.
Failure to recognize the correct definition contributed to the failure to identify and correct the unacceptable ECCS lineup.
Incorrect application   ofsingle failure criteria Failing to properly apply single failure criteria could potentially result in a system being unable to perform its intended function. Short-term assessment actions were considered necessary to address this concern.
To establish the point at which the unacceptable lineup first appeared, earlier revisions of the ES-1.3 for both units and the UFSAR were examined.
The unacceptable lineup was incorporated into these procedures during revision 2. This revision was intended to make the procedures consistent with the sequence of steps specified in the FSAR for switching to the recirculation mode of ECCS and CTS operation as well as to provide for more inventory transfer from the RWST to the recirculation sump.
The preparer was not able to provide any additional information to provide an understanding of the apparent inconsistency between his intention to incorporate the procedure specified in the FSAR into ES-1.3 and the fact that the procedure and the FSAR do not match.
Proper incorporation of the FSAR steps would have precluded the single failure vulnerability introduced by revision 2.
The root causes associated with CALItem 4 are:
~
Lack ofconsideration ofBernoulli effect on level instrumentation
~
Incorrect application ofsingle failure criteria Ste 2-Consideration ofIm lications Lack ofconsideration ofBernoulli effect on level instrumentation Failing to consider potential biases on instrumentation could potentially result in a system
'eing unable to 'perform its intended function.
Short-term assessment actions were considered necessary to address this concern.
Incorrect application ofsingle failure criteria Failing to properly apply single failure criteria could potentially result in a system being unable to perform its intended function.
Short-term assessment actions were considered necessary to address this concern.
Page A-11
Page A-11


Short Term Assessment Program Rev. 2 Appendix A CAL Item 5: Compressed Air Overpressure Ste   1 Root Cause Determination The problem statement focused on why overpressure protection was not provided on the 20-, 50-, and 85-psig control air headers.
Short Term Assessment Program Rev. 2 Appendix A CALItem 5: Compressed AirOverpressure Ste 1 Root Cause Determination The problem statement focused on why overpressure protection was not provided on the 20-, 50-, and 85-psig control air headers.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
~   The compressed air systems at Cook Plant, including plant air and control air, are of the same design as compressed air systems installed in AEP fossil generating plants during the same time frame.
~
Bailey Controls Publication G18-2, "Product Instructions for Connecting Tubing and Accessories for Pneumatic Control and Transmission," provides six typical installations for either two or three low-pressure header connections. Safety valves are provided on pressure vessels but not on the downstream side of pressure regulators. These arrangements are typical of the Cook Nuclear Plant air systems.
The compressed air systems at Cook Plant, including plant air and control air, are of the same design as compressed air systems installed in AEP fossil generating plants during the same time frame.
~   Information Notice 87-28, "Air System Problems at U.S. Light Water Reactors,"
Bailey Controls Publication G18-2, "Product Instructions for Connecting Tubing and Accessories for Pneumatic Control and Transmission," provides six typical installations for either two or three low-pressure header connections.
focused on the assumption that safety related equipment would fail to a safe position on loss-of-air or perform its intended function with the assistance of safety related back-up supplies. Subsequently, Generic Letter 88-14, "Instrument Air Supply Problems Affecting Safety Related Equipment," identified that the performance of air-operated safety related components may not be in accordance with their intended safety function because of deficiencies in design, installation, and maintenance. The primary focus of the GL and AEP's response was to assure that safety related components function under loss-of-air. None of the examples dealt with overpressure events. Information Notice 88-24, "Failures of Air-Operated Valves Affecting Safety Related Systems," focused on 3-way solenoid valves not operating properly against the supplied air pressure.
Safety valves are provided on pressure vessels but not on the downstream side of pressure regulators.
~   In accordance with the original FSAR, the design code for the air system vessels is ASME Section VIII. Safety valves are provided as required by code. The remainder of the system is designed in accordance with ANSI B31.1, which does not require safety valves ifthe piping downstream of the regulators is designed to withstand the unregulated upstream pressure. This condition applies to the Cook Nuclear Plant design.
These arrangements are typical ofthe Cook Nuclear Plant air systems.
~   The reliability of air regulators at Cook Nuclear Plant has been excellent.
~
The team determined the root cause primarily through document review and personnel interviews. The facts led the team to conclude that the designers of the air system did not recognize that overpressure protection was necessary because this was a non-safety related system, the components had a successful history in AEP fossil applications, and the arrangement was typical of industrial applications where high reliability was important. The designers did not recognize all credible failure modes.
Information Notice 87-28, "AirSystem Problems at U.S. Light Water Reactors,"
The root cause associated with CAL Item 5 is:
focused on the assumption that safety related equipment would fail to a safe position on loss-of-air or perform its intended function with the assistance of safety related back-up supplies.
Subsequently, Generic Letter 88-14, "Instrument Air Supply Problems Affecting Safety Related Equipment," identified that the performance of air-operated safety related components may not be in accordance with their intended safety function because of deficiencies in design, installation, and maintenance.
The primary focus ofthe GL and AEP's response was to assure that safety related components function under loss-of-air. None of the examples dealt with overpressure events.
Information Notice 88-24, "Failures of Air-Operated Valves Affecting Safety Related Systems," focused on 3-way solenoid valves not operating properly against the supplied air pressure.
~
In accordance with the original FSAR, the design code for the air system vessels is ASME Section VIII. Safety valves are provided as required by code.
The remainder ofthe system is designed in accordance with ANSI B31.1, which does not require safety valves ifthe piping downstream ofthe regulators is designed to withstand the unregulated upstream pressure.
This condition applies to the Cook Nuclear Plant design.
~
The reliabilityofair regulators at Cook Nuclear Plant has been excellent.
The team determined the root cause primarily through document review and personnel interviews. The facts led the team to conclude that the designers ofthe air system did not recognize that overpressure protection was necessary because this was a non-safety related system, the components had a successful history in AEP fossil applications, and the arrangement was typical of industrial applications where high reliability was important. The designers did not recognize all credible failure modes.
The root cause associated with CALItem 5 is:
Page A-12
Page A-12


Short Term Assessment Program Rev. 2 Appendix A
Short Term Assessment Program Rev. 2 Appendix A
~   Failure to identify a non-safety system failure mode that could impact safety system components Ste   2-Consideration ofIm lications Failure to identify a non-safety system failure mode that could impact safety system components Failing to identify that a non-safety related system could potentially cause the failure of redundant safety related equipment has serious and far-reaching implications. Short-term assessment actions were considered necessary to address this concern.
~
CAI Item   6- RHR Suction Valve Interlock Ste   1 Root Cause Determination The problem statement focused on the fact that defeating the interlocks for the RHR suction isolation valves prior to venting the RCS to atmosphere places the plant in a condition outside its design basis.
Failure to identify a non-safety system failure mode that could impact safety system components Ste 2-Consideration ofIm lications Failure to identify a non-safety system failure mode that could impact safety system components Failing to identify that a non-safety related system could potentially cause the failure of redundant safety related equipment has serious and far-reaching implications. Short-term assessment actions were considered necessary to address this concern.
CAI Item 6-RHR Suction Valve Interlock Ste 1 Root Cause Determination The problem statement focused on the fact that defeating the interlocks for the RHR suction isolation valves prior to venting the RCS to atmosphere places the plant in a condition outside its design basis.
Pertinent facts brought forth during the investigation include:
Pertinent facts brought forth during the investigation include:
Information Notice 80-20, "Loss of Decay Heat Removal Capability at Davis-Besse Unit 1 while in a Refueling Mode," and IE Bulletin 80-12, "Decay Heat Removal System Operability," prompted AEP to implement procedure changes in June 1980. The changes involved removing power from the RHR suction isolation valves gMO-128 and ICM-129) after opening the valves, which typically occurs at an RCS pressure of about 400 psig.
Information Notice 80-20, "Loss of Decay Heat Removal Capability at Davis-Besse Unit 1 while in a Refueling Mode," and IE Bulletin 80-12, "Decay Heat Removal System Operability," prompted AEP to implement procedure changes in June 1980.
~   The procedure change was accomplished via a Procedure Temporary Change Sheet.
The changes involved removing power from the RHR suction isolation valves gMO-128 and ICM-129) after opening the
FSAR Section 9.3.2 states, "The suction line valves are interlocked through separate channels of the Reactor Coolant System pressure signals to provide auto>atic closure of both valves whenever the RCS pressure exceeds design pressure of the RHR system." The same section later states, "Overpressure protection in the RHR system is provided by relief valves discharging to the Pressurizer Relief Tank in the RCS coupled with interlocking of the RCS to RHR suction valves to close whenever RCS pressure exceeds design pressure of the RHR system."
: valves, which typically occurs at an RCS pressure ofabout 400 psig.
~   The AEP response to IE Bulletin 80-12 describes the RHR suction valves having power removed "ifthe RCS is vented to atmosphere," but it does not describe (or preclude) the practice of removing power for the entire time RHR is in service.
~
~   AEP:NRC:1033, response in November 1987 to Generic Letter 87-12, "Loss of Residual Heat Removal while the Reactor Coolant System is Partially Filled,"
The procedure change was accomplished via a Procedure Temporary Change Sheet.
discussed the RHR suction valve interlocks as described in the FSAR. The Page A-13
FSAR Section 9.3.2 states, "The suction line valves are interlocked through separate channels of the Reactor Coolant System pressure signals to provide auto>atic closure of both valves whenever the RCS pressure exceeds design pressure of the RHR system."
The same section later states, "Overpressure protection in the RHR system is provided by relief valves discharging to the Pressurizer Relief Tank in the RCS coupled with interlocking ofthe RCS to RHR suction valves to close whenever RCS pressure exceeds design pressure of the RHR system."
~
The AEP response to IE Bulletin 80-12 describes the RHR suction valves having power removed "ifthe RCS is vented to atmosphere," but it does not describe (or preclude) the practice ofremoving power for the entire time RHR is in service.
~
AEP:NRC:1033, response in November 1987 to Generic Letter 87-12, "Loss of Residual Heat Removal while the Reactor Coolant System is Partially Filled,"
discussed the RHR suction valve interlocks as described in the FSAR.
The Page A-13


Short Term Assessment Program Rev. 2 Appendix A response does not note that the isolation valves are opened and deenergized the entire time RHR is in service. The normal operating procedure was apparently not reviewed when developing this response.
Short Term Assessment Program Rev. 2 Appendix A response does not note that the isolation valves are opened and deenergized the entire time RHR is in service.
~   AEP:NRC:1033C, response in February 1989 to Generic Letter 88-17, "Loss of Decay Heat Removal Program Enhancements," correctly noted that control power is removed &om the RHR suction isolation valves whenever RHR is in service, as suggested by GL 87-12.
The normal operating procedure was apparently not reviewed when developing this response.
~   Low temperature overpressure protection (LTOP) relies on the RHR suction isolation valves being blocked open; however none       of the various LTOP reviews identified the conflict with the UFSAR.
~
AEP:NRC:1033C, response in February 1989 to Generic Letter 88-17, "Loss of Decay Heat Removal Program Enhancements,"
correctly noted that control power is removed &om the RHR suction isolation valves whenever RHR is in service, as suggested by GL 87-12.
~
Low temperature overpressure protection (LTOP) relies on the RHR suction isolation valves being blocked open; however none of the various LTOP reviews identified the conflict with the UFSAR.
The root cause team concluded that the original procedure change was made with good technical justification and attention to actual safety implication. However, the procedures and processes in place did not successfully lead the individuals involved to identify the discrepancy created with the UFSAR and technical specifications.
The root cause team concluded that the original procedure change was made with good technical justification and attention to actual safety implication. However, the procedures and processes in place did not successfully lead the individuals involved to identify the discrepancy created with the UFSAR and technical specifications.
Secondly, the change made to the plant in 1980 would be covered under the design change process using today's design control program and procedures.               The team concluded that a design change would have given the change more visibility and would be expected to find the UFSAR and technical specification discrepancies. The team also expressed concern that a number of formal reviews over the last 17 years provided opportunity for the inconsistency to be noted.
Secondly, the change made to the plant in 1980 would be covered under the design change process using today's design control program and procedures.
The root causes associated with CAL Item 6 are:
The team concluded that a design change would have given the change more visibilityand would be expected to find the UFSAR and technical specification discrepancies.
~   Processes   in place did not emphasize the UFSAR, resulting in an inadequate safety review
The team also expressed concern that a number of formal reviews over the last 17 years provided opportunity for the inconsistency to be noted.
~   Design change was accomplished via procedure revision Ste   2-ConsiderationofIm lications Processes in place (at the time) did not emphasize the     FSAR, resulting   in an inadequate safety review The implications of this cause are mitigated by the fact that engineering reviews were properly performed and the plant was actually configured and operated in the desired manner. Failure to recognize the inconsistency of the desired configuration with the FSAR led to being outside the design basis, but did not represent any threat to system functionality. No short-term assessment actions were considered necessary.
The root causes associated with CALItem 6 are:
Design change accomplished via procedure revision The implications of this cause are mitigated by the fact that engineering reviews weie properly performed and the plant was actually configured and operated in the desired manner. Failure to identify the FSAR inconsistency and failure to recognize that the technical specification surveillance was superfluous did not represent any threat to system function or operability. No short-term assessment actions were considered necessary.
~
Processes in place did not emphasize the UFSAR, resulting in an inadequate safety review
~
Design change was accomplished via procedure revision Ste 2-ConsiderationofIm lications Processes in place (at the time) did not emphasize the FSAR, resulting in an inadequate safety review The implications of this cause are mitigated by the fact that engineering reviews were properly performed and the plant was actually configured and operated in the desired manner.
Failure to recognize the inconsistency of the desired configuration with the FSAR led to being outside the design basis, but did not represent any threat to system functionality. No short-term assessment actions were considered necessary.
Design change accomplished viaprocedure revision The implications of this cause are mitigated by the fact that engineering reviews weie properly performed and the plant was actually configured and operated in the desired manner.
Failure to identify the FSAR inconsistency and failure to recognize that the technical specification surveillance was superfluous did not represent any threat to system function or operability.
No short-term assessment actions were considered necessary.
Page A-14
Page A-14


Short Term Assessment Program Rev. 2 Appendix A CAL Item 7: Fibrous Material in Containment Ste   1 Root Cause Determination In September 1997, fibrous material was found in an electrical cable tray in the Unit 2 containment. The purpose of the investigation was to determine why fibrous material was in containment.
Short Term Assessment Program Rev. 2 Appendix A CALItem 7: Fibrous Material in Containment Ste 1 Root Cause Determination In September 1997, fibrous material was found in an electrical cable tray in the Unit 2 containment.
The purpose of the investigation was to determine why fibrous material was in containment.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
~   Interview information: From original construction until late 1992, a contractor was used for all plant insulation installation and repair work. The contractor was under the control of AEP, but was relied upon to plan and execute insulation work with minimal direct supervision. The AEP thermal insulation specification (DCC-NEMP-450-QCS) was not often used or referenced during planning or installation. Instead, skill-of-the-craft and knowledge of the planners was used.
~
The design specification for fire barrier penetration seals and its implementing procedures allowed noncombustible damming material to remain in place following seal installation. Based on interview information, the authors of revisions to the design specification were unaware of the concern with fibrous material in containment.
Interview information:
A review of three design     change packages for installation of fire stops or fire breaks revealed that the safety reviews did not mention concerns on the use of fibrous material.
From original construction until late 1992, a contractor was used for all plant insulation installation and repair work. The contractor was under the control ofAEP, but was relied upon to plan and execute insulation work with minimal direct supervision.
~   Interview informa'tion: A January 1989 engineering memo allowed the use of stainless steel mesh to encapsulate blanket-type insulation on a temporary basis in of 0.010-inch stainless steel. The memo provided explicit instructions to     'ieu replace the temporary insulation with reflective metallic insulation (RMI) at the first convenient outage. The author intended the memo to be used on a one-time basis for a specific circumstance where pieces of RMI were missing or damaged at the completion of the Unit 2 steam generator replacement. However, plant personnel continued to use that memo as justification to use mesh-encapsulated blanket insulation when necessary to meet ALARAand production concerns. A process to remove such "temporary" installations was not implemented, and the thermal insulation specification was not revised to incorporate the practice.
The AEP thermal insulation specification (DCC-NEMP-450-QCS) was not often used or referenced during planning or installation. Instead, skill-of-the-craft and knowledge ofthe planners was used.
Information Notices 88-28, 90-07, 93-34, 95-06, and 96-59, IE Bulletin 93-02, and Generic Letter 85-22, all dealing with the potential for loss of post-LOCA recirculation capability due to debris blockage, were evaluated by AEP. The reviews focused on specified insulation materials and did not consider actual plant conditions.
The design specification for fire barrier penetration seals and its implementing procedures allowed noncombustible damming material to remain in place following seal installation.
Based on interview information, the authors of revisions to the design specification were unaware of the concern with fibrous material in containment.
A review of three design change packages for installation of fire stops or fire breaks revealed that the safety reviews did not mention concerns on the use of fibrous material.
~
Interview informa'tion: A January 1989 engineering memo allowed the use of stainless steel mesh to encapsulate blanket-type insulation on a temporary basis in
'ieu of 0.010-inch stainless steel.
The memo provided explicit instructions to replace the temporary insulation with reflective metallic insulation (RMI) at the first convenient outage.
The author intended the memo to be used on a one-time basis for a specific circumstance where pieces of RMI were missing or damaged at the completion of the Unit 2 steam generator replacement.
However, plant personnel continued to use that memo as justification to use mesh-encapsulated blanket insulation when necessary to meet ALARAand production concerns.
A process to remove such "temporary" installations was not implemented, and the thermal insulation specification was not revised to incorporate the practice.
Information Notices 88-28, 90-07, 93-34, 95-06, and 96-59, IE Bulletin 93-02, and Generic Letter 85-22, all dealing with the potential for loss of post-LOCA recirculation capability due to debris blockage, were evaluated by AEP.
The reviews focused on specified insulation materials and did not consider actual plant conditions.
Page A-15
Page A-15


Short Term Assessment Program Rev. 2 Appendix A The team used a combination of event charting, cause-and-effect             analysis, barrier analysis, interviews, document reviews, and mini-MORT.
Short Term Assessment Program Rev. 2 Appendix A The team used a combination of event
: charting, cause-and-effect
: analysis, barrier analysis, interviews, document reviews, and mini-MORT.
The reason fibrous material was introduced to containment was determined to be a lack of procedures implementing the requirements of the thermal insulation specification
The reason fibrous material was introduced to containment was determined to be a lack of procedures implementing the requirements of the thermal insulation specification
, during planning and implementation, coupled with a failure to address the sump plugging potential of fibrous material in the specification itself. Incomplete evaluation of NRC Information Notices and IE Bulletins resulted in a series of missed opportunities to identify and encapsulate or remove fibrous material.
, during planning and implementation, coupled with a failure to address the sump plugging potential of fibrous material in the specification itself.
The root causes associated with CAL Item 7 are:
Incomplete evaluation of NRC Information Notices and IE Bulletins resulted in a series of missed opportunities to identify and encapsulate or remove fibrous material.
Lack of procedures for implementing the requirements       of the thermal insulation specification
The root causes associated with CALItem 7 are:
  ~   Failure to address sump-plugging potential   of fibrous insulation material installed in containment Ste   2- Consideration   of Im lications Lack ofprocedures   for implementing an insulation specification Failure to have a detailed procedure was considered to be a symptom of the more fundamental concern of failing to recognize and preserve multiple functional design requirements of some installed plant features.         Short-term assessment actions were considered necessary to address this concern.
Lack of procedures for implementing the requirements of the thermal insulation specification
Failure to address sump-plugging potential       offibrous insulation material installed in containment Failing to recognize multiple functional design requirements of SSCs could result in systems being unable to perform their intended function. Short-term assessment actions were considered necessary to address this concern.
~
CAL Item S: Leak Back to RWST during Recirculation Ste   1 Root Cause Determination The problem was stated as:     Only two of six mini-flow recirculation line valves have leakage verification tests.
Failure to address sump-plugging potential of fibrous insulation material installed in containment Ste 2-Consideration ofIm lications Lack ofprocedures forimplementing an insulation specification Failure to have a detailed procedure was considered to be a symptom of the more fundamental concern of failing to recognize and preserve multiple functional design requirements of some installed plant features.
Short-term assessment actions were considered necessary to address this concern.
Failure to address sump-plugging potential offibrous insulation material installed in containment Failing to recognize multiple functional design requirements of SSCs could result in systems being unable to perform their intended function.
Short-term assessment actions were considered necessary to address this concern.
CALItem S: Leak Back to RWST during Recirculation Ste 1 Root Cause Determination The problem was stated as:
Only two of six mini-flow recirculation line valves have leakage verification tests.
Pertinent facts brought forth in this investigation include:
Pertinent facts brought forth in this investigation include:
  ~   Information Notice 91-56, "Potential Radioactive Leakage to Tank Vented to Atmosphere,", was issued to alert the industry of a potential problem resulting from leakage of ECCS recirculation isolation valves to safety injection water storage tanks (RWST at Cook Plant).
~
Information Notice 91-56, "Potential Radioactive Leakage to Tank Vented to Atmosphere,", was issued to alert the industry of a potential problem resulting from leakage of ECCS recirculation isolation valves to safety injection water storage tanks (RWST at Cook Plant).
Page A-16
Page A-16


Short Term Assessment Program Rev. 2 Appendix   A
Short Term Assessment Program Rev. 2 Appendix A
~   IN 91-56 was assigned to Nuclear Safety and Licensing in AEP's corporate headquarters. The document trail for IN 91-56 is incomplete, although the team's report includes a chronology of events occurring in NSEcL and at the plant.
~
The team 'concluded that this was a valid issue. Additional valve testing should have been accomplished, or in its absence, sound engineering basis should have been documented to justify actions or non-actions resulting from review of IN 91-56. It was evident that the reviewer did recognize that the IN impacted Cook Plant. Calculations were performed to determine dose received from a postulated leak path back to the RWST. In addition, a change was made to the UFSAR, a test procedure was developed, some valves were tested, and ASME valve categories were revised. The decisions and actions were not well documented; however, evidence clearly demonstrates that the IN, was evaluated and acted upon.
IN 91-56 was assigned to Nuclear Safety and Licensing in AEP's corporate headquarters.
The relevant root cause associated with CAL Item 8 is:
The document trail for IN 91-56 is incomplete, although the team's report includes a chronology ofevents occurring in NSEcL and at the plant.
~ Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Ste   2- Consideration   of Im lications Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Failing to ensure that analysis assumptions are met could potentially result in a system being unable to perform its intended function. Short-term assessment actions were considered necessary to address this concern.
The team 'concluded that this was a valid issue.
Additional valve testing should have been accomplished, or in its absence, sound engineering basis should have been documented to justify actions or non-actions resulting from review ofIN 91-56. It was evident that the reviewer did recognize that the IN impacted Cook Plant.
Calculations were performed to determine dose received from a postulated leak path back to the RWST. In addition, a change was made to the UFSAR, a test procedure was developed, some valves were tested, and ASME valve categories were revised.
The decisions and actions were not well documented; however, evidence clearly demonstrates that the IN, was evaluated and acted upon.
The relevant root cause associated with CALItem 8 is:
~
Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Ste 2-Consideration ofIm lications Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Failing to ensure that analysis assumptions are met could potentially result in a system being unable to perform its intended function.
Short-term assessment actions were considered necessary to address this concern.
Lake Temperature Design Basis Discrepancies (CR-97-2196) and Lake Temperature Effect on Control Room Ventilation (CR-97-2390)
Lake Temperature Design Basis Discrepancies (CR-97-2196) and Lake Temperature Effect on Control Room Ventilation (CR-97-2390)
Ste   1- Root Cause   Determination The problem is defined as allowing the use of a higher, and thus less conservative, maximum lake water temperature value than listed in UFSAR Table 9.5-3.
Ste 1-Root Cause Determination The problem is defined as allowing the use of a higher, and thus less conservative, maximum lake water temperature value than listed in UFSAR Table 9.5-3.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
~   The weather in 1988 was unprecedented, with both extremely high temperatures and drought. Actual lake temperature data identified a high lake temperature of 83.9'F on August 17, 1988.
~
~   Although the effects of higher lake temperature on important plant parameters were evaluated, a comprehensive 10 CFR 50.59 review was not completed to support operation at the higher lake temperature.       All potentially relevant calculations were not reviewed to determine the impact of lake temperature higher Page A-17
The weather in 1988 was unprecedented, with both extremely high temperatures and drought.
Actual lake temperature data identified a high lake temperature of 83.9'F on August 17, 1988.
~
Although the effects of higher lake temperature on important plant parameters were evaluated, a comprehensive 10 CFR 50.59 review was not completed to support operation at the higher lake temperature.
All potentially relevant calculations were not reviewed to determine the impact oflake temperature higher Page A-17


Short Term Assessment Program Rev. 2 Appendix   A than the UFSAR value of    76'. The review did not identify that the UFSAR and other related documents needed to be changed. '
Short Term Assessment Program Rev. 2 Appendix A than the UFSAR value of76'. The review did not identify that the UFSAR and other related documents needed to be changed.
The lake temperature value of 76'F is listed in a UFSAR Chapter 9 component data table falls within 10 CFR 50.2 and the recently issued DIR-2300-04 definition of "design bases."
The lake temperature value of 76'F is listed in a UFSAR Chapter 9 component data table falls within 10 CFR 50.2 and the recently issued DIR-2300-04 definition of"design bases."
~ Memorandum "Operation at Elevated Essential Service Water Temperature" from D. B. Black dated July 29, 1988 established criteria for evaluating increased ESW temperatures. The stated criteria was, "Operation of Cook Nuclear Plant with ESW temperatures greater than 76'F is not necessarily precluded (that is, operating is an unanalyzed condition) as long as:
~
a margin exists between the peak pressure and the design pressure, and; the sensitivity of the change in calculated peak pressure due to changes in ESW temperature are known."
Memorandum "Operation at Elevated Essential Service Water Temperature" from D. B. Black dated July 29, 1988 established criteria for evaluating increased ESW temperatures.
~   While analysis has shown that higher temperatures are acceptable for containment heat removal, no single analysis identified and resolved all effects of the change in design basis lake temperature. Design inputs were not "correctly translated into
The stated criteria was, "Operation of Cook Nuclear Plant with ESW temperatures greater than 76'F is not necessarily precluded (that is, operating is an unanalyzed condition) as long as:
[all affectedJ specifications, drawings, procedures, or instructions", as required by 10 CFR Appendix B and ANSI N45.2.11.
a margin exists between the peak pressure and the design pressure, and; the sensitivity ofthe change in calculated peak pressure due to changes in ESW temperature are known."
~   In 1988 when the lake temperature was above (or projected to be above)       76',   a reevaluation of control room HVAC for higher ESW temperature was performed.
~
The result was that the then-current technical specification control room temperature limit of 120'       would not be exceeded at or below 87.5'F lake temperature. Operability of the control room HVAC and decay heat removal was evaluated at the time, but a comprehensive 10 CFR 50.59 review was not found to acknowledge the use of non-conservative higher temperatures or that it was a deviation from the UFSAR. Not all affected ESW heat loads were specifically addressed.
While analysis has shown that higher temperatures are acceptable for containment heat removal, no single analysis identified and resolved all effects ofthe change in design basis lake temperature.
~   A July 29,1988 memorandum from D. B. Black to B. A. Svensson           states a prior maximum lake temperature of 79.5'           was identified. Based upon interview information, no engineering reevaluations were performed for the earlier high lake temperature condition of 79.5' mentioned in the memo.
Design inputs were not "correctly translated into
The root cause investigation was performed by documenting the time-line of related events using an events and causal factors chart. Identifying, collecting, and reviewing documents associated with the events supported the events and causal factors chart.
[all affectedJ specifications, drawings, procedures, or instructions", as required by 10 CFR Appendix B and ANSIN45.2.11.
Interviews of involved personnel were then conducted.
~
The root cause of the events is a failure to recognize that deviation from the UFSAR value of 76' for ESW temperature constituted a deviation from a design basis value.
In 1988 when the lake temperature was above (or projected to be above) 76', a reevaluation ofcontrol room HVACfor higher ESW temperature was performed.
The result was that the then-current technical specification control room temperature limit of 120' would not be exceeded at or below 87.5'F lake temperature.
Operability ofthe control room HVAC and decay heat removal was evaluated at the time, but a comprehensive 10 CFR 50.59 review was not found to acknowledge the use of non-conservative higher temperatures or that it was a deviation from the UFSAR. Not all affected ESW heat loads were specifically addressed.
~
A July 29,1988 memorandum from D. B. Black to B. A. Svensson states a prior maximum lake temperature of 79.5' was identified. Based upon interview information, no engineering reevaluations were performed for the earlier high lake temperature condition of79.5' mentioned in the memo.
The root cause investigation was performed by documenting the time-line of related events using an events and causal factors chart.
Identifying, collecting, and reviewing documents associated with the events supported the events and causal factors chart.
Interviews ofinvolved personnel were then conducted.
The root cause of the events is a failure to recognize that deviation from the UFSAR value of76' for ESW temperature constituted a deviation from a design basis value.
Contributing causes include 1) rising standards for UFSAR compliance and design basis definitions were not implemented within the organization and 2) design change Page A-18
Contributing causes include 1) rising standards for UFSAR compliance and design basis definitions were not implemented within the organization and 2) design change Page A-18


Short Term Assessment Program Rev. 2 Appendix   A procedures in place at the time of these events did not require or compel considering a change to design basis value as a design change.
Short Term Assessment Program Rev. 2 Appendix A procedures in place at the time of these events did not require or compel considering a change to design basis value as a design change.
The root causes   of the lake temperature issue are:
The root causes ofthe lake temperature issue are:
~
~
  ~ Failure to recognize a UFSAR value as a design basis parameter
~
  ~ Failure to recognize interrelationships between a UFSAR value and other design aspects Ste   2- Consideration   of Im lications Failure to recognize a UFSAR value as a design basis parameter This cause is associated with the confusion surrounding justification for plant operation when the lake is above     76'. It is clear that AEP nuclear generation pexsonnel did not consider all UFSAR values design basis parameters.           This cause is at the heart of concerns raised by the design inspection team.           However, no instances (including investigation of a substantial number of condition reports arising from the UFSAR revalidation efforts, both before and after the design inspection) were noted where failure to recognize UFSAR values as design basis values led to failure to perform technical reviews when warranted. Failure to recognize UFSAR values as design basis parameters may lead to being outside the plant design basis by definition, but has not been identified as posing a threat to system functionality. No additional short-term assessment actions were considered necessary. The longer-term pxogram arising from the design inspection willaddress this basic concern.
Failure to recognize a UFSAR value as a design basis parameter
Failure to recognize interrelationships behveen a UFSAR value and other design aspects This cause is also associated with plant operation when the lake is above       76',     but centers on deficiencies in the evaluation of control room instrumentation. The potential impact of higher control room temperatures on instrumentation life was recognized by AEP and was evaluated. At the time of the evaluation, the technical specification limit for control room temperature was 120' temperature. Per the basis of the technical specifications, this limit was consistent with the continuous duty rating of control room equipment. Subsequent to these reviews (c. 1992), it,was determined that not all equipment   was qualified for continuous duty to 120'       and the technical specification limit for normal operation was lowered to       95'. While it is clear that AEP nuclear generation personnel did not consider all UFSAR values to be design basis parameters, no instances have been noted where this failure led to failure to perform technical reviews when warranted. No additional short-term assessment actions were considered necessary.
~
Failure to recognize interrelationships between a UFSAR value and other design aspects Ste 2-Consideration ofIm lications Failure to recognize a UFSAR value as a design basis parameter This cause is associated with the confusion surrounding justification for plant operation when the lake is above 76'.
It is clear that AEP nuclear generation pexsonnel did not consider all UFSAR values design basis parameters.
This cause is at the heart of concerns raised by the design inspection team.
: However, no instances (including investigation of a substantial number of condition reports arising from the UFSAR revalidation efforts, both before and after the design inspection) were noted where failure to recognize UFSAR values as design basis values led to failure to perform technical reviews when warranted.
Failure to recognize UFSAR values as design basis parameters may lead to being outside the plant design basis by definition, but has not been identified as posing a threat to system functionality. No additional short-term assessment actions were considered necessary.
The longer-term pxogram arising from the design inspection willaddress this basic concern.
Failure to recognize interrelationships behveen a UFSAR value and other design aspects This cause is also associated with plant operation when the lake is above 76', but centers on deficiencies in the evaluation of control room instrumentation.
The potential impact of higher control room temperatures on instrumentation life was recognized by AEP and was evaluated.
At the time of the evaluation, the technical specification limit for control room temperature was 120' temperature.
Per the basis of the technical specifications, this limitwas consistent with the continuous duty rating of control room equipment.
Subsequent to these reviews (c.
1992), it,was determined that not all equipment was qualified for continuous duty to 120' and the technical specification limit for normal operation was lowered to 95'.
While it is clear that AEP nuclear generation personnel did not consider all UFSAR values to be design basis parameters, no instances have been noted where this failure led to failure to perform technical reviews when warranted.
No additional short-term assessment actions were considered necessary.
Page A-19
Page A-19


Short Term Assessment Program Rev. 2 Appendix A Unit 2 Full Core Off-load with Concurrent CCW Dual Train Outage (CR-97-2341)
Short Term Assessment Program Rev. 2 Appendix A Unit 2 Full Core Off-load with Concurrent CCW Dual Train Outage (CR-97-2341)
Ste   1-Root   Cause Determination The problem was defined as: The dual train CCW outage which had occurred during the 1996 Unit 2 refueling outage did not have a sufficient 10 CFR 50.59 safety evaluation to support it.
Ste 1-Root Cause Determination The problem was defined as: The dual train CCW outage which had occurred during the 1996 Unit 2 refueling outage did not have a sufficient 10 CFR 50.59 safety evaluation to support it.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
~   The purpose of the safety evaluation for this evolution was to evaluate whether or not the configuration represented by a full-core offload for U2R96 represented an unreviewed safety question. The safety evaluation assumed the unavailability of one train of spent fuel pool cooling to evaluate the adequacy of heat removal in the full core offload condition.
~
~   The SER for the spent fuel pool re-rack states that it is not necessary to assume less than two trains of spent fuel pool cooling are available.
The purpose ofthe safety evaluation for this evolution was to evaluate whether or not the configuration represented by a full-core offload for U2R96 represented an unreviewed safety question.
~   The safety evaluation was supported by calculation N96-01-01 which demonstrated that with a full core offload and only one train of SFP cooling in operation, the spent fuel pool temperature would be maintained less than 150'.
The safety evaluation assumed the unavailability of one train of spent fuel pool cooling to evaluate the adequacy of heat removal in the fullcore offload condition.
~
The SER for the spent fuel pool re-rack states that it is not necessary to assume less than two trains ofspent fuel pool cooling are available.
~
The safety evaluation was supported by calculation N96-01-01 which demonstrated that with a full core offload and only one train of SFP cooling in operation, the spent fuel pool temperature would be maintained less than 150'.
This is within the UFSAR design basis temperature of 159.54'.
This is within the UFSAR design basis temperature of 159.54'.
~   UFSAR Section 9.4.1 states, "Any spent fuel pool loading scenario which meets the 160'       peak bulk pool temperature and 5.74 hours to boil criteria is acceptable."
~
~   Based on heat load and the supporting calculation, the spent fuel pool was clearly within the thermal hydraulic design basis with 'this configuration, since it met a peak bulk pool temperature of less than 160'       and a minimum boiling time of much longer than 5.74 hours.
UFSAR Section 9.4.1 states, "Any spent fuel pool loading scenario which meets the 160' peak bulk pool temperature and 5.74 hours to boil criteria is acceptable."
~   The shutdown risk assessment dated March 22, 1997 did not completely document how the licensing issues for a dual train CCW outage were addressed.
~
Based on heat load and the supporting calculation, the spent fuel pool was clearly within the thermal hydraulic design basis with 'this configuration, since it met a peak bulk pool temperature of less than 160' and a minimum boiling time of much longer than 5.74 hours.
~
The shutdown risk assessment dated March 22, 1997 did not completely document how the licensing issues for a dual train CCW outage were addressed.
In particular, it did not address a postulate LOCA on Unit 1 while the Unit 2 dual-train CCW outage was in progress.
In particular, it did not address a postulate LOCA on Unit 1 while the Unit 2 dual-train CCW outage was in progress.
~   The shutdown risk assessment did reference abnormal operating procedures designed to provide SFP cooling in the event that CCW cooling was lost.
~
The investigation concluded that the safety reviewer performed an adequate review of the full core offload. During the outage, no condition outside the design basis or licensing basis was incurred. A risk assessment was performed during the planning of the schedule. Documentation of the licensing issues involving spent fuel pool cooling with a dual train CCW outage in Unit 2 and a postulated LOCA in Unit 1 was not complete.
The shutdown risk assessment did reference abnormal operating procedures designed to provide SFP cooling in the event that CCW cooling was lost.
The investigation concluded that the safety reviewer performed an adequate review ofthe full core offload. During the outage, no condition outside the design basis or licensing basis was incurred.
A risk assessment was performed during the planning of the schedule.
Documentation ofthe licensing issues involving spent fuel pool cooling with a dual train CCW outage in Unit 2 and a postulated LOCA in Unit 1 was not complete.
However, as evidenced by the contingency planning to ensure adequate cooling in the event CCW cooling was lost, the design basis and licensing basis issues were addressed.
However, as evidenced by the contingency planning to ensure adequate cooling in the event CCW cooling was lost, the design basis and licensing basis issues were addressed.
The root cause of the failure to fully document the licensing issues during the planning for this evolution was personnel error. The issues were addressed. Previously, a Shift Page A-20
The root cause of the failure to fully document the licensing issues during the planning for this evolution was personnel error.
The issues were addressed.
Previously, a Shift Page A-20


Short Term Assessment Program Rev. 2 Appendix   A Technical Advisor performed the risk assessment. The procedure now requires a group including, an operations shift supervisor, a scheduling person, a Shift Technical Advisor, and an engineer from the Safety Analysis group.
Short Term Assessment Program Rev. 2 Appendix A Technical Advisor performed the risk assessment.
Since the safety evaluation and USQD are considered adequate,             no root cause was developed. The implication that should be addressed, however, is:
The procedure now requires a group including, an operations shift supervisor, a scheduling person, a Shift Technical Advisor, and an engineer from the Safety Analysis group.
~   10 CFR 50.59 reviews may be inadequate Ste   2 Consideration   of Im lications 10 CFR 50.59 reviews may be inadequate The root cause investigation as described above represents the basis for our retraction of the LER associated with this issue and for originally concluding that no short term assessment actions were necessary to address potential 10 CFR 50.59 inadequacies.
Since the safety evaluation and USQD are considered
Following discussions with NRR and Region III staff on December 22, 1997, we now understand that the change represents an unreviewed safety question due to reduction in margin, and have agreed to conduct a self-assessment of safety screenings and evaluations in the short term. This review will look for unreviewed safety questions and operability concerns.
: adequate, no root cause was developed.
Note that this additional review is not reflected in Tables 1, 2, and 3.
The implication that should be addressed, however, is:
Restriction of CCW Temperature During Unit 2 Core Off-load (CR-97-2342)
~
Ste   1 Root Cause Determination The problem was defined as: Inadequate safety evaluation performed for establishment of a 90 degree F upper limitfor CCW during the Unit 2 1996 refueling outage.
10 CFR 50.59 reviews may be inadequate Ste 2 Consideration ofIm lications 10 CFR 50.59 reviews may be inadequate The root cause investigation as described above represents the basis for our retraction of the LER associated with this issue and for originally concluding that no short term assessment actions were necessary to address potential 10 CFR 50.59 inadequacies.
Following discussions with NRR and Region III staff on December 22, 1997, we now understand that the change represents an unreviewed safety question due to reduction in
: margin, and have agreed to conduct a
self-assessment of safety screenings and evaluations in the short term. This review willlook for unreviewed safety questions and operability concerns.
Note that this additional review is not reflected in Tables 1, 2, and 3.
Restriction ofCCW Temperature During Unit 2 Core Off-load (CR-97-2342)
Ste 1 Root Cause Determination The problem was defined as:
Inadequate safety evaluation performed for establishment ofa 90 degree F upper limitfor CCW during the Unit2 1996 refueling outage.
Pertinent facts brought forth in the investigation. include:
Pertinent facts brought forth in the investigation. include:
A   10 CFR 50.59 safety evaluation addressing the U2R96 proposed full core offload was issued on March 11, 1996. An addendum was issued on March 20, 1996. The safety evaluation discussed the Spent Fuel Pool Cooling System heat load analysis, assuming: 1) the existing fuel assembly inventory, 2) a full core offload, 3) a bounding lake temperature for the March/April time frame, 4) a maximum CCW temperature of 80.5', and 5) a single train of Spent Fuel Pool Cooling. Addendum 1 revised the CCW temperature to 90.7'.
A 10 CFR 50.59 safety evaluation addressing the U2R96 proposed full core offload was issued on March 11, 1996. An addendum was issued on March 20, 1996.
~   Although the analysis demonstrated that the Spent Fuel Pool temperature remained below the limit of         160',       an Unreviewed Safety Question Determination was performed since the CCW temperature and system cooling capacity was different than that found in the UFSAR (Table 9.4-2). It concluded that although the assumed CCW temperature was less than the UFSAR value, the CCW temperature and the SFPCS heat removal values are nominal design values Page A-21
The safety evaluation discussed the Spent Fuel Pool Cooling System heat load analysis, assuming:
: 1) the existing fuel assembly inventory, 2) a full core offload, 3) a bounding lake temperature for the March/April time frame, 4) a maximum CCW temperature of80.5', and 5) a single train of Spent Fuel Pool Cooling. Addendum 1 revised the CCW temperature to 90.7'.
~
Although the analysis demonstrated that the Spent Fuel Pool temperature remained below the limit of 160',
an Unreviewed Safety Question Determination was performed since the CCW temperature and system cooling capacity was different than that found in the UFSAR (Table 9.4-2). It concluded that although the assumed CCW temperature was less than the UFSAR value, the CCW temperature and the SFPCS heat removal values are nominal design values Page A-21


Short Term Assessment Program Rev. 2 Appendix A and modification   of these values on an outage basis does not require a change to the FSAR;
Short Term Assessment Program Rev. 2 Appendix A and modification of these values on an outage basis does not require a change to the FSAR;
~   The Condition Report was written because the safety evaluation did not recognize the CCW temperature change as a design change, to the SFPCS heat exchanger CCW inlet temperature. This value is listed in Table 9.4-2 of the UFSAR as 90'.
~
95',
The Condition Report was written because the safety evaluation did not recognize the CCW temperature change as a design change, to the SFPCS heat exchanger CCW inlet temperature.
and was to be administratively limited to The purpose of the safety evaluation was to assess the acceptability of the SFP heat loads for the Unit 2 refueling outage, based on the analysis and conditions that existed at the time. The CCW temperatures were obtained based on projected SFP heat loads, a bounding lake temperature for March/April and a single train of SFP cooling, and the approved limiting design basis temperature of 160'.
This value is listed in Table 9.4-2 of the UFSAR as 95',
The investigation concluded that limiting the CCW temperature to 90' maintained the SFP below the maximum design basis temperature of 160';. therefore the probability or consequences of a release from the SFP was not increased. Since this was a temporary procedure change based on the specific SFP heat removal requirements for the Unit 2 refueling outage, it was not considered a design change and did not require a permanent change to the UFSAR. The USQD performed to address the change adequately covered the temporary change in CCW temperature. Therefore, it is concluded that the plant was not outside of its design basis.
and was to be administratively limited to 90'.
Since the safety evaluation and USQD are considered adequate,           no root cause was developed. The implication that should be addressed, however, is:
The purpose of the safety evaluation was to assess the acceptability of the SFP heat loads for the Unit 2 refueling outage, based on the analysis and conditions that existed at the time. The CCW temperatures were obtained based on projected SFP heat loads, a bounding lake temperature for March/April and a single train of SFP cooling, and the approved limitingdesign basis temperature of160'.
~   The adequacy of the 10 CFR 50.59 review was questioned, although subsequently found to be acceptable Ste   2- Consideration   of Im lications 10 CFR 50.59 reviews may be inadequate The root cause investigation as described above represents the basis for our retraction of the LER associated with this issue and for originally concluding that no short term assessment actions were necessary to address potential 10 CFR 50;59 inadequacies.
The investigation concluded that limiting the CCW temperature to 90' maintained the SFP below the maximum design basis temperature of 160';. therefore the probability or consequences of a release from the SFP was not increased.
Following discussions with NRR and Region III staff on December 22, 1997, we now understand that the change may represent an unreviewed safety question due to reduction in margin, and have agreed to conduct a self-assessment of safety screenings and evaluations in the short term. This review will look for unreviewed safety questions and operability concerns.
Since this was a temporary procedure change based on the specific SFP heat removal requirements for the Unit 2 refueling outage, it was not considered a design change and did not require a permanent change to the UFSAR. The USQD performed to address the change adequately covered the temporary change in CCW temperature.
Therefore, it is concluded that the plant was not outside ofits design basis.
Since the safety evaluation and USQD are considered
: adequate, no root cause was developed. The implication that should be addressed, however, is:
~
The adequacy ofthe 10 CFR 50.59 review was questioned, although subsequently found to be acceptable Ste 2-Consideration ofIm lications 10 CFR 50.59 reviews may be inadequate The root cause investigation as described above represents the basis for our retraction of the LER associated with this issue and for originally concluding that no short term assessment actions were necessary to address potential 10 CFR 50;59 inadequacies.
Following discussions with NRR and Region IIIstaff on December 22, 1997, we now understand that the change may represent an unreviewed safety question due to reduction in margin, and have agreed to conduct a self-assessment of safety screenings and evaluations in the short term. This review willlook for unreviewed safety questions and operability concerns.
Note that this additional review is not reflected in Tables 1, 2, and 3.
Note that this additional review is not reflected in Tables 1, 2, and 3.
Page A-22
Page A-22


Short Term Assessment Program Rev. 2 Appendix A RWST minimum volume for Appendix R (CR-97-2358)
Short Term Assessment Program Rev. 2 Appendix A RWST minimum volume for Appendix R (CR-97-2358)
Ste   1 Root Cause Determination The problem was identified as: Calculation TH 90-02 determined that the minimum RWST level required to support the other unit's shutdown for Appendix R considerations to be 87,000 gallons. Operating procedure OHP 4021.018.008 requires the RWST level to be above 10%, which is less than 87,000 gallons.
Ste 1 Root Cause Determination The problem was identified as:
Calculation TH 90-02 determined that the minimum RWST level required to support the other unit's shutdown for Appendix R considerations to be 87,000 gallons.
Operating procedure OHP 4021.018.008 requires the RWST level to be above 10%, which is less than 87,000 gallons.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
Calculation TH 90-02 states, "The 87,000 gallons required is less than both the 90,000 gallons specified in technical specification 3.1.2.7 for Modes 5 and 6 and the 350,000 gallons specified in technical specification 3.5.5 for Modes 1, 2, 3, and 4 (both units)."
Calculation TH 90-02 states, "The 87,000 gallons required is less than both the 90,000 gallons specified in technical specification 3.1.2.7 for Modes 5 and 6 and the 350,000 gallons specified in technical specification 3.5.5 for Modes 1, 2, 3, and 4 (both units)."
~   Technical specification 3.1.2.7 allows the RWST level to fall below 90,000 gallons ifboric acid storage system requirements of 3.1.2.7.a are met. Therefore, it cannot be relied upon to meet the requirements of calculation TH 90-02.
~
Technical specification 3.1.2.7 allows the RWST level to fall below 90,000 gallons ifboric acid storage system requirements of 3.1.2.7.a are met. Therefore, it cannot be relied upon to meet the requirements ofcalculation TH 90-02.
Calculation TH 90-02 relied on an incorrect interpretation of the technical specifications that in all modes, the RWST water level would be above the calculated required water level.. It is surmised that TH 90-02 therefore was not distributed or used to revise procedures to maintain the calculated water level.
Calculation TH 90-02 relied on an incorrect interpretation of the technical specifications that in all modes, the RWST water level would be above the calculated required water level.. It is surmised that TH 90-02 therefore was not distributed or used to revise procedures to maintain the calculated water level.
The root cause   of this issue is:
The root cause ofthis issue is:
Misinterpretation of technical   specifications resulted in failure to translate calculation assumptions and results into operating procedures.
Misinterpretation of technical specifications resulted in failure to translate calculation assumptions and results into operating procedures.
Ste   2-Consideration ofIm lications Misinterpretation of technical specification resulted in failure to translate calculation assumptions and results into operating procedures This case represents an instance where an individual performed a calculation to determine an operating requirement, found an existing technical specification value that he believed encompassed the new requirement, and stopped. However, his understanding of the technical specification was incomplete and, in fact, the operating requirement was not necessarily covered under all scenarios.           Subsequent investigation revealed that compliance had always been maintained, albeit accidentally.             Although human performance is the root cause, discussion of the implications of this occurrence resulted in considering it a calculation issue. Short-term assessment actions were considered necessary to address this concern.
Ste 2-Consideration ofIm lications Misinterpretation oftechnical specification resulted in failure to translate calculation assumptions and results into operating procedures This case represents an instance where an individual performed a calculation to determine an operating requirement, found an existing technical specification value that he believed encompassed the new requirement, and stopped.
However, his understanding of the technical specification was incomplete and, in fact, the operating requirement was not necessarily covered under all scenarios.
Subsequent investigation revealed that compliance had always been maintained, albeit accidentally.
Although human performance is the root cause, discussion of the implications of this occurrence resulted in considering it a calculation issue.
Short-term assessment actions were considered necessary to address this concern.
Page A-23
Page A-23


Short Term Assessment Program Rev. 2 Appendix A 2-CD Battery Cell Left on Charge for an Extended Period (CR-97-1821)
Short Term Assessment Program Rev. 2 Appendix A 2-CD Battery Cell Left on Charge for an Extended Period (CR-97-1821)
Ste   1 Root Cause Determination The problem was defined as: 2-CD battery cell left on charge for an extended period.
Ste 1 Root Cause Determination The problem was defined as: 2-CD battery cell left on charge for an extended period.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
Cell 34 was placed on individual cell charge (ICC) aAer it was discovered on 3une 19 1997 that the cell was below the technical specification minimum voltage of 2.13VDC. The cell was left on charge until August 8, 1997 when it was decided to replace the cell.
Cell 34 was placed on individual cell charge (ICC) aAer it was discovered on 3une 19 1997 that the cell was below the technical specification minimum voltage of 2.13VDC. The cell was left on charge until August 8, 1997 when it was decided to replace the cell.
~   C&D Vendor Technical Manual, Section VI states, "Minimum acceptable voltage is the point at which plans should be made to provide equalize charge. It does not if imply that the battery is malfunctioning or that it will not provide power called upon. Some equipment may not have equalizing potentials available. In such cases, a single cell charger with complete AC line protection may be paralleled across the affected cell while still a part of the overall battery to provide an over-if voltage to that cell. Do not be alarmed such charging must continue for several weeks, particularly considering the currents actually passing through the cells are very small."
~
~   IEEE Std 450-1987, Appendix D4 states, "When an individual cell voltage corrected for temperature is below 2.13V, corrective action should be initiated immediately. It can be accomplished by providing an equalizing charge to the entire battery. However, it is oAen more convenient to apply the equalizing charge to the individual cell."
C&D Vendor Technical Manual, Section VI states, "Minimumacceptable voltage is the point at which plans should be made to provide equalize charge. It does not imply that the battery is malfunctioning or that it willnot provide power ifcalled upon.
~   Cell 34 was raised above its minimum technical specification potential (2.13VDC) within the two-hour LCO window. The charge was planned to continue until it reached 2.5VDC. While the cell reached 2.5VDC on August 8, 1997, it was left on charge to provide additional assurance that the cell would provide satisfactory service until the scheduled battery bank replacement during the outage. Cell 34 was replaced on August 11, 1997.
Some equipment may not have equalizing potentials available.
In such
: cases, a single cell charger with complete AC line protection may be paralleled across the affected cell while still a part ofthe overall battery to provide an over-voltage to that cell. Do not be alarmed ifsuch charging must continue for several weeks, particularly considering the currents actually passing through the cells are very small."
~
IEEE Std 450-1987, Appendix D4 states, "When an individual cell voltage corrected for temperature is below 2.13V, corrective action should be initiated immediately. It can be accomplished by providing an equalizing charge to the entire battery.
However, it is oAen more convenient to apply the equalizing charge to the individual cell."
~
Cell 34 was raised above its minimum technical specification potential (2.13VDC) within the two-hour LCO window.
The charge was planned to continue until it reached 2.5VDC. While the cell reached 2.5VDC on August 8, 1997, it was left on charge to provide additional assurance that the cell would provide satisfactory service until the scheduled battery bank replacement during the outage.
Cell 34 was replaced on August 11, 1997.
The root cause team concluded that, based on standard industry practice and their understanding of the ability of Cell 34 to meet its technical specification requirements, the extended charging was considered satisfactory. No root cause was determined.
The root cause team concluded that, based on standard industry practice and their understanding of the ability of Cell 34 to meet its technical specification requirements, the extended charging was considered satisfactory. No root cause was determined.
Ste   2- Consideration   of Im lications Since the extended charging was considered an acceptable practice, no implications were identified and no short-term assessment items were considered necessary. Subsequent to the root cause evaluation, we received the design inspection report. The report notes that "there was not adequate evidence to suggest that the battery train could not perform its function without the cell." However, the report leaves operability of the cell, per technical specification requirements, as an unresolved item. Since the battery could Page A-24
Ste 2-Consideration ofIm lications Since the extended charging was considered an acceptable practice, no implications were identified and no short-term assessment items were considered necessary.
Subsequent to the root cause evaluation, we received the design inspection report. The report notes that "there was not adequate evidence to suggest that the battery train could not perform its function without the cell."
However, the report leaves operability of the cell, per technical specification requirements, as an unresolved item.
Since the battery could Page A-24


Short Term Assessment Program Rev. 2 Appendix A perform its overall function, we still conclude that short-term assessment actions are not necessary.
Short Term Assessment Program Rev. 2 Appendix A perform its overall function, we still conclude that short-term assessment actions are not necessary.
Code Discrepancies in CC% System Safety Valves (CR-97-2437)
Code Discrepancies in CC% System Safety Valves (CR-97-2437)
Ste   1 Root Cause Determination The problem was defined as manual valves located between the reactor coolant thermal barrier cooling coil and the CCW surge tank relief valve do not conform to the applicable B31.1 piping code, which states that an intercepting stop valve cannot be located between the source of pressure and the pressure relief device credited for protecting the pipe.
Ste 1 Root Cause Determination The problem was defined as manual valves located between the reactor coolant thermal barrier cooling coil and the CCW surge tank reliefvalve do not conform to the applicable B31.1 piping code, which states that an intercepting stop valve cannot be located between the source ofpressure and the pressure reliefdevice credited for protecting the pipe.
Pertinent facts brought forth in the investigation include:
Pertinent facts brought forth in the investigation include:
~   UFSAR Section 9.5 states, "The relief valve on the component cooling surge tank is sized to relieve the maximum fiow rate of water that would enter the surge tank following a rupture of a reactor coolant pump thermal barrier cooling coil. The set pressure assures that the design pressure of the CCW system is not exceeded."
~
UFSAR Section 9.5 states, "The reliefvalve on the component cooling surge tank is sized to relieve the maximum fiowrate ofwater that would enter the surge tank following a rupture of a reactor coolant pump thermal barrier cooling coil. The set pressure assures that the design pressure ofthe CCW system is not exceeded."
Paragraph 122.6.1 of B31.1 states, "There shall be no intervening stop valves between piping being protected and its protective device or devices."
Paragraph 122.6.1 of B31.1 states, "There shall be no intervening stop valves between piping being protected and its protective device or devices."
~   There are a total of four manual CCW system valves in each unit that are defined as intervening stop or blocking valves per B31.1. These valves are in the open position during operation of the CCW system. They are used as isolation valves for maintenance activities during outages.
~
~   There are no administrative controls in place to prevent them from being inadvertently closed.
There are a total offour manual CCW system valves in each unit that are defined as intervening stop or blocking valves per B31.1.
B31.1 does not provide guidance on locking or sealing open intervening stop valves. However, other codes have provided direction. For example, ASME Section VIII, Appendix A, A-,104(a) states, "...a full area stop valve (is acceptable) for inspection and repair purposes only. When such a stop valve is provided, it shall be so arranged that it can be locked or sealed open and it shall not be closed."
These valves are in the open position during operation ofthe CCW system.
~   The Authorized Nuclear Inspector, the ASME B31 Mechanical Design Technical Committee Chairman, and an ASME B31 Mechanical Design Technical if Committee have stated that a valve is sealed open, it would not be considered an intervening stop valve.
They are used as isolation valves for maintenance activities during outages.
~   An operating procedure that controls valve position has been revised to include sealing these valves and periodically verifying they are in the open position.
~
The investigation could not determine why these             valves   were   not originally administratively controlled as required by B31.1.
There are no administrative controls in place to prevent them from being inadvertently closed.
B31.1 does not provide guidance on locking or sealing open intervening stop valves.
However, other codes have provided direction.
For example, ASME Section VIII, Appendix A, A-,104(a)
: states,
"...a full area stop valve (is acceptable) for inspection and repair purposes only.
When such a stop valve is provided, it shall be so arranged that it can be locked or sealed open and it shall not be closed."
~
The Authorized Nuclear Inspector, the ASME B31 Mechanical Design Technical Committee
: Chairman, and an ASME B31 Mechanical Design Technical Committee have stated that ifa valve is sealed open, it would not be considered an intervening stop valve.
~
An operating procedure that controls valve position has been revised to include sealing these valves and periodically verifying they are in the open position.
The investigation could not determine why these valves were not originally administratively controlled as required by B31.1.
The root cause associated with this issue is:
The root cause associated with this issue is:
~   Failure to translate design requirements into operating procedures Page A-25
~
Failure to translate design requirements into operating procedures Page A-25


Short Term Assessment Program Rev. 2 Appendix A Ste   2- Consideration   of Im lications Failure to translate design requirements into operating procedures Full conformance with the B31.1 piping code was not met in this case; however, the condition did not cause the CCW system to be inoperable. Plant procedures did require the valves to be open, but they were not administratively controlled as needed for literal code compliance. The potential for similar safety valve inconsistencies was evaluated as part of the condition report investigation and found not a concern. No additional short-term assessment items were considered necessary.
Short Term Assessment Program Rev. 2 Appendix A Ste 2-Consideration ofIm lications Failure to translate design requirements into operating procedures Full conformance with the B31.1 piping code was not met in this case; however, the condition did not cause the CCW system to be inoperable.
Plant procedures did require the valves to be open, but they were not administratively controlled as needed for literal code compliance.
The potential for similar safety valve inconsistencies was evaluated as part of the condition report investigation and found not a concern.
No additional short-term assessment items were considered necessary.
Procedures Allowing'Avo RHR Pumps to Run with the RCS Vented (CR-97-2480)
Procedures Allowing'Avo RHR Pumps to Run with the RCS Vented (CR-97-2480)
Ste   1- Root Cause     Determination The problem was defined as follows: Chapter 9 of the UFSAR (July 1994) states: "Only one RHR pump will be operated when the RCS is open to atmosphere to prevent damaging both pumps in the unlikely event that suction should be lost." 'Operating procedures for the RHR System do not prevent operation of both RHR pumps when the Coolant System is open to atmosphere.                                             'eactor O
Ste 1-Root Cause Determination The problem was defined as follows: Chapter 9 ofthe UFSAR (July 1994) states:
Pertinent facts brought fourth in the investigation include:
"Only one RHR pump will be operated when the RCS is open to atmosphere to prevent damaging both pumps in the unlikely event that suction should be lost." 'Operating procedures for the RHR System do not prevent operation of both RHR pumps when the
~   UFSAR Section 9.3.3, "System Design Evaluation," states, "Only one RHR pump will be operated when the RCS is open to atmosphere to prevent damaging both pumps in the unlikely event that suction is lost."
'eactor Coolant System is open to atmosphere.
V UFSAR Section 9.3.6.2.a, "Limiting Conditions For Operation," states, "A requirement to have only one RHR pump in operation whenever the RCS is drained to half-loop and vented, has been incorporated into applicable operating procedures."
O Pertinent facts brought fourth in the investigation include:
~   Past procedure revisions showed that a change sheet dated May 18, 1978, added the following precaution to the RHR operating procedure: "Do not operate both RHR pumps with Reactor Coolant System drained to half-loop. Sufficient suction head is not available for two pump operations."
~
UFSAR Section 9.3.3, "System Design Evaluation," states, "Only one RHR pump willbe operated when the RCS is open to atmosphere to prevent damaging both pumps in the unlikely event that suction is lost."
V UFSAR Section 9.3.6.2.a, "Limiting Conditions For Operation,"
: states, "A
requirement to have only one RHR pump in operation whenever the RCS is drained to half-loop and vented, has been incorporated into applicable operating procedures."
~
Past procedure revisions showed that a change sheet dated May 18, 1978, added the following precaution to the RHR operating procedure:
"Do not operate both RHR pumps with Reactor Coolant System drained to half-loop. Sufficient suction head is not available for two pump operations."
The investigation could not identify why the FSAR requirements were originally not incorporated into the procedures.
The investigation could not identify why the FSAR requirements were originally not incorporated into the procedures.
Safety screenings related to subsequent procedure           changes did not identify the discrepancy between the UFSAR and plant procedures.
Safety screenings related to subsequent procedure changes did not identify the discrepancy between the UFSAR and plant procedures.
The root cause associated with this issue is:
The root cause associated with this issue is:
~   Failure to translate UFSAR requirements into operating procedures Page A-26
~
Failure to translate UFSAR requirements into operating procedures Page A-26


Short Term Assessment Program Rev. 2 Appendix A Ste 2 Consideration of Im lications Failure to translate UFSAR requirements into operating procedures Plant operating procedures allowed operation outside the design basis. This condition does not cause the RHR system to be inoperable. No additional short-term assessment actions were considered necessary. However, this is another example where the UFSAR was not maintained and used as a top-tier design basis document. The longer-term programs arising from the design inspection will focus on this basic concern.
Short Term Assessment Program Rev. 2 Appendix A Ste 2 Consideration ofIm lications Failure to translate UFSAR requirements into operating procedures Plant operating procedures allowed operation outside the design basis.
This condition does not cause the RHR system to be inoperable.
No additional short-term assessment actions were considered necessary.
However, this is another example where the UFSAR was not maintained and used as a top-tier design basis document.
The longer-term programs arising from the design inspection willfocus on this basic concern.
Page A-27
Page A-27


ATTACHMENT 2 TO AEP:NRC:1260G4 10 CFR 50.59 PROGRAM to  AEP:NRC:1260G4                                Page 1 10 CFR 50.59 PROGRAM General Descri    tion Cook  Nuclear Plant's      program to evaluate proposed plant and procedures    changes    and  tests or experiments is based on the guidelines provided in NSAC-125 and is in compliance with the requirements of 10 CFR 50.59. The program described below includes procedures, training, oversight and feedback mechanisms designed to maintain the current licensing basis of the plant. The quality of the 10 CFR 50.59 screenings and safety evaluations is of the utmost importance to the management of Cook Nuclear Plant. As a result, improvements have been, and will continue to be made to facilitate the efforts of those performing the screenings and safety evaluations to ensure that program objectives will be achieved.
ATTACHMENT 2 TO AEP:NRC:1260G4 10 CFR 50.59 PROGRAM
Some of the most recent program improvements.are:identified below, a number of which are in direct response'o lessons learned from the architect engineering (AE) desi.gn inspection.
Pro ram    ualit The  quality of the 10 CFR 50.59 screenings and unreviewed safety question determinations is based on the program's procedures, personnel qualifications, training and oversight.        In addition, interfaces with industry organizations, such as INPO, NEI, and the NRC,  ensure that rising expectations with respect to the performance of 10 CFR 50.59 reviews are implemented.
Procedures Management's    expectations and the methodology to be used in implementing 10 CFR 50.59 screening and evaluations are provided through the program's procedures.        Currently, there are three procedures that address the reviews of proposed changes to the facility. These procedures invoke the guidance provided in NSAC-125 and provide both general and specific direction to safety reviewers. These .procedures have also been subjected to a number of internal and external inspections and audits over the years and have been revised numerous times to address suggested improvements that increase the quality of the safety reviews. Lessons learned from Cook Nuclear Plant 10 CFR 50.59s are. also a source of many of the changes made to these procedures.      These changes include, but are not limited to, the need to provide further-guidance, address programmatic shortcomings, ensure consistency in the, level of documentation, or to reinforce management's expectations.
~Trainin To ensure that personnel have the requisite knowledge of the procedures as well as the necessary plant knowledge to successfully implement the 10 CFR 50.59 program, screeners and safety evaluators must meet minimum qualifications. Management selects candidates to perform screenings and safety evaluations who have demonstrated a sufficient level of plant knowledge to understand the specifics of the licensing basis and recognize challenges to    it. Candidates are trained on the expectations and methodology contained in the procedures and must demonstrate proficiency by passing a written test before qualifying as either a screener or a safety evaluator.
Once qualified, screeners and safety evaluators must annually re-qualify by attend'ing refresher training and demonstrating a to AEP:NRC:1260G4                                Page 2 continued proficiency with the process through an annual written re-qualification test.
OversicVht Effectiveness of the 10 CFR 50.59 program is monitored by oversight provided by the plant nuclear safety review committee (PNSRC), the nuclear safety and design review committee (NSDRC),, audits performed by the performance assurance department, and during NRC inspections. A discussion of each of these is provided below.
PNSRC As  required by technical specifications (T/Ss), the      PNSRC  reviews and approves proposed design and procedure changes to ensure that there are no potential unreviewed safety questions and -.that the evaluations are well documented in accordance with plant procedures. This review is a challenging one for safety evaluators because of the high standards set by the PNSRC. In this context, the PNSRC review represents an opportunity for a select group of managers to coach the safety reviewers, who are from different parts of the organization, on their expectations. This has been an effective method to communicate to the reviewers the importance of their responsibility.
NSDRC The NSDRC subcommittee      on proposed changes conducts reviews of safety evaluations previously approved by the PNSRC and sample safety screenings of procedure changes.              This provides an additional layer of assurance that 10 CFR 50.59 reviews are completed in accordance with procedures.
Performance Assurance Performance assurance audits the 10 CFR 50.59 program on an annual basis to verify the adequacy and implementation of the safety evaluation program. 10 CFR 50.59 screenings and evaluations are also reviewed as part of other audits, surveillances, and procedure reviews'hese audits, surveillances and r'eviews determine if:
screenings  and evaluations  are conducted when required, screenings adequately      identify  and - consider source information,.
evaluations adequately answer any screening yes answers    and    consider    source  information correctly, evaluations adequately answer the unreviewed safety question determination questions, and the informat'ion is adequate for PNSRC to make safety decisions.
NRC  routine inspections conducted by the resident inspector regularly sample 10 CFR 50.59 screenings and evaluations to verify


Attachment   2 to AEP:NRC:126064                             Page 3 that proposed     changes are processed in accordance with 10 CFR 50.59,   and   that conclusions reached in these reviews are justifiable and well documented. Additionally, past special NRC safety inspections on the 10 CFR 50.59 program determined that procedures were well-written and contained detailed instructions and appropriate examples.     Past inspections, however, have noted some screenings that incorrectly concluded that safety evaluations were not required.       Consequently, procedures and training were strengthened to emphasize the need to clearly document screenings and to make reviewers more sensitive to changes that potentially could impact the UFSAR or design basis.
Attachment 2 to AEP:NRC:1260G4 Page 1
Recent Im rovements There have been many improvements     in the 10 CFR 50.59 program at Cook Nuclear   Plant over the past ten years. Earlier improvements were centered on providing better overall guidance to safety reviewers so that 10 CFR 50.59 reviews would provide the in-depth analysis that was required in a consistent, well documented manner such that 10 CFR 50.59 requirements could be met and our licensing basis could be preserved.       Recent improvements have focused on providing computer search tools, increasing the feedback mechanisms to our safety reviewers, and enhancing existing procedures in a way that provides a greater level of assurance in the quality of our program. Below are listed program improvements since 1995.
10 CFR 50.59 PROGRAM General Descri tion Cook Nuclear Plant's program to evaluate proposed plant and procedures changes and tests or experiments is based on the guidelines provided in NSAC-125 and is in compliance with the requirements of 10 CFR 50.59.
FOLIO Search En ine To facilitate the safety reviewer's task of identifying potential impacts on our current licensing basis due to proposed changes, computer search engines have been provided over the past two-years.
The program described below includes procedures, training, oversight and feedback mechanisms designed to maintain the current licensing basis of the plant.
The quality of the 10 CFR 50.59 screenings and safety evaluations is of the utmost importance to the management of Cook Nuclear Plant.
As a result, improvements have been, and will continue to be made to facilitate the efforts of those performing the screenings and safety evaluations to ensure that program objectives will be achieved.
Some of the most recent program improvements.are:identified
: below, a number of which are in direct response'o lessons learned from the architect engineering (AE) desi.gn inspection.
Pro ram ualit The quality of the 10 CFR 50.59 screenings and unreviewed safety question determinations is based on the program's procedures, personnel qualifications, training and oversight.
In addition, interfaces with industry organizations, such as INPO, NEI, and the
: NRC, ensure that rising expectations with respect to the performance of 10 CFR 50.59 reviews are implemented.
Procedures Management's expectations and the methodology to be used in implementing 10 CFR 50.59 screening and evaluations are provided through the program's procedures.
Currently, there are three procedures that address the reviews of proposed changes to the facility.
These procedures invoke the guidance provided in NSAC-125 and provide both general and specific direction to safety reviewers.
These.procedures have also been subjected to a number of internal and external inspections and audits over the years and have been revised numerous times to address suggested improvements that increase the quality of the safety reviews.
Lessons learned from Cook Nuclear Plant 10 CFR 50.59s are. also a source of many of the changes made to these procedures.
These changes include, but are not limited to, the need to provide further-guidance, address programmatic shortcomings, ensure consistency in the, level of documentation, or to reinforce management's expectations.
~Trainin To ensure that personnel have the requisite knowledge of the procedures as well as the necessary plant knowledge to successfully implement the 10 CFR 50.59 program, screeners and safety evaluators must meet minimum qualifications.
Management selects candidates to perform screenings and safety evaluations who have demonstrated a
sufficient level of plant knowledge to understand the specifics of the licensing basis and recognize challenges to it.
Candidates are trained on the expectations and methodology contained in the procedures and must demonstrate proficiency by passing a written test before qualifying as either a screener or a safety evaluator.
Once qualified, screeners and safety evaluators must annually re-qualify by attend'ing refresher training and demonstrating a
 
Attachment 2 to AEP:NRC:1260G4 Page 2
continued proficiency with the process through an annual written re-qualification test.
OversicVht Effectiveness of the 10 CFR 50.59 program is monitored by oversight provided by the plant nuclear safety review committee (PNSRC), the nuclear safety and design review committee (NSDRC),,
audits performed by the performance assurance department, and during NRC inspections.
A discussion of each of these is provided below.
PNSRC As required by technical specifications (T/Ss),
the PNSRC reviews and approves proposed design and procedure changes to ensure that there are no potential unreviewed safety questions and -.that the evaluations are well documented in accordance with plant procedures.
This review is a challenging one for safety evaluators because of the high standards set by the PNSRC.
In this context, the PNSRC review represents an opportunity for a select group of managers to coach the safety reviewers, who are from different parts of the organization, on their expectations.
This has been an effective method to communicate to the reviewers the importance of their responsibility.
NSDRC The NSDRC subcommittee on proposed changes conducts reviews of safety evaluations previously approved by the PNSRC and sample safety screenings of procedure changes.
This provides an additional layer of assurance that 10 CFR 50.59 reviews are completed in accordance with procedures.
Performance Assurance Performance assurance audits the 10 CFR 50.59 program on an annual basis to verify the adequacy and implementation of the safety evaluation program.
10 CFR 50.59 screenings and evaluations are also reviewed as part of other audits, surveillances, and procedure reviews'hese
: audits, surveillances and r'eviews determine if:
screenings and evaluations are conducted when
: required, screenings adequately identify and - consider source information,.
evaluations adequately answer any screening yes answers and consider source information correctly, evaluations adequately answer the unreviewed safety question determination questions, and the informat'ion is adequate for PNSRC to make safety decisions.
NRC routine inspections conducted by the resident inspector regularly sample 10 CFR 50.59 screenings and evaluations to verify
 
Attachment 2 to AEP:NRC:126064 Page 3
that proposed changes are processed in accordance with 10 CFR 50.59, and that conclusions reached in these reviews are justifiable and well documented.
Additionally, past special NRC safety inspections on the 10 CFR 50.59 program determined that procedures were well-written and contained detailed instructions and appropriate examples.
Past inspections,
: however, have noted some screenings that incorrectly concluded that safety evaluations were not required.
Consequently, procedures and training were strengthened to emphasize the need to clearly document screenings and to make reviewers more sensitive to changes that potentially could impact the UFSAR or design basis.
Recent Im rovements There have been many improvements in the 10 CFR 50.59 program at Cook Nuclear Plant over the past ten years.
Earlier improvements were centered on providing better overall guidance to safety reviewers so that 10 CFR 50.59 reviews would provide the in-depth analysis that was required in a consistent, well documented manner such that 10 CFR 50.59 requirements could be met and our licensing basis could be preserved.
Recent improvements have focused on providing computer search tools, increasing the feedback mechanisms to our safety reviewers, and enhancing existing procedures in a way that provides a greater level of assurance in the quality of our program.
Below are listed program improvements since 1995.
FOLIO Search En ine To facilitate the safety reviewer's task of identifying potential impacts on our current licensing basis due to proposed
: changes, computer search engines have been provided over the past two-years.
At Cook Nuclear Plant, the primary search tool is called FOLIO.
At Cook Nuclear Plant, the primary search tool is called FOLIO.
FOLIO is a text-searchable computer program. The current databases that are loaded and available include access to references such as the UFSAR, design basis documents, various regulatory documents such's bulletins, generic letters and notices, AEP/NRC correspondence,     previous safety review memos, reportability
FOLIO is a text-searchable computer program.
, reviews, operability reviews, environmental qualifications list, emergency plan and the final environmental statement. Each of the data bases is available to a wide portion of the plant population via the company's local area computer network. Also available is access to the commitment database that provides both a listing of commitments and an automatic link to the parent document where the commitment is located.       This database greatly aids the safety reviewer in finding licensing commitments that may be affected by a proposed design or procedure change, test or experiment.       The information available via the computer and the databases are continuing to be improved with additional references such as quality assurance program description (QAPD) and the fire protection program manual anticipated to be added in the future.
The current databases that are loaded and available include access to references such as the
: UFSAR, design basis documents, various regulatory documents such's bulletins, generic letters and
: notices, AEP/NRC correspondence, previous safety review
: memos, reportability
, reviews, operability reviews, environmental qualifications list, emergency plan and the final environmental statement.
Each of the data bases is available to a wide portion of the plant population via the company's local area computer network.
Also available is access to the commitment database that provides both a listing of commitments and an automatic link to the parent document where the commitment is located.
This database greatly aids the safety reviewer in finding licensing commitments that may be affected by a proposed design or procedure
: change, test or experiment.
The information available via the computer and the databases are continuing to be improved with additional references such as quality assurance program description (QAPD) and the fire protection program manual anticipated to be added in the future.
In addition to FOLIO, the T/Ss are expected to be added to the search engine with word search capability over the next year.
In addition to FOLIO, the T/Ss are expected to be added to the search engine with word search capability over the next year.
UFSAR Revalidation Effort The principal reference documents used in the 10 CFR 50.59 program are the UFSAR, and the design basis documents (DBDs) that are being generated for many of the plant systems. A review of the UFSAR has been underway since January 1997 to re-validate the information contained therein. The changes to the UFSAR resulting from this revalidation will improve the quality of the UFSAR. In conjunction to AEP:NRC:1260G4                               Page 4 with the UFSAR re-validation, a review of the completed DBDs will be integrated into future UFSAR reviews that will improve the quality of both the UFSAR and the DBDs. Improvements in the UFSAR and the DBDs will make the 10 CFR 50.59 program reviews easier to perform with a corresponding increase in quality.
UFSAR Revalidation Effort The principal reference documents used in the 10 CFR 50.59 program are the UFSAR, and the design basis documents (DBDs) that are being generated for many of the plant systems.
A review of the UFSAR has been underway since January 1997 to re-validate the information contained therein.
The changes to the UFSAR resulting from this revalidation will improve the quality of the UFSAR.
In conjunction
 
Attachment 2 to AEP:NRC:1260G4 Page 4
with the UFSAR re-validation, a review of the completed DBDs will be integrated into future UFSAR reviews that will improve the quality of both the UFSAR and the DBDs.
Improvements in the UFSAR and the DBDs will make the 10 CFR 50.59 program reviews easier to perform with a corresponding increase in quality.
Definin the Desi n and Licensin Bases and Sin le Failures Deficiencies in our personnel's understanding of the design and licensing bases of the plant, as well as the definition of a single failure, were discovered during the recent AE design inspection.
Definin the Desi n and Licensin Bases and Sin le Failures Deficiencies in our personnel's understanding of the design and licensing bases of the plant, as well as the definition of a single failure, were discovered during the recent AE design inspection.
To address this issue, we issued a policy statement and associated directive in November 1997 to define the terms "design basis",
To address this issue, we issued a policy statement and associated directive in November 1997 to define the terms "design basis",
"licensing basis", and "single failure". In addition, training was provided on the new procedures to ensure that the staff understood the terms, their importance to maintaining Cook .Nuclear Plant's design and licensing basis, and their relationship to the UFSAR and the 10 CFR 50.59 program. These efforts were performed: to ensure that past deficiencies in our change process at Cook Nuclear Plant are not repeated.     A review of the condition reports issued since September 15, 1997, indicates that the message has been received throughout our organization. As of December 18, 1997, at least 131 condition reports, by five different plant organizations, have been issued to document discrepancies of a similar type as those identified during the AE design inspection.             This includes discrepancies   found in the UFSAR.
"licensing basis",
Additionally, condition reports, open at the time the procedures discussed above were implemented, were reviewed with increased awareness of the design and licensing basis.         Those condition reports that documented conditions having the potential to adversely impact the design basis were identified. These condition reports will be resolved prior to entry into a mode where the condition is applicable.
and "single failure". In addition, training was provided on the new procedures to ensure that the staff understood the
Desi     Basis Chan es as Desi n Chan   e As a   result of the recent AE inspection, the plant procedure on design change control was modified to recognize that changes to design basis information must also be treated and processed in the same manner as physical design changes to the facility. This means that changes to design basis information will follow a strict path of rigorous multi-discipline design review and 'erification, including completion of a safety evaluation,               prior to implementation. Consequently, such changes will be subject to a high level of quality assurance standards that will help ensure design configuration control.
: terms, their importance to maintaining Cook.Nuclear Plant's design and licensing basis, and their relationship to the UFSAR and the 10 CFR 50.59 program.
Non-Intent Procedure Chan es As a result of the AE design inspection, plant procedures have been revised to require 10 CFR 50.59 safety-screening reviews of senior reactor operator (SRO) change sheets prior to making the changes effective.     Previously, non-intent procedure changes could be implemented as long as an approved 10 CFR 50.59 screening was performed within fourteen days of the change. The new procedural requirements direct the SRO to withhold approval of any procedure change sheets unless submitted with an approved safety screening.
These efforts were performed: to ensure that past deficiencies in our change process at Cook Nuclear Plant are not repeated.
A review of the condition reports issued since September 15,
: 1997, indicates that the message has been received throughout our organization.
As of December 18, 1997, at least 131 condition reports, by five different plant organizations, have been issued to document discrepancies of a similar type as those identified during the AE design inspection.
This includes discrepancies found in the UFSAR.
Additionally, condition reports, open at the time the procedures discussed above were implemented, were reviewed with increased awareness of the design and licensing basis.
Those condition reports that documented conditions having the potential to adversely impact the design basis were identified.
These condition reports will be resolved prior to entry into a mode where the condition is applicable.
Desi Basis Chan es as Desi n Chan e
As a result of the recent AE inspection, the plant procedure on design change control was modified to recognize that changes to design basis information must also be treated and processed in the same manner as physical design changes to the facility. This means that changes to design basis information will follow a strict path of rigorous multi-discipline design review and 'erification, including completion of a
safety evaluation, prior to implementation.
Consequently, such changes will be subject to a high level of quality assurance standards that will help ensure design configuration control.
Non-Intent Procedure Chan es As a result of the AE design inspection, plant procedures have been revised to require 10 CFR 50.59 safety-screening reviews of senior reactor operator (SRO) change sheets prior to making the changes effective.
Previously, non-intent procedure changes could be implemented as long as an approved 10 CFR 50.59 screening was performed within fourteen days of the change.
The new procedural requirements direct the SRO to withhold approval of any procedure change sheets unless submitted with an approved safety screening.
This guidance applies to all SRO change sheets.
This guidance applies to all SRO change sheets.
to AEP:NRC:1260G4                              Page 5 Feedback  of Lessons Learned As a result of previous inteinal audits, procedures and standards have been strengthened and training conducted.      This has resulted in a more conservative approach when conducting safety screenings and, as shown below, has resulted in a dramatic increase in the number of safety evaluations performed.
En ineerin Section        1996        1997 Nuclear Safety              50          160 Mechanical                  50          90 Structural                  20          30 Electrical                  40          60 Total                      160          340 Future Planned Im rovements The 10 CFR 50.59 procedure    will  be revised,  following the  NEI workshop  in January  1998; to reflect the guidelines in NEI 96-07.
This revision  will be issued during the first half of 1998.


ATTACHMENT 3 TO AEP:NRC: 1260G4 CALCULATIONAL REVIEWS
Attachment 2 to AEP:NRC:1260G4 Page 5
Feedback of Lessons Learned As a result of previous inteinal audits, procedures and standards have been strengthened and training conducted.
This has resulted in a more conservative approach when conducting safety screenings
: and, as shown below, has resulted in a dramatic increase in the number of safety evaluations performed.
En ineerin Section 1996 1997 Nuclear Safety Mechanical Structural Electrical 50 50 20 40 160 90 30 60 Total 160 340 Future Planned Im rovements The 10 CFR 50.59 procedure will be revised, following the NEI workshop in January 1998; to reflect the guidelines in NEI 96-07.
This revision will be issued during the first half of 1998.
 
ATTACHMENT 3 TO AEP:NRC: 1260G4 CALCULATIONALREVIEWS


ATTACitMENT3 to AEP:NRC:1260G4                                                                                                                                 PAGE     i
ATTACitMENT3 to AEP:NRC:1260G4 PAGE i


==SUMMARY==
==SUMMARY==
The purpose ofour review was to establish confidence that similar issues identified during the AE design inspection did not exist in our calculations.
The approach was to analyze and review calculations for issues similar to those identified in the AE design inspection, such as incorrect assumptions, calculation errors, and process measurcmcnt effect on instrument calculations.
The main focus of our analysis was to look for deficiencies that would result in equipment being inoperable. While thc review revealed both technical and administrative deficiencies, none Icd to any inoperability.
The corrective and preventive action needed to bring our calculations up to today' standards willbe part ofour longer-term actions.
The total number ofcalculations reviewed as a result ofissues raised during the AE design inspection was 324, summarized below.
Pccr Group Reviews (review considered lessons learned from AE design inspection)
System Functional Rcvicws (review considered lessons learned from AE design inspection)
Westinghouse Analyses review (focused on valid assumptions and interface)
IACCalculations (focused on instrument bias and process measurement)
Prc-AE Inspection Existing Calcs 41 20 19 114 Ncw Calcs Total 130 171 20 19 114
:.Calc'ulitloii'i':Rev'icw'c'1!ai'.Part'.of:Sho'it'<<'Term'his'cssm'e'uter:-.':::1948';:l'::Ll@HSit~~~
i 130N i''324~i~':::.:'::
In addition to these 324 calculation reviews, we also looked at the proccsscs and issues for groups of calculations to establish confidence that these previously completed calculations did not contain similar issues identified by the AE design inspection
. These groups arc summarized below.
Large Bore Piping Reconstitution Program Electrical Calculations (incorporated lessons learned from EDSFI)
.':Calcula'tlons'.Prc'vio'u'sl"': Co'm"'Ictcd<''i!'.l",i'l.':.',ll:::M.".::..""'i"':.'';:":::."!:;:ll:::";';Pi'i":.:
Total 178 l'289,".F4


The purpose of our review was to establish confidence that similar issues identified during the AE design inspection did not exist in our calculations. The approach was to analyze and review calculations for issues similar to those identified in the AE design inspection, such as incorrect assumptions, calculation errors, and process measurcmcnt effect on instrument calculations.
ATfACHMENT3 to AEP:NRC:1260G4 PAGE 2 POST AE DESIGN INSPECTION REVIEWS
The main focus of our analysis was to look for deficiencies that would result in equipment being inoperable. While thc review revealed both technical and administrative deficiencies, none Icd to any inoperability. The corrective and preventive action needed to bring our calculations up to today' standards willbe part of our longer-term actions.
~
The total number of calculations reviewed as a result                        of issues          raised during the AE design inspection was 324, summarized below.
PEER GROUP REVIEW EFFORT The UFSAR Revalidation Project conducted a review ofa number calculations to obtain 1) validation of various parameters, and/or 2) to resolve apparent document discrepancies.
Prc-AE                                Ncw Inspection                          Calcs      Total Existing Calcs Pccr Group Reviews 41                                    130        171 (review considered            lessons    learned    from AE design inspection)
The review of the calculations identified a number ofgeneric issues that called into question thc administrative quality, as well as the technical accuracy, of the calculation results.
System Functional Rcvicws 20                                              20 (review considered            lessons    learned    from AE design inspection)
Condition rcport CR 97-2525 was initiated to investigate and resolve the issues associated with the quality ofcalculations.
Westinghouse Analyses review 19                                              19 (focused on valid assumptions and interface)
Management evaluation of thc condition rcport (CR 97-2525) revealed that the administrative and tcchnical issues brought out by thc condition rcport were similar to ones identified by thc AE design inspection The issues associated with condition report CR 97-2525 calculations were deemed to potentially impact restart issues. It was decided that all calculations involved in resolution of a restart item would be reviewed, through a Peer Group review eQort, prior,to restart.
IAC Calculations 114                                              114 (focused on instrument bias and process measurement)
A total of 171 calculations were reviewed in this elrort.
:.Calc'ulitloii'i':Rev'icw'c'1!ai'.Part'.of:Sho'it'<<'Term'his'cssm'e'uter:-.':::1948';:l'::Ll@HSit~~~                                      i 130N  i''324~i~':::.:'::
The review teams consisted of a functional engineering'manager; an<engineer~m the functional area (but not involved in generating the calculation), and an engineer from outside the functional area.
In addition to these 324 calculation reviews, we also looked at the proccsscs and issues for groups of calculations to establish confidence that these previously completed calculations did not contain similar issues identified by the AE design inspection . These groups arc summarized below.
The Peer Group rcvicw eQort was intended to serve as an interim measure to verify that calculations are performed in accordance with the existing procedure to identify human performance issues, as well as being technically correct.
Total Large Bore Piping Reconstitution Program 178 Electrical Calculations (incorporated lessons learned from EDSFI)
Long-term improvements are being developed as part of the prcvcntive actions to condition report CR 97-2525.
                      .':Calcula'tlons'.Prc'vio'u'sl"': Co'm"'Ictcd<''i!'.l",i'l.':.',ll:::M.".::..""'i"':.'';:":::."!:;:ll:::";';Pi'i":.:l'289,".F4
 
ATfACHMENT3 to AEP:NRC:1260G4                                                                       PAGE 2 POST AE DESIGN INSPECTION REVIEWS
~   PEER GROUP REVIEW EFFORT The UFSAR Revalidation Project conducted a review of a number calculations to obtain 1) validation of various parameters, and/or 2) to resolve apparent document discrepancies. The review of the calculations identified a number of generic issues that called into question thc administrative quality, as well as the technical accuracy, of the calculation results.         Condition rcport CR 97-2525 was initiated to investigate and resolve the issues associated with the quality of calculations.
Management evaluation of thc condition rcport (CR 97-2525) revealed that the administrative and tcchnical issues brought out by thc condition rcport were similar to ones identified by thc AE design inspection . The issues associated with condition report CR 97-2525 calculations were deemed to potentially impact restart issues. It was decided that all calculations involved in resolution of a restart item would be reviewed, through a Peer Group review eQort, prior,to restart. A total of 171 calculations were reviewed in this elrort.
The review teams consisted of a functional engineering'manager; an<engineer~m the functional area (but not involved in generating the calculation), and an engineer from outside the functional area. The Peer Group rcvicw eQort was intended to serve as an interim measure to verify that calculations are performed in accordance with the existing procedure to identify human performance issues, as well as being technically correct. Long-term improvements are being developed as part of the prcvcntive actions to condition report CR 97-2525.
The Peer Group's instructions placed emphasis on the following seven attributes, in addition to the general procedural requirements:
The Peer Group's instructions placed emphasis on the following seven attributes, in addition to the general procedural requirements:
: l. Assumptions are listed and are correct for purposes   of thc calculation.
l.
: 2. References arc listed and are validated to be current.
Assumptions are listed and are correct for purposes ofthc calculation.
: 3. Purpose and intended use   of the calculation are clearly stated.
2.
        '4. Models and computations are included for unique calculations.               (Where spreadsheet calculations are used, thc formulas should be printed out and attached to the calculation. For calculations that are repetitive in nature, the standard program used must be identified; inputs and results must be included'in'thc calculation.).
References arc listed and are validated to be current.
: 5. Ifinput data   is taken from a secondly source, its usc:is clearly,justified,and documented.
3.
(For example,   ifa nominal tank volume is taken from a system description or the technical specifications, the calculation must document why it is justified and conservative to use the nominal volume. Otherwise, the volume should be recalculated from primary source documents such as ccrtificd vendor drawings and then adjusted to provide appropriate conservatism.)
Purpose and intended use ofthe calculation are clearly stated.
: 6. Earlier calculations which are superseded or require revision as a result of the new calculation are clearly identified and the appropriate changes to the earlier calculations have been made.
'4.
: 7. Allblanks on the cover sheet and design verification forms arc completed or N/A'd Also, experienced contractors provided expert advice on the Peer Group review eQort as well as served as team members on some of the Peer Group review teams for these reviews.
Models and computations are included for unique calculations.
(Where spreadsheet calculations are used, thc formulas should be printed out and attached to the calculation. For calculations that are repetitive in nature, the standard program used must be identified; inputs and results must be included'in'thc calculation.).
: 5. Ifinput data is taken from a secondly source, its usc:is clearly,justified,and documented.
(For example, ifa nominal tank volume is taken from a system description or the technical specifications, the calculation must document why it is justified and conservative to use the nominal volume.
Otherwise, the volume should be recalculated from primary source documents such as ccrtificd vendor drawings and then adjusted to provide appropriate conservatism.)
6.
Earlier calculations which are superseded or require revision as a result of the new calculation are clearly identified and the appropriate changes to the earlier calculations have been made.
7.
Allblanks on the cover sheet and design verification forms arc completed or N/A'd Also, experienced contractors provided expert advice on the Peer Group review eQort as well as served as team members on some ofthe Peer Group review teams for these reviews.


ATTACHMENT3 to AEP:NRC: l260G4                                                                     PAGE 3
ATTACHMENT3 to AEP:NRC: l260G4 PAGE 3
~     REVIEW OF WESTINGHOUSE ANALYSES During the course of the Architect Engineer Inspection, a number of issues came to light that suggested it would be prudent to review the calculations performed for the Donald C. Cook Nuclear Plant by the Westinghouse Electric Corporation for accuracy. An engineering asscssmcnt of the design basis calculations performed by Westinghouse in support of thc Cook Nuclear Plant was performed. That assessment was performed in August and September of 1997.
~
REVIEW OF WESTINGHOUSE ANALYSES During the course of the Architect Engineer Inspection, a number of issues came to light that suggested it would be prudent to review the calculations performed for the Donald C. Cook Nuclear Plant by the Westinghouse Electric Corporation for accuracy. An engineering asscssmcnt of the design basis calculations performed by Westinghouse in support of thc Cook Nuclear Plant was performed. That assessment was performed in August and September of 1997.
Three principal areas for review were identified for review during the assessment:
Three principal areas for review were identified for review during the assessment:
: 1. A subset of questions identified regarding the RHR cooldown analysis by the AE Inspection Team was addressed.
1.
: 2. The interface between AEP and Westinghouse was addressed.           Thc interface had been identified as a potential problem in recent years. This item was included in the review to address past concerns and to assess the effectiveness of the. changes implemented in recent years.
A subset of questions identified regarding the RHR cooldown analysis by the AE Inspection Team was addressed.
: 3. A sample of 19 calculation packages was reviewed to.,assess. the. potential.for;additional problem areas in thc calculations performed for the Cook Plant units by Westinghouse.
2.
The engineering assessment of Westinghouse Electric Corporation also responded to specific questions raised by thc AE design inspection team. It did not result in any new observations in this area. The discussion of interface issues resulted in a number of recommendations for further improvement. Thc review of calculations performed during the assessment identified only one additional calculation which required revision. The modification to thc calculation was not related directly to the issues arising from the AE Inspection. This calculation was the post-LOCA subcriticality calculation which is checked every cycle to ensure that the core will remain subcritical aAer a large break LOCA assuming all control rods do not insert. The ice mass used in the analysis had to bc increased to a value that bounded plant operation. Although the cold leg recirculation mode cooling subcriticality requirement continued to be met despite thc increase in ice mass, the hot lcg recirculation cooling mode subcriticality requirement needed credit for the hot leg nozzle gap to demonstrate compliance. Taking credit for the nozzle gap to address this issue is not unusual because nearly all Westinghouse units usc this to address this issue. Thc long-term containment analysis was
The interface between AEP and Westinghouse was addressed.
  '-known to.have a problem due to the erroneous modeling of the CCW heat exchanger. For this analysis, margin was identified that compensated for the error.
Thc interface had been identified as a potential problem in recent years.
In general, the participants concluded that the: Westinghouse analyses, are performed with suQicient margin to accommodate identified errors; The. participants noted. improvement in, the interface between Westinghouse and AEP in recent years. However,.as.expected, improvements in this interface appeared to provide the best opportunity to further improve the reliability of Westinghouse analyses. Furthermore, the items identified in thc AE inspection which impacted the Westinghouse
This item was included in the review to address past concerns and to assess the effectiveness of the. changes implemented in recent years.
    'nalyses related to the inadequate functioning of this interface. The participants concluded that, the analyses performed by Westinghouse remained acceptable and that there existed available margin to address issues identified in thc NRC AE Inspection and in this assessment.
3.
~     SYSTEM FUNCTIONALCALCULATIONREVIEWS To develop confidence in the calculations performed by AEP, a sample of the system functional calculations were reviewed. This review concluded that there were no system inoperabilities as a result of calculation deficiencies.
A sample of 19 calculation packages was reviewed to.,assess. the. potential.for;additional problem areas in thc calculations performed for the Cook Plant units by Westinghouse.
The engineering assessment of Westinghouse Electric Corporation also responded to specific questions raised by thc AE design inspection team. It did not result in any new observations in this area.
The discussion of interface issues resulted in a number of recommendations for further improvement.
Thc review of calculations performed during the assessment identified only one additional calculation which required revision.
The modification to thc calculation was not related directly to the issues arising from the AE Inspection.
This calculation was the post-LOCA subcriticality calculation which is checked every cycle to ensure that the core willremain subcritical aAer a large break LOCA assuming all control rods do not insert.
The ice mass used in the analysis had to bc increased to a value that bounded plant operation.
Although the cold leg recirculation mode cooling subcriticality requirement continued to be met despite thc increase in ice mass, the hot lcg recirculation cooling mode subcriticality requirement needed credit for the hot leg nozzle gap to demonstrate compliance. Taking credit for the nozzle gap to address this issue is not unusual because nearly all Westinghouse units usc this to address this issue.
Thc long-term containment analysis was
'-known to.have a problem due to the erroneous modeling of the CCW heat exchanger.
For this analysis, margin was identified that compensated for the error.
In general, the participants concluded that the: Westinghouse analyses, are performed with suQicient margin to accommodate identified errors; The. participants noted. improvement in,the interface between Westinghouse and AEP in recent years.
However,.as.expected, improvements in this interface appeared to provide the best opportunity to further improve the reliability of Westinghouse analyses.
Furthermore, the items identified in thc AE inspection which impacted the Westinghouse
'nalyses related to the inadequate functioning of this interface.
The participants concluded that, the analyses performed by Westinghouse remained acceptable and that there existed available margin to address issues identified in thc NRC AE Inspection and in this assessment.
~
SYSTEM FUNCTIONALCALCULATIONREVIEWS To develop confidence in the calculations performed by AEP, a sample of the system functional calculations were reviewed.
This review concluded that there were no system inoperabilities as a result ofcalculation deficiencies.
Multi4isciplinary engineering reviews were conducted, using the Peer Group review guidelines, to verify that the selMed systems are capable of performing their intended safety functions (i.e., there werc no inopcrabilities). The Peer Groups for these calculations also focused on assumption control
Multi4isciplinary engineering reviews were conducted, using the Peer Group review guidelines, to verify that the selMed systems are capable of performing their intended safety functions (i.e., there werc no inopcrabilities). The Peer Groups for these calculations also focused on assumption control


ATTACHMENT3, to AEP:NRC:1260G4                                                                       PAGE 4 and results/methodology validation. The reviews included reviews of design basis documents to verify the appropriateness     of the design assumptions, boundary conditions, and models (when applicable).. The sample was selected as follows:
ATTACHMENT3, to AEP:NRC:1260G4 PAGE 4 and results/methodology validation.
0   Ten risk significant systems were selected for inclusion in thc sample population based on the IPE risk significance. This resulted in 139 functionally significant calculations from the following systems to select from for the system functional reviews:
The reviews included reviews of design basis documents to verify the appropriateness of the design assumptions, boundary conditions, and models (when applicable).. The sample was selected as follows:
0 Ten risk significant systems were selected for inclusion in thc sample population based on the IPE risk significance. This resulted in 139 functionally significant calculations from the followingsystems to select from for the system functional reviews:
Essential Service Water [25 calculations]
Essential Service Water [25 calculations]
Component Cooling Water [8 calculations]
Component Cooling Water [8 calculations]
Reactor Protection System/ESFAS [1 calculation]
Reactor Protection System/ESFAS
Residual Heat Removal System [   11 calculations]
[1 calculation]
Residual Heat Removal System [ 11 calculations]
Emergency Power [7 calculations]
Emergency Power [7 calculations]
Auxiliary Fcedwater System [32 calculations]
AuxiliaryFcedwater System [32 calculations]
Containment Spray System [18 calculations]
Containment Spray System [18 calculations]
250 VDC [25 calculations]
250 VDC [25 calculations]
ECCS -(Accumulators,       Safety Injection. System, RCS     Pressure   Relief) [7 calculations]
ECCS
-(Accumulators, Safety Injection.
: System, RCS Pressure Relief)
[7 calculations]
CVCS (Charging Pumps) [5 calculations]
CVCS (Charging Pumps) [5 calculations]
0   Twenty calculations 'werc then sclccted from this population of 139 based upon their complexity and potential to contain issues similar to those identified by the AE design inspection team (see Table 3) .
0 Twenty calculations 'werc then sclccted from this population of 139 based upon their complexity and potential to contain issues similar to those identified by the AE design inspection team (see Table 3).
~     INDEPENDENT VERIFICATION As an additional verification, an AEP contractor performed an independent review of two safety
~
    'significant calculations from the above population of 191 calculations to identify any common deficiencies/concerns with thc reviewed calculations and to provide an outside contractor's perspective on the AEP calculation process and controlling proccdurc(s).       The contractor reviews identified no inoperabilitics.
INDEPENDENTVERIFICATION As an additional verification, an AEP contractor performed an independent review of two safety
PRE-AE DESIGN INSPECTION REVIEWS The scope of our review effort was impacted by calculations.that'had'previously, been performed for programs such as the Large Bore Piping Reconstitution Program, and calculations that.has been upgraded following the EDSFI.
'significant calculations from the above population of 191 calculations to identify any common deficiencies/concerns with thc reviewed calculations and to provide an outside contractor's perspective on the AEP calculation process and controlling proccdurc(s).
      ~   LARGE BORE PIPING RECONSTITUTION PROGRAM The Large Bore Piping Reconstitution Program (LBPRP), performed pipe stress analysis and pipe support calculations for 2 1/2 inch and larger safety system piping between 1991 and 1997.
The contractor reviews identified no inoperabilitics.
There were 178 calculation',packages. which include the pipe stress analysis and pipe stress qualification for 5314 pipe supports for normal, upset and cmergcncy conditions. The NRC reviewed this program and the calculations being performed in December 1991 and indicated that "the LBPRP is very comprehensive and thorough...[and]... The aggressive use of more rigorous analytical techniques shows a strong commitment to quality." Also, the review of specific calculations resulted in the conclusion that "No discrepancies were noted while comparing the as-built documentation and computer code inputs".
PRE-AE DESIGN INSPECTION REVIEWS The scope of our review effort was impacted by calculations.that'had'previously, been performed for programs such as the Large Bore Piping Reconstitution Program, and calculations that.has been upgraded followingthe EDSFI.
~
LARGE BORE PIPING RECONSTITUTION PROGRAM The Large Bore Piping Reconstitution Program (LBPRP), performed pipe stress analysis and pipe support calculations for 2 1/2 inch and larger safety system piping between 1991 and 1997.
There were 178 calculation',packages. which include the pipe stress analysis and pipe stress qualification for 5314 pipe supports for normal, upset and cmergcncy conditions.
The NRC reviewed this program and the calculations being performed in December 1991 and indicated that "the LBPRP is very comprehensive and thorough...[and]... The aggressive use of more rigorous analytical techniques shows a strong commitment to quality."
Also, the review of specific calculations resulted in the conclusion that "No discrepancies were noted while comparing the as-built documentation and computer code inputs".
Forty-five pipe support calculations for the CCW system were subsequently reviewed aAer the AE
Forty-five pipe support calculations for the CCW system were subsequently reviewed aAer the AE


ATTACHMENT3 to AEP:NRC:1260G4                                                                     PAGE 5 design inspection as part of the Peer Group review effort. The review looked at the issues from the AE design inspection, and the process used in conducting the calculations. Our review provides reasonable assurance that the pipe supports for safety systems are in compliance with the design bases for these systems.
ATTACHMENT3 to AEP:NRC:1260G4 PAGE 5 design inspection as part of the Peer Group review effort. The review looked at the issues from the AE design inspection, and the process used in conducting the calculations.
    ~   ELECTRICAL CALCULATIONS Recognized documentation weakness (in our design basis calculations) identified in the EDSFI conducted in 1992 as well as thc results of an electrical cnginecring group review of calculations
Our review provides reasonable assurance that the pipe supports for safety systems are in compliance with the design bases for these systems.
        ,pre-EDSFI, lcd to a significant effort to upgrade calculations in the 250 Vdc, 120 Vac, and 4kV systems. Thc electrical engineering group launched a calculation upgrade program, which revisited design basis calculations to assure thc calculations would meet regulatory and internal staildards.
~
In all, 111 electrical calculations were revised or developed between 1992 and 1997. Several reviews" and audits,"pcrformcd on the electrical calculations,'yielded only minor, calculation comments.
ELECTRICALCALCULATIONS Recognized documentation weakness (in our design basis calculations) identified in the EDSFI conducted in 1992 as well as thc results ofan electrical cnginecring group review of calculations
,pre-EDSFI, lcd to a significant effort to upgrade calculations in the 250 Vdc, 120 Vac, and 4kV systems.
Thc electrical engineering group launched a calculation upgrade program, which revisited design basis calculations to assure thc calculations would meet regulatory and internal staildards.
In all, 111 electrical calculations were revised or developed between 1992 and 1997.
Several reviews" and audits,"pcrformcd on the electrical calculations,'yielded only minor, calculation comments.
In addition, electrical calculations reviewed as part of the system functional calculation review eflort revealed that calculation administrative deficiencies did not cause equipmcnt to be inoperable.
In addition, electrical calculations reviewed as part of the system functional calculation review eflort revealed that calculation administrative deficiencies did not cause equipmcnt to be inoperable.
PROBLEMS AND RELEVANCE
PROBLEMS ANDRELEVANCE
~   The Peer Group reviews of 171 calculations as well as the review of 20 system functional calculations, utilizing lessons learned from the AE design inspection, identified a number of administrative and tcchnical deficiencies similar to those identified in the AE design inspection.           Examples of administrative deficiencies included the following:
~
0   assumptions not clearly defined 0   variables in equation not well defined 0   drawing rcfercnccs do not have revision number 0     calculation purpose not clearly stated 0     references not provided 0     diQicult to follow the calculation flow 0     cover sheets not filled out/completed consistently 0     page numbers not properly recorded Examples     of technical deficiencies included the following:
The Peer Group reviews of 171 calculations as well as the review of20 system functional calculations, utilizing lessons learned from the AE design inspection, identified a number of administrative and tcchnical deficiencies similar to those identified in the AE design inspection.
0 - treatment of instrument uncertainties was not clearly documented 0   justification for assumed inputs used in some calculations was not documented 0     formula for flowratcs not provided However, although there werc a number of deficiencies identiTied in the reviews (see Table 2), the subsequent reviews revealed that no systems were inoperable.
Examples of administrative deficiencies included the following:
0 assumptions not clearly defined 0
variables in equation not well defined 0
drawing rcfercnccs do not have revision number 0
calculation purpose not clearly stated 0
references not provided 0
diQicult to followthe calculation flow 0
cover sheets not filledout/completed consistently 0
page numbers not properly recorded Examples oftechnical deficiencies included the following:
0 -
treatment ofinstrument uncertainties was not clearly documented 0
justification for assumed inputs used in some calculations was not documented 0
formula for flowratcs not provided However, although there werc a number of deficiencies identiTied in the reviews (see Table 2), the subsequent reviews revealed that no systems were inoperable.


ATrACHMENT3 to AEP:NRC: l260G4                                                                   PAGE 6
ATrACHMENT3 to AEP:NRC: l260G4 PAGE 6
~ The review of Westinghouse calculations identified a number of discrepancies which required evaluation. In spite of these discrcpancics the review team participants concluded that the analyses of record results remained acceptable with conservatism available to address issues identified by thc AE design inspection. Subsequent to the analyses review a number of as-found operability analyses were performed to document the effect of the identified discrepancies and issues raised during the AE design inspection. Analyses using actual plant data that were completed for Unit One cycle 16 and Unit Two cycle 11, confirmed the acceptability of the analyses results and demonstrated that the Cook Nuclear Plant systems remained operablc.
~
The review of Westinghouse calculations identified a number of discrepancies which required evaluation. In spite ofthese discrcpancics the review team participants concluded that the analyses of record results remained acceptable with conservatism available to address issues identified by thc AE design inspection.
Subsequent to the analyses review a number of as-found operability analyses were performed to document the effect of the identified discrepancies and issues raised during the AE design inspection.
Analyses using actual plant data that were completed for Unit One cycle 16 and Unit Two cycle 11, confirmed the acceptability of the analyses results and demonstrated that the Cook Nuclear Plant systems remained operablc.


MATRIXOF CALCULATIONREVIE%S PERFORMED le         1 Electrical                                     TOTAL= 3 (273 in calc database)                         FUNC. CALC. REVIEW 3 Mechanical                                     TOTAL= 54 (1529 in calc database)                       WESTINGHOUSE ANALYSES 18 PEER GROUP REVIEW 22 FUNC. CALC. REVIEW 14 I8r,C                                         TOTAL= 145 (330 in IAC database)                         WESTINGHOUSE ANALYSES 1 PROCESS MEASUREMENT. ('97) 114 (218 system related, and 112 uncertainty)
MATRIXOF CALCULATIONREVIE%S PERFORMED le 1
PEER GROUP REVIEW 29 FUNC. CALC. REVIEW 1 Structural                                    TOTAL= 116 (2410 in calc database)                       PEER GROUP REVIEW;- 116 Other                                        TOTAL= 6 (526 in calc database)                        PEER GROUP REVIEW 4
Electrical (273 in calc database)
* FUNC. CALC. REVIEW 2
TOTAL= 3 FUNC. CALC. REVIEW3 Mechanical (1529 in calc database)
                                            ,-'.,Total'.':Numb'er';.'of::.:".Caic':Review's''324.','-'-;;,;=",::;,'",;":::;,.;.:
I8r,C (330 in IAC database)
(218 system related, and 112 uncertainty)
Structural (2410 in calc database)
Other (526 in calc database)
TOTAL= 54 WESTINGHOUSE ANALYSES18 PEER GROUP REVIEW22 FUNC. CALC. REVIEW14 TOTAL= 145 WESTINGHOUSE ANALYSES1 PROCESS MEASUREMENT. ('97) 114 PEER GROUP REVIEW29 FUNC. CALC. REVIEW1 TOTAL= 116 PEER GROUP REVIEW;- 116 TOTAL= 6 PEER GROUP REVIEW4 FUNC. CALC. REVIEW2
,-'.,Total'.':Numb'er';.'of::.:".Caic':Review's''324.','-'-;;,;=",::;,'",;":::;,.;.:


Table 2
Table 2
                              ~
~
SHORT TERM ASSESSMKNT PEER GROUP REVIEW OF CALCULATIONS CR 97-2802         Calculations were run on the non-QA DOS PC-based version of E/PDSTRUDL because of a software litch in the A M1CROVAXversion.
SHORT TERM ASSESSMKNT PEER GROUP REVIEW OF CALCULATIONS CR 97-2802 CR 97-2809 CR 97-2805 CR 97-2829 CR 97-2842 CR 97-2843 CR 97-2935 CR 97-3057 Pdentt/led during system/'uncttonal revIews)
                  "
CR 97-3143 Pdenttfted durlng systemtu notional reviews)
CR 97-2809        DC-D-HV-12-ABevaluated the impact of higher CCW temperatures on auxiliary building ventilation.
CR 97-3215 Pdentt/led during system functtonal reviews)
The basis for using an average CCW temperature of 135 F was not documented. The engineer subsequently documented his basis for the assumption, which was an evaluation by the system engineer of relative surface areas and temperatures throughout the system confirming that 135 F was a conservative value to usc in this calculation.
Calculations were run on the non-QA DOS PC-based version ofE/PDSTRUDL because ofa software litch in the AM1CROVAXversion.
CR 97-2805        ENSM 970606JJR evaluated the potential for vortexing in the RWST. Set points noted in the calculation did not include instrument uncertainty and it was felt that the potential for the results to bc misapplied by the end user (1&C) was high. The calculation:was clarified with respect to uncertainty.
DC-D-HV-12-ABevaluated the impact ofhigher CCW temperatures on auxiliary building ventilation.
Pro r use of the results b I&Cwas verified.
The basis for using an average CCW temperature of 135 F was not documented.
CR 97-2829        ENSM 971001CV determined RWST volume required for Appendix R support of the opposite unit.
The engineer subsequently documented his basis for the assumption, which was an evaluation by the system engineer ofrelative surface areas and temperatures throughout the system confirming that 135 F was a conservative value to usc in this calculation.
Reference for formula was omitted, basis for assumption that pressure/temperature ramp down linearly over 72 hours was not provided, and the PORV flow rate taken from the FSAR was not identified as being a conservative value. Formula was confirmed to be correct and all assumptions were reviewed to ensure they were conservative. PORV flow rate was actually increased for the final calculation, but combined with other refinement of other assumptions, the original calculation results were shown to be conservative.
ENSM 970606JJR evaluated the potential forvortexing in the RWST. Set points noted in the calculation did not include instrument uncertainty and it was felt that the potential for the results to bc misapplied by the end user (1&C) was high. The calculation:was clarified with respect to uncertainty.
CR 97-2842        HXP 911210AF, Rcv. 2 determined CCW temperatures for RHR cooldown for LBPRP. The calculation was technically acceptable. However, Rcv. 2 superseded only part of Rev. 1 so both revisions were currently valid. Rev. 2 willbecome a stand-alone calculation that incorporates all of the remainin valid rtions of Rev. 1.
Pro r use ofthe results b I&Cwas verified.
CR 97-2843        ENSM 970926QSL determined the impact of a thermal barrier rupture on the CCW system. Bases for selecting the RCS pressure and for considering 547 F a conservative RCS temperature were not rovidcd. Desi n ressure of CCW. stem was not documented. Results were valid.
ENSM 971001CV determined RWST volume required for Appendix R support ofthe opposite unit.
CR 97-2935        ENSM 970929TWF determined CTS flow to the containment annulus via CEQ fan stairwells. Bases for assumptions were not documented. Review and refinement of assumptions and recalculation confirmed that ori inal results were valid.
Reference for formula was omitted, basis for assumption that pressure/temperature ramp down linearly over 72 hours was not provided, and the PORV flowrate taken from the FSAR was not identified as being a conservative value. Formula was confirmed to be correct and all assumptions were reviewed to ensure they were conservative.
CR 97-3057        RS-C-0280 determined short-term maximum pH for containment sump after LBLOCA. The calculated value was 12.97 (for a period of 18 minutes); which is above the -12.9.upper limit for EQ Pdentt/led during  specifications. However, removing other overly conservative assumptions'within:the calculations system/'uncttonal revIews)
PORV flowrate was actually increased for the final calculation, but combined with other refinement ofother assumptions, the original calculation results were shown to be conservative.
(most notably assuming a 10% reduction in sodium tetraborate from!ice sublimation) will reduce thc calculated value to below 12.9. Additionally, the corrosion affect of pH 12.97 versus 12.9 for a short riod of time is not measurablc or si 'cant. Calculation is bein redone usin ro r assum tions CR 97-3143        HXP 740226FK and HXP 900629AF both deal with ESW system flow rcquiremcnts. The review identified potential discrepancies with current values in FSAR Table 9.5-2 and questioned whether the Pdenttfted durlng  SFP heat exchanger load had been properly considered. Consequences of the discrepancies were systemtu notional reviews) determined to be minimal. Calculation NEMP 950612AF had subsequently been performed and confirms that the 1990 calculation results arc still valid. All of the calculations are being revised a ro riatel .
HXP 911210AF, Rcv. 2 determined CCW temperatures forRHR cooldown for LBPRP. The calculation was technically acceptable.
CR 97-3215          HV 12CC01N veriTied the "adequacy" of the CCW emergency ventilation supply fans. Assumptions and methodology were not well documented, and the reviewers raised numerous questions.
However, Rcv. 2 superseded only part ofRev.
Pdentt/led during  Evaluation by HVAC cnginccrs subsequently determined that the calculation results werc valid.
1 so both revisions were currently valid. Rev. 2 willbecome a stand-alone calculation that incorporates all of the remainin valid rtions ofRev. 1.
system functtonal reviews)
ENSM 970926QSL determined the impact ofa thermal barrier rupture on the CCW system.
Bases for selecting the RCS pressure and for considering 547 F a conservative RCS temperature were not rovidcd. Desi n ressure ofCCW.
stem was not documented.
Results were valid.
ENSM 970929TWF determined CTS flowto the containment annulus via CEQ fan stairwells.
Bases for assumptions were not documented.
Review and refinement ofassumptions and recalculation confirmed that ori inal results were valid.
RS-C-0280 determined short-term maximum pH for containment sump after LBLOCA. The calculated value was 12.97 (for a period of 18 minutes); which is above the -12.9.upper limitfor EQ specifications.
However, removing other overly conservative assumptions'within:the calculations (most notably assuming a 10% reduction in sodium tetraborate from!ice sublimation) willreduce thc calculated value to below 12.9. Additionally, the corrosion affect ofpH 12.97 versus 12.9 for a short riod oftime is not measurablc or si
'cant.
Calculation is bein redone usin ro r assum tions HXP 740226FK and HXP 900629AF both deal with ESW system flowrcquiremcnts.
The review identified potential discrepancies with current values in FSAR Table 9.5-2 and questioned whether the SFP heat exchanger load had been properly considered.
Consequences ofthe discrepancies were determined to be minimal. Calculation NEMP 950612AF had subsequently been performed and confirms that the 1990 calculation results arc stillvalid. Allofthe calculations are being revised a
ro riatel HV 12CC01N veriTied the "adequacy" ofthe CCW emergency ventilation supply fans. Assumptions and methodology were not well documented, and the reviewers raised numerous questions.
Evaluation by HVACcnginccrs subsequently determined that the calculation results werc valid.


Table 3 Syst           ctional Reviews Q,::!$:Qkk".PC(%&+~i:,;,
Table 3 Syst ctional Reviews Q,::!$:Qkk".PC(%&+~i:,;,
MINIMUMAND MAXIMUMBUS PS-4KVD-003, FAULTS 4KV, 600V, AND 480V REV 0 SYSTEMS PS-4KVP-009,           4KV RCP UNDERVOLTAGE RELAY REV 0            SETTINGS PS-EDGL-001,           EDG 1AB STEADY STATE LOADING REV 0            AND VOLTAGE DROP                4KV AFWS PUMPS - TECHNICAL ENSM740501FK1, SPECIFICATIONS, BY F. KUO, 5/1/74 5/1974 AUXILIARYFEEDWATER PUMP HXP721130FK-2 SUCTION - NPSH AVAILABLE, 11/1972 AFWS NPSH CALCULATION, HXP740226FK FEBRUARY 26, 1974 MAXIMUNALLOWABLEPUMP HXP850508AF            DEGRADATION OF THE UNIT 1 PUMP, 1/2/86 AFW FLOWRATES IN SUPPORT OF HXP910619AF, SAFETY VALVESETPOINT             AFW REV 0 INCREASE Page 1, 12/24/97
PS-4KVD-003, REV 0 MINIMUMAND MAXIMUMBUS FAULTS 4KV, 600V, AND 480V SYSTEMS PS-4KVP-009, REV 0 4KV RCP UNDERVOLTAGERELAY SETTINGS PS-EDGL-001, REV 0 EDG 1AB STEADY STATE LOADING ANDVOLTAGEDROP 4KV ENSM740501FK1, 5/1/74 HXP721130FK-2 AFWS PUMPS - TECHNICAL SPECIFICATIONS, BY F. KUO, 5/1974 AUXILIARYFEEDWATER PUMP SUCTION - NPSH AVAILABLE, 11/1972 HXP740226FK AFWS NPSH CALCULATION, FEBRUARY 26, 1974 HXP850508AF MAXIMUNALLOWABLEPUMP DEGRADATIONOF THE UNIT 1 PUMP, 1/2/86 HXP910619AF, REV 0 AFW FLOWRATES IN SUPPORT OF SAFETY VALVESETPOINT AFW INCREASE Page 1, 12/24/97


Table 3 Syst       notional Reviews Pi~i~:ci:"-:@LYNN%!~j%:"j~4~~)iiy',;8)4fA.
Table 3 Syst notional Reviews NEMH930601AF Pi~i~:ci:"-:@LYNN%!~j%:"j~4~~)iiy',;8)4fA.
DETERMINE AMOUNTOF PUMP DEGRADATION THAT IS ALLOWED NEMH930601AF WHICH MEETS SAFETY ANALYSIS FLOW REQUIREMENTS, REV 0, 6/21/93 CCW PUMP AREA VENTILATION DCCHV1 2CC01N                                      CCW SYSTEM DESIGN, 12/8/89 CCW MOV PRESSURE HXP910419, RO                                     CCW DIFFERENTIAL HEAT GAIN CALCULATION,AES         CTMT DCCHV12AE06-N SYSTEM, REV 1, JUNE 2, 1992       SPRAY DOSE TO CONTROL ROOM RD-88-01     OPERATORS FOLLOWING A LOCA SPRAY REV1, NOV28, 1988 SHORT TERM MAXPH FOR RS-C-0280    CONTAINMENTSUMP IN A LARGE BREAK LOCA, AUGUST 31, 1995       ~pappy HXP890525AF, UNIT 1 WEST CENTRIFUGAL DATED JUNE 19, CHARGING PUMP FLOW                   CVCS 1989      REDUCING ORIFICE DCCHV12ES03N, LOSS OF HVAC - ESW PUMP ROOM REV 0                                          ESW TEMPERATURE, APRIL 22, 1991 Page 2, 12/24/97
DETERMINEAMOUNTOF PUMP DEGRADATIONTHATIS ALLOWED WHICH MEETS SAFETY ANALYSIS FLOW REQUIREMENTS, REV 0, 6/21/93 DCCHV12CC01N CCW PUMP AREA VENTILATION SYSTEM DESIGN, 12/8/89 CCW HXP910419, RO CCW MOVPRESSURE DIFFERENTIAL CCW DCCHV12AE06-N HEAT GAIN CALCULATION,AES SYSTEM, REV 1, JUNE 2, 1992 CTMT SPRAY RD-88-01 RS-C-0280 DOSE TO CONTROL ROOM OPERATORS FOLLOWINGA LOCA SPRAY REV1, NOV28, 1988 SHORT TERM MAXPH FOR CONTAINMENTSUMP IN A LARGE
~pappy BREAK LOCA, AUGUST 31, 1995 HXP890525AF, DATEDJUNE 19, 1989 UNIT 1 WEST CENTRIFUGAL CHARGING PUMP FLOW REDUCING ORIFICE CVCS DCCHV12ES03N, REV 0 LOSS OF HVAC-ESW PUMP ROOM ESW TEMPERATURE, APRIL22, 1991 Page 2, 12/24/97


Table 3 Syst       nctional Reviews DETERMINE ESW PUMP HXP900627AF      OPERATION DURING FULL POWER      ESW UNIT OPERATION, JULY 6, 1990 ESW FLOW REQUIREMENTS, HXP900629AF                                      ESW 6/29/90 NEMP950810AF, ESW FLOW TO EDGs, AUGUST 18, REV 0       1995 ESW ECP-1-2-N2-07,   MID-LOOP PHENOMENA AND 4/27/93, R8                                     RHR INSTRUMENTATION Page 3, 12/24/97
Table 3 Syst nctional Reviews HXP900627AF DETERMINE ESW PUMP OPERATION DURING FULLPOWER UNITOPERATION, JULY 6, 1990 ESW HXP900629AF ESW FLOW REQUIREMENTS, 6/29/90 ESW NEMP950810AF, REV 0 ECP-1-2-N2-07, 4/27/93, R8 ESW FLOW TO EDGs, AUGUST 18, 1995 MID-LOOP PHENOMENA AND INSTRUMENTATION ESW RHR Page 3, 12/24/97


ATTACHMENT 4 TO AEP:NRC:1260G4 PRESENTATION MATERIALS FOR DECEMBER 16, 1997 PUBLIC MEETING RESPONSE TO CONFIRMATORY ACTION LETTER ISSUES
ATTACHMENT 4 TO AEP:NRC:1260G4 PRESENTATION MATERIALS FOR DECEMBER 16, 1997 PUBLIC MEETING
 
===RESPONSE===
TO CONFIRMATORY ACTION LETTER ISSUES


December 16, 1H7
December 16, 1H7
                'MERICAN'lECl'RIC POWER
'MERICAN'lECl'RIC POWER


a     I       I i This meeting willdiscuss AEP's resolution of               AEP's conclusion is that Cook Nuclear Plant is issues documented in the NRC's Confirmatory                 ready to resume power'peration pending receipt Action Letter of September 19, 1997 and provide             of necessary technical specificatioh changes and reasonable assurance that these issues do not affect     'ompletion of the resolution plans.
a I
the operability of other safety systems.
I i This meeting willdiscuss AEP's resolution of issues documented in the NRC's Confirmatory Action Letter of September 19, 1997 and provide reasonable assurance that these issues do not affect the operability of other safety systems.
Agenda I. Introduction Eugene E. Fitzpatrick, executive vice president Nuclear Generation Group, Buchanan II. Confirmatory Action Letter No. RIII 97-011 Issues & Resolutions A.C I Issues1 4 San 2 Jeb B. Kingseed, section manager-nuclear safety and analysis Nuclear Generation Group, Buchanan Paul Schoepf, P.E., mechanical systems manager.
AEP's conclusion is that Cook Nuclear Plant is ready to resume power'peration pending receipt of necessary technical specificatioh changes and
Nuclear Generation Group, Cook Nuclear Plant C. nstrument Uncertain es C         I u 9 Stanley K. Farlow, P.E,, manager-I&C engineering, production engineering Nuclear Generation Group, Cook Nuclear Plant III. Short Term Assessment Program A.S ort-Tem ses e t eve                 e t Joel S. Wiebe, manager-performance     engineering & analysis Nuclear Generation Group, Buchanan B. S ort-Te     ssess e t Results James A. Kobyra, P.E., chief nuclear engineer Nuclear Generation Group, Buchanan IV. Additional Assurance of Operability of Systems A. Alan Blind, site vice president Nuclear ~neration Group, Cook Nuclear Plant V. Conclusion Eugene E. Fitzpatrick, executive v'ice president Nuclear Generation Group, Buchanan
'ompletion of the resolution plans.
Agenda I.
Introduction Eugene E. Fitzpatrick, executive vice president Nuclear Generation Group, Buchanan II. Confirmatory Action Letter No. RIII97-011 Issues &Resolutions A.C I Issues1 4 San 2
Jeb B. Kingseed, section manager-nuclear safety and analysis Nuclear Generation Group, Buchanan Paul Schoepf, P.E., mechanical systems manager.
Nuclear Generation Group, Cook Nuclear Plant C. nstrument Uncertain es C I
u 9
Stanley K. Farlow, P.E,, manager-I&C engineering, production engineering Nuclear Generation Group, Cook Nuclear Plant III. Short Term Assessment Program A.S ort-Tem ses e t eve e t Joel S. Wiebe, manager-performance engineering &analysis Nuclear Generation Group, Buchanan B. S ort-Te ssess e t Results James A. Kobyra, P.E., chief nuclear engineer Nuclear Generation Group, Buchanan IV. Additional Assurance of Operability of Systems A. Alan Blind, site vice president Nuclear ~neration Group, Cook Nuclear Plant V. Conclusion Eugene E. Fitzpatrick, executive v'ice president Nuclear Generation Group, Buchanan


Resolution     of CAL Issues Meeting                     Resolution of CAL Issues Meeting Issues or resolution           rior lo restart Gene Fitzpatrick                        I. Recirculation sump inventory Executive Vice President                    20    Recirculation sump venting Nuclear Generation Group                      3. 36-hour coo!down American Electric Power                    4. ES 13 switchover procedure S. Compressed air overpressurc Introduction                        6. RHR suction valve interlock Meeting Overview                        70    Fibrous material
Resolution ofCALIssues Meeting Resolution ofCALIssues Meeting Gene Fitzpatrick Executive Vice President Nuclear Generation Group American Electric Power Introduction Meeting Overview I.
: 8. Backlcakage to RWST g macaw A enda Resolution     of CAL Issues Meeting Jeb Ktn           SI    Reetreutatlon Sum lnvenio Issue or discussion rior to restart                                  S4   ES 19 Switchover Procedure SS   Baetdeabaae to RWST Instrument uncertainties incorporated into                                SZ   Reetreulatton Sump Venttnx procedures and analyses                              Paul Sehoepf            Hbrous Material In Containment SS   Sd.hour Cooldown Short-term assessment rior to restart                                  ttd RHR Suction Valve AutoCtose To determine whether same type engineering                                SS   Compressed AirOverpressure problems exist ln other safety-related                Stan Farlow      itt Instrument Uncertainty Joel Wiebe        Short Term Assessment Development systems and whether they alfect system                Jim Kobyra        Short Term Assessment Results operability                                          Al Blind          Additional Assurance of Operability of Systems Conclusion Reclrculatlon Sump Inventory                              Reclrculatlon Sump Inventory Con irmoto     Action Letter issue                       Issue resolved Pumps used to coot.the reactor and containment building   o Analyses demonstrated emergency core may not have enough water supply to allow long-term       cooling system/containment spray system operation of the systems operability                           h Commitment                                                'etermined sump level margin above Analysis willbe performed to detnonstratc that the          602'0" exists recirculation sump level is adequate to prevent        o Subtititted Tcchnical Specification vonexing, or appropriate ntodifications will be made      amendment to credit morc existing icc
20 3.
                                                                                                        +aneajeasr
4.
S.
6.
70 8.
Issues or resolution rior lo restart Recirculation sump inventory Recirculation sump venting 36-hour coo!down ES 13 switchover procedure Compressed air overpressurc RHR suction valve interlock Fibrous material Backlcakage to RWST g macaw Resolution ofCALIssues Meeting Issue or discussion riorto restart Instrument uncertainties incorporated into procedures and analyses Short-term assessment riorto restart To determine whether same type engineering problems exist ln other safety-related systems and whether they alfect system operability Jeb Ktn Paul Sehoepf Stan Farlow Joel Wiebe Jim Kobyra AlBlind A enda S I Reetreutatlon Sum lnvenio S4 ES 19 Switchover Procedure SS Baetdeabaae to RWST SZ Reetreulatton Sump Venttnx Hbrous Material In Containment SS Sd.hour Cooldown ttd RHR Suction Valve AutoCtose SS Compressed AirOverpressure itt Instrument Uncertainty Short Term Assessment Development Short Term Assessment Results Additional Assurance ofOperability of Systems Conclusion Reclrculatlon Sump Inventory Con irmoto Action Letter issue Pumps used to coot.the reactor and containment building may not have enough water supply to allow long-term operation ofthe systems Commitment Analysis willbe performed to detnonstratc that the recirculation sump level is adequate to prevent vonexing, or appropriate ntodifications willbe made Reclrculatlon Sump Inventory Issue resolved o Analyses demonstrated emergency core cooling system/containment spray system operability h
'etermined sump level margin above 602'0" exists o Subtititted Tcchnical Specification amendment to credit morc existing icc
+aneajeasr


Recirculation Sump Inventory                               Recirculation Sump Inventor A~nal sls                                                 ~nal sls
Recirculation Sump Inventory A~nal sls
  'ump configuration                                        ~   Large-brcak loss of coolant accident and
'ump configuration
  'loNlpaths                                                    spectrum of small-brcak loss of coolant accidents o Transient analysis
'loNlpaths
  'nalyses o Icc melt credited
'nalyses
  'esults
'esults gestate Recirculation Sump Inventor
                                                              'ctive/inactive         sumps modeled o Revised ES-1.3
~nal sls
                                                              'WST level uncertainty gestate                                                      gaatatcase Recirculation Sump Inventory'/                             Recirculation Sump Inventory A~nal   sir resnlrs                                         Issue resolved o Water level >602'0" for large and small                 o Analyses demonstrated emergency core break loss of coolant accidents                            cooling system/containment spray system o Technical'Specification                                      operability amendment o Determined sump Icvcl margin above 602'0" exists o Submitted Tech'nical Specification amendment to credit more existing icc A ende k introduction                               ES-1.3 Switchover Procedure Jch Ktngsccd        Nl     Redreutstton Sum Invento
~ Large-brcak loss ofcoolant accident and spectrum ofsmall-brcak loss ofcoolant accidents o Transient analysis o Icc melt credited
                    <<e     KS ID Switchover Procedure       Con rrmoro        Afenon    Leuer issue ca gc to eg:.'e. Rcdrcutatton Sum Venting p                Adequacy of current procedures during switchover &xn thc Paul Schoepf        <<y Hbrous Material ln Contalnmcnt           emergency water supply tank to thc eontahunent sump for Stan Fartow Joel Wtebe Jim Kobyra NS     3&cur Cooldown
'ctive/inactive sumps modeled o Revised ES-1.3
                    <<d RHR Sucdon Valve AutoCtosc irS Comprcsscd AlrOvcrpressure Instrument Unccrtdnty Short Tcrtn Assasmcnt Devdopmcnt Short Tenn Asscssmcnt Resulrs Commllmenl Changes to thc cmcrgency    ~
'WST level uncertainty gaatatcase Recirculation Sump Inventory'/
long<can post~dent operations used for switchover of the cmcrgency core cooling and containmcnt spray pumps to tbe rcdreutsncu Nanp willbc hnplcmcntaL These changes wi1I provide ssurance there will be adequate Al Blind            Additional Assurance of Operability of Systems                                    sump volume, with lroper consideration of instrument bias Gene pttspatrtck    Conduslon                                    and single>>failure criteria
A~nal sir resnlrs o Water level >602'0" for large and small break loss ofcoolant accidents o Technical'Specification amendment Recirculation Sump Inventory Issue resolved o Analyses demonstrated emergency core cooling system/containment spray system operability o Determined sump Icvcl margin above 602'0" exists o Submitted Tech'nical Specification amendment to credit more existing icc k
                                                                                                                  +   aatatcasr
Jch Ktngsccd Paul Schoepf Stan Fartow Joel Wtebe Jim Kobyra Al Blind Gene pttspatrtck A ende introduction Nl Redreutstton Sum Invento
<<e KS IDSwitchover Procedure ca gc to eg:.'e. Rcdrcutatton Sum p Venting
<<y Hbrous Material ln Contalnmcnt NS 3&curCooldown
<<d RHR Sucdon Valve AutoCtosc irS Comprcsscd AlrOvcrpressure Instrument Unccrtdnty Short Tcrtn Assasmcnt Devdopmcnt Short Tenn Asscssmcnt Resulrs Additional Assurance ofOperability of Systems Conduslon ES-1.3 Switchover Procedure Con rrmoro Afenon Leuer issue Adequacy ofcurrent procedures during switchover &xnthc emergency water supply tank to thc eontahunent sump for long<can post~dent operations Commllmenl Changes to thc cmcrgency~ used forswitchover of the cmcrgency core cooling and containmcnt spray pumps to tbe rcdreutsncu Nanp willbc hnplcmcntaL These changes wi1I provide ssurance there willbe adequate sump volume, withlroper consideration ofinstrument bias and single>>failure criteria
+aatatcasr


ES-1.3 Switchover Procedure                                   ESo1.3 Switchover Procedure issue resolved                                               ~noesis Implemented changes to ES-1.3 to incrcasc                         Refueling water storage tank level water injection, eliminated single-failure                     measurement bias vulnerability, and account for refueling                    ~ Accident analysis assumptions water storage tank level bias                               ~ Single-failure ESo1.3   Switchover Procedure                                          Switchover Procedure Aeuons                   t                                   Acuons
ES-1.3 Switchover Procedure ESo1.3 Switchover Procedure issue resolved Implemented changes to ES-1.3 to incrcasc water injection, eliminated single-failure vulnerability, and account forrefueling water storage tank level bias
~ Refueling water storage tank level                         ~  Accident analyses assumptions measurement bias                                               -Rceriticality
~noesis Refueling water storage tank level measurement bias
    -Flow Induced errors (acoul level > indicjgtcd)               -Containment pressure Resolution                                                         -Long-tenn cooling
~ Accident analysis assumptions
'oved refueling pates         stomge tank         RRRRRRRRJI'S-1.3 Resolotloo level transmitter tap                                       'ssumptions      satislied
~ Single-failure ESo1.3 Switchover Procedure Aeuons t
~ Refueling water storage tank level measurement bias
-Flow Induced errors (acoul level > indicjgtcd)
Resolution
'oved refueling pates stomge tank level transmitter tap
'nstrument uncertainty
'nstrument uncertainty
                                              ~~
~~
ES-1.3 Switchover Procedure                                   ES-1.3 Switchover Procedure Actions                                                       Resolullon summa
RRRRRRRRJI'S-1.3 Switchover Procedure Acuons
'ingle-failure       <g..                                         Eliminated refueling water supply tank
~ Accident analyses assumptions
    -One   residual heat removal (RHR) pump supplied             level measurement bias high-head emergency core cooling system (ECCS) pumps during transition
-Rceriticality
                                                              'et    accident analyses limitations
-Containment pressure
                                                              ~ Considered worst case, credible single active
-Long-tenn cooling Resolotloo
'ssumptions satislied ES-1.3 Switchover Procedure ES-1.3 Switchover Procedure Actions
'ingle-failure <g..
-One residual heat removal (RHR) pump supplied high-head emergency core cooling system (ECCS) pumps during transition
'esolution
'esolution
    -New transfer sotuencc ensures                               failure
-New transfer sotuencc ensures no loss ofinjection with single-failure Resolullon summa Eliminated refueling water supply tank level measurement bias
                                                              ~ Validated procedure and trained operating no loss of injection with single-failure crews
'et accident analyses limitations
                                                                                                        +   Agggggdggr
~ Considered worst case, credible single active failure
~ Validated procedure and trained operating crews
+ Agggggdggr


A enda ck   Introduction                           Back-Leakage to Refueling Water Storage Tank Jcb IGnaseed       Nl Rccircutatfon Sump Inventory Ns   KS ID Switchover Procedure       Con irmato       Action Letter issue Na    Backleakaac to RWST              Scat leak testing of valves may not be adequate to N      ec feil a oii nip cnbng            identify potential backllow from the containment to Paul Scboepf        N7    Fibrous Material ln Containment N3    3ti hour Cooidown                    thc RWST during the LOCA recirculation phase Nd    RHR Suction Valve Auto<lose      Commitment Ns    Comprcsscd AirOvcrpressure        Only two of six mini-flowrecirculation line valves have Stan Fariow        Np    Instrument Uncertaint                leakage verification tests. Justification will be Joel Wiebe          Short Term Asscssmcnt Development          provided that the total leakage for the six valves is
Paul Scboepf Stan Fariow Joel Wiebe
  -
-Jim Kobyra AIBlind tAcne Fitzpatrick N
Jim Kobyra          Short Term Assessment Results              <10 gpm to ensure that Part l00 limits are not AI Blind            Additional Assurance of Operability of exceeded ifcontainmcnt sump water werc to leak back Systems tAcne Fitzpatrick  Conclusion to RWST during a design basis accident
ec feil a oii nip cnbng N7 Fibrous Material ln Containment N3 3ti hour Cooidown Nd RHR Suction Valve Auto<lose Ns Comprcsscd AirOvcrpressure Np Instrument Uncertaint Short Term Asscssmcnt Development Short Term Assessment Results Additional Assurance ofOperability of Systems Conclusion A enda ck Introduction Jcb IGnaseed Nl Rccircutatfon Sump Inventory Ns KS IDSwitchover Procedure Na Backleakaac to RWST Back-Leakage to Refueling Water Storage Tank Con irmato Action Letter issue Scat leak testing ofvalves may not be adequate to identify potential backllow from the containment to thc RWST during the LOCArecirculation phase Commitment Only two ofsix mini-flowrecirculation line valves have leakage verification tests. Justification willbe provided that the total leakage forthe six valves is
                                                                                                                      ~ UCTaic Back. Leakage to Refueling Water Storage Tank             Back-Leakage to Refueling Water Storage Tank r    issue resolved                                          A~nal sla o Included    fiow paths in                              'our back flow paths in-service testing program                                -Leak testing   in place for two of the four paths o Implemented new procedure: seat leakage          -Two paths   not included in in.service testing testing of valves at each refueling outage to                program ensure < 10 gpm total leakage alcawasr cUcvalc Back-Leakage to Refueling Water Storage Tank             Back4.eakage to Refueling Water Storage Tank Actions                                                   issue resolved o Testing                                                 o  Included flow paths in in-scrv ice testing progranr results
<10 gpm to ensure that Part l00 limitsare not exceeded ifcontainmcnt sump water werc to leak back to RWST during a design basis accident
        -Tested valves already included ln testing program      program
~UCTaic Back.Leakage to Refueling Water Storage Tank r
          -Added five valves pcr unit to testing program       o Implemented new procedure:
issue resolved o Included fiowpaths in in-service testing program o Implemented new procedure: seat leakage testing ofvalves at each refueling outage to ensure < 10 gpm total leakage Back-Leakage to Refueling Water Storage Tank A~nal sla
        -Test  results                                          seat leakage testing of valves*at each rcfucling outage to ensure < 10 gpm total leakage
'our back flowpaths
-Leak testing in place fortwo ofthe four paths
-Two paths not included in in.service testing program alcawasr cUcvalc Back-Leakage to Refueling Water Storage Tank Back4.eakage to Refueling Water Storage Tank Actions o Testing progranr results
-Tested valves already included ln testing program
-Added five valves pcr unit to testing program
-Test results issue resolved o Included flowpaths in in-scrvice testing program o Implemented new procedure:
seat leakage testing ofvalves*at each rcfucling outage to ensure < 10 gpm total leakage


A enda Introduction                           Reclrculatfon Sump Venting Jcb Kln            Nt Rcdrcutatton Sump lnwntory N4   KS ID Switchover Procedure       Con irmato      Action Letter issue W
Jcb Kln Paul Scboepf Stan Farlow Joel Wlebe Jim Kobyra AlBlind Cene Rtzpatrtctt A enda Introduction Nt Rcdrcutatton Sump lnwntory N4 KS IDSwitchover Procedure W
NX   Rcdrculatton Sum Vcntins         May not be adequate venting of air underneath the roof 'f Paul Scboepf              ibrous   tc   n   n nmcnt           the containmcnt building recirculation sump
NX Rcdrculatton Sum Vcntins ibrous tc n
                  <<S   36Jiour Coowown tte RHR Suction Valve AutoClose
n nmcnt
                  <<5 Compressed AirOwrpressure         Commitment Stan Farlow        <<p instrument Unccrtatnty Joel Wlebe Venting will be rcinstallcd in the recirculation sump Short Term Asscssmcnt Dcvelopmcnt Jim Kobyra        Short Terai Assessment Results           cover. The design will incorporate forcignmaterial Al Blind          Additional Assurance of OperabNty of      exclusion requirements for thc sump Systems Cene Rtzpatrtctt  Conduslon ReclrculaVon Sump Venting                              Reclrculatlon Sump Venting
<<S 36Jiour Coowown tte RHR Suction Valve AutoClose
  /ssue resolved                                         ~nial sls Reinstalled recirculation sump cover vents with         '977/78     Alden Labs study a design that prevents foreign material from        o Vent holes added to sump cover in 1919 as an entering through thc holes                            enhancement Reclrculatlon Sump Venting                             ReclrculaVon Sump Venting
<<5 Compressed AirOwrpressure
~nal~ls                                                 ~ctlons Holes plugged in4996 and 1997 to address           I/4" ~  Venting reinstalled foreign material exclusion concern                 o Design   now incorporates foreign material exclusion provisions
<<p instrument Unccrtatnty Short Term Asscssmcnt Dcvelopmcnt Short Terai Assessment Results Additional Assurance ofOperabNty of Systems Conduslon Reclrculatfon Sump Venting Con irmato Action Letter issue May not be adequate venting ofair underneath the roof
'f the containmcnt building recirculation sump Commitment Venting willbe rcinstallcd in the recirculation sump cover. The design willincorporate forcignmaterial exclusion requirements for thc sump ReclrculaVon Sump Venting
/ssue resolved Reinstalled recirculation sump cover vents with a design that prevents foreign material from entering through thc holes Reclrculatlon Sump Venting
~nial sls
'977/78 Alden Labs study o Vent holes added to sump cover in 1919 as an enhancement Reclrculatlon Sump Venting ReclrculaVon Sump Venting
~nal~ls Holes plugged in4996 and 1997 to address I/4" foreign material exclusion concern
~ctlons
~ Venting reinstalled o Design now incorporates foreign material exclusion provisions


A enda ReclrculaVon Sump VenVng                           Cene Htspatrlck      Introduction Jab Moesccd        II    Rcdrcutattoa Sump Inventory Issue resolved                                                           I4 ES ID Switchover Procedure Ia Backtcakaee io RWST recirculation sump cover vents with
ReclrculaVon Sump VenVng Issue resolved
                  'einstalled a design that prevents foreign material from     Paul Schoe r        IT    Hbrous Material In Contatnmcut entering through the holes I3       hour Cooidowu RHR Suction Valve Auto@toss Is Comprssscdhlrovcrprcssurc Stan Farlow        Iti Instrument Uncertainty Jod Wtsbc          Short Term Asscssmeut Dcvdopmeut Jim Kobyra          Short Term hsscssmcnt Results Al Blind            hddt ttouat Assurauco of Operability or Systams Ceno Hispatrlck    Coodusiou Fibrous Materfal In Containment                       Fibrous Material In Containment Con irmalo       Aclion Lerrer issue                   ~nal  sos Fibrous material in containment building               'nstallation of cable tray fire stops
'einstalled recirculation sump cover vents with a design that prevents foreign material from entering through the holes Stan Farlow Jod Wtsbc Jim Kobyra AlBlind Ceno Hispatrlck I3 hour Cooidowu RHR Suction Valve Auto@toss Is Comprssscdhlrovcrprcssurc Iti Instrument Uncertainty Short Term Asscssmeut Dcvdopmeut Short Term hsscssmcnt Results hddt ttouat Assurauco ofOperability or Systams Coodusiou A enda Cene Htspatrlck Introduction Jab Moesccd II Rcdrcutattoa Sump Inventory I4 ES IDSwitchover Procedure Ia Backtcakaee io RWST Paul Schoe r IT Hbrous Material In Contatnmcut Fibrous Materfal In Containment Fibrous Material In Containment Con irmalo Aclion Lerrer issue Fibrous material in containment building Commllmenl Removal offibrous material from containmcnt building that could clog the recirculation sump willbe complctcd
                                                            -Fibrous material used ai "damming material" Commllmenl                                                  -Installation specification did not require removal of material in containment Removal of fibrous material from containmcnt building that could clog the recirculation sump willbe complctcd Fibrous Material In Containment                         Fibrous Material In Containment Acllons                                                   cllons
~nal sos
'emoved       fibrctus damming material               'eviewed      operating experience and regulatory
'nstallation ofcable tray fire stops
    -l2 locations in Unit I                               information IS locations In Unit 2                            o Performed extensive walkdowns
-Fibrous material used ai "damming material"
    -Annulus and lnstnuncnt Room                       o Identified and addressed other fibrous insulation
-Installation specification did not require removal of material in containment Fibrous Material In Containment Fibrous Material In Containment Acllons cllons
'emoved fibrctus damming material
-l2 locations in Unit I IS locations In Unit2
-Annulus and lnstnuncnt Room
'eviewed operating experience and regulatory information o Performed extensive walkdowns o Identified and addressed other fibrous insulation


A enda Fibrous Naterfaf ln Contafnment                         Cene Fttspatrtck   5n trod uction Jcb Ktnssced       Nt   Redrculation Sump Inventory Issue resolved                                                              tt4   ES 13 Switchover Procedure
Fibrous Naterfaf ln Contafnment Issue resolved Removed fibrous insulation material from containment building that could clog thc recirculation sump Cene Fttspatrtck Jcb Ktnssced Paul Scboc f Stan Fart ow Joel Wtcbc Jim Kobyrn hl Blind
                                                                            <<S ~ Bacldcakaae to RWST Removed fibrous insulation material from                                    <<3   Recirculation Sump Ycnttna containment building that could clog thc              Paul Scboc  f    trt   Rbrous tatcrfsl tn Containmcnt
" Cene Htspatrtck A enda 5n troduction Nt Redrculation Sump Inventory tt4 ES 13 Switchover Procedure
                                                                            <<3   3@hour Coo!down recirculation sump                                                                              ve on ttS   Comprcsscd Airoverpressure Stan Fart ow      ttp   instrument Uncertainty Joel Wtcbc        Short Term Assessment Development Jim Kobyrn        Sbort Tenn Assasment Rauits hl Blind          Addldonal Assurance of Operability of Systems
<<S
                                                        "
~ Bacldcakaae to RWST
Cene Htspatrtck    Conduston 36.Hour Coofdown                                           36 Hour Cooldown Can mmata         Action Letter issue                       Issue resolved Calculation needs to be performed that shows one train     Analyses completed to demonstrate 36-hour of cooling water system is surtcient to rcmove the         cooldown capability with onc train of cooling units from service Commitment Analyses will bc performed that willdemonstrate the capability to cooldown the units consistent with the design bash requiranents and necessary changes to procedures willbc completol 36 Hour Cooldown                                           36.Hour Cooldown
<<3 Recirculation Sump Ycnttna trt Rbrous tatcrfsl tn Containmcnt
~nal sls                                                  ~nial sls o Original Westinghouse performance                       '6    hour cooldown analysis revisited for requirement for normal cooldown                           Unit 2 uprate
<<3 3@hour Coo!down on ve ttS Comprcsscd Airoverpressure ttp instrument Uncertainty Short Term Assessment Development Sbort Tenn Assasment Rauits Addldonal Assurance ofOperability of Systems Conduston 36.Hour Coofdown 36 Hour Cooldown Can mmata Action Letter issue Calculation needs to be performed that shows one train ofcooling water system is surtcient to rcmove the units from service Commitment Analyses willbc performed that willdemonstrate the capability to cooldown the units consistent with the design bash requiranents and necessary changes to procedures willbc completol Issue resolved Analyses completed to demonstrate 36-hour cooldown capability with onc train ofcooling 36 Hour Cooldown 36.Hour Cooldown
    -Plant canbe eoolcd down in 36 hours with onc              -Design inspection    issue: discrepancy in CCW heat train ofcooling                                           exchanger type assumed in uptate cooldown
~nal sls o Original Westinghouse performance requirement fornormal cooldown
    -Consequence: cotnponcnt cooling water supply               calculation temperature can reach l20F during this evolution         -Original cooldown calculation contained heat exchanger modeling error
-Plant canbe eoolcd down in 36 hours withonc train ofcooling
-Consequence:
cotnponcnt cooling water supply temperature can reach l20F during this evolution
~nial sls
'6 hour cooldown analysis revisited for Unit2 uprate
-Design inspection issue: discrepancy in CCW heat exchanger type assumed in uptate cooldown calculation
-Original cooldown calculation contained heat exchanger modeling error


36 Hour Cooldown                                      36-Hour Cooldown Actions                                                Actions
36 Hour Cooldown Actions
~ Demonstrated       thermal hydraulic capability for e Component     cooling water design temperature a 36-hour cooldown                                    increased to 120'F for single train cooldown via deign change
~ Demonstrated thermal hydraulic capability for a 36-hour cooldown 36-Hour Cooldown Actions e Component cooling water design temperature increased to 120'F for single train cooldown via deign change
                                                            -Equipment evaluations
-Equipment evaluations
                                                            -Piping evaluations
-Piping evaluations
                                                            -Operating procedure change gmnaur 36.Hour Cooldown                                       36 Hour Cooldown ui ment evaluation                                     ui ment evaluation cont.
-Operating procedure change gmnaur 36.Hour Cooldown 36 Hour Cooldown ui ment evaluation Flow balance criteria increased slightly based on NSSS vendor recommendation to preserve heat trarisfer capability during 36-hour cooldown
Flow balance criteria increased slightly based on   e Planned non-Technical    Specification radiation NSSS vendor recommendation to preserve heat             monitor replacement rescheduled - location of trarisfer capability during 36-hour cooldown           new monitors in lower temperature location
-Safety injection pumps
    -Safety injection pumps
-Centrifugal charging pumps
    -Centrifugal charging pumps
-Residual heat removal pumps Operability not challenged forprevious fiow limits based on GL 91-18
    -Residual heat removal pumps Operability not challenged for previous fiow limits based on GL 91-18                   ~tt 36.Hour Cooldown                                       36-Hour Coofdown fssue resolved
~tt ui ment evaluation cont.
                  ~ e Four minor pipe hanger moditications due to           Confirmed 36-hour cooldown capability with one higher stresses associated with increased               train of cooling water temperatures
e Planned non-Technical Specification radiation monitor replacement rescheduled - location of new monitors in lower temperature location 36.Hour Cooldown 36-Hour Coofdown
~ Change driven by desire to handle 36-hour cooldown as a "nornial" condition - no changes required ifhandled as emergency condition
~ e Four minor pipe hanger moditications due to higher stresses associated with increased temperatures
~ Change driven by desire to handle 36-hour cooldown as a "nornial" condition - no changes required ifhandled as emergency condition fssue resolved Confirmed 36-hour cooldown capability with one train ofcooling water


0 0
0 0


A enda Gene Htspatrtek     introduction                            Residual Heat Removal Suction Vahte Auto@lose Jeb Ktnaseed       Nt Recirculation Sump inventory
Gene Htspatrtek Jeb Ktnaseed Paul Schoepf Stan Fartow Joel Wtebe Jim Kobyra At Blind Cene Fitzpatrick A enda introduction Nt Recirculation Sump inventory
                    <<4     ES 13 Switchover Procedure       Con u moto      Action Letter issue ea     Baetdeakaae to RWST tran   Reetreutatton Sump Venttna       Conflicts bctwcen operating procedures and Tcchnical Paul Schoepf        <<1- Fibrous htaterhl in Containment       S pecilications for residual heat removal system Commitment ttd   R16t Suction Yatve Au~ose Ns       ompressed Air   erpressure   A technical specification change to allow operation in Stan Fartow        ep    instrument Uncertainty            Mode 4 with the residual heat removal suction valves Joel Wtebe          Short Term Asussment Development open and power removed is being processed.
<<4 ES 13 Switchover Procedure ea Baetdeakaae to RWST tran Reetreutatton Sump Venttna
Jim Kobyra          Short Term Assessment Results At Blind            Additional Assurance of Operability of    Approval of this change by NRC will bc required Systems                                prior to restart Cene Fitzpatrick    Co net uslon                                                                                ~~ rstrra assrewasr le Residual Heat Removal Suction VaNe Auto@lose             Residual Heat Removal Suction Valve Auto@lose Issue resolved Technical Specification amendment approved               'unction dcsigncd       originally to protect residual heat removal system from ovcrpressurc
<<1-Fibrous htaterhl in Containment ttd R16t Suction Yatve Au~ose Ns ompressed Air erpressure ep instrument Uncertainty Short Term Asussment Development Short Term Assessment Results Additional Assurance ofOperability of Systems Co net uslon Residual Heat Removal Suction Vahte Auto@lose Con u moto Action Letter issue Conflicts bctwcen operating procedures and Tcchnical Specilications forresidual heat removal system Commitment A technical specification change to allow operation in Mode 4 with the residual heat removal suction valves open and power removed is being processed.
                                                            'perational practice dcfcats thc auto-closure whcncvcr valves are open
Approval ofthis change by NRC willbc required prior to restart
                                                              -Concern for loss ofdecay heat removal
~~ assrewasr rstrra le Residual Heat Removal Suction VaNe Auto@lose Residual Heat Removal Suction Valve Auto@lose Issue resolved Technical Specification amendment approved
                                                              -Low temperature  ovetpressure system operation e Impact on Tcchnical Specifications and Final Safety Analysis Report not identified Residual Meat Removal Suction Vahte Auto@lose             Residual Heat Removal Suction Valve Auto@lose Actions                                                   Issue resolved
'unction dcsigncd originallyto protect residual heat removal system from ovcrpressurc
'ubmitted Technical           Specification amendmcnt     Tcchnical Specification amendment approved
'perational practice dcfcats thc auto-closure whcncvcr valves are open
    -Removes surveillance requirement for val ve a~losure
-Concern forloss ofdecay heat removal
    -Takes credit for low temperature ovetprcssure system protection for raided heat removal system
-Lowtemperature ovetpressure system operation e Impact on Tcchnical Specifications and Final Safety Analysis Report not identified Residual Meat Removal Suction Vahte Auto@lose Residual Heat Removal Suction Valve Auto@lose Actions
    -Operating procedures, UFSAR and Tcchnical Specifications aligned
'ubmitted Technical Specification amendmcnt
-Removes surveillance requirement for valve a~losure
-Takes credit for low temperature ovetprcssure system protection forraided heat removal system
-Operating procedures, UFSAR and Tcchnical Specifications aligned Issue resolved Tcchnical Specification amendment approved
 
Gene Fitspatrick Jeb IQngseed Paul Sehoe f Sian Fartow Joel Wiebe Jim Kobyra AlBlind Gene Htspatrtck A Nnda introduction Nt Recirculation Sump fnventosy Ns ES IDSwltebowr Procedure Na Baetdeakage to RWST Ng Recirculation Sump Venting Fibrous Material in Containment NJ 3ts hour Cooldown V
N5 Com ressed AlrOve ressure Np nstrument neerta nry Short Term Assessment Dewtopment Short Term Assessment Results AddMonat Assurance ofOperabpdty of Systems Cond uston Compressed AlrOverpressure Con irmato Action Letter issue Adequacy ofpressure protection forsome components in thc compressed air system from equipment malfunction Commitment Ovcrprcssurc protection willbe provided downstream of thc 20 psig, 50 psig, and 85 psig control air regulators to mitigate the effects ofa postulated failed regulator Compressed AlrOverpressure Issue rei alved
'nstalled redundant, safety-grade reliefvalves and eliminated ovcrpressure potential o Eliminated potential forcommon-mode failure Compressed AlrOverpressure A~nal sls o System design
-Non-safety related
-"Failsafe" on loss ofair
-Activevalves change state on safety grade solenoid valve actuation
-Ovcrprcssurc protection forthe system but not for system loads Compressed AlrOverpressure A~nal sls
'nitial findings'.
-Potential common-mode failure ofequipment resulting from ovcrpressurization
-Many coinponents not rated forfullinitial pressure
-Component failures anticipated Compressed AlrOverpressure Issue resolved
'nstalled redundant safety grade reliefvalves and eliminated overprcssure potential o Eliminated potential forcommon-mode failure


A Nnda Gene Fits patrick  introduction                            Compressed AlrOverpressure Jeb IQngseed        Nt Recirculation Sump fnventosy Ns    ES ID Swltebowr Procedure        Con irmato      Action Letter issue Na    Baetdeakage to RWST Ng    Recirculation Sump Venting      Adequacy of pressure protection for some components in Paul Sehoe  f            Fibrous Material in Containment    thc compressed air system from equipment NJ    3ts hour Cooldown                  malfunction V
0
Commitment N5    Com ressed  AlrOve  ressure Sian Fartow        Np    nstrument neerta nry            Ovcrprcssurc protection will be provided downstream of Joel Wiebe          Short Term Assessment Dewtopment thc 20 psig, 50 psig, and 85 psig control air regulators Jim Kobyra          Short Term Assessment Results Al Blind            AddMonat Assurance of Operabpdty of to mitigate the effects of a postulated failed regulator Systems Gene Htspatrtck    Cond  uston Compressed        AlrOverpressure                        Compressed AlrOverpressure Issue rei alved                                          A~nal sls
  'nstalled    redundant, safety-grade relief valves      o System design and eliminated ovcrpressure potential                    -Non-safety related o  Eliminated potential for common-mode failure              -"Fail safe" on loss of air
                                                              -Active valves change    state on safety grade solenoid valve actuation
                                                              -Ovcrprcssurc protection for the system but not for system loads Compressed        AlrOverpressure                        Compressed AlrOverpressure A~nal sls                                                Issue resolved
  'nitial findings    '.                                  'nstalled    redundant safety grade relief valves
    -Potential common-mode failure of equipment              and eliminated overprcssure potential resulting from ovcrpressurization                  o Eliminated potential for common-mode failure
    -Many coinponents not rated for full initial pressure
    -Component failures anticipated


0 A endg Cene Htspatrlck     Introducdon                             Instrument UncertaInty Jcb Kingsccd       gl     Rcdrcutadon Sump Inventory gg KS ID Switchover Procedure         Con trmoto          Action Lc'tter Issue gg Backlcakagc to R%ST g2     Rcdrculatton Sump Venting       Instrument uncertainties incorporate! into proccdurcs Paul Schoepl       ttr Hbrous Material ln Containmcnt         and analyses g3     3&ear CooMown                   Comnritment ttd   RHR Suction YalvchutoClose Emergency procedures and other important-to-safety Stan Fartow                Instrument uncertainty              procedures, calculations, or analyses willbc rcvicwed o      bc              rt crm Asscssmcnt          opmcnt    to account for instrument uncertainties Jim Kobyra          Short Term Asscssmcnt Results          lt is understood that resolution of this issue requires a AI Blind            Additkinal Assurance of Operability of    long-tenn program continuing beyond restart Systems Cene Htzpatrick    Conclusion                                                                                    Qmaicatr Instrument UncertaInty                                   Instrument UncertaInty 4~nal sis                                                 Issue resolution
Stan Fartow Instrument uncertainty o
  'reas     for improvement                               o Program elements
bc Jim Kobyra AIBlind rt crm Asscssmcnt opmcnt Short Term Asscssmcnt Results AdditkinalAssurance ofOperability of Systems Cene Htzpatrick Conclusion A endg Cene Htspatrlck Introducdon Jcb Kingsccd gl Rcdrcutadon Sump Inventory gg KS IDSwitchover Procedure gg Backlcakagc to R%ST g2 Rcdrculatton Sump Venting Paul Schoepl ttr Hbrous Material ln Containmcnt g3 3&ear CooMown ttd RHR Suction YalvchutoClose Instrument UncertaInty Con trmoto Action Lc'tter Issue Instrument uncertainties incorporate! into proccdurcs and analyses Comnritment Emergency procedures and other important-to-safety procedures, calculations, or analyses willbc rcvicwed to account for instrument uncertainties lt is understood that resolution ofthis issue requires a long-tenn program continuing beyond restart Qmaicatr Instrument UncertaInty Instrument UncertaInty 4~nal sis
    -Control usc of Instrument    uncertainties in
'reas for improvement
                                                                -Control use of uncertainties calculations, procedures, and analysis                       ~ Ahninistrative control
-Control usc ofInstrument uncertainties in calculations, procedures, and analysis
    -Improve control of uncertainty calculation inputs             ~ Paramctcis used  to assure Tcchnical Spedgcation
-Improve control ofuncertainty calculation inputs
    -Process measurement error ca! culations                         ccmp4ancc
-Process measurement error ca!culations
    -Provide training to other disciplines                         'ntegrate with nNmal operating procohimupgrade
-Provide training to other disciplines
    -Increase number of parameters under formal                      program that was committed to!n our NRC control                                                        submittal AEFNRC I260H Instrument UncertaInty                                   Instrument UncertaInty
-Increase number ofparameters under formal control Issue resolution o Program elements
'rogram       ciemontg                                   o Instrument uncertainties under           formal control
-Control use ofuncertainties
    -Plant specific methodology                              -Reactor trip and   engineered safety feature actuation
~ Ahninistrative control
        'ethod    to calculate Instmmcnt unccrtaindcs            system sctpdnts Rcfcicnce NRC Branch Tcchnical Posidcn              -Emergency and abnormal opcradng procohucs HICB-12                                            -Operations, surveillance and test procedures
~ Paramctcis used to assure Tcchnical Spedgcation ccmp4ancc
    -Review existing calculations                            -Plant perfamancc     data used in analysis w Ebminatc rcplicue caicidations                      -Scipoints for plant alarms assodatcd with moaitcdng
'ntegrate with nNmal operating procohimupgrade program that was committed to!n our NRC submittal AEFNRC I260H Instrument UncertaInty Instrument UncertaInty
        ~ NRC Inspection raccdure 93807                          Tcchnical Specigcation con pl lance Tralnmg                                        X
'rogram ciemontg
-Plant specific methodology
'ethod to calculate Instmmcnt unccrtaindcs Rcfcicnce NRC Branch Tcchnical Posidcn HICB-12
-Review existing calculations w Ebminatc rcplicue caicidations
~ NRC Inspection raccdure 93807 Tralnmg X
o Instrument uncertainties under formal control
-Reactor trip and engineered safety feature actuation system sctpdnts
-Emergency and abnormal opcradng procohucs
-Operations, surveillance and test procedures
-Plant perfamancc data used in analysis
-Scipoints forplant alarms assodatcd withmoaitcdng Tcchnical Specigcation con pllance


lnstmment Uncertainty                                  Instrtrment Uncertainty Actions corn leted                                       ctions cpm leted cont.
lnstmment Uncertainty Actions corn leted
~ Reviewed level instrumentation for velocity eifcct   ~ Generated administrative    control procedures
~ Reviewed level instrumentation forvelocity eifcct
~ Reviewed and rcviscd emergency operating             ~ Reviewed EOP sctpoint documentation procedures for switchover to recirculation          ~ Reviewed license bases o Reviewed and rcviscd Technical Specification        ~ Addressed related non-programmatic unrcsolvcd surveillance procedure used by operations              issues from the inspection report
~ Reviewed and rcviscd emergency operating procedures forswitchover to recirculation o Reviewed and rcviscd Technical Specification surveillance procedure used by operations
'enerated      parameter list for Technical            ~ Complctcd plant spcciific methodology manual Specification compliance A enda Instrlrment Uncertainty                            Gene Htspatrkk       introduction Jcb Kluasccd         Nt Recirculation Suaip inventory ahedule                                                                  N4     ES lD Switchover Procedure SS     Backteakaae to RWSP Complete all reviews and calculations in 1998                          <<S   Recirculation Sump Vcndng Paul Scbocpr         N Hbrous titatcrtat ln Contalnuicnt SS   36.hour Cooldosrn e6   RHR Suction Valve Auto%lose Ns   Coin pressed AirOvcrprcssure Stan Fartovr         09 tnsrrumcot ncertain Joel Wicbe           Short Term Asscssincnt Dcvciopiucnt lla                     rt erin       aleut     is Al Blind            Additional Assurance or Operability or Ssstccas Gene Htspatrtck     Conclusion Development       of Short      Term Assessment       Development of Short Tenn Assessment Corrective action process                            o Purpose     of short term assessment
'enerated parameter list forTechnical Specification compliance Instrtrment Uncertainty ctions cpm leted cont.
  -Investigatiori of issue                              To determine whether similar issues may exist
~ Generated administrative control procedures
  -Root cause    analy'sis                              in other safety systems, and ifthey do, whether
~ Reviewed EOP sctpoint documentation
  -Correction of issue                                  they affect system operability
~ Reviewed license bases
  -Action to prevent    recurrence
~ Addressed related non-programmatic unrcsolvcd issues from the inspection report
~ Complctcd plant spcciific methodology manual Instrlrment Uncertainty ahedule Complete all reviews and calculations in 1998 A enda Gene Htspatrkk introduction Jcb Kluasccd Nt Recirculation Suaip inventory N4 ES lDSwitchover Procedure SS Backteakaae to RWSP
<<S Recirculation Sump Vcndng Paul Scbocpr N
Hbrous titatcrtat ln Contalnuicnt SS 36.hour Cooldosrn e6 RHR Suction Valve Auto%lose Ns Coin pressed AirOvcrprcssure Stan Fartovr 09 tnsrrumcot ncertain Joel Wicbe Short Term Asscssincnt Dcvciopiucnt lla rt erin aleut is AlBlind Additional Assurance or Operability or Ssstccas Gene Htspatrtck Conclusion Development ofShort Term Assessment Corrective action process
-Investigatiori ofissue
-Root cause analy'sis
-Correction ofissue
-Actionto prevent recurrence Development ofShort Tenn Assessment o Purpose ofshort term assessment To determine whether similar issues may exist in other safety systems, and ifthey do, whether they affect system operability


Development     of Short    Tenn Assessment          Development of Short Tenn Assessment Independent root cause analysis teams               'enior management          review of causes (CAL issues l-8)                                       -CAL items 1-8
Development ofShort Tenn Assessment Independent root cause analysis teams (CAL issues l-8)
    -Root cause analyst                                   -Causes
-Root cause analyst
    -Outside technical analyst(s)                         -Potential impact on operability
-Outside technical analyst(s)
    -Individual knowledgeable of issue                    -Identified and   discussed implications Result: Five issues with potential to impact operability Development     of Short    Tenn Assessment          Development of Short Tenn Assessment o Root cause   of other design                         o Senior management review of causes inspection issues
-Individual knowledgeable ofissue Development ofShort Tenn Assessment
    -Root cause analyst                                   -Compared to CAL issue causes and short tenn
'enior management review ofcauses
    -Outside technical analyst(s)                           assesQllcnt o Allroot causes additionally reviewed                 o Result by independent senior industry peers                       -No additional issues were identified
-CALitems 1-8
                                                          -Some specific actions added A enda Development     of Short    Tenn Assessment       Ceno Htspatrtck    Introdncdon Job IQnesccd        et    Rcrtrcutatlon Sump lnwntory o Issues with potential to impact operability                               ES ID Ssiltcbovcr Procedure
-Causes
  -Analyses with ptors or incorrect assumptions                       ea   Backtcakaao to RWST
-Potential impact on operability
                                                                        <<3   Rcrtrcutadon Sump Ycndng
-Identified and discussed implications Result: Five issues with potential to impact operability Development ofShort Tenn Assessment o Root cause ofother design inspection issues
  -Non-safety related systems failure modes        Paul Schocpf       N Hbrous htatcrtat ln Containment
-Root cause analyst
  -Lcvcl instrument bias duc to Bcrnoulli effec                        e3   36@our CooMosrn
-Outside technical analyst(s) o Allroot causes additionally reviewed by independent senior industry peers Development ofShort Tenn Assessment o Senior management review ofcauses
  -Containmcnt sump attribute not prescrvcd                                  RHR Suction Yatvo AuorQosc
-Compared to CAL issue causes and short tenn assesQllcnt o Result
                                                                        <<5   Compressed hlrovcrprcssure
-No additional issues were identified
  -Improper application ofsingle failure criteria, Stan Fartovr       ep   Instrument Uncertainty Itl           cnt Jins Kobyra         Short Term Asscssmcnt Results I                         rance o para     iy or Systems Ceno Hts patrtck    Conduslon
-Some specific actions added Development ofShort Tenn Assessment o Issues with potential to impact operability
-Analyses withptors or incorrect assumptions
-Non-safety related systems failure modes
-Lcvcl instrument bias duc to Bcrnoullieffec
-Containmcnt sump attribute not prescrvcd
-Improper application ofsingle failure criteria, A enda Ceno Htspatrtck Introdncdon Job IQnesccd et Rcrtrcutatlon Sump lnwntory ES IDSsiltcbovcr Procedure ea Backtcakaao to RWST
<<3 Rcrtrcutadon Sump Ycndng Paul Schocpf N
Hbrous htatcrtat ln Containment e3 36@our CooMosrn RHR Suction Yatvo AuorQosc
<<5 Compressed hlrovcrprcssure Stan Fartovr ep Instrument Uncertainty Itl cnt Jins Kobyra Short Term Asscssmcnt Results I
rance o para iyor Systems Ceno Htspatrtck Conduslon


0 0
0 0


Short Tenn Assessment Results                                 Short Term Assessment Results c Engineering issues                                         'esolution      process I. Analyses with errors or incorrect assumptions             -Scope and deliverable
Short Tenn Assessment Results Short Term Assessment Results c Engineering issues I. Analyses with errors or incorrect assumptions
: 2. Non-safety related systems failure modes                 -Operations and engineering management
: 2. Non-safety related systems failure modes
: 3. Level instrument bias duc to Bcrnoulli effec             -Initial results Indicated further expansion
: 3. Level instrument bias duc to Bcrnoulli effec
: 4. Some contalnmcnt attributes not preserved                 -Closure defined documented reports S. Improper application of single failure criteria Short Tenn Assessment Isragrem                               Short Term Assessment Results- Issue Nf
: 4. Some contalnmcnt attributes not preserved S. Improper application ofsingle failure criteria
                                                              ~ Analyses   crmts or incorrect assumptions 10 root causes      ~nfinn safety analyses     of record with petanttat      -Evaluate heat exchanger modeling opcrabmty kiipact
'esolution process
                                                                -Dctcrmine extent ofcalculation problems Exit&0 kneAdge ISSR, Iavdlsncas, procedures, ate.)
-Scope and deliverable
Short Tenn Assessment Results- Issue O1                     'hort Tenn Assessment               Results- Issue O1
-Operations and engineering management
~ Confirmation ofanalyses ofrecord                           'afety-related      heat exchangers    will
-Initialresults Indicated further expansion
  -Seven pcrsoir team to the NSSS offic                       perform their function
-Closure defined documented reports Short Tenn Assessment Isragrem 10 root causes withpetanttat opcrabmty kiipact Exit&0kneAdge ISSR, Iavdlsncas, procedures, ate.)
  -IWcpthrcvtcw df Unit I gt 2 analyses                       -Residual heat removal heat exchanger
Short Term Assessment Results-Issue Nf
  -Minor findings- Interface assumptions                       -Containment spray heat exchanger
~ Analyses crmts or incorrect assumptions
  -Analyses of record- conservative                           -Component cooling water heat exchanger
~nfinn safety analyses ofrecord
  -ECCS, CTS, RHR, Containment, AFW, CCW                       -Spent fuel pool heat exchanger
-Evaluate heat exchanger modeling
                                                                -EDG jacket water and lube oil heat cxchangcrs
-Dctcrmine extent ofcalculation problems Short Tenn Assessment Results-Issue O1
                                                                    ~ Counter cow versus TKhfA E
'hort Tenn Assessment Results-Issue O1
                                                                    ~ Csiculadoas revised
~ Confirmation ofanalyses ofrecord
-Seven pcrsoir team to the NSSS offic
-IWcpthrcvtcwdfUnit I gt 2 analyses
-Minorfindings-Interface assumptions
-Analyses ofrecord-conservative
-ECCS, CTS, RHR, Containment, AFW,CCW
'afety-related heat exchangers will perform their function
-Residual heat removal heat exchanger
-Containment spray heat exchanger
-Component cooling water heat exchanger
-Spent fuel pool heat exchanger
-EDGjacket water and lube oil heat cxchangcrs
~ Counter cow versus TKhfAE
~ Csiculadoas revised


Short Tenn Assessment Results - Issue &#xb9;1         Short Term Assessment Results -Issue &#xb9;1
Short Tenn Assessment Results - Issue &#xb9;1 Short Term Assessment Results -Issue &#xb9;1
'ssuring     confidence   of AEP calculations     'ssuring       confidence ofAEP calculations Total Reviewed            ~ Recent calculation program efforts Electrical          273        119                -LBPRP Mechanical          1529      6                  -MOVcalculations
'ssuring confidence ofAEP calculations Total Reviewed Electrical 273 119 Mechanical 1529 6
                                                        -Electrical distribution calculations Instrument Structural 330 2410 157 294
Instrument 330 157 Structural 2410 294 Other 526 6
                                                      -I&C Instrument uncertainty calculations
5068 632
                                                  ~ Peer   review Other              526        6                  -l71 Design Inspection calculations 5068      632                -20 functional calculations Short Tenn Assessment Results - Issue         &#xb9;1 Short Term Assessment Results- Issue &#xb9;1
'ssuring confidence ofAEP calculations
'EP functional calculations                       'eer Review Total    Reviewed            -Team Inspection- Management involvement Electrical          32        3                    -Addition to thc vcriTication Mechanical          79        16 Safety'related systems
~ Recent calculation program efforts
                                                      -Emergency core cooling water Other              28        3
-LBPRP
                                                      -Essential service water 139      22                  -Containment spray
-MOVcalculations
                                                      -Auxiliatyfccdwatcr
-Electrical distribution calculations
                                                      -Eicctrical distribution
-I&CInstrument uncertainty calculations
                                                      -Chemical volume and control Short Term Assessment Results- Issue &#xb9;1           Short Term Assessment Results -Issue &#xb9;1
~ Peer review
~ Peer review results                               We have confidence that AEP calculations are
-l71 Design Inspection calculations
  -Administrative issues                           sufficiently conservative to assure system
-20 functional calculations Short Tenn Assessment Results - Issue &#xb9;1 Short Term Assessment Results-Issue &#xb9;1 Electrical Mechanical Other
  -Technical quest'tons raised (10)                 operability
'EP functional calculations Total Reviewed 32 3
  -No effect on system   operability             ~ Achieved through
79 16 28 3
                                                      -'The peer review results
139 22
                                                      -Our reconstitution   programs
'eer Review
                                                      -Conclusion ofsafety system functional inspections performed on the ESW and electrical distribution aystctlls
-Team Inspection-Management involvement
-Additionto thc vcriTication Safety'related systems
-Emergency core cooling water
-Essential service water
-Containment spray
-Auxiliatyfccdwatcr
-Eicctrical distribution
-Chemical volume and control Short Term Assessment Results-Issue &#xb9;1 Short Term Assessment Results -Issue &#xb9;1
~ Peer review results
-Administrative issues
-Technical quest'tons raised (10)
-No effect on system operability We have confidence that AEP calculations are sufficiently conservative to assure system operability
~ Achieved through
-'The peer review results
-Our reconstitution programs
-Conclusion ofsafety system functional inspections performed on the ESW and electrical distribution aystctlls


Short Term Assessment Results-Issue                         &#xb9;2 Short Tenn Assessment Results - Issue             &#xb9;2
Short Term Assessment Results-Issue &#xb9;2 Short Tenn Assessment Results - Issue &#xb9;2
'on-safety         related system interface                   'on-safety      related system evaluations
'on-safety related system interface
  -Effect on safety     related system performance               -Modified control air system
-Effect on safety related system performance
  -Selection process for rcvicw                                  -Reactor control system
-Selection process forrcvicw
        ~ Safety &, nan~ety related systems
~ Safety &,nan~ety related systems
                                                                  -Condcnsatc/ fcedwaterrmain stcam
. 'ignigcauce ofinterface withsafety related systems
    . 'ignigcauce of interface with safety  related systems     -Circulating water
~ Potentially unicvtcwed tost/failure modes
        ~ Potentially unicvtcwed tost/failure modes             ~ -Non-essential service water
-Comparison with maintenance rule risk significance
  -Comparison with maintenance rule risk                          .Electricaldistribution significance
'on-safety related system evaluations
                                                                  -Pressuriscr heaters u No adverse effects Short Tenn Assessment Results - Issue                       &#xb9;2 Short Tenn Assessment Results - Issue             &#xb9;3
-Modifiedcontrol air system
'onclusion                                                     e Appropriate application of process
-Reactor control system
  -Postulated failures of non.safety related systems             measurement effects do not affect safety system operability                     -Team approach with industry consultants
-Condcnsatc/
                                                                  -Compared AEP engineering guides to industry ttandards
fcedwaterrmain stcam
                                                                  -Appropriate process measuremcnt effect Bemoulli effect on level instrumentation
-Circulating water
                                                                  -Non.standard process location
~
                                                                  -No guidance     in engineering guides Short Tenn Assessment Results- Issue                       &#xb9;3 Short Tenn Assessment Results - Issue             &#xb9;3 Bcmoulli effect on level instrumentation                    e  Bemoulli effect on level instrumentation
-Non-essential service water
  -Allsafety relet@I level instruments cval usted                -idcC <<ngineering guide rcviscd
.Electricaldistribution
  -Condensate storage tank                                       -Calculations account foi the flow induced effects
-Pressuriscr heaters u No adverse effects Short Tenn Assessment Results - Issue &#xb9;2 Short Tenn Assessment Results - Issue &#xb9;3
      'fcct is present but iaslgnigcaut                             on process level instruments
'onclusion
  -Mid-loop RCS
-Postulated failures ofnon.safety related systems do not affect safety system operability e Appropriate application ofprocess measurement effects
      'tfcct ls present but iasignigcant
-Team approach with industry consultants
  -RVLlS i Etfcct is present and was tuctudot
-Compared AEP engineering guides to industry ttandards
  -Level instruments       appropriately account for Bcrnoulli effect bias
-Appropriate process measuremcnt effect Bemoulli effect on level instrumentation
-Non.standard process location
-No guidance in engineering guides Short Tenn Assessment Results-Issue &#xb9;3 Short Tenn Assessment Results - Issue &#xb9;3 Bcmoulli effect on level instrumentation
-Allsafety relet@I level instruments cvalusted
-Condensate storage tank
'fcct is present but iaslgnigcaut
-Mid-loopRCS
'tfcct ls present but iasignigcant
-RVLlS iEtfcct is present and was tuctudot
-Level instruments appropriately account for Bcrnoulli effect bias e Bemoulli effect on level instrumentation
-idcC <<ngineering guide rcviscd
-Calculations account foithe flowinduced effects on process level instruments


Short Tenn Assessment Results - Issue             &#xb9;3     Short Tenn Assessment Results- Issue                 &#xb9;3
Short Tenn Assessment Results - Issue &#xb9;3 Short Tenn Assessment Results-Issue &#xb9;3
'tructures   as systems                                   o  Auxiliary Building Interior Walls
'tructures as systems
  -Structural and mechanical functions                       -HELB analyses in 1996
-Structural and mechanical functions
  -Functions may not bc survcil led                          -HELB boundary drawings
-Functions may not bc survcilled
'tructures     considered                                     Containment complex structure
'tructures considered
  -Containmcnt                                               -Structural integrity
-Containmcnt
  -Auxiliarybuilding walls                                   -Multiplycompartments
-Auxiliarybuilding walls
  -Control room complex                                     -Interior flow paths to support     ECCS functions
-Control room complex
  -Forebay and discharge vault Short Tenn Assessment Results - Issue             &#xb9;0 .,   Short Tenn Assessment Results - Issue                 &#xb9;5 o Containment attributes Application of single failure criteria
-Forebay and discharge vault o AuxiliaryBuildingInterior Walls
  -Multkllscipline inspection    team                        -"Ftuiure to run" scenarios are considered ln
-HELBanalyses in 1996
  -Focused on perfonnance attributes                          analyses by both Westinghouse and AEP
-HELBboundary drawings Containment complex structure
  -Technical and housekeeping questions raised              -Crossied safety-related     system evaluations
-Structural integrity
  -Actions were taken to disposition findings                -Essential service water system
-Multiplycompartments
  -No new issues  raised that affect operability
-Interior flowpaths to support ECCS functions Short Tenn Assessment Results - Issue &#xb9;0.,
                                                                  ~ Normsl pocsatkxt
Short Tenn Assessment Results - Issue &#xb9;5 o Containment attributes
                                                              -AFW, CVCS, CCW, ESW, clectricat distribution o
-Multkllsciplineinspection team
Emergency crossde A enda Short Tenn Assessment Results                           Cene Htrpstrkk       latroductloa Jcb Klnasccd         Nl Rcctreutsttoa Sump Inventory o Conclusion                                                                  N4   ES LS Switchover Procedure NS   Boctdcoksae to RWST
-Focused on perfonnance attributes
  -Results firmlysupport our conclusion, there                              Ns   Recirculation Sump Ycnttna exists reasottabie assurance that the              Paul Schocpf         rrr Hbrous Mstcrtst la Contsfnmcnt problems of the type found during the                                        SAeor Cooldown Design Inspection do not impact operability NS N6 NS RHR Suction Valve  Au~
-Technical and housekeeping questions raised
Compressed AlrOvcrprcssure of the other safety systems                        Stoa Farhnr         NN   lastnuncnt Unccrtslnty Joel Wlebe           Short Tenn Asscssmcnt Development Al Blind s~         *ddt~A ~orOp               r Mttyol S toms
-Actions were taken to disposition findings
-No new issues raised that affect operability Applicationofsingle failure criteria
-"Ftuiure to run" scenarios are considered ln analyses by both Westinghouse and AEP
-Crossied safety-related system evaluations
-Essential service water system
~ Normsl pocsatkxt
-AFW,CVCS, CCW, ESW, clectricat distribution o Emergency crossde Short Tenn Assessment Results o Conclusion
-Results firmlysupport our conclusion, there exists reasottabie assurance that the problems ofthe type found during the Design Inspection do not impact operability ofthe other safety systems A enda Cene Htrpstrkk latroductloa Jcb Klnasccd Nl Rcctreutsttoa Sump Inventory N4 ES LS Switchover Procedure NS Boctdcoksae to RWST Ns Recirculation Sump Ycnttna Paul Schocpf rrr Hbrous Mstcrtst la Contsfnmcnt NS SAeor Cooldown N6 RHR Suction ValveAu~
NS Compressed AlrOvcrprcssure Stoa Farhnr NN lastnuncnt Unccrtslnty Joel Wlebe Short Tenn Asscssmcnt Development AlBlind s~
*ddt~A ~orOp r Mttyol S
toms


A endN Cene HtspaMk Introduction Jcb IQngsced Nl Rcclrculadon Sump Inventory N4   KS ID Switchover Procedure NN   Backlcakage to RWST NI Rcclrculadon Sump Vcndng Paul Schocpf Ny Hbrous MatcrhLI ln Containment N3   36-hour CooMown Nd   RHR Sucdon Valve AuloClose NS   Comprcsscd AirOverpressure Stan Farfow  NP   Instrument Uncertainty Joel Wcbe    Short Torus Asscssmcnt Dcvelopmcnt Jim Kobyra  Short Term Assessment Results Al BUnd      Addidonal Amuran<<e of OpcrabiUty of S terna Conclusion
Cene HtspaMk Jcb IQngsced Paul Schocpf Stan Farfow Joel Wcbe Jim Kobyra AlBUnd A endN Introduction Nl Rcclrculadon Sump Inventory N4 KS IDSwitchover Procedure NN Backlcakage to RWST NI Rcclrculadon Sump Vcndng Ny Hbrous MatcrhLI ln Containment N3 36-hour CooMown Nd RHR Sucdon Valve AuloClose NS Comprcsscd AirOverpressure NP Instrument Uncertainty Short Torus Asscssmcnt Dcvelopmcnt Short Term Assessment Results Addidonal Amuran<<e ofOpcrabiUty of S
terna Conclusion


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0 Confirmatory Action Letter Issue     1 I    '
0
Re i u           it         Tt       ittttt ttt 1         11 used to cool the reactor and 1'umps g                                                                                containment building may not have enough water supply to allow long-term operation N                            6t2'                                              of the systems.
 
J>>U 8
I Confirmatory Action Letter Issue 1
Active Sump inactive                                                                AEP Commitment Sump                602-10'g8'-g                '6IO'4'eactor        Analyses willbe performed to demonstrate that the 'recirculation sump level is adequate to prevent vortexing, or appropriate Cavity modifications will be made.
Re i u
Resolution
it Tt ittttt ttt g
                                                                                        ~ Analyses demonstrated emergency core cooling system/containment spray system I      ~
N J>>U 8
operability.
inactive Sump 6t2' Active Sump 602-10'g8'-g
                                                                                        ~ Determined that sump level will remain
'6IO'4'eactor Cavity 1
                              ~
11 1'umps used to cool the reactor and containment building may not have enough water supply to allow long-term operation of the systems.
('ontainmcnt Spr~y t(;rS)                            above 602'0" throughout long-term recirculation phase.
AEP Commitment Analyses willbe performed to demonstrate that the 'recirculation sump level is adequate to prevent vortexing, or appropriate modifications willbe made.
                                                                                        ~ Submitted Technical Specification t~nvcr        tfppcsc                I'",.:., Steam Reactor,'ti(YS Cont.          (oritI:        C amendment to credit more existing ice Nozdcs        Nozzle                                S mass and other contributing sources of Uquld                water in sump inventory calculations.
I
Nozzle vh         vh                           ice Fan       stalnveU     via               Melt Accumuhtor                  RelueUng           and Rooms                    Canal             Condensed Orahs             Steam Reactor Inactive Sump                    Active Sump                 Cavity 4>>t 47z>>Y
~
~
('ontainmcnt Spr~y t(;rS) t~nvcr tfppcsc Cont.
(oritI:
Nozdcs Nozzle Uquld I'",.:., Steam Reactor,'ti(YS C
S Resolution
~ Analyses demonstrated emergency core cooling system/containment spray system operability.
~ Determined that sump level willremain above 602'0" throughout long-term recirculation phase.
~ Submitted Technical Specification amendment to credit more existing ice mass and other contributing sources of water in sump inventory calculations.
vh vh Fan stalnveU Accumuhtor Rooms Inactive Sump Nozzle ice via Melt RelueUng and Canal Condensed Orahs Steam Active Sump Reactor Cavity 4>>t 47z>>Y


Confirmatory Action Letter Issue 4
I
                                                        '
~
I      ~                    r            I                                          I        R i tt i         tt rett.llnlttcllt spnly t( 1st Current    procedures  implementing hmnnutators                               t(WZt'g~+Ltt switchover from the Refueling Water t.ower          tfppcr,            tcc      Steam    ttc actor    li('('8              Storage Tank (RWST) to the containment
r I
('.ont.        Cttntri-    ('undcnscr              (.out;ult Nor~los        Noxztcs'                              Systrnn                          sump may not be adequate for long-term, rs                                        post-accident operations.
Confirmatory Action Letter Issue 4 I
Uqutd Nozzle                          8reaft via         vta             Flow tce                        Flow Fan       stairwell     via           Melt r
R i
AEP Commjtment Accumulator                Refueling and Rooms                    Canal        Condensed Changes to the emergency procedure used Drains        Steam                                              for switchover of the emergency core Reactor inactive Sump                  Active Sump                Cavity                          cooling and containment spray pumps to the recirculation sump will be implemented.
tt i tt t.ower
g  asltarcaN steers re JOWLS These changes will provide assurance there will be adequate sump volume, with proper consideration of instrument bias and single failure criteria.
('.ont.
Nor~los
: tfppcr, Cttntri-Noxztcs' rett.llnlttclltspnly t( 1st hmnnutators tcc Steam ttcactor li('('8
(.out;ult Systrnn
('undcnscr rs t(WZt'g~+Ltt Current procedures implementing switchover from the Refueling Water Storage Tank (RWST) to the containment sump may not be adequate for long-term, post-accident operations.
via vta Fan stairwell Accumulator Rooms inactive Sump via Melt Refueling and Canal Condensed Drains Steam Uqutd 8reaft Flow Active Sump Reactor Cavity Nozzle Flow tce r
g asltarcaN steers re JOWLS AEP Commjtment Changes to the emergency procedure used for switchover of the emergency core cooling and containment spray pumps to the recirculation sump willbe implemented.
These changes willprovide assurance there willbe adequate sump volume, with proper consideration of instrument bias and single failure criteria.
Resolution
Resolution
                                                                                            ~ Prepared, validated and trained all operating crews on revisions to ES-1.3 "Transfer to Cold Leg Recirculation". '
~ Prepared, validated and trained all operating crews on revisions to ES-1.3 "Transfer to Cold Leg Recirculation". '
Revision reasonably assures an adequate recirculation sump level and eliminates the potential single failure vulnerability that existed during the transition from injection to recirculation phase.
Revision reasonably assures an adequate recirculation sump level and eliminates the potential single failure vulnerability that existed during the transition from injection to recirculation phase.
                                                                                            ~ RWST water level tap was relocated to account for the bias that may have existed.
~ RWST water level tap was relocated to account for the bias that may have existed.
                                                                                            ~ The RWST, recirculation sump, ECCS and CTS pumps are operable with ES-1.3
~ The RWST, recirculation sump, ECCS and CTS pumps are operable with ES-1.3
                                                                                              . Revision 5.
. Revision 5.


Confirmatory Action Letter Issue S I '          '      I    I                                                Wa                     W T
I '
                                                                              '-F     R i Tl i   >  ii Testing of Mini-Flow Recirculation Lines may not be adequate to assure that back-leakage to RWST will not exceed acceptable levels during a design basis accident.
I I
AEP Commitment Only two of six mini-flow recirculation line valves have leakage verification tests.
Confirmatory Action Letter Issue S Wa W T
Justification willbe provided that the total leakage for the six valves is less than 10 gallons per minute (gpm) to ensure that Part 100 limits are not exceeded if containment sump water were to leak back to the RWST during a design basis accident.
'-F R i Tl i ii Testing of Mini-FlowRecirculation Lines may not be adequate to assure that back-leakage to RWST willnot exceed acceptable levels during a design basis accident.
AEP Commitment Only two of six mini-flowrecirculation line valves have leakage verification tests.
Justification willbe provided that the total leakage for the six valves is less than 10 gallons per minute (gpm) to ensure that Part 100 limits are not exceeded ifcontainment sump water were to leak back to the RWST during a design basis accident.
Resolution
Resolution
                                                                        ~ Testing of the valves not previously tested showed that total leakage for these paths back to the RWST was well below 10 gpm value in the UFSAR.
~ Testing of the valves not previously tested showed that total leakage for these paths back to the RWST was well below 10 gpm value in the UFSAR.
                                                                        ~ Included affected flow paths in the In-Service Testing program.
~ Included affected flow paths in the In-Service Testing program.
                                                                        ~ Implemented new procedures: seat leakage testing of valves at each refueling outage to ensure < 10 gpm total leakage.
~ Implemented new procedures: seat leakage testing of valves at each refueling outage to ensure < 10 gpm total leakage.
Confirmatory Action Letter Issue 2 T     I Venting of air underneath the roof of the containment building recirculation sump may not be adequate.
Crane Wal O'Venl
O'Venl
<S) sra'irrsni Hears B. IOS'4' Coarse 4 Fino Screen r i
                                  <S) sra'irrsni Hears Crane              B. IOS'4'                            AEP Commitment Wal Venting willbe re-installed in the Coarse 4 Fino Screen recirculation sump cover. The design     will incorporate foreign material exclusion r    i    ~ rQ~~              requirements for the sump.
~
To AHA
rQ~~
            <
Confirmatory Action Letter Issue 2 T
Resolution and CTS Surrisn           Aeo'ro Sranp                         7             ~ Venting has been reinstalled in the (2> I 8'ncs
I Venting of air underneath the roof of the containment building recirculation sump may not be adequate.
                                                            +aaacsnic ~   recirculation sump cover in both TTnits.
AEP Commitment Venting willbe re-installed in the recirculation sump cover. The design will incorporate foreign material exclusion requirements for the sump.
POWER
To AHA and CTS <
                                                                        ~ Vents incorporate screening to satisfy the
Surrisn (2> I8'ncs Aeo'ro Sranp 7
                                                                        'oreign material exclusion requirements.
+aaacsnic POWER Resolution
                                                                        ~ Recirculation sumps have been returned to their approved design configuration.
~ Venting has been reinstalled in the
~
recirculation sump cover in both TTnits.
~ Vents incorporate screening to satisfy the
'oreign material exclusion requirements.
~ Recirculation sumps have been returned to their approved design configuration.


Confirmatory Action Letter Issue 7 l             1   I   11 Fibrous material located in containment COneammenl Wae buildings may clog the recirculation sump.
Reeeelea san eu p COneammenl Wae CI<<ls was Qo 0
CI<<ls was AEP Commitment Removal of fibrous material from containment that could clog the Qo                                      recirculation sump will be completed.
Confirmatory Action Letter Issue 7 l
0                                      Resolution
1 I
                                                                                    ~ Containment inspections were conducted in Units 1 and 2.
11 Fibrous material located in containment buildings may clog the recirculation sump.
Reeeelea san                                                                        ~ identified and removed unencapsulated eu p fibrous insulation materials from 12 locations in Unit 1, 15 locations in Unit 2, in the aiuxulus and instrument rooms.
AEP Commitment Removal of fibrous material from containment that could clog the recirculation sump willbe completed.
Confirmatory Action Letter Issue 3 1      1          lf Calculation needs to be performed that sxeaeI shows, one train of cooling water is xi PIee<<ee Reeee veeme sufficient to remove the units from service.
Resolution
~ Containment inspections were conducted in Units 1 and 2.
~ identified and removed unencapsulated fibrous insulation materials from 12 locations in Unit 1, 15 locations in Unit 2, in the aiuxulus and instrument rooms.
sxeaeI xi I't Recolor II
/
Suction Valves PIee<<ee Reeee veeme Valve +
Preeevu<<
Preeevu<<
Valve
peo Iee locales Reeeluil Heel Removal Pump Rexecu<<
                                                    +        Reeeluil Heel Removal peo Iee  locales              Pump AEP Commitment Suction Valves                                    Analyses willbe performed that will I
Heel Renoval Exonanp<<
                  't I
CCW Heel Pxlnenp<<
Recolor                                                    demonstrate the capability to cool down the R execu<<    CCW
CIeeneel seInee ee<<<<
  /
Confirmatory Action Letter Issue 3 1
I Heel Renoval Heel Pxlnenp<<
1 lf Calculation needs to be performed that shows, one train of cooling water is sufficient to remove the units from service.
units consistent with design basis Exonanp<<              requirements and necessary changes to C Ieeneel seInee procedures willbe completed.
AEP Commitment Analyses willbe performed that will demonstrate the capability to cool down the units consistent with design basis requirements and necessary changes to procedures willbe completed.
ee<<<<
Resolution
Resolution
                                                                                    ~ Thermal hydraulic analysis concluded that a single train of residual heat removal/component cooling water/essential service water is capable of cooling down the reactor coolant system in 36 hours.
~ Thermal hydraulic analysis concluded that a single train of residual heat removal/component cooling water/essential service water is capable of cooling down the reactor coolant system in 36 hours.
                                                                                    ~ Operating procedure revisions were made to reflect a higher maximum component cooling water supply temperature limit (increased to 120'F).
~ Operating procedure revisions were made to reflect a higher maximum component cooling water supply temperature limit (increased to 120'F).
                                                                                  '
Four pipe supports were also modified.
Four pipe supports were also modified.
* Confirmatory Action Letter Issue tl
 
                                                                                                '
Preccverxer Precerxe Acier valvee Verve axcvrie rcxacae Aepavri Hear eerxrvai Pvrep
lH             I     R V
* Confirmatory Action Letter Issue tl lH I
Conflicts between operating procedures and Technical Specifications for Residual Heat Precerxe Acier valvee Removal Suction Valve Autoclosure Verve                Aepavri Hear Interlock.
R V
Preccverxer                                      eerxrvai axcvrie rcxacae                  Pvrep Svceea Varvec                                                    AEP Commitment f     Aeacccr Aea acr                      r A Technical Specification change to allow I                             Ccccarc Puntp Aecxarel Heal Aervxrval CCV/
Conflicts between operating procedures and Technical Specifications for Residual Heat Removal Suction Valve Autoclosure Interlock.
Heal fxcrraeger   operation in Mode 4 with the RHR suction Heal Kxcaarper                        valves open and power removed is being ICornea vrvveer  processed. Approval of this change by the Welvr NRC will be required prior to restart.
f Aeacccr I
Svceea Varvec Aeaacr Ccccarc Puntp Aecxarel r
Heal Aervxrval Heal Kxcaarper CCV/
Heal fxcrraeger Ivrvveer Cornea Welvr AEP Commitment ATechnical Specification change to allow operation in Mode 4 with the RHR suction valves open and power removed is being processed.
Approval of this change by the NRC willbe required prior to restart.
Resolution
Resolution
                                                                                            ~ Submitted a proposed Technical Specification change to the NRC that eliminates the need for the RHR Suction Valve Autoclosure interlock when in a shutdown cooling configuration. The Technical Specification change has been approved by the NRC.
~ Submitted a proposed Technical Specification change to the NRC that eliminates the need for the RHR Suction Valve Autoclosure interlock when in a shutdown cooling configuration. The Technical Specification change has been approved by the NRC.
Confirmatory Action Letfer Issue 5 Overpressure protection for some
~ 200 Air Confirmatory Action Letfer Issue 5 Overpressure protection for some components served by the compressed air system may not be adequate in the event of a postulated air regulator failure.
                                                                        ~    200 Air components served by the compressed air system may not be adequate in the event of a postulated air regulator failure.
1000, ~
AEP Commifmenf 1000, Alr Supply
Alr '
      '~                                                                      500 Alr Overpressure protection will be provided downstream of the 20 psig, 50 psig, and 85
Supply
                                                                        /Valve              psig control air regulators to mitigate the effects of a postulated failed regulator.
/Valve 500 Alr AEP Commifmenf Overpressure protection willbe provided downstream of the 20 psig, 50 psig, and 85 psig control air regulators to mitigate the effects of a postulated failed regulator.
050 Atr Resolution AeCrIarcr Q AacrAIcur   ~ Installed redundant, safety-grade relief valves on all of the control headers (20 psig, 50 psig, and 85 psig) and eliminated overpressure potential.
AeCrIarcr 050 Atr Q AacrAIcur Resolution
                                                                                            ~ Eliminated potential for common-mode failure due to overpressurization.
~ Installed redundant, safety-grade relief valves on all of the control headers (20 psig, 50 psig, and 85 psig) and eliminated overpressure potential.
                                                                                            ~ Safety related systems and components supported by the control air system are operable.
~ Eliminated potential for common-mode failure due to overpressurization.
~ Safety related systems and components supported by the control air system are operable.


Confirmatory Action Letter Issue g                   Resoiution 1     I     I     1 I                             ~ Actions completed Need to incorporate instrument uncertainties into       - Reviewed level instrumentation For velocity procedures and analyses.                                  effect.
Confirmatory Action Letter Issue g 1
                                                        - Reviewed and revised emergency       operating AEP Commitment                                            procedures for switchover to recirculation.
I I
Emergency procedures and other important-to-            - Reviewed and revised technical specification safety procedures, calculations, or analyses will be      surveillance procedure used by Operations.
1 I
reviewed to account for instrument uncertainties.      - Generated parameter list for technical specification compliance.
Need to incorporate instrument uncertainties into procedures and analyses.
                                                        - Generated Administrative control procedures.
AEP Commitment Emergency procedures and other important-to-safety procedures, calculations, or analyses willbe reviewed to account for instrument uncertainties.
                                                        - Reviewed EOP Setpoint Documentation.
Resoiution
                                                        - Reviewed License Bases.
~ Actions completed
                                                        - Addressed all related non-programmatic Unresolved Issues from the inspection report.
- Reviewed level instrumentation For velocity effect.
                                                        - Completed Plant Specific Methodology Manual.
- Reviewed and revised emergency operating procedures for switchover to recirculation.
                                                    ~ Continuing Actions
- Reviewed and revised technical specification surveillance procedure used by Operations.
                                                        - Developed a plan to:
- Generated parameter list for technical specification compliance.
                                                            - control instrument uncertainty and incorporate it into procedures, calculations, and analyses.
- Generated Administrative control procedures.
                                                            - complete reviews, training, and calculations by December 1, 1998.
- Reviewed EOP Setpoint Documentation.
                                                        - Checklist, based on current NRC guidelines, willbe used to review existing and future instrument uncertainty calculations.
- Reviewed License Bases.
                                                        - Developing a plant specific methodology manual to calculate instrument uncertainties; manual willbe an expansion of existing engineering guide.
- Addressed all related non-programmatic Unresolved Issues from the inspection report.
                                                        - Developing administrative controls to ensure that instrument uncertainties are considered whenever procedures, calculations and analyses are developed or revised.
- Completed Plant Specific Methodology Manual.
                                                        -'ntegrating instrument uncertainty program with the upgraded normal operating procedure and emergency operating procedure reviews.
~ Continuing Actions
- Developed a plan to:
- control instrument uncertainty and incorporate it into procedures, calculations, and analyses.
- complete reviews, training, and calculations by December 1, 1998.
- Checklist, based on current NRC guidelines, willbe used to review existing and future instrument uncertainty calculations.
- Developing a plant specific methodology manual to calculate instrument uncertainties; manual willbe an expansion of existing engineering guide.
- Developing administrative controls to ensure that instrument uncertainties are considered whenever procedures, calculations and analyses are developed or revised.
-'ntegrating instrument uncertainty program with the upgraded normal operating procedure and emergency operating procedure reviews.


Purpose                                             Roof Cause Analysis of other Oesign To assess whether issues similar to the eight listed Inspection Issues in the confirmatory action letter (CAL) may exist   Root causes of other issues raised during the in other safety systems, and if they do, to         design inspection that were not included in the determine whether they affect system operability. CAL were also reviewed.
Purpose To assess whether issues similar to the eight listed in the confirmatory action letter (CAL) may exist in other safety systems, and ifthey do, to determine whether they affect system operability.
                                                                                'oot Cause Investigation and Evaluation           Independent Review by Senior Industry Peers ol CAL issues                                        All final root cause analyses were reviewed by Independent teams comprised of AEP Nuclear           independent senior industry peers.
Roof Cause Analysis of other Oesign Inspection Issues Root causes of other issues raised during the design inspection that were not included in the CALwere also reviewed.
Generation Group and outside technical analyst(s) conducted root cause evaluations of the eight CAL   Senior Management Review and Action issues.                                              A group of senior managers and staff reviewed the root causes of the CAL and AE issues. Action plans were developed to further assess those issues that had the potential to create operability concerns in other systems.
'oot Cause Investigation and Evaluation ol CALissues Independent teams comprised of AEP Nuclear Generation Group and outside technical analyst(s) conducted root cause evaluations of the eight CAL issues.
Independent Review by Senior Industry Peers Allfinal root cause analyses were reviewed by independent senior industry peers.
Senior Management Review and Action A group of senior managers and staff reviewed the root causes of the CALand AE issues.
Action plans were developed to further assess those issues that had the potential to create operability concerns in other systems.


Identified Five Engineering Issues                   Evaluation and Revietv Senior management endorsed action plans for five     Each engineering issue was evaluated and engineering issues identified for short-term         reviewed by experienced teams of engineering and assessment that had both generic implications and   management personnel. Each evaluation were deemed likely to affect safety-related system   considered existing system assessments, design operability.                                         assessments, safety analyses and reports. These
Identified Five Engineering Issues Senior management endorsed action plans for five engineering issues identified for short-term assessment that had both generic implications and were deemed likely to affect safety-related system operability.
    ~ Some analyses were found to contain errors     documents helped focus review efforts in specific and incorrect assumptions.                    areas of vulnerability.
~ Some analyses were found to contain errors and incorrect assumptions.
    ~ Some containment attributes, such those related to sump performance, were not         Conclusion adequately preserved.                         The short-term assessment provides reasonable
~ Some containment attributes, such those related to sump performance, were not adequately preserved.
    ~ Failure to consider a credible failure mode on assurance that issues of the type found during the a non-safety-related system interfacing with   design inspection do not impact the operability of a safety-related system.                      other safety systems at Cook Nuclear Plant.
~ Failure to consider a credible failure mode on a non-safety-related system interfacing with a safety-related system.
    ~ Failure to consider level instrument bias due to Bernoulli effect.
~ Failure to consider level instrument bias due to Bernoulli effect.
    ~ improper application of single failure criterion.
~ improper application of single failure criterion.
Evaluation and Revietv Each engineering issue was evaluated and reviewed by experienced teams of engineering and management personnel.
Each evaluation considered existing system assessments, design assessments, safety analyses and reports.
These documents helped focus review efforts in specific areas of vulnerability.
Conclusion The short-term assessment provides reasonable assurance that issues of the type found during the design inspection do not impact the operability of other safety systems at Cook Nuclear Plant.


Charts s   li.                                     Matrices represent a series of critical reviews condu'cted to provide reasonable assurance that safety systems will perform their intended functions. Included in the matrices are short term assessments X    X      X  X    X X
s li.
conducted after the design inspection and X    X      X  X  X X previously performed safety system functional inspections (SSFI). These reviews
X X
    'X            X X          X were performed by the NRC, contractor, and X    X>>            X X AEP Nuclear Generation Group staffs.
X X
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                    >>                      Matrices firmly support the conclusion that g urn~
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CISCTRK Charts Matrices represent a series of critical reviews condu'cted to provide reasonable assurance that safety systems willperform their intended functions. Included in the matrices are short term assessments conducted after the design inspection and previously performed safety system functional inspections (SSFI). These reviews were performed by the NRC, contractor, and AEP Nuclear Generation Group staffs.
Conclusion Matrices firmlysupport the conclusion that there is reasonable assurance that the safety systems are capable of fulfillingtheir intended design function.
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Latest revision as of 13:30, 7 January 2025

Documents Info Re Three Specific Issues Discussed at 971222 Meeting.Attachment 1 to Ltr Contains Root Cause Analysis & Short Term Assessment Program Development
ML17334B675
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 12/24/1997
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1260G4, CAL, NUDOCS 9801050374
Download: ML17334B675 (114)


Text

CATEGORY 1 REGULATO INFORMATIOh DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9801050374 DOC.DATE: 97/12/24 NOTARIZED: NO DOCKET FACIL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana M

05000315 50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Indiana M

05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.

American Electric Power Co., Inc.

+ gp2 RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

I.

SUBJECT:

Documents info re three specific issues discussed at 971222 C

meeting. Attachment 1 to ltr contains root cause analysis short term assessment program development.

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SIZE: 0 l TITLE: Immediate/Confirmatory Action Ltr (50 Dkt-Other Than Emergency Prepar E

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N NOTE TO ALL "RIDS" RECIPIENTS:

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44 Indiana Michigan Power Company 500 Circle Drive Buchanan, Ml 491071395 IItIOIANA MICHIGAN IrQBfM December 24, 1997 AEP:NRC:1260G4 Docket Nos.:

50-315 50-316 U.S. Nuclear Regulatory Commission ATTN:

Document Control Desk Mail Stop 0-Pl-17 Washington, DC 20555-0001 Gentlemen:

Donald C.

Cook Nuclear Plant Units 1 and 2

CONFIRMATORY ACTION LETTER (CAL) SUPPLEMENTAL RESPONSE On December 16,

1997, a public meeting was held with the NRC to discuss issues associated with the NRC's confirmatory action letter dated September 19, 1997.

Subsequent to the

meeting, we were informed that further information regarding three specific issues was needed.

These issues were the root cause analyses we performed for the architect engineering (AE) inspection items and the development of our short term assessment

program, our 10 CFR 50.59
program, and calculations reviewed as part of the short term assessment program.

These issues were discussed with the NRC staff at a

meeting held in Lisle, Illinois on December 22, 1997.

ra AQUA i Jvv.

At that meeting, we agreed to perform additional reviews of design

changes, procedure
changes, and 10 CFR 50.59 screenings to review for the types of problems identified during the AE inspection.

The results of this review will be forwarded to the NRC under separate correspondence.

While the additional 10 CFR 50.59 reviews and our short term assessment represent specific actions taken to ensure that the types of problems found during the AE design =inspection do not affect the operability of other safety systems, we also recognize that operability and maintenance of design basis are continuous processes.

As a licensee, we must continually assess plant and external conditions to assure ourselves that systems remain within their licensing and design

bases, and where instances of degradation or non-conformance are identified, we must expeditiously evaluate operability of potentially affected equipment.

A questioning attitude by our staff ensures that safety reviews, calculations, and procedures are challenged.

As an example, at least,131 condition reports by five different plant organizations have been

issued, since the AE design inspection, to document potential discrepancies of a

type similar to those identified during the inspection.

This includes discrepancies found in the UFSAR.

Additionally, condition reports open at the time of the inspection were reviewed with increased awareness of the design and licensing basis.

'hose 'ondition reports that documented conditions having the potential to adversely impact the design or licensing bases or operability were identified and flagged for resolution prior to entry into a mode where the condition is applicable.

980%050374 971224 PDR ADQCK 050003i5 P

PDRQ IIIIIIIIIIIIIIII,llllilllilllllllllill

U.S. Nuclear Regulatory Commission Page 2

AEP: NRC: 1260G4 This letter dockets the information related to the three specific issues discussed at the December 22,

1997, meeting.

Attachment 1

to this letter contains the root cause analysis and short term assessment program development.

Attachment 2

contains our 10 CFR 50.59 program.

Attachment 3

contains the calculation review program.

Attachment 4 documents the presentation materials for our response to the confirmatory action letter issues that were provided during the December 16, 1997, public meeting.

Sincerely, g-Q4 E.

E. Fitzpatrick Vice President

/vlb Attachments A. A. Blind A. B. Beach MDEQ -

DW & RPD NRC Resident inspector J.

A. Abramson

ATTACHMENT 1 TO AEP:NRC: 1260G4 ROOT CAUSE ANALSYIS AND SHORT TERM ASSESSMENT PROGRAM DEVELOPMENT

Short Term Assessment Program Introduction In Confirmatory Action Letter No. RIII-97-011, the NRC Region III Administrator stated, "Lastly, given the limited scope ofour inspection and its substantial findings, it is necessary to determine the extent of problems and their potential impact on other systems.

It is my understanding, in the short term, you will perform an assessment to determine whether these types of engineering problems exist in other safety related.

systems and whether they affect system operability."

This paper documents the approach taken to develop the short-term assessment program.

In particular, it captures the process used to identify the engineering issues to be addressed and provides rationale for selecting specific short-term actions for each engineering issue.

In keeping with the guidance of the CAL, the short-term assessment is intentionally focused on operability ofsystems within the guidelines of'Generic Letter 91-18, Revision 1

and its attachments and references.

Some root causes identified during the investigation of design inspection findings are not relevant to the operability of safety

systems, and were therefore excluded from the short-term assessment program.

The arguments used to exclude some root causes are not intended to downplay the significance of nonconforming conditions found during the design inspection.

We are committed to addressing these important issues in longer-term programs to assure these kinds of engineering problems are promptly identified, thoroughly evaluated, and resolved.

Development Approach Development of the short-term assessment program is shown in Figure 1. The first task in developing the assessment program was to determine what constituted "these types of engineering problems." This task was accomplished in three steps.

1.

Root causes ofissues identified during the design inspection were identified.

Independent teams comprised ofAEP and contractor personnel conducted root cause evaluations ofthe eight individual CAL items.

Root causes ofother concerns identified during the design inspection, but not addressed in the CAL,were determined within the standard framework ofour corrective action'system.

They were independently reviewed.

Additionally, senior industry peers reviewed all root cause investigation reports.

2.

The root causes were reviewed by a group ofsenior managers and staff in several working sessions.

Implications of the various root causes were identified and Page 1 of 13

Short Term Assessment Program Rev. 2 discussed, with particular attention given to causes with potentially broader implications.

3.

The final step involved evaluating and identifying engineering issues that have the potential to impact operability ofother safety systems.

A total offive issues were identified.

The next task was to identify specific actions necessary to determine whether these five issues were present in other safety systems, and ifthey were, whether operability of the systems was affected.

Action plans were endorsed by senior management and staff and were approved by the Nuclear Safety and Design Review Committee.

Identification of"These Types ofEngineering Problems" Ste s

1 and 2-Root Cause Determination and Consideration ofIm lications Root cause determination (Step

1) and consideration of the implications (Step 2) are described in Appendix A for each of the eight CAL items and other design inspection concerns.

Results are summarized in Tables 1 and 2.

A total of 15 design inspection issues were included in the formal root cause determination (Table 1, Column 1).

Although this is less than the number of findings presented in the NRC's design inspection report, in some cases the issues included in our root cause evaluation encompassed multiple findings.

Twenty-two separate root causes or significant contributors were identified (Table 1,

Column 2. (Although there are 24 entries in the column, two are duplicates and in one case the root cause team did not determine a cause.)

Comparing these causes against a simplified diagram of our change processes, represented in Figure 2, reveals that five processes or sub-processes were involved:

design development, configuration management, design documentation, procedure development, and 10 CFR 50.59 safety reviews (Table 1, Column 3).

Ste 3 Identification ofRelevant En ineerin Issues The process or sub-process associated with each cause was broken down further into a descriptive category to identify where or how the process failed (Table 1, Column 4). Of the 22 causes identified, 13 were considered as potentially affecting operability of other safety systems (Table 1, Column 5).

Ofinterest is the fact that eight ofthe causes that did not potentially affect operability of other safety systems fell under the category of "failure to consider UFSAR as top-tier design basis."

These causes were associated with several processes or sub-processes.

Although not specifically included in short-term assessment

actions, our failure to recognize UFSAR information as design basis will be a focus of our longer-term program.

The 13 causes potentially affecting operability were then grouped under their common category (Columns 1 and 2, Table 2). The five broad engineering issues were:

Page 2 of 13

Short Term Assessment Program Rev. 2 1.

Calculation deficiencies 2.

Adverse effects ofnon-safety related systems on safety related systems 3.

Improper consideration ofinstrument bias 4.

Failure to consider and preserve multiple functional design requirements 5.

Failure to properly apply single failure criteria Identification ofSpecific Assessment Actions The five broad issues, ifconsidered in the absence ofexisting knowledge, could generate an extensive list of follow-up items to ensure that they did not render safety systems at Cook Plant inoperable.

For most of these items, however, substantial documentation or other rationale already existed that provided confidence that these potential follow-up items did not significantly impact other systems.

For example, the failure to consider the Bernoulli effect on RWST level measurement suggested that instrument biases in general might be a concern.

However, this concern was dispelled by a review of instrument calculation procedures and instrument calculations that provides confidence that other biases are recognized and are routinely applied.

Therefore, the scope of new actions to undertake prior to restart was focused on assessing the Bernoulli effect on process measurement.

Some issues, such as improper application of single failure criteria could not be limited.

The implications and factors affecting the potential significance and scope of problems associated with each cause were determined (Column 3, Table 2). Consideration ofthese factors allowed the issues to be focused (Column 4, Table 2).

The final statement ofeach issue approved by the NSDRC is as follows:

1.

Some AEP/Westinghouse analyses were found to contain errors.

2.

Lack of consideration of a credible failure mode on a non-safety related systems interfacing with safety related systems 3.

Lack ofconsideration oflevel instrument bias due to Bernoulli effect 4.

Some containment attributes such as those related to sump performance have not been adequately preserved 5.

Improper application ofsingle failure criteria Short-term assessment actions identified and approved for each engineering issue are summarized in Table 3.

Page 3 of 13

Short Term Assessment Program Rev. 2 Summary Development of the short-term assessment program was thorough and rigorous.

Root causes of the CAL items and other issues identified during the design inspection were evaluated.

Substantial documentation or other rationale existed in many cases to limitthe additional actions required prior to restart, and some of the root causes are more appropriately addressed in the longer-term programs aimed at assuring that these kinds of engineering problems are promptly identified, thoroughly evaluated, and resolved.

This latter group includes human performance deficiencies and organizational weaknesses that were recognized to some extent in all ofthe issues, but were not germane to determining the scope and impact of identified problems on the operability of other safety systems.

Satisfactory completion of the short-term assessment actions, coupled. with the existing information used to determine the scope ofthe assessment, provides reasonable assurance that the kinds of engineering problems found during the design inspection do not affect the operability ofother safety systems.

Page 4 of 13

Figure 1

Short-Term Assessment Program Development Design inspection findings Root causes Root causes that could impact operability Existing knowledge (SSFI, surveillances, procedures, etc.)

Issue 1

Issue 2 Issue 3 Issue 4 Issue 5 Short-term assessment actions Short Term Assessment Program Rev. 2 Page 5 of 13

Iden rk activity Perform work Figure 2 - Simplified nge Process Is it a change' Work control Design Basis Licensing Basis Engineering Basis Design Documenfafion Yes Physical change Type of change Operational change Typical change process Gather information Select tools and methods Technical change Select solution Analyze and develop alternative solutions Administrative change Design or Procedure Oevelopmenf

-10 CFR 50.59 Review Potential regulatory impact

~~Yes Is USQD req'd'?

Yes Is the change a USQ?

Submit under 10 CFR 50.92 Obtain NRC approval No No Short Term Assessment Program Rev. 2 Page 6 of 13 Configuration control Implement change

- Configuration Managemenf

Short Term Assessment Program Rev. 2 Table I - Summary and InitialCategorization ofRoot Causes Design Inspection Finding Idcntificd Root Cause or Contributor Related Process or Sub-proccss Category Operability Implications CALItem I:

Recirculation sump inventory CALItem 2:

Recirculation sump cover venting CALItem 3: 36-hour cooldown CALItem 4:

Switchover from injection to recirculation CALItem 5:

Compressed air overpressure Lack ofthorough engineering review Inadequate design control during initial plant design Improper implementation ofwell defined design expectations Foreign material exclusion (FME) protection not installed Design change not properly incorporated into design documentation Design and licensing basis information not retrieved in a timely manner Design parameters for all system conditions were not described in the UFSAR Analysis used an unverified (and incorrect) assumption ofheat exchangertype Lack ofconsideration of Bernoulli effect on level instrumentation Incorrect application of single failure criteria Failure to identify a non-safety system failure mode that could impact safety system components Design development Design development Configuration management Design development Design documentation Design documentation Design documentation Design development Design development Design development Design development Calculation deficiencies Failure to consider multiple functional requirements Failure to preserve multiple functional requirements Failure to consider multiple functional

'equirements Failure to consider multiple functional requirements Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Calculation deficiency Improper consideration of instrument bias Failure to properly apply single failure criteria Adverse effects of non-safety related systems on safety related systems Yes Yes Yes Yes Yes No No Yes Yes Yes Yes Page 7 of 13

Short Term Assessment Program Rev. 2 Table ISummary and InitialCategorization ofRoot Causes (cont'd)

Design Inspection Finding Identified Root Cause or Contributor Related Process or Sub-process Category Operability Implications

'p CALItem6: RHR suction valve interlock CALItem 7:

Fibrous material in containment CALItem 8: Leak back to RWST during recirculation Lake temperature design basis discrepancies Unit 2 fullcore off-load with concurrent CCW dual train outage Restriction of CCW temperature during Unit 2 full, core off-load Processes in place (at the time) did not emphasize the UFSAR, resulting in an inadequate safety review Design change accomplished via procedure revision Lack ofprocedures for implementing an insulation specification Failure to address sump-plugging potential of fibrous insulation material installed in containment Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Failure to recognize a'FSAR value as a design basis parameter Failure to recognize inter-relationships between a UFSAR value and other design aspects 10 CFR 50.59 reviews may be inadequate 10 CFR 50.59 reviews may be inadequate Procedure development Procedure development Configuration management Design development Design development 10 CFR 50.59 safety reviews 10 CFR 50.59 safety reviews 10 CFR 50.59 safety reviews 10 CFR 50.59 safety reviews Failure to consider UFSAR as top-tier design basis Configuration management Failure to preserve multiple functional design requirements Failure to consider multiple functional design requirements Calculation deficiencies Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Failure to consider UFSAR as top-tier design basis Literally inoperable per T/S, but no effect on functionality No Yes Yes Yes No No (see discussion Iil Appendix A)

No (see discussion in Appendix A)

No (see discussion in Appendix A)

Page 8 of 13

Short Term Assessment Program Rev. 2 Table 1-Summary and InitialCategorization ofRoot Causes (cont'tl)

Design Inspection Finding Identified Root Cause or Contributor Related Process or Sub-process Category Operability Implications

'P RWST minimum volume for Appendix R 2-CD battery cell left on charge for an extended period Code discrepancy in CCW system safety valves Procedures allowing both RHR pumps to run with the RCS vented Misinterpretation ofT/S resulted in failure to translate calculation assumptions and results into operating procedures N/Ano cause determined by root cause team Failure to translate design requirements into operating procedures Failure to translate UFSAR requirements into operating procedures Design development N/A Procedure development Procedure development Calculation deficiencies N/A Configuration management Failure to consider UFSAR as top-tier design basis Yes No (see discussion ill Appendix A)

No No Page 9 of 13

Short Term Assessment Program Rev. 2 Table 2-Implications ofRoot Causes Potentially Affecting Operability Broad Category Calculation deficiencies Adverse effects ofnon-safety related systems on safety related systems Improper consideration of instrument bias IdcntiTicd Root Cause (or Contributor)

Lack ofthorough engineering review (From CALItem 1)

Analysis used an unverified (and incorrect) assumption ofheat exchanger type (From CALItem 3)

Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations (From CALItem 8)

Misinterpretation of T/S resulted in failure to translate calculation assumptions and results into operating procedures (from RWST minimum volume for Appendix R)

Failure to identify a non-safety system failure mode that could impact safety system components (From CALItem 5)

Lack ofconsideration of Bernoulli effect on level instrumentation (From CAL Item 4)

Implications and Factors Affecting Scope ofReview

~ Involved Westinghouse-AEP interface

~ Systems could not be functionally tested

~ First-of-a-kind design

~ Error occurred almost 30 years ago

~ Involved Westinghouse-AEP interface

~ Original error occurred almost 30 years ago

~ Controls need to be in place to assure that assumptions remain valid

~ End use ofcalculation needs to be understood

~ Controls need to be in place to assure that assumptions remain valid

~ Vulnerability is limited to non-safety related systems that interface with safety systems

~ I&Cprocedure includes other bias terms but not velocity effects

~ Calculation review confirmed that other biases are considered

~ 1993 system-based I&C inspection addressed bias Enginccring Issue Some AEP/Westinghouse analyses were found to contain errors.

Lack ofconsideration ofa credible failure mode on a non-safety related system interfacing with safety related systems Lack ofconsideration of level instrument bias due to Bernoulli effect Page 10 of 13

Short Term Assessment Program Rev. 2 Table 2-Implications ofRoot Causes Potentially Affecting Operability (cont'd)

Broad Category Failure to consider and preserve multiple functional design requirements Identified Root Cause (or Contributor)

Inadequate design control during initialplant design (From CALItem I),

Improper implementation ofwell-defined design expectations (From CALItem I)

Design change not properly incorporated into design documentation (From CALItem 2)

Implications and Factors Affecting Scope ofReview

~ Involved Westinghouse-AEP interface

~ Considered unique case Sump cannot be tested, but relies on analysis for demonstrating adequacy Unlike typical cases where analysis is the only tool, this relies on totally plant-specific assumptions and calculations

~ Error occurred almost 30 years ago

~ Design feature is not functionally tested

~ Minoraspect ofa larger design change

~ Design function was negligible, with no impact on operability

~ Feature was functioning outside its discipline (structural feature performing mechanical function)

~ Feature was not tested or part ofinspection program

~ Other structures with mechanical functions are typically controlled, e.g.

doors acting as HELB barriers

~ Containment is the most notable example ofa system that cannot be functionally tested in its accident response mode

~ Search ofmaintenance work system provides assurance that plant mods are not made via work orders; controls exist to prevent unauthorized mods Engineering Issue Some containment attributes such as those related to sump performance have not been adequately preserved Page I I of 13

Short Term Assessment Program Rev. 2 Table 2-Implications ofRoot Causes Potentially Affecting Operability (cont'd)

Broad Category Cont'd from previous page Failure to consider and preserve multiple functional design requirements Failure to properly apply single failure criteria Idcntificd Root Cause (or Contributor)

Foreign material exclusion (FME) protection not installed (From CALItem 2)

Lack ofprocedures for implementing an insulation specification (From CALItem 7)

Failure to address sump-plugging potential of fibrous insulation material installed in containment (From CAL Item 7)

Incorrect application of single failure criteria (From CALItem 4)

Implications and Factors Affecting Scope ofReview

~ Unprotected vent holes were found by NRC resident during a containment walkdown

~ Recent focus on FME has led to better controls since this problem was identified in 1996

~ Contractor work was not closely supervised by AEP

~ Engineering involvement was minimal

~ This problem was found by NRC inspector during a containment walkdown

~ Interpretation ofactive failure definition may have led to error

~ Systems with crosstie capabilities between trains or units are susceptible Engineering Issue Cont'd from previous page Some containment attributes such as those related to sump performance have not been adequately preserved Improper application of single failure criteria Page 12 of 13.

Table 3 - Short Assessment Plan

Purpose:

To determine whether these issues exist in other safety related systems and ifso, whether they affect system operability Engineering Issue Short Term Scope Deliverables Owner Date 1.

Some AEP/Westinghouse analyses were found to contain errors.

2.

Lack ofconsideration ofa credible failure mode on a non-safety related systems interfacing with safety related systems 3.

Lack ofconsideration oflevel instrument bias due to Bernoulli effect 4.

Some containment attributes such as those related to sump performance have not been adequately preserved 5.

Improper application ofsingle failure criteria

~ Conduct assessment ofWestinghouse analyses

~ Confirm that Westinghouse analyses accurately depict the type ofheat exchanger for CCW, RHR, and CTS systems

~ Confirm that Holtec analyses accurately depict the type ofheat exchanger for SFP cooling system

~ Confirm that AEP internal analyses accurately depict the type ofheat exchanger for these same systems

~ Perform peer review ofcalculations referenced in CR 97-2525, calculations performed in support ofrestart, and representative historic calculations from other safety systems

~ Develop rationale for selecting other non-safety related systems for further FMEA

~ Perform FMEAofcontrol air system

~ Confirm that FMEA on reactor control system adequately covered failure modes

~ Perform FMEAofpressurizer heaters

~ Review safety-related tank level indication

~ Review mid-loop monitoring and RVLIS

~ Perform containment walkdown, focusing on factors like those affecting sump performance, especially items which are not surveilled

~ Resolve containment walkdown questions

~ Clarify definition ofsingle failure and incorporate into procedures

~ Verifythat "failure-to-run" was considered in Westinghouse and AEP analyses

~ Verifythat AFW, ESW, CVCS, 250 v. DC, and electrical distribution system crosstie capabilities have been properly evaluated for use in procedures

~ Assessment report

~ Assessment report

~ Letter from Holtec with confirming memo from Malin

~ CR 97-2316

~ Summary report

~ White paper

~ CR 97-2447

~ White paper

~ White paper

~ White paper

~ White paper

~ Walkdown report

~ Summary report

~ List procedures and revise

~ White paper, with Westinghouse letter

~ White paper, including selection criteria Scope Revision 1 Status Updated 11/5/97 9:30 AM Page13 of13

Short Term Assessment Program APPENDIXA Root Cause Determination and Consideration ofImplications Page A-1

Short Term Assessment Program Rev. 2 Appendix A CALItem 1: Recirculation Sump Inventory Ste 1 Root Cause Determination The problem was defined as "minimum required recirculation sump level to protect against pump vortexing could not be assured for all accident conditions."

(Note - The inability to assure adequate sump level was due in part to potential RWST level instrument bias, which was addressed in another investigation.)

Pertinent facts brought forth in the investigation include:

In late 1967, AEP deviated from Westinghouse's original containment spray system (CTS) design of"a four pump, four heat exchanger configuration per unit" and selected a design that utilized the residual heat removal (RHR) system to supplement CTS.

The CTS design also included the addition of lower volume spray headers for iodine removal capability.

Implications of the spray header additions with respect to system performance were not discussed in design memoranda.

~

A September 1968 document discussing containment drainage indicates that the annulus should be designed to exclude recirculation water.

An October 1968 update to the document notes the need to install drains from the accumulator/fan rooms to the active sump.

It also suggests an alternate discharge from the pipe annulus to the recirculation sump "foruse during recirc mode in case of a leak in the safety system piping within the access tunnel."

These documents reflect an incomplete understanding of the containment,

design, as large amounts of recirculation water would be sprayed into the fan accumulator rooms and subsequently drain through the floor gaps and gratings into the pipe annulus.

A Nuclear Safeguards Design Memo from July 1971 addresses the subject of containment flood-up, including the sequence of flooding various containment compartments during a design basis accident.

The memo mentions that 300 gpm flow will be diverted via the accumulator/fan rooms to the pipe annulus.

The sequence described does not mention entry'of water into the accumulator/fan rooms or pipe annulus until after the lower containment (inside the crane wall),

lower reactor cavity, and seal table area are filled, at which time water spills into the accumulator/fan rooms.

The section of the memo titled "Small Loss-of-Coolant Accident Flood-up" states that the flood-up sequence is the same as the design basis accident case.

The review uses the design basis flood-up scheme to conclude that there will be sufficient NPSH to accomplish the switchover to recirculation phase when needed.

~

In Question 212.29 of FSAR Appendix Q, the NRC requested a detailed description of our calculations for the ECCS pumps during LOCA conditions.

The calculation provided assumes that the entire volume of the RWST from the minimum level to the low alarm level is transferred to the active sump, resulting in flood-up to elevation 602'-10" in containment.

Page A-2

Short Term Assessment Program Rev. 2 Appendix A

~

'The LOTIC computer analysis models the active sump as a fixed volume and the inactive sump as an "overflow" from the active sump.

It does not consider inventory lost to the inactive sump during recirculation.

The simplified modeling is an indication that the LOTIC code was not intended to evaluate containment sump performance.

This root cause determination employed the fault tree method.

The root cause team used a variety of resources, including the original FSAR, early-revision drawings, condition reports, design basis documents and associated reference notebooks, design memoranda, and Westinghouse WCAP documents.

AEP and Westinghouse personnel were consulted as needed.

The team initiallyidentified five contributors to this issue:

1) loss of inventory via CTS flow to accumulator/fan rooms, 2) loss of inventory via stairwells, 3) loss of inventory into the reactor cavity, 4) loss of inventory through unsealed penetrations in the crane wall, and 5) incomplete knowledge regarding the response of plant systems to events requiring operation in the recirculation mode.

The first contributor, loss of inventory via CTS flow to the accumulator/fan rooms, is a consequence ofthe original plant design.

Awareness of CTS flowdiversion is evident in early documents.

However, the drains that were installed to return this diverted water from the accumulator/fan rooms to the active sump are elevated several inches above the floor, and are ineffective due to a competing flow path into the annulus through floor drains, floor grating, and structural gaps.

The team questioned why these competing flow paths were not recognized during design.

Similarly, the team questioned why additional scrutiny ofsmall break LOCA response followingthe Three Mile Island accident did not address containment sump inventory questions, but rather focused only on core response.

Lack of thorough review was identified as a root cause of this contributor.

Change control was also identified as a root cause, specifically with regard to the change from the original Westinghouse design that led to lack ofthorough review.

The second contributor, loss ofinventory via stairwells, was considered by the team to be analogous to the first contributor, and hence had the same cause.

Inventory loss to the reactor cavity was subsequently determined by the team not to be a contributor.

Historically, this aspect of containment inventory has been dealt with appropriately.

Documentation shows that penetrations in the crane wall were intended to be sealed to restrict flow into the annulus.

Failure to seal some of the penetrations resulted from improper implementation ofthe well-defined design expectations.

The team considered this problem not directly related in terms ofcause to the other inventory loss mechanisms under consideration.

(Note Although the root cause team did not include "improper implementation ofwell-defined design expectations" in their summary of root causes, it was identified in their report.

Management considered this a relevant root cause or contributor and included it in the discussions of root causes that could potentially affect operability ofsafety systems.)

Page A-3

Short Term Assessment Program Rev. 2 Appendix A With regard to the fifth contributor, until recently there was incomplete knowledge pertaining to the effect of the inactive sump on recirculation sump inventory during accident scenarios.

The team concluded that, while this condition warrants concern, the cause of this contributor is rooted in the lack of identification of the issue on a more fundamental level.

Since the concern had never been identified, the operations and engineering staff could not be expected to be knowledgeable on the subject.

The root causes associated with CALItem 1 are:

Lack ofthorough engineering review

~ ~

Inadequate design control during initialplant design

~

Improper implementation ofwell defined design expectations Ste 2 - Consideration ofIm lications Lack ofthorough engineering review Design reviews addressing the recirculation sump incorporated simplifying assumptions that were considered bounding, but did not consider the entire range of conditions under which the equipment could be required to function.

For example, small break LOCA concerns were generally considered bounded by large break LOCA analysis.

Assumptions were made that small break LOCA scenarios did not need to be reviewed with respect to recirculation sump performance and that additional evaluations were not needed to supplement the simplified methodology utilized in the LOTIC code to model containment performance for large break scenarios.

Hence the true dynamic nature of recirculation sump level was never recognized.

Lack of thoroughness in reviews of safety related equipment could result in systems being unable to perform their intended function.

Short-term assessment actions were considered necessary to address this concern.

Inadequate design control during initialplant design This concern centered on failure of AEP and Westinghouse to ensure that all design'equirements were met for a system that had shared engineering responsibility.

This

,example is considered unique.

First, the adequacy of containment sump inventory can not be functionally tested.

Unlike other design aspects that rely solely on analyses to demonstrate their acceptability (e.g. evaluating core response during transients using industry-accepted assumptions and analysis techniques), the assumptions and analytical techniques needed to assess sump performance are plant-specific.

The ability to functionally test other interfacing systems and the use of industry-accepted methodologies on other important safety analyses were considered adequate to preclude this cause from affecting other safety systems.

Although specific short-term actions were not identified for this root cause due to the uniqueness of the situation, this was considered another general example of failure to consider multiple functional design requirements ofan SSC, which was addressed in the 'short-term assessment.

Page A-4

Short Term Assessment Program Rev. 2 Appendix A Improper implementation ofmell defined design expectations The expectations for crane wall penetration sealing were clearly defined, but were not implemented.

Although it was recently determined that sealing of the crane wall penetrations was not necessary to ensure adequate inventory, the implications of improperly implementing and maintaining design expectations on SSCs are significant.

Short-term assessment actions were considered necessary to address this concern.

CALItem 2: Recirculation Sump Cover Venting Ste 1 Root Cause Determination The problem was defined as "plant design was changed by plugging the holes in the roof ofcontainment recirculation sump without considering the design and licensing bases for the holes."

Pertinent facts brought forth in the investigation include:

~

The design change, RFC 12-2361, contained a description and reason for boring the holes in the sump cover.

Hole locations were accurately defined on a core bore request sketch in the field installation portion ofthe RFC.

~

The basis for the holes in the Units 1 and 2 sump cover is contained in submittal AEP:NRC:0110, which was a commitment from the FSAR questions and answers.

This correspondence leads the Alden Lab sump model study report.

The vent holes were plugged under job orders in response to condition report investigations in 1996 and 1997.

One of the job orders identified that the holes were assumed abandoned bolt holes.

~

RFC 12-2361 was inadequate in that:

Changes made were not fullyreflected in design documents; the holes were shown on a structural drawing, but not on flow diagrams or system description.

The foreign material exclusion (FME) zone for the sump was relocated upstream when the internal plate was removed and a fine mesh screen was added at the sump entrance.

However, steps were not taken to assure particle retention criteria were maintained for other sump inlets (such as the sump cover vent holes).

~

A search of the computerized licensing database (using FOLIO) for "sump holes" provides an immediate link to AEP:NRC:0110.

FOLIO was not available to system engineers until mid-1997.

The root cause determination employed change analysis, barrier analysis, interviewing, and event and causal factor charting.

The root cause team summarized their findings Page A-5

0

Short Term Assessment Program Rev. 2 Appendix A primarily in terms of human performance issues, but more direct causes can be, derived from their investigation:

The relevant root causes associated with CALItem 2 are:

~

FME protection not installed (considered as another example of "improper implementation ofwell-defined design expectations" noted in CALItem 1)

~

Design change not properly incorporated into design documentation

~

Design and licensing basis not retrieved in a timely manner Ste 2-ConsiderationofIm lications FMEprotection not installed Failure to consider FME requirements in this case occurred nearly 20 years ago.

FME, particularly with regard to recirculation sump performance, has been a,focus area in recent years. In'act, heightened awareness ofthe importance ofFME led to plugging the holes in the sump cover.

No specific short-term efforts were considered necessary to address FME protection. However, this situation was considered an example offailing to implement design expectations and failing to preserve design requirements, which were considered necessary to address in the short-term assessment.

Design change notproperly incorporatedinto design documentation Although the root cause as stated could indicate a fundamental weakness in configuration management, there are reasons for limiting the scope of concern.

First, this was a case where a minor aspect of a larger design change was overlooked in some portions of the documentation.

Safety system operability was not threatened by this oversight.

There is no basis for concluding from this example that functionally significant features have been omitted from design documentation.

Second, this design feature was functioning outside its typical discipline; the holes were a structural feature that was performing a mechanical function. The structural drawings portrayed the holes, but their function (i.e., vent holes) was not indicated.

They were not included on the mechanical flow diagrams.

Finally, a third factor is that this design feature could not be tested and was not included in an inspection program.

While the first point supports a conclusion that operability of safety systems is not threatened by design documentation deficiencies, it was concluded that some additional actions be included in the short-term assessment actions.

l Although it was not designated as a root cause or significant contributor by the investigating team, the management group also discussed the implications of plugging these holes under a maintenance action request.

To provide assurance that there is not a programmatic weakness allowing modifications to be done under a work order, a search of the computerized maintenance work order system was conducted using various key words that could indicate modifications were being done.

No maintenance action requests were found that improperly implemented modifications. The management group concluded that that appropriate programmatic controls to prevent unauthorized modifications are in place.

In the case of the sump cover holes, the system engineer believed that plugging the holes was necessary to return the sump to its intended Page A-6

Short Term Assessment Program Rev. 2 Appendix A configuration and therefore made a conscious (but incorrect) decision that the work was not a modification.

Design atid licensing basis information not retrieved in a timely manner Two facts help mitigate the implications of this cause.

First, the design information in question was a minor aspect of the overall sump modification package and was not properly documented.

Second, the system engineers now have access to FOLIO, which increases the efficiency with which obscure licensing information can be retrieved.

No additional short-term assessment actions were considered necessary.

Cal 3: 36-hour Cooldown Ste 1 Root Cause Determination The root cause investigation focused on two problems.

First, discrepancies were

'identified between the CCW system design temperature of95' contained in the UFSAR and the procedural temperature allowance of 120'.

Second, CCW heat exchanger modeling errors were discovered in the 36-hour cooldown analysis performed by Westinghouse.

For the first problem area, the team found that as early as 1969, the Westinghouse design criteria and functional requirements for the CCW system (transmitted via Westinghouse letter AEW-640) has verbiage describing 95' as the normal operating value, with allowance for operation at 120' during cooldown of the plant.

Review of other documentation and discussions with Westinghouse led the team to conclude that the design basis was intended to allow higher temperature operation during single train cooldown, but the UFSAR contained an incomplete description of the intended design basis.

'For the second problem area, the team found that the CCW heat exchanger, a TEMA-E type procured by AEP, was assumed by Westinghouse to be a counterflow type, which was consistent with CCW heat exchangers typically supplied by Westinghouse.

The root causes associated with CALItem 3 are:

Design parameters for all system conditions were not described in the UFSAR

~

Analysis used an unverified (and incorrect) assumption ofheat exchanger type Ste 2-ConsiderationofIm lications Design parameters forall system conditions were not describedin the UFSAR Failure to totally describe the intended design basis ofthe CCW system in the FSAR led to being outside the design basis by definition, but did not represent a threat to system function or operability. No short-term assessment actions were considered necessary.

Page A-7

Short Term Assessment Program Rev. 2 Appendix A Analysis used an unverified (and incorrect) assumption ofheat exchanger type Using incorrect heat exchanger information in the analysis model could potentially result in a system being unable to perform its intended function.

This instance could also be considered another example of "inadequate design control during initial plant design."

Short-term assessment actions were considered necessary to address this concern.

CALItem 4: Switchover from Injection to Recirculation Ste 1-Root Cause Determination Two problems were investigated.

The first addressed refueling water storage tank (RWST) level instrumentation not reflecting actual RWST level. The second addressed a

procedure-directed alignment where a single active failure of the west residual heat removal (RHR) pump could cause a loss of all high head safety injection pumps duririg transfer to cold leg recirculation.

Pertinent facts for the RWST level problem included:

~

Westinghouse originally designed the system with the level instrumentation located on the RWST.

AEP moved the instrumentation from the tank to the ECCS pump suction piping.

~

Start-up tests did not identify the error introduced by the instrument location, although it should be noted that identification of such errors was not the purpose ofthe testing.

~

AEP did not recognize that relocation of the instruments from the RWST to the pipe introduced significant water velocity induced error in the level measurements, which are used by the operators and provide input to the automatic RHR pump trips.

In 1993, the NRC identified that AEP calculations supporting relocation of the instrument tap had not considered the velocity-induced bias.

~

AEP attempted to address the identified NRC concern. No changes were made to the instrumentation, but in the effort to resolve the issue, two errors occurred:

Only part of the velocity induced error was recognized.

The friction losses associated with elbows and straight sections ofpipe were addressed, but the entrance losses and the dynamic head losses were not addressed.

Only the need to prevent pump damage that could result from operation at too low an RWST level was recognized.

The need to assure that sufficient water was transferred

&om the RWST to the active sump was not recognized.

Therefore, it was concluded that since the friction error made the indicated water level in the RWST appear lower than actual, the error was conservative because it would trip the RHR pumps sooner, thereby Page A-8

Short Term Assessment Program Rev. 2 Appendix A providing even better protection for the RHR pumps.

It was not recognized that the same error was non-conservative with regard to the second purpose of the instrumentation, i.e., to transfer sufficient water from the RWST for long-term core cooling and containment protection.

In that case, the operator would believe more water had been transferred to the sump than actually had been transferred.

~

It has since been determined that locating the level instrument on the process pipe is unacceptable.

The instrumerit tap has been moved and the containment sump levels designated in procedure OHP-4023.ES-1.3 have been revised to provide for proper water levels to protect the pumps from vortexing and ensure adequate water inventory in the sump for long-term cooling.

This root cause determination was conducted using fault tree analysis methodology.

The evaluation team used a variety of resources, including condition reports, design basis documents and notebooks, early-revision drawings, and interviews with AEP personnel.

The team identified four contributors to this problem:

1) using this type of instrumentation in a non-standard location, 2) failure to recognize the physics of the location, 3) incomplete understanding ofthe purposes ofthe instrumentation, and 4) lack ofstrong interdisciplinary reviews.

The first contributor, use of an instrument in a non-standard location, resulted from AEP changing the location of the instrument tap from the tank to the ECCS pump suction piping during the original design of the plant.

Although no documentation could be found describing why the position was changed, some AEP personnel indicated that they believe the instrument was moved to provide better protection from cold weather.

The second contributor, failure to recognize the physics of the instrument location, resulted from relocation ofthe instrument. AEP personnel did not recognize that the pipe location introduced velocity effects not present in the original location.

Therefore, the calculations that supported the relocation made no provisions for the velocity effects.

The plant remained in that condition until 1993 when an NRC inspection identified those velocity effects had not been considered.

Atthat time,'EP revisited the calculations and addressed some, but not all the velocity induced effects The third contributor, incomplete understanding of the purposes of the instrumentation, resulted in some instrument bias not being included in the RWST level setpoint.

Since the velocity friction losses that were identified tend to make the RWST level appear lower than actual, it was decided they were conservative because they would cause the RHR pumps to trip sooner and provide better protection of the RHR pumps from vortexing.

The second, unrecognized purpose is to assure that adequate water is transferred from the RWST for long term cooling of the core and containment.

No changes to the instrumentation or procedure were made.

The plant remained in the same condition until the recent extensive reviews in 1997.

The fourth contributor was lack of a strong interdisciplinary review.

Although the calculations were verified by I&Cpersonnel, interdisciplinary reviews ofthe calculations were not conducted.

Such reviews might have recognized the oversight.

Page A-9

Short Term Assessment Program Rev. 2 Appendix A Pertinent facts related to the problem ofthe procedure configuration where a single active failure ofthe west RHR pump could cause a loss ofall high head safety injection pumps during transfer to cold leg recirculation include:

Procedure OHP 4023.ES-1.3, Rev 1, provided an alignment sequence for switchover from ECCS injection to recirculation phase which established SI pump flow via the west RHR train and CCP flow via the east RHR train prior to isolation ofthe RWST as a suction source for the CCPs.

This sequence does not establish dependence of all high head safety injection on either RHR pump and therefore precludes single failure vulnerability.

~

ES-1.3, Rev 2, provided an alignment sequence for switchover from ECCS injection to recirculation which established both trains of safety injection (SI) pump flow and centrifugal charging pump (CCP) flow simultaneously from the west RHR train, with the RWST suction source for both the CCPs and SI pumps isolated. At this point, the suction source &om the east RHR train would not be available.

This sequence established dependence ofall high head safety injection pumps on the west RHR pump.

The failure of the pump under these conditions could have resulted in the loss ofall high head safety injection pumps.

~

During the time frame of the preparation of ES-1.3, Rev 2 the sequence of switchover from injection to recirculation mode of ECCS and CTS operation was described in Table 6.2-10 ofthe updated FSAR (pages 6.2-52 and 6.2-53).

This sequence provides for establishment ofthe RHR suction source for the CCPs from the east RHR train prior to the isolation of the RWST suction supply.

This sequence does not establish dependence ofall high head safety injection on either RHR pump.

~

The unreviewed safety question determination for ES-1.3, Rev 2 (for both units) is contained in a June 8, 1992 safety review memorandum.

The review is more extensive than many such reviews and discusses a considerable number of open items, but it does not identify or discuss the switchover sequence which resulted in the dependency ofall high head safety injection on the west RHR pump.

~

The definition of "single active failure" contained in Section 6.2 of both the original FSAR and the updated FSAR in effect at the time of the generation of ES-1.3, Rev 2 states that active failure is the "inability of any single dynamic component or instrument to perform its design function when called upon to do so by the proper actuation signal."

The FSAR/UFSAR also states, "Table 6.2-6 summarizes the results of the single failure analysis applied during the injection phase.

All failures during this phase are assumed to be active failures.

It is during this phase that the pumps are starting and automatic isolation valves are required to move.

All credible active failures are considered."

The failures described in Table 6.2-6 for RHR pumps in both the injection and recirculation phases are noted as "failure to start."

This root cause analysis was performed using the fault tree method.

During the root cause investigation of this event, the team consulted a variety of information resources, Page A-10

Short Term Assessment Program Rev. 2 Appendix A including earlier revisions of ES-1.3 and associated safety screenings and safety reviews, condition reports, and the original FSAR, current UFSAR, and intermediate revisions of the UFSAR. AEP personnel were consulted as needed.

The team identified three contributors for additional investigation:

1) definition of "single active failure", 2) development of the procedure revision which directed the improper equipment alignment, and 3) reviews of the procedure revision that failed to identify the problem.

The team considered the definition of "single active failure" with respect to ambiguity and lack of consistency between internal documents, within the UFSAR, and in regulatory documents.

While contributing factors may lie in these

areas, the primary consideration impacting the situation under review was the fact that the ECCS alignment of concern did not appear to be a "single active failure" requiring review under the criteria of the plant's design basis (original FSAR).

Failure to recognize the correct definition contributed to the failure to identify and correct the unacceptable ECCS lineup.

To establish the point at which the unacceptable lineup first appeared, earlier revisions of the ES-1.3 for both units and the UFSAR were examined.

The unacceptable lineup was incorporated into these procedures during revision 2. This revision was intended to make the procedures consistent with the sequence of steps specified in the FSAR for switching to the recirculation mode of ECCS and CTS operation as well as to provide for more inventory transfer from the RWST to the recirculation sump.

The preparer was not able to provide any additional information to provide an understanding of the apparent inconsistency between his intention to incorporate the procedure specified in the FSAR into ES-1.3 and the fact that the procedure and the FSAR do not match.

Proper incorporation of the FSAR steps would have precluded the single failure vulnerability introduced by revision 2.

The root causes associated with CALItem 4 are:

~

Lack ofconsideration ofBernoulli effect on level instrumentation

~

Incorrect application ofsingle failure criteria Ste 2-Consideration ofIm lications Lack ofconsideration ofBernoulli effect on level instrumentation Failing to consider potential biases on instrumentation could potentially result in a system

'eing unable to 'perform its intended function.

Short-term assessment actions were considered necessary to address this concern.

Incorrect application ofsingle failure criteria Failing to properly apply single failure criteria could potentially result in a system being unable to perform its intended function.

Short-term assessment actions were considered necessary to address this concern.

Page A-11

Short Term Assessment Program Rev. 2 Appendix A CALItem 5: Compressed AirOverpressure Ste 1 Root Cause Determination The problem statement focused on why overpressure protection was not provided on the 20-, 50-, and 85-psig control air headers.

Pertinent facts brought forth in the investigation include:

~

The compressed air systems at Cook Plant, including plant air and control air, are of the same design as compressed air systems installed in AEP fossil generating plants during the same time frame.

Bailey Controls Publication G18-2, "Product Instructions for Connecting Tubing and Accessories for Pneumatic Control and Transmission," provides six typical installations for either two or three low-pressure header connections.

Safety valves are provided on pressure vessels but not on the downstream side of pressure regulators.

These arrangements are typical ofthe Cook Nuclear Plant air systems.

~

Information Notice 87-28, "AirSystem Problems at U.S. Light Water Reactors,"

focused on the assumption that safety related equipment would fail to a safe position on loss-of-air or perform its intended function with the assistance of safety related back-up supplies.

Subsequently, Generic Letter 88-14, "Instrument Air Supply Problems Affecting Safety Related Equipment," identified that the performance of air-operated safety related components may not be in accordance with their intended safety function because of deficiencies in design, installation, and maintenance.

The primary focus ofthe GL and AEP's response was to assure that safety related components function under loss-of-air. None of the examples dealt with overpressure events.

Information Notice 88-24, "Failures of Air-Operated Valves Affecting Safety Related Systems," focused on 3-way solenoid valves not operating properly against the supplied air pressure.

~

In accordance with the original FSAR, the design code for the air system vessels is ASME Section VIII. Safety valves are provided as required by code.

The remainder ofthe system is designed in accordance with ANSI B31.1, which does not require safety valves ifthe piping downstream ofthe regulators is designed to withstand the unregulated upstream pressure.

This condition applies to the Cook Nuclear Plant design.

~

The reliabilityofair regulators at Cook Nuclear Plant has been excellent.

The team determined the root cause primarily through document review and personnel interviews. The facts led the team to conclude that the designers ofthe air system did not recognize that overpressure protection was necessary because this was a non-safety related system, the components had a successful history in AEP fossil applications, and the arrangement was typical of industrial applications where high reliability was important. The designers did not recognize all credible failure modes.

The root cause associated with CALItem 5 is:

Page A-12

Short Term Assessment Program Rev. 2 Appendix A

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Failure to identify a non-safety system failure mode that could impact safety system components Ste 2-Consideration ofIm lications Failure to identify a non-safety system failure mode that could impact safety system components Failing to identify that a non-safety related system could potentially cause the failure of redundant safety related equipment has serious and far-reaching implications. Short-term assessment actions were considered necessary to address this concern.

CAI Item 6-RHR Suction Valve Interlock Ste 1 Root Cause Determination The problem statement focused on the fact that defeating the interlocks for the RHR suction isolation valves prior to venting the RCS to atmosphere places the plant in a condition outside its design basis.

Pertinent facts brought forth during the investigation include:

Information Notice 80-20, "Loss of Decay Heat Removal Capability at Davis-Besse Unit 1 while in a Refueling Mode," and IE Bulletin 80-12, "Decay Heat Removal System Operability," prompted AEP to implement procedure changes in June 1980.

The changes involved removing power from the RHR suction isolation valves gMO-128 and ICM-129) after opening the

valves, which typically occurs at an RCS pressure ofabout 400 psig.

~

The procedure change was accomplished via a Procedure Temporary Change Sheet.

FSAR Section 9.3.2 states, "The suction line valves are interlocked through separate channels of the Reactor Coolant System pressure signals to provide auto>atic closure of both valves whenever the RCS pressure exceeds design pressure of the RHR system."

The same section later states, "Overpressure protection in the RHR system is provided by relief valves discharging to the Pressurizer Relief Tank in the RCS coupled with interlocking ofthe RCS to RHR suction valves to close whenever RCS pressure exceeds design pressure of the RHR system."

~

The AEP response to IE Bulletin 80-12 describes the RHR suction valves having power removed "ifthe RCS is vented to atmosphere," but it does not describe (or preclude) the practice ofremoving power for the entire time RHR is in service.

~

AEP:NRC:1033, response in November 1987 to Generic Letter 87-12, "Loss of Residual Heat Removal while the Reactor Coolant System is Partially Filled,"

discussed the RHR suction valve interlocks as described in the FSAR.

The Page A-13

Short Term Assessment Program Rev. 2 Appendix A response does not note that the isolation valves are opened and deenergized the entire time RHR is in service.

The normal operating procedure was apparently not reviewed when developing this response.

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AEP:NRC:1033C, response in February 1989 to Generic Letter 88-17, "Loss of Decay Heat Removal Program Enhancements,"

correctly noted that control power is removed &om the RHR suction isolation valves whenever RHR is in service, as suggested by GL 87-12.

~

Low temperature overpressure protection (LTOP) relies on the RHR suction isolation valves being blocked open; however none of the various LTOP reviews identified the conflict with the UFSAR.

The root cause team concluded that the original procedure change was made with good technical justification and attention to actual safety implication. However, the procedures and processes in place did not successfully lead the individuals involved to identify the discrepancy created with the UFSAR and technical specifications.

Secondly, the change made to the plant in 1980 would be covered under the design change process using today's design control program and procedures.

The team concluded that a design change would have given the change more visibilityand would be expected to find the UFSAR and technical specification discrepancies.

The team also expressed concern that a number of formal reviews over the last 17 years provided opportunity for the inconsistency to be noted.

The root causes associated with CALItem 6 are:

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Processes in place did not emphasize the UFSAR, resulting in an inadequate safety review

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Design change was accomplished via procedure revision Ste 2-ConsiderationofIm lications Processes in place (at the time) did not emphasize the FSAR, resulting in an inadequate safety review The implications of this cause are mitigated by the fact that engineering reviews were properly performed and the plant was actually configured and operated in the desired manner.

Failure to recognize the inconsistency of the desired configuration with the FSAR led to being outside the design basis, but did not represent any threat to system functionality. No short-term assessment actions were considered necessary.

Design change accomplished viaprocedure revision The implications of this cause are mitigated by the fact that engineering reviews weie properly performed and the plant was actually configured and operated in the desired manner.

Failure to identify the FSAR inconsistency and failure to recognize that the technical specification surveillance was superfluous did not represent any threat to system function or operability.

No short-term assessment actions were considered necessary.

Page A-14

Short Term Assessment Program Rev. 2 Appendix A CALItem 7: Fibrous Material in Containment Ste 1 Root Cause Determination In September 1997, fibrous material was found in an electrical cable tray in the Unit 2 containment.

The purpose of the investigation was to determine why fibrous material was in containment.

Pertinent facts brought forth in the investigation include:

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Interview information:

From original construction until late 1992, a contractor was used for all plant insulation installation and repair work. The contractor was under the control ofAEP, but was relied upon to plan and execute insulation work with minimal direct supervision.

The AEP thermal insulation specification (DCC-NEMP-450-QCS) was not often used or referenced during planning or installation. Instead, skill-of-the-craft and knowledge ofthe planners was used.

The design specification for fire barrier penetration seals and its implementing procedures allowed noncombustible damming material to remain in place following seal installation.

Based on interview information, the authors of revisions to the design specification were unaware of the concern with fibrous material in containment.

A review of three design change packages for installation of fire stops or fire breaks revealed that the safety reviews did not mention concerns on the use of fibrous material.

~

Interview informa'tion: A January 1989 engineering memo allowed the use of stainless steel mesh to encapsulate blanket-type insulation on a temporary basis in

'ieu of 0.010-inch stainless steel.

The memo provided explicit instructions to replace the temporary insulation with reflective metallic insulation (RMI) at the first convenient outage.

The author intended the memo to be used on a one-time basis for a specific circumstance where pieces of RMI were missing or damaged at the completion of the Unit 2 steam generator replacement.

However, plant personnel continued to use that memo as justification to use mesh-encapsulated blanket insulation when necessary to meet ALARAand production concerns.

A process to remove such "temporary" installations was not implemented, and the thermal insulation specification was not revised to incorporate the practice.

Information Notices 88-28, 90-07, 93-34, 95-06, and 96-59, IE Bulletin 93-02, and Generic Letter 85-22, all dealing with the potential for loss of post-LOCA recirculation capability due to debris blockage, were evaluated by AEP.

The reviews focused on specified insulation materials and did not consider actual plant conditions.

Page A-15

Short Term Assessment Program Rev. 2 Appendix A The team used a combination of event

charting, cause-and-effect
analysis, barrier analysis, interviews, document reviews, and mini-MORT.

The reason fibrous material was introduced to containment was determined to be a lack of procedures implementing the requirements of the thermal insulation specification

, during planning and implementation, coupled with a failure to address the sump plugging potential of fibrous material in the specification itself.

Incomplete evaluation of NRC Information Notices and IE Bulletins resulted in a series of missed opportunities to identify and encapsulate or remove fibrous material.

The root causes associated with CALItem 7 are:

Lack of procedures for implementing the requirements of the thermal insulation specification

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Failure to address sump-plugging potential of fibrous insulation material installed in containment Ste 2-Consideration ofIm lications Lack ofprocedures forimplementing an insulation specification Failure to have a detailed procedure was considered to be a symptom of the more fundamental concern of failing to recognize and preserve multiple functional design requirements of some installed plant features.

Short-term assessment actions were considered necessary to address this concern.

Failure to address sump-plugging potential offibrous insulation material installed in containment Failing to recognize multiple functional design requirements of SSCs could result in systems being unable to perform their intended function.

Short-term assessment actions were considered necessary to address this concern.

CALItem S: Leak Back to RWST during Recirculation Ste 1 Root Cause Determination The problem was stated as:

Only two of six mini-flow recirculation line valves have leakage verification tests.

Pertinent facts brought forth in this investigation include:

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Information Notice 91-56, "Potential Radioactive Leakage to Tank Vented to Atmosphere,", was issued to alert the industry of a potential problem resulting from leakage of ECCS recirculation isolation valves to safety injection water storage tanks (RWST at Cook Plant).

Page A-16

Short Term Assessment Program Rev. 2 Appendix A

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IN 91-56 was assigned to Nuclear Safety and Licensing in AEP's corporate headquarters.

The document trail for IN 91-56 is incomplete, although the team's report includes a chronology ofevents occurring in NSEcL and at the plant.

The team 'concluded that this was a valid issue.

Additional valve testing should have been accomplished, or in its absence, sound engineering basis should have been documented to justify actions or non-actions resulting from review ofIN 91-56. It was evident that the reviewer did recognize that the IN impacted Cook Plant.

Calculations were performed to determine dose received from a postulated leak path back to the RWST. In addition, a change was made to the UFSAR, a test procedure was developed, some valves were tested, and ASME valve categories were revised.

The decisions and actions were not well documented; however, evidence clearly demonstrates that the IN, was evaluated and acted upon.

The relevant root cause associated with CALItem 8 is:

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Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Ste 2-Consideration ofIm lications Failure to ensure that plant equipment met assumptions incorporated in licensing basis calculations Failing to ensure that analysis assumptions are met could potentially result in a system being unable to perform its intended function.

Short-term assessment actions were considered necessary to address this concern.

Lake Temperature Design Basis Discrepancies (CR-97-2196) and Lake Temperature Effect on Control Room Ventilation (CR-97-2390)

Ste 1-Root Cause Determination The problem is defined as allowing the use of a higher, and thus less conservative, maximum lake water temperature value than listed in UFSAR Table 9.5-3.

Pertinent facts brought forth in the investigation include:

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The weather in 1988 was unprecedented, with both extremely high temperatures and drought.

Actual lake temperature data identified a high lake temperature of 83.9'F on August 17, 1988.

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Although the effects of higher lake temperature on important plant parameters were evaluated, a comprehensive 10 CFR 50.59 review was not completed to support operation at the higher lake temperature.

All potentially relevant calculations were not reviewed to determine the impact oflake temperature higher Page A-17

Short Term Assessment Program Rev. 2 Appendix A than the UFSAR value of76'. The review did not identify that the UFSAR and other related documents needed to be changed.

The lake temperature value of 76'F is listed in a UFSAR Chapter 9 component data table falls within 10 CFR 50.2 and the recently issued DIR-2300-04 definition of"design bases."

~

Memorandum "Operation at Elevated Essential Service Water Temperature" from D. B. Black dated July 29, 1988 established criteria for evaluating increased ESW temperatures.

The stated criteria was, "Operation of Cook Nuclear Plant with ESW temperatures greater than 76'F is not necessarily precluded (that is, operating is an unanalyzed condition) as long as:

a margin exists between the peak pressure and the design pressure, and; the sensitivity ofthe change in calculated peak pressure due to changes in ESW temperature are known."

~

While analysis has shown that higher temperatures are acceptable for containment heat removal, no single analysis identified and resolved all effects ofthe change in design basis lake temperature.

Design inputs were not "correctly translated into

[all affectedJ specifications, drawings, procedures, or instructions", as required by 10 CFR Appendix B and ANSIN45.2.11.

~

In 1988 when the lake temperature was above (or projected to be above) 76', a reevaluation ofcontrol room HVACfor higher ESW temperature was performed.

The result was that the then-current technical specification control room temperature limit of 120' would not be exceeded at or below 87.5'F lake temperature.

Operability ofthe control room HVAC and decay heat removal was evaluated at the time, but a comprehensive 10 CFR 50.59 review was not found to acknowledge the use of non-conservative higher temperatures or that it was a deviation from the UFSAR. Not all affected ESW heat loads were specifically addressed.

~

A July 29,1988 memorandum from D. B. Black to B. A. Svensson states a prior maximum lake temperature of 79.5' was identified. Based upon interview information, no engineering reevaluations were performed for the earlier high lake temperature condition of79.5' mentioned in the memo.

The root cause investigation was performed by documenting the time-line of related events using an events and causal factors chart.

Identifying, collecting, and reviewing documents associated with the events supported the events and causal factors chart.

Interviews ofinvolved personnel were then conducted.

The root cause of the events is a failure to recognize that deviation from the UFSAR value of76' for ESW temperature constituted a deviation from a design basis value.

Contributing causes include 1) rising standards for UFSAR compliance and design basis definitions were not implemented within the organization and 2) design change Page A-18

Short Term Assessment Program Rev. 2 Appendix A procedures in place at the time of these events did not require or compel considering a change to design basis value as a design change.

The root causes ofthe lake temperature issue are:

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Failure to recognize a UFSAR value as a design basis parameter

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Failure to recognize interrelationships between a UFSAR value and other design aspects Ste 2-Consideration ofIm lications Failure to recognize a UFSAR value as a design basis parameter This cause is associated with the confusion surrounding justification for plant operation when the lake is above 76'.

It is clear that AEP nuclear generation pexsonnel did not consider all UFSAR values design basis parameters.

This cause is at the heart of concerns raised by the design inspection team.

However, no instances (including investigation of a substantial number of condition reports arising from the UFSAR revalidation efforts, both before and after the design inspection) were noted where failure to recognize UFSAR values as design basis values led to failure to perform technical reviews when warranted.

Failure to recognize UFSAR values as design basis parameters may lead to being outside the plant design basis by definition, but has not been identified as posing a threat to system functionality. No additional short-term assessment actions were considered necessary.

The longer-term pxogram arising from the design inspection willaddress this basic concern.

Failure to recognize interrelationships behveen a UFSAR value and other design aspects This cause is also associated with plant operation when the lake is above 76', but centers on deficiencies in the evaluation of control room instrumentation.

The potential impact of higher control room temperatures on instrumentation life was recognized by AEP and was evaluated.

At the time of the evaluation, the technical specification limit for control room temperature was 120' temperature.

Per the basis of the technical specifications, this limitwas consistent with the continuous duty rating of control room equipment.

Subsequent to these reviews (c.

1992), it,was determined that not all equipment was qualified for continuous duty to 120' and the technical specification limit for normal operation was lowered to 95'.

While it is clear that AEP nuclear generation personnel did not consider all UFSAR values to be design basis parameters, no instances have been noted where this failure led to failure to perform technical reviews when warranted.

No additional short-term assessment actions were considered necessary.

Page A-19

Short Term Assessment Program Rev. 2 Appendix A Unit 2 Full Core Off-load with Concurrent CCW Dual Train Outage (CR-97-2341)

Ste 1-Root Cause Determination The problem was defined as: The dual train CCW outage which had occurred during the 1996 Unit 2 refueling outage did not have a sufficient 10 CFR 50.59 safety evaluation to support it.

Pertinent facts brought forth in the investigation include:

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The purpose ofthe safety evaluation for this evolution was to evaluate whether or not the configuration represented by a full-core offload for U2R96 represented an unreviewed safety question.

The safety evaluation assumed the unavailability of one train of spent fuel pool cooling to evaluate the adequacy of heat removal in the fullcore offload condition.

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The SER for the spent fuel pool re-rack states that it is not necessary to assume less than two trains ofspent fuel pool cooling are available.

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The safety evaluation was supported by calculation N96-01-01 which demonstrated that with a full core offload and only one train of SFP cooling in operation, the spent fuel pool temperature would be maintained less than 150'.

This is within the UFSAR design basis temperature of 159.54'.

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UFSAR Section 9.4.1 states, "Any spent fuel pool loading scenario which meets the 160' peak bulk pool temperature and 5.74 hours8.564815e-4 days <br />0.0206 hours <br />1.223545e-4 weeks <br />2.8157e-5 months <br /> to boil criteria is acceptable."

~

Based on heat load and the supporting calculation, the spent fuel pool was clearly within the thermal hydraulic design basis with 'this configuration, since it met a peak bulk pool temperature of less than 160' and a minimum boiling time of much longer than 5.74 hours8.564815e-4 days <br />0.0206 hours <br />1.223545e-4 weeks <br />2.8157e-5 months <br />.

~

The shutdown risk assessment dated March 22, 1997 did not completely document how the licensing issues for a dual train CCW outage were addressed.

In particular, it did not address a postulate LOCA on Unit 1 while the Unit 2 dual-train CCW outage was in progress.

~

The shutdown risk assessment did reference abnormal operating procedures designed to provide SFP cooling in the event that CCW cooling was lost.

The investigation concluded that the safety reviewer performed an adequate review ofthe full core offload. During the outage, no condition outside the design basis or licensing basis was incurred.

A risk assessment was performed during the planning of the schedule.

Documentation ofthe licensing issues involving spent fuel pool cooling with a dual train CCW outage in Unit 2 and a postulated LOCA in Unit 1 was not complete.

However, as evidenced by the contingency planning to ensure adequate cooling in the event CCW cooling was lost, the design basis and licensing basis issues were addressed.

The root cause of the failure to fully document the licensing issues during the planning for this evolution was personnel error.

The issues were addressed.

Previously, a Shift Page A-20

Short Term Assessment Program Rev. 2 Appendix A Technical Advisor performed the risk assessment.

The procedure now requires a group including, an operations shift supervisor, a scheduling person, a Shift Technical Advisor, and an engineer from the Safety Analysis group.

Since the safety evaluation and USQD are considered

adequate, no root cause was developed.

The implication that should be addressed, however, is:

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10 CFR 50.59 reviews may be inadequate Ste 2 Consideration ofIm lications 10 CFR 50.59 reviews may be inadequate The root cause investigation as described above represents the basis for our retraction of the LER associated with this issue and for originally concluding that no short term assessment actions were necessary to address potential 10 CFR 50.59 inadequacies.

Following discussions with NRR and Region III staff on December 22, 1997, we now understand that the change represents an unreviewed safety question due to reduction in

margin, and have agreed to conduct a

self-assessment of safety screenings and evaluations in the short term. This review willlook for unreviewed safety questions and operability concerns.

Note that this additional review is not reflected in Tables 1, 2, and 3.

Restriction ofCCW Temperature During Unit 2 Core Off-load (CR-97-2342)

Ste 1 Root Cause Determination The problem was defined as:

Inadequate safety evaluation performed for establishment ofa 90 degree F upper limitfor CCW during the Unit2 1996 refueling outage.

Pertinent facts brought forth in the investigation. include:

A 10 CFR 50.59 safety evaluation addressing the U2R96 proposed full core offload was issued on March 11, 1996. An addendum was issued on March 20, 1996.

The safety evaluation discussed the Spent Fuel Pool Cooling System heat load analysis, assuming:

1) the existing fuel assembly inventory, 2) a full core offload, 3) a bounding lake temperature for the March/April time frame, 4) a maximum CCW temperature of80.5', and 5) a single train of Spent Fuel Pool Cooling. Addendum 1 revised the CCW temperature to 90.7'.

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Although the analysis demonstrated that the Spent Fuel Pool temperature remained below the limit of 160',

an Unreviewed Safety Question Determination was performed since the CCW temperature and system cooling capacity was different than that found in the UFSAR (Table 9.4-2). It concluded that although the assumed CCW temperature was less than the UFSAR value, the CCW temperature and the SFPCS heat removal values are nominal design values Page A-21

Short Term Assessment Program Rev. 2 Appendix A and modification of these values on an outage basis does not require a change to the FSAR;

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The Condition Report was written because the safety evaluation did not recognize the CCW temperature change as a design change, to the SFPCS heat exchanger CCW inlet temperature.

This value is listed in Table 9.4-2 of the UFSAR as 95',

and was to be administratively limited to 90'.

The purpose of the safety evaluation was to assess the acceptability of the SFP heat loads for the Unit 2 refueling outage, based on the analysis and conditions that existed at the time. The CCW temperatures were obtained based on projected SFP heat loads, a bounding lake temperature for March/April and a single train of SFP cooling, and the approved limitingdesign basis temperature of160'.

The investigation concluded that limiting the CCW temperature to 90' maintained the SFP below the maximum design basis temperature of 160';. therefore the probability or consequences of a release from the SFP was not increased.

Since this was a temporary procedure change based on the specific SFP heat removal requirements for the Unit 2 refueling outage, it was not considered a design change and did not require a permanent change to the UFSAR. The USQD performed to address the change adequately covered the temporary change in CCW temperature.

Therefore, it is concluded that the plant was not outside ofits design basis.

Since the safety evaluation and USQD are considered

adequate, no root cause was developed. The implication that should be addressed, however, is:

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The adequacy ofthe 10 CFR 50.59 review was questioned, although subsequently found to be acceptable Ste 2-Consideration ofIm lications 10 CFR 50.59 reviews may be inadequate The root cause investigation as described above represents the basis for our retraction of the LER associated with this issue and for originally concluding that no short term assessment actions were necessary to address potential 10 CFR 50;59 inadequacies.

Following discussions with NRR and Region IIIstaff on December 22, 1997, we now understand that the change may represent an unreviewed safety question due to reduction in margin, and have agreed to conduct a self-assessment of safety screenings and evaluations in the short term. This review willlook for unreviewed safety questions and operability concerns.

Note that this additional review is not reflected in Tables 1, 2, and 3.

Page A-22

Short Term Assessment Program Rev. 2 Appendix A RWST minimum volume for Appendix R (CR-97-2358)

Ste 1 Root Cause Determination The problem was identified as:

Calculation TH 90-02 determined that the minimum RWST level required to support the other unit's shutdown for Appendix R considerations to be 87,000 gallons.

Operating procedure OHP 4021.018.008 requires the RWST level to be above 10%, which is less than 87,000 gallons.

Pertinent facts brought forth in the investigation include:

Calculation TH 90-02 states, "The 87,000 gallons required is less than both the 90,000 gallons specified in technical specification 3.1.2.7 for Modes 5 and 6 and the 350,000 gallons specified in technical specification 3.5.5 for Modes 1, 2, 3, and 4 (both units)."

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Technical specification 3.1.2.7 allows the RWST level to fall below 90,000 gallons ifboric acid storage system requirements of 3.1.2.7.a are met. Therefore, it cannot be relied upon to meet the requirements ofcalculation TH 90-02.

Calculation TH 90-02 relied on an incorrect interpretation of the technical specifications that in all modes, the RWST water level would be above the calculated required water level.. It is surmised that TH 90-02 therefore was not distributed or used to revise procedures to maintain the calculated water level.

The root cause ofthis issue is:

Misinterpretation of technical specifications resulted in failure to translate calculation assumptions and results into operating procedures.

Ste 2-Consideration ofIm lications Misinterpretation oftechnical specification resulted in failure to translate calculation assumptions and results into operating procedures This case represents an instance where an individual performed a calculation to determine an operating requirement, found an existing technical specification value that he believed encompassed the new requirement, and stopped.

However, his understanding of the technical specification was incomplete and, in fact, the operating requirement was not necessarily covered under all scenarios.

Subsequent investigation revealed that compliance had always been maintained, albeit accidentally.

Although human performance is the root cause, discussion of the implications of this occurrence resulted in considering it a calculation issue.

Short-term assessment actions were considered necessary to address this concern.

Page A-23

Short Term Assessment Program Rev. 2 Appendix A 2-CD Battery Cell Left on Charge for an Extended Period (CR-97-1821)

Ste 1 Root Cause Determination The problem was defined as: 2-CD battery cell left on charge for an extended period.

Pertinent facts brought forth in the investigation include:

Cell 34 was placed on individual cell charge (ICC) aAer it was discovered on 3une 19 1997 that the cell was below the technical specification minimum voltage of 2.13VDC. The cell was left on charge until August 8, 1997 when it was decided to replace the cell.

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C&D Vendor Technical Manual,Section VI states, "Minimumacceptable voltage is the point at which plans should be made to provide equalize charge. It does not imply that the battery is malfunctioning or that it willnot provide power ifcalled upon.

Some equipment may not have equalizing potentials available.

In such

cases, a single cell charger with complete AC line protection may be paralleled across the affected cell while still a part ofthe overall battery to provide an over-voltage to that cell. Do not be alarmed ifsuch charging must continue for several weeks, particularly considering the currents actually passing through the cells are very small."

~

IEEE Std 450-1987, Appendix D4 states, "When an individual cell voltage corrected for temperature is below 2.13V, corrective action should be initiated immediately. It can be accomplished by providing an equalizing charge to the entire battery.

However, it is oAen more convenient to apply the equalizing charge to the individual cell."

~

Cell 34 was raised above its minimum technical specification potential (2.13VDC) within the two-hour LCO window.

The charge was planned to continue until it reached 2.5VDC. While the cell reached 2.5VDC on August 8, 1997, it was left on charge to provide additional assurance that the cell would provide satisfactory service until the scheduled battery bank replacement during the outage.

Cell 34 was replaced on August 11, 1997.

The root cause team concluded that, based on standard industry practice and their understanding of the ability of Cell 34 to meet its technical specification requirements, the extended charging was considered satisfactory. No root cause was determined.

Ste 2-Consideration ofIm lications Since the extended charging was considered an acceptable practice, no implications were identified and no short-term assessment items were considered necessary.

Subsequent to the root cause evaluation, we received the design inspection report. The report notes that "there was not adequate evidence to suggest that the battery train could not perform its function without the cell."

However, the report leaves operability of the cell, per technical specification requirements, as an unresolved item.

Since the battery could Page A-24

Short Term Assessment Program Rev. 2 Appendix A perform its overall function, we still conclude that short-term assessment actions are not necessary.

Code Discrepancies in CC% System Safety Valves (CR-97-2437)

Ste 1 Root Cause Determination The problem was defined as manual valves located between the reactor coolant thermal barrier cooling coil and the CCW surge tank reliefvalve do not conform to the applicable B31.1 piping code, which states that an intercepting stop valve cannot be located between the source ofpressure and the pressure reliefdevice credited for protecting the pipe.

Pertinent facts brought forth in the investigation include:

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UFSAR Section 9.5 states, "The reliefvalve on the component cooling surge tank is sized to relieve the maximum fiowrate ofwater that would enter the surge tank following a rupture of a reactor coolant pump thermal barrier cooling coil. The set pressure assures that the design pressure ofthe CCW system is not exceeded."

Paragraph 122.6.1 of B31.1 states, "There shall be no intervening stop valves between piping being protected and its protective device or devices."

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There are a total offour manual CCW system valves in each unit that are defined as intervening stop or blocking valves per B31.1.

These valves are in the open position during operation ofthe CCW system.

They are used as isolation valves for maintenance activities during outages.

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There are no administrative controls in place to prevent them from being inadvertently closed.

B31.1 does not provide guidance on locking or sealing open intervening stop valves.

However, other codes have provided direction.

For example, ASME Section VIII, Appendix A, A-,104(a)

states,

"...a full area stop valve (is acceptable) for inspection and repair purposes only.

When such a stop valve is provided, it shall be so arranged that it can be locked or sealed open and it shall not be closed."

~

The Authorized Nuclear Inspector, the ASME B31 Mechanical Design Technical Committee

Chairman, and an ASME B31 Mechanical Design Technical Committee have stated that ifa valve is sealed open, it would not be considered an intervening stop valve.

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An operating procedure that controls valve position has been revised to include sealing these valves and periodically verifying they are in the open position.

The investigation could not determine why these valves were not originally administratively controlled as required by B31.1.

The root cause associated with this issue is:

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Failure to translate design requirements into operating procedures Page A-25

Short Term Assessment Program Rev. 2 Appendix A Ste 2-Consideration ofIm lications Failure to translate design requirements into operating procedures Full conformance with the B31.1 piping code was not met in this case; however, the condition did not cause the CCW system to be inoperable.

Plant procedures did require the valves to be open, but they were not administratively controlled as needed for literal code compliance.

The potential for similar safety valve inconsistencies was evaluated as part of the condition report investigation and found not a concern.

No additional short-term assessment items were considered necessary.

Procedures Allowing'Avo RHR Pumps to Run with the RCS Vented (CR-97-2480)

Ste 1-Root Cause Determination The problem was defined as follows: Chapter 9 ofthe UFSAR (July 1994) states:

"Only one RHR pump will be operated when the RCS is open to atmosphere to prevent damaging both pumps in the unlikely event that suction should be lost." 'Operating procedures for the RHR System do not prevent operation of both RHR pumps when the

'eactor Coolant System is open to atmosphere.

O Pertinent facts brought fourth in the investigation include:

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UFSAR Section 9.3.3, "System Design Evaluation," states, "Only one RHR pump willbe operated when the RCS is open to atmosphere to prevent damaging both pumps in the unlikely event that suction is lost."

V UFSAR Section 9.3.6.2.a, "Limiting Conditions For Operation,"

states, "A

requirement to have only one RHR pump in operation whenever the RCS is drained to half-loop and vented, has been incorporated into applicable operating procedures."

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Past procedure revisions showed that a change sheet dated May 18, 1978, added the following precaution to the RHR operating procedure:

"Do not operate both RHR pumps with Reactor Coolant System drained to half-loop. Sufficient suction head is not available for two pump operations."

The investigation could not identify why the FSAR requirements were originally not incorporated into the procedures.

Safety screenings related to subsequent procedure changes did not identify the discrepancy between the UFSAR and plant procedures.

The root cause associated with this issue is:

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Failure to translate UFSAR requirements into operating procedures Page A-26

Short Term Assessment Program Rev. 2 Appendix A Ste 2 Consideration ofIm lications Failure to translate UFSAR requirements into operating procedures Plant operating procedures allowed operation outside the design basis.

This condition does not cause the RHR system to be inoperable.

No additional short-term assessment actions were considered necessary.

However, this is another example where the UFSAR was not maintained and used as a top-tier design basis document.

The longer-term programs arising from the design inspection willfocus on this basic concern.

Page A-27

ATTACHMENT 2 TO AEP:NRC:1260G4 10 CFR 50.59 PROGRAM

Attachment 2 to AEP:NRC:1260G4 Page 1

10 CFR 50.59 PROGRAM General Descri tion Cook Nuclear Plant's program to evaluate proposed plant and procedures changes and tests or experiments is based on the guidelines provided in NSAC-125 and is in compliance with the requirements of 10 CFR 50.59.

The program described below includes procedures, training, oversight and feedback mechanisms designed to maintain the current licensing basis of the plant.

The quality of the 10 CFR 50.59 screenings and safety evaluations is of the utmost importance to the management of Cook Nuclear Plant.

As a result, improvements have been, and will continue to be made to facilitate the efforts of those performing the screenings and safety evaluations to ensure that program objectives will be achieved.

Some of the most recent program improvements.are:identified

below, a number of which are in direct response'o lessons learned from the architect engineering (AE) desi.gn inspection.

Pro ram ualit The quality of the 10 CFR 50.59 screenings and unreviewed safety question determinations is based on the program's procedures, personnel qualifications, training and oversight.

In addition, interfaces with industry organizations, such as INPO, NEI, and the

NRC, ensure that rising expectations with respect to the performance of 10 CFR 50.59 reviews are implemented.

Procedures Management's expectations and the methodology to be used in implementing 10 CFR 50.59 screening and evaluations are provided through the program's procedures.

Currently, there are three procedures that address the reviews of proposed changes to the facility.

These procedures invoke the guidance provided in NSAC-125 and provide both general and specific direction to safety reviewers.

These.procedures have also been subjected to a number of internal and external inspections and audits over the years and have been revised numerous times to address suggested improvements that increase the quality of the safety reviews.

Lessons learned from Cook Nuclear Plant 10 CFR 50.59s are. also a source of many of the changes made to these procedures.

These changes include, but are not limited to, the need to provide further-guidance, address programmatic shortcomings, ensure consistency in the, level of documentation, or to reinforce management's expectations.

~Trainin To ensure that personnel have the requisite knowledge of the procedures as well as the necessary plant knowledge to successfully implement the 10 CFR 50.59 program, screeners and safety evaluators must meet minimum qualifications.

Management selects candidates to perform screenings and safety evaluations who have demonstrated a

sufficient level of plant knowledge to understand the specifics of the licensing basis and recognize challenges to it.

Candidates are trained on the expectations and methodology contained in the procedures and must demonstrate proficiency by passing a written test before qualifying as either a screener or a safety evaluator.

Once qualified, screeners and safety evaluators must annually re-qualify by attend'ing refresher training and demonstrating a

Attachment 2 to AEP:NRC:1260G4 Page 2

continued proficiency with the process through an annual written re-qualification test.

OversicVht Effectiveness of the 10 CFR 50.59 program is monitored by oversight provided by the plant nuclear safety review committee (PNSRC), the nuclear safety and design review committee (NSDRC),,

audits performed by the performance assurance department, and during NRC inspections.

A discussion of each of these is provided below.

PNSRC As required by technical specifications (T/Ss),

the PNSRC reviews and approves proposed design and procedure changes to ensure that there are no potential unreviewed safety questions and -.that the evaluations are well documented in accordance with plant procedures.

This review is a challenging one for safety evaluators because of the high standards set by the PNSRC.

In this context, the PNSRC review represents an opportunity for a select group of managers to coach the safety reviewers, who are from different parts of the organization, on their expectations.

This has been an effective method to communicate to the reviewers the importance of their responsibility.

NSDRC The NSDRC subcommittee on proposed changes conducts reviews of safety evaluations previously approved by the PNSRC and sample safety screenings of procedure changes.

This provides an additional layer of assurance that 10 CFR 50.59 reviews are completed in accordance with procedures.

Performance Assurance Performance assurance audits the 10 CFR 50.59 program on an annual basis to verify the adequacy and implementation of the safety evaluation program.

10 CFR 50.59 screenings and evaluations are also reviewed as part of other audits, surveillances, and procedure reviews'hese

audits, surveillances and r'eviews determine if:

screenings and evaluations are conducted when

required, screenings adequately identify and - consider source information,.

evaluations adequately answer any screening yes answers and consider source information correctly, evaluations adequately answer the unreviewed safety question determination questions, and the informat'ion is adequate for PNSRC to make safety decisions.

NRC routine inspections conducted by the resident inspector regularly sample 10 CFR 50.59 screenings and evaluations to verify

Attachment 2 to AEP:NRC:126064 Page 3

that proposed changes are processed in accordance with 10 CFR 50.59, and that conclusions reached in these reviews are justifiable and well documented.

Additionally, past special NRC safety inspections on the 10 CFR 50.59 program determined that procedures were well-written and contained detailed instructions and appropriate examples.

Past inspections,

however, have noted some screenings that incorrectly concluded that safety evaluations were not required.

Consequently, procedures and training were strengthened to emphasize the need to clearly document screenings and to make reviewers more sensitive to changes that potentially could impact the UFSAR or design basis.

Recent Im rovements There have been many improvements in the 10 CFR 50.59 program at Cook Nuclear Plant over the past ten years.

Earlier improvements were centered on providing better overall guidance to safety reviewers so that 10 CFR 50.59 reviews would provide the in-depth analysis that was required in a consistent, well documented manner such that 10 CFR 50.59 requirements could be met and our licensing basis could be preserved.

Recent improvements have focused on providing computer search tools, increasing the feedback mechanisms to our safety reviewers, and enhancing existing procedures in a way that provides a greater level of assurance in the quality of our program.

Below are listed program improvements since 1995.

FOLIO Search En ine To facilitate the safety reviewer's task of identifying potential impacts on our current licensing basis due to proposed

changes, computer search engines have been provided over the past two-years.

At Cook Nuclear Plant, the primary search tool is called FOLIO.

FOLIO is a text-searchable computer program.

The current databases that are loaded and available include access to references such as the

UFSAR, design basis documents, various regulatory documents such's bulletins, generic letters and
notices, AEP/NRC correspondence, previous safety review
memos, reportability

, reviews, operability reviews, environmental qualifications list, emergency plan and the final environmental statement.

Each of the data bases is available to a wide portion of the plant population via the company's local area computer network.

Also available is access to the commitment database that provides both a listing of commitments and an automatic link to the parent document where the commitment is located.

This database greatly aids the safety reviewer in finding licensing commitments that may be affected by a proposed design or procedure

change, test or experiment.

The information available via the computer and the databases are continuing to be improved with additional references such as quality assurance program description (QAPD) and the fire protection program manual anticipated to be added in the future.

In addition to FOLIO, the T/Ss are expected to be added to the search engine with word search capability over the next year.

UFSAR Revalidation Effort The principal reference documents used in the 10 CFR 50.59 program are the UFSAR, and the design basis documents (DBDs) that are being generated for many of the plant systems.

A review of the UFSAR has been underway since January 1997 to re-validate the information contained therein.

The changes to the UFSAR resulting from this revalidation will improve the quality of the UFSAR.

In conjunction

Attachment 2 to AEP:NRC:1260G4 Page 4

with the UFSAR re-validation, a review of the completed DBDs will be integrated into future UFSAR reviews that will improve the quality of both the UFSAR and the DBDs.

Improvements in the UFSAR and the DBDs will make the 10 CFR 50.59 program reviews easier to perform with a corresponding increase in quality.

Definin the Desi n and Licensin Bases and Sin le Failures Deficiencies in our personnel's understanding of the design and licensing bases of the plant, as well as the definition of a single failure, were discovered during the recent AE design inspection.

To address this issue, we issued a policy statement and associated directive in November 1997 to define the terms "design basis",

"licensing basis",

and "single failure". In addition, training was provided on the new procedures to ensure that the staff understood the

terms, their importance to maintaining Cook.Nuclear Plant's design and licensing basis, and their relationship to the UFSAR and the 10 CFR 50.59 program.

These efforts were performed: to ensure that past deficiencies in our change process at Cook Nuclear Plant are not repeated.

A review of the condition reports issued since September 15,

1997, indicates that the message has been received throughout our organization.

As of December 18, 1997, at least 131 condition reports, by five different plant organizations, have been issued to document discrepancies of a similar type as those identified during the AE design inspection.

This includes discrepancies found in the UFSAR.

Additionally, condition reports, open at the time the procedures discussed above were implemented, were reviewed with increased awareness of the design and licensing basis.

Those condition reports that documented conditions having the potential to adversely impact the design basis were identified.

These condition reports will be resolved prior to entry into a mode where the condition is applicable.

Desi Basis Chan es as Desi n Chan e

As a result of the recent AE inspection, the plant procedure on design change control was modified to recognize that changes to design basis information must also be treated and processed in the same manner as physical design changes to the facility. This means that changes to design basis information will follow a strict path of rigorous multi-discipline design review and 'erification, including completion of a

safety evaluation, prior to implementation.

Consequently, such changes will be subject to a high level of quality assurance standards that will help ensure design configuration control.

Non-Intent Procedure Chan es As a result of the AE design inspection, plant procedures have been revised to require 10 CFR 50.59 safety-screening reviews of senior reactor operator (SRO) change sheets prior to making the changes effective.

Previously, non-intent procedure changes could be implemented as long as an approved 10 CFR 50.59 screening was performed within fourteen days of the change.

The new procedural requirements direct the SRO to withhold approval of any procedure change sheets unless submitted with an approved safety screening.

This guidance applies to all SRO change sheets.

Attachment 2 to AEP:NRC:1260G4 Page 5

Feedback of Lessons Learned As a result of previous inteinal audits, procedures and standards have been strengthened and training conducted.

This has resulted in a more conservative approach when conducting safety screenings

and, as shown below, has resulted in a dramatic increase in the number of safety evaluations performed.

En ineerin Section 1996 1997 Nuclear Safety Mechanical Structural Electrical 50 50 20 40 160 90 30 60 Total 160 340 Future Planned Im rovements The 10 CFR 50.59 procedure will be revised, following the NEI workshop in January 1998; to reflect the guidelines in NEI 96-07.

This revision will be issued during the first half of 1998.

ATTACHMENT 3 TO AEP:NRC: 1260G4 CALCULATIONALREVIEWS

ATTACitMENT3 to AEP:NRC:1260G4 PAGE i

SUMMARY

The purpose ofour review was to establish confidence that similar issues identified during the AE design inspection did not exist in our calculations.

The approach was to analyze and review calculations for issues similar to those identified in the AE design inspection, such as incorrect assumptions, calculation errors, and process measurcmcnt effect on instrument calculations.

The main focus of our analysis was to look for deficiencies that would result in equipment being inoperable. While thc review revealed both technical and administrative deficiencies, none Icd to any inoperability.

The corrective and preventive action needed to bring our calculations up to today' standards willbe part ofour longer-term actions.

The total number ofcalculations reviewed as a result ofissues raised during the AE design inspection was 324, summarized below.

Pccr Group Reviews (review considered lessons learned from AE design inspection)

System Functional Rcvicws (review considered lessons learned from AE design inspection)

Westinghouse Analyses review (focused on valid assumptions and interface)

IACCalculations (focused on instrument bias and process measurement)

Prc-AE Inspection Existing Calcs 41 20 19 114 Ncw Calcs Total 130 171 20 19 114

.Calc'ulitloii'i':Rev'icw'c'1!ai'.Part'.of:Sho'it'<<'Term'his'cssm'e'uter:-.':::1948';:l'::Ll@HSit~~~

i 130N i324~i~':::.:'::

In addition to these 324 calculation reviews, we also looked at the proccsscs and issues for groups of calculations to establish confidence that these previously completed calculations did not contain similar issues identified by the AE design inspection

. These groups arc summarized below.

Large Bore Piping Reconstitution Program Electrical Calculations (incorporated lessons learned from EDSFI)

.':Calcula'tlons'.Prc'vio'u'sl"': Co'm"'Ictcd<i!'.l",i'l.':.',ll:::M.".::..""'i"':.;:":::."!:;:ll:::";';Pi'i":.:

Total 178 l'289,".F4

ATfACHMENT3 to AEP:NRC:1260G4 PAGE 2 POST AE DESIGN INSPECTION REVIEWS

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PEER GROUP REVIEW EFFORT The UFSAR Revalidation Project conducted a review ofa number calculations to obtain 1) validation of various parameters, and/or 2) to resolve apparent document discrepancies.

The review of the calculations identified a number ofgeneric issues that called into question thc administrative quality, as well as the technical accuracy, of the calculation results.

Condition rcport CR 97-2525 was initiated to investigate and resolve the issues associated with the quality ofcalculations.

Management evaluation of thc condition rcport (CR 97-2525) revealed that the administrative and tcchnical issues brought out by thc condition rcport were similar to ones identified by thc AE design inspection The issues associated with condition report CR 97-2525 calculations were deemed to potentially impact restart issues. It was decided that all calculations involved in resolution of a restart item would be reviewed, through a Peer Group review eQort, prior,to restart.

A total of 171 calculations were reviewed in this elrort.

The review teams consisted of a functional engineering'manager; an<engineer~m the functional area (but not involved in generating the calculation), and an engineer from outside the functional area.

The Peer Group rcvicw eQort was intended to serve as an interim measure to verify that calculations are performed in accordance with the existing procedure to identify human performance issues, as well as being technically correct.

Long-term improvements are being developed as part of the prcvcntive actions to condition report CR 97-2525.

The Peer Group's instructions placed emphasis on the following seven attributes, in addition to the general procedural requirements:

l.

Assumptions are listed and are correct for purposes ofthc calculation.

2.

References arc listed and are validated to be current.

3.

Purpose and intended use ofthe calculation are clearly stated.

'4.

Models and computations are included for unique calculations.

(Where spreadsheet calculations are used, thc formulas should be printed out and attached to the calculation. For calculations that are repetitive in nature, the standard program used must be identified; inputs and results must be included'in'thc calculation.).

5. Ifinput data is taken from a secondly source, its usc:is clearly,justified,and documented.

(For example, ifa nominal tank volume is taken from a system description or the technical specifications, the calculation must document why it is justified and conservative to use the nominal volume.

Otherwise, the volume should be recalculated from primary source documents such as ccrtificd vendor drawings and then adjusted to provide appropriate conservatism.)

6.

Earlier calculations which are superseded or require revision as a result of the new calculation are clearly identified and the appropriate changes to the earlier calculations have been made.

7.

Allblanks on the cover sheet and design verification forms arc completed or N/A'd Also, experienced contractors provided expert advice on the Peer Group review eQort as well as served as team members on some ofthe Peer Group review teams for these reviews.

ATTACHMENT3 to AEP:NRC: l260G4 PAGE 3

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REVIEW OF WESTINGHOUSE ANALYSES During the course of the Architect Engineer Inspection, a number of issues came to light that suggested it would be prudent to review the calculations performed for the Donald C. Cook Nuclear Plant by the Westinghouse Electric Corporation for accuracy. An engineering asscssmcnt of the design basis calculations performed by Westinghouse in support of thc Cook Nuclear Plant was performed. That assessment was performed in August and September of 1997.

Three principal areas for review were identified for review during the assessment:

1.

A subset of questions identified regarding the RHR cooldown analysis by the AE Inspection Team was addressed.

2.

The interface between AEP and Westinghouse was addressed.

Thc interface had been identified as a potential problem in recent years.

This item was included in the review to address past concerns and to assess the effectiveness of the. changes implemented in recent years.

3.

A sample of 19 calculation packages was reviewed to.,assess. the. potential.for;additional problem areas in thc calculations performed for the Cook Plant units by Westinghouse.

The engineering assessment of Westinghouse Electric Corporation also responded to specific questions raised by thc AE design inspection team. It did not result in any new observations in this area.

The discussion of interface issues resulted in a number of recommendations for further improvement.

Thc review of calculations performed during the assessment identified only one additional calculation which required revision.

The modification to thc calculation was not related directly to the issues arising from the AE Inspection.

This calculation was the post-LOCA subcriticality calculation which is checked every cycle to ensure that the core willremain subcritical aAer a large break LOCA assuming all control rods do not insert.

The ice mass used in the analysis had to bc increased to a value that bounded plant operation.

Although the cold leg recirculation mode cooling subcriticality requirement continued to be met despite thc increase in ice mass, the hot lcg recirculation cooling mode subcriticality requirement needed credit for the hot leg nozzle gap to demonstrate compliance. Taking credit for the nozzle gap to address this issue is not unusual because nearly all Westinghouse units usc this to address this issue.

Thc long-term containment analysis was

'-known to.have a problem due to the erroneous modeling of the CCW heat exchanger.

For this analysis, margin was identified that compensated for the error.

In general, the participants concluded that the: Westinghouse analyses, are performed with suQicient margin to accommodate identified errors; The. participants noted. improvement in,the interface between Westinghouse and AEP in recent years.

However,.as.expected, improvements in this interface appeared to provide the best opportunity to further improve the reliability of Westinghouse analyses.

Furthermore, the items identified in thc AE inspection which impacted the Westinghouse

'nalyses related to the inadequate functioning of this interface.

The participants concluded that, the analyses performed by Westinghouse remained acceptable and that there existed available margin to address issues identified in thc NRC AE Inspection and in this assessment.

~

SYSTEM FUNCTIONALCALCULATIONREVIEWS To develop confidence in the calculations performed by AEP, a sample of the system functional calculations were reviewed.

This review concluded that there were no system inoperabilities as a result ofcalculation deficiencies.

Multi4isciplinary engineering reviews were conducted, using the Peer Group review guidelines, to verify that the selMed systems are capable of performing their intended safety functions (i.e., there werc no inopcrabilities). The Peer Groups for these calculations also focused on assumption control

ATTACHMENT3, to AEP:NRC:1260G4 PAGE 4 and results/methodology validation.

The reviews included reviews of design basis documents to verify the appropriateness of the design assumptions, boundary conditions, and models (when applicable).. The sample was selected as follows:

0 Ten risk significant systems were selected for inclusion in thc sample population based on the IPE risk significance. This resulted in 139 functionally significant calculations from the followingsystems to select from for the system functional reviews:

Essential Service Water [25 calculations]

Component Cooling Water [8 calculations]

Reactor Protection System/ESFAS

[1 calculation]

Residual Heat Removal System [ 11 calculations]

Emergency Power [7 calculations]

AuxiliaryFcedwater System [32 calculations]

Containment Spray System [18 calculations]

250 VDC [25 calculations]

ECCS

-(Accumulators, Safety Injection.

System, RCS Pressure Relief)

[7 calculations]

CVCS (Charging Pumps) [5 calculations]

0 Twenty calculations 'werc then sclccted from this population of 139 based upon their complexity and potential to contain issues similar to those identified by the AE design inspection team (see Table 3).

~

INDEPENDENTVERIFICATION As an additional verification, an AEP contractor performed an independent review of two safety

'significant calculations from the above population of 191 calculations to identify any common deficiencies/concerns with thc reviewed calculations and to provide an outside contractor's perspective on the AEP calculation process and controlling proccdurc(s).

The contractor reviews identified no inoperabilitics.

PRE-AE DESIGN INSPECTION REVIEWS The scope of our review effort was impacted by calculations.that'had'previously, been performed for programs such as the Large Bore Piping Reconstitution Program, and calculations that.has been upgraded followingthe EDSFI.

~

LARGE BORE PIPING RECONSTITUTION PROGRAM The Large Bore Piping Reconstitution Program (LBPRP), performed pipe stress analysis and pipe support calculations for 2 1/2 inch and larger safety system piping between 1991 and 1997.

There were 178 calculation',packages. which include the pipe stress analysis and pipe stress qualification for 5314 pipe supports for normal, upset and cmergcncy conditions.

The NRC reviewed this program and the calculations being performed in December 1991 and indicated that "the LBPRP is very comprehensive and thorough...[and]... The aggressive use of more rigorous analytical techniques shows a strong commitment to quality."

Also, the review of specific calculations resulted in the conclusion that "No discrepancies were noted while comparing the as-built documentation and computer code inputs".

Forty-five pipe support calculations for the CCW system were subsequently reviewed aAer the AE

ATTACHMENT3 to AEP:NRC:1260G4 PAGE 5 design inspection as part of the Peer Group review effort. The review looked at the issues from the AE design inspection, and the process used in conducting the calculations.

Our review provides reasonable assurance that the pipe supports for safety systems are in compliance with the design bases for these systems.

~

ELECTRICALCALCULATIONS Recognized documentation weakness (in our design basis calculations) identified in the EDSFI conducted in 1992 as well as thc results ofan electrical cnginecring group review of calculations

,pre-EDSFI, lcd to a significant effort to upgrade calculations in the 250 Vdc, 120 Vac, and 4kV systems.

Thc electrical engineering group launched a calculation upgrade program, which revisited design basis calculations to assure thc calculations would meet regulatory and internal staildards.

In all, 111 electrical calculations were revised or developed between 1992 and 1997.

Several reviews" and audits,"pcrformcd on the electrical calculations,'yielded only minor, calculation comments.

In addition, electrical calculations reviewed as part of the system functional calculation review eflort revealed that calculation administrative deficiencies did not cause equipmcnt to be inoperable.

PROBLEMS ANDRELEVANCE

~

The Peer Group reviews of 171 calculations as well as the review of20 system functional calculations, utilizing lessons learned from the AE design inspection, identified a number of administrative and tcchnical deficiencies similar to those identified in the AE design inspection.

Examples of administrative deficiencies included the following:

0 assumptions not clearly defined 0

variables in equation not well defined 0

drawing rcfercnccs do not have revision number 0

calculation purpose not clearly stated 0

references not provided 0

diQicult to followthe calculation flow 0

cover sheets not filledout/completed consistently 0

page numbers not properly recorded Examples oftechnical deficiencies included the following:

0 -

treatment ofinstrument uncertainties was not clearly documented 0

justification for assumed inputs used in some calculations was not documented 0

formula for flowratcs not provided However, although there werc a number of deficiencies identiTied in the reviews (see Table 2), the subsequent reviews revealed that no systems were inoperable.

ATrACHMENT3 to AEP:NRC: l260G4 PAGE 6

~

The review of Westinghouse calculations identified a number of discrepancies which required evaluation. In spite ofthese discrcpancics the review team participants concluded that the analyses of record results remained acceptable with conservatism available to address issues identified by thc AE design inspection.

Subsequent to the analyses review a number of as-found operability analyses were performed to document the effect of the identified discrepancies and issues raised during the AE design inspection.

Analyses using actual plant data that were completed for Unit One cycle 16 and Unit Two cycle 11, confirmed the acceptability of the analyses results and demonstrated that the Cook Nuclear Plant systems remained operablc.

MATRIXOF CALCULATIONREVIE%S PERFORMED le 1

Electrical (273 in calc database)

TOTAL= 3 FUNC. CALC. REVIEW3 Mechanical (1529 in calc database)

I8r,C (330 in IAC database)

(218 system related, and 112 uncertainty)

Structural (2410 in calc database)

Other (526 in calc database)

TOTAL= 54 WESTINGHOUSE ANALYSES18 PEER GROUP REVIEW22 FUNC. CALC. REVIEW14 TOTAL= 145 WESTINGHOUSE ANALYSES1 PROCESS MEASUREMENT. ('97) 114 PEER GROUP REVIEW29 FUNC. CALC. REVIEW1 TOTAL= 116 PEER GROUP REVIEW;- 116 TOTAL= 6 PEER GROUP REVIEW4 FUNC. CALC. REVIEW2

,-'.,Total'.':Numb'er';.'of::.:".Caic':Review's324.','-'-;;,;=",::;,'",;":::;,.;.:

Table 2

~

SHORT TERM ASSESSMKNT PEER GROUP REVIEW OF CALCULATIONS CR 97-2802 CR 97-2809 CR 97-2805 CR 97-2829 CR 97-2842 CR 97-2843 CR 97-2935 CR 97-3057 Pdentt/led during system/'uncttonal revIews)

CR 97-3143 Pdenttfted durlng systemtu notional reviews)

CR 97-3215 Pdentt/led during system functtonal reviews)

Calculations were run on the non-QA DOS PC-based version ofE/PDSTRUDL because ofa software litch in the AM1CROVAXversion.

DC-D-HV-12-ABevaluated the impact ofhigher CCW temperatures on auxiliary building ventilation.

The basis for using an average CCW temperature of 135 F was not documented.

The engineer subsequently documented his basis for the assumption, which was an evaluation by the system engineer ofrelative surface areas and temperatures throughout the system confirming that 135 F was a conservative value to usc in this calculation.

ENSM 970606JJR evaluated the potential forvortexing in the RWST. Set points noted in the calculation did not include instrument uncertainty and it was felt that the potential for the results to bc misapplied by the end user (1&C) was high. The calculation:was clarified with respect to uncertainty.

Pro r use ofthe results b I&Cwas verified.

ENSM 971001CV determined RWST volume required for Appendix R support ofthe opposite unit.

Reference for formula was omitted, basis for assumption that pressure/temperature ramp down linearly over 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> was not provided, and the PORV flowrate taken from the FSAR was not identified as being a conservative value. Formula was confirmed to be correct and all assumptions were reviewed to ensure they were conservative.

PORV flowrate was actually increased for the final calculation, but combined with other refinement ofother assumptions, the original calculation results were shown to be conservative.

HXP 911210AF, Rcv. 2 determined CCW temperatures forRHR cooldown for LBPRP. The calculation was technically acceptable.

However, Rcv. 2 superseded only part ofRev.

1 so both revisions were currently valid. Rev. 2 willbecome a stand-alone calculation that incorporates all of the remainin valid rtions ofRev. 1.

ENSM 970926QSL determined the impact ofa thermal barrier rupture on the CCW system.

Bases for selecting the RCS pressure and for considering 547 F a conservative RCS temperature were not rovidcd. Desi n ressure ofCCW.

stem was not documented.

Results were valid.

ENSM 970929TWF determined CTS flowto the containment annulus via CEQ fan stairwells.

Bases for assumptions were not documented.

Review and refinement ofassumptions and recalculation confirmed that ori inal results were valid.

RS-C-0280 determined short-term maximum pH for containment sump after LBLOCA. The calculated value was 12.97 (for a period of 18 minutes); which is above the -12.9.upper limitfor EQ specifications.

However, removing other overly conservative assumptions'within:the calculations (most notably assuming a 10% reduction in sodium tetraborate from!ice sublimation) willreduce thc calculated value to below 12.9. Additionally, the corrosion affect ofpH 12.97 versus 12.9 for a short riod oftime is not measurablc or si

'cant.

Calculation is bein redone usin ro r assum tions HXP 740226FK and HXP 900629AF both deal with ESW system flowrcquiremcnts.

The review identified potential discrepancies with current values in FSAR Table 9.5-2 and questioned whether the SFP heat exchanger load had been properly considered.

Consequences ofthe discrepancies were determined to be minimal. Calculation NEMP 950612AF had subsequently been performed and confirms that the 1990 calculation results arc stillvalid. Allofthe calculations are being revised a

ro riatel HV 12CC01N veriTied the "adequacy" ofthe CCW emergency ventilation supply fans. Assumptions and methodology were not well documented, and the reviewers raised numerous questions.

Evaluation by HVACcnginccrs subsequently determined that the calculation results werc valid.

Table 3 Syst ctional Reviews Q,::!$:Qkk".PC(%&+~i:,;,

PS-4KVD-003, REV 0 MINIMUMAND MAXIMUMBUS FAULTS 4KV, 600V, AND 480V SYSTEMS PS-4KVP-009, REV 0 4KV RCP UNDERVOLTAGERELAY SETTINGS PS-EDGL-001, REV 0 EDG 1AB STEADY STATE LOADING ANDVOLTAGEDROP 4KV ENSM740501FK1, 5/1/74 HXP721130FK-2 AFWS PUMPS - TECHNICAL SPECIFICATIONS, BY F. KUO, 5/1974 AUXILIARYFEEDWATER PUMP SUCTION - NPSH AVAILABLE, 11/1972 HXP740226FK AFWS NPSH CALCULATION, FEBRUARY 26, 1974 HXP850508AF MAXIMUNALLOWABLEPUMP DEGRADATIONOF THE UNIT 1 PUMP, 1/2/86 HXP910619AF, REV 0 AFW FLOWRATES IN SUPPORT OF SAFETY VALVESETPOINT AFW INCREASE Page 1, 12/24/97

Table 3 Syst notional Reviews NEMH930601AF Pi~i~:ci:"-:@LYNN%!~j%:"j~4~~)iiy',;8)4fA.

DETERMINEAMOUNTOF PUMP DEGRADATIONTHATIS ALLOWED WHICH MEETS SAFETY ANALYSIS FLOW REQUIREMENTS, REV 0, 6/21/93 DCCHV12CC01N CCW PUMP AREA VENTILATION SYSTEM DESIGN, 12/8/89 CCW HXP910419, RO CCW MOVPRESSURE DIFFERENTIAL CCW DCCHV12AE06-N HEAT GAIN CALCULATION,AES SYSTEM, REV 1, JUNE 2, 1992 CTMT SPRAY RD-88-01 RS-C-0280 DOSE TO CONTROL ROOM OPERATORS FOLLOWINGA LOCA SPRAY REV1, NOV28, 1988 SHORT TERM MAXPH FOR CONTAINMENTSUMP IN A LARGE

~pappy BREAK LOCA, AUGUST 31, 1995 HXP890525AF, DATEDJUNE 19, 1989 UNIT 1 WEST CENTRIFUGAL CHARGING PUMP FLOW REDUCING ORIFICE CVCS DCCHV12ES03N, REV 0 LOSS OF HVAC-ESW PUMP ROOM ESW TEMPERATURE, APRIL22, 1991 Page 2, 12/24/97

Table 3 Syst nctional Reviews HXP900627AF DETERMINE ESW PUMP OPERATION DURING FULLPOWER UNITOPERATION, JULY 6, 1990 ESW HXP900629AF ESW FLOW REQUIREMENTS, 6/29/90 ESW NEMP950810AF, REV 0 ECP-1-2-N2-07, 4/27/93, R8 ESW FLOW TO EDGs, AUGUST 18, 1995 MID-LOOP PHENOMENA AND INSTRUMENTATION ESW RHR Page 3, 12/24/97

ATTACHMENT 4 TO AEP:NRC:1260G4 PRESENTATION MATERIALS FOR DECEMBER 16, 1997 PUBLIC MEETING

RESPONSE

TO CONFIRMATORY ACTION LETTER ISSUES

December 16, 1H7

'MERICAN'lECl'RIC POWER

a I

I i This meeting willdiscuss AEP's resolution of issues documented in the NRC's Confirmatory Action Letter of September 19, 1997 and provide reasonable assurance that these issues do not affect the operability of other safety systems.

AEP's conclusion is that Cook Nuclear Plant is ready to resume power'peration pending receipt of necessary technical specificatioh changes and

'ompletion of the resolution plans.

Agenda I.

Introduction Eugene E. Fitzpatrick, executive vice president Nuclear Generation Group, Buchanan II. Confirmatory Action Letter No. RIII97-011 Issues &Resolutions A.C I Issues1 4 San 2

Jeb B. Kingseed, section manager-nuclear safety and analysis Nuclear Generation Group, Buchanan Paul Schoepf, P.E., mechanical systems manager.

Nuclear Generation Group, Cook Nuclear Plant C. nstrument Uncertain es C I

u 9

Stanley K. Farlow, P.E,, manager-I&C engineering, production engineering Nuclear Generation Group, Cook Nuclear Plant III. Short Term Assessment Program A.S ort-Tem ses e t eve e t Joel S. Wiebe, manager-performance engineering &analysis Nuclear Generation Group, Buchanan B. S ort-Te ssess e t Results James A. Kobyra, P.E., chief nuclear engineer Nuclear Generation Group, Buchanan IV. Additional Assurance of Operability of Systems A. Alan Blind, site vice president Nuclear ~neration Group, Cook Nuclear Plant V. Conclusion Eugene E. Fitzpatrick, executive v'ice president Nuclear Generation Group, Buchanan

Resolution ofCALIssues Meeting Resolution ofCALIssues Meeting Gene Fitzpatrick Executive Vice President Nuclear Generation Group American Electric Power Introduction Meeting Overview I.

20 3.

4.

S.

6.

70 8.

Issues or resolution rior lo restart Recirculation sump inventory Recirculation sump venting 36-hour coo!down ES 13 switchover procedure Compressed air overpressurc RHR suction valve interlock Fibrous material Backlcakage to RWST g macaw Resolution ofCALIssues Meeting Issue or discussion riorto restart Instrument uncertainties incorporated into procedures and analyses Short-term assessment riorto restart To determine whether same type engineering problems exist ln other safety-related systems and whether they alfect system operability Jeb Ktn Paul Sehoepf Stan Farlow Joel Wiebe Jim Kobyra AlBlind A enda S I Reetreutatlon Sum lnvenio S4 ES 19 Switchover Procedure SS Baetdeabaae to RWST SZ Reetreulatton Sump Venttnx Hbrous Material In Containment SS Sd.hour Cooldown ttd RHR Suction Valve AutoCtose SS Compressed AirOverpressure itt Instrument Uncertainty Short Term Assessment Development Short Term Assessment Results Additional Assurance ofOperability of Systems Conclusion Reclrculatlon Sump Inventory Con irmoto Action Letter issue Pumps used to coot.the reactor and containment building may not have enough water supply to allow long-term operation ofthe systems Commitment Analysis willbe performed to detnonstratc that the recirculation sump level is adequate to prevent vonexing, or appropriate ntodifications willbe made Reclrculatlon Sump Inventory Issue resolved o Analyses demonstrated emergency core cooling system/containment spray system operability h

'etermined sump level margin above 602'0" exists o Subtititted Tcchnical Specification amendment to credit morc existing icc

+aneajeasr

Recirculation Sump Inventory A~nal sls

'ump configuration

'loNlpaths

'nalyses

'esults gestate Recirculation Sump Inventor

~nal sls

~ Large-brcak loss ofcoolant accident and spectrum ofsmall-brcak loss ofcoolant accidents o Transient analysis o Icc melt credited

'ctive/inactive sumps modeled o Revised ES-1.3

'WST level uncertainty gaatatcase Recirculation Sump Inventory'/

A~nal sir resnlrs o Water level >602'0" for large and small break loss ofcoolant accidents o Technical'Specification amendment Recirculation Sump Inventory Issue resolved o Analyses demonstrated emergency core cooling system/containment spray system operability o Determined sump Icvcl margin above 602'0" exists o Submitted Tech'nical Specification amendment to credit more existing icc k

Jch Ktngsccd Paul Schoepf Stan Fartow Joel Wtebe Jim Kobyra Al Blind Gene pttspatrtck A ende introduction Nl Redreutstton Sum Invento

<<e KS IDSwitchover Procedure ca gc to eg:.'e. Rcdrcutatton Sum p Venting

<<y Hbrous Material ln Contalnmcnt NS 3&curCooldown

<<d RHR Sucdon Valve AutoCtosc irS Comprcsscd AlrOvcrpressure Instrument Unccrtdnty Short Tcrtn Assasmcnt Devdopmcnt Short Tenn Asscssmcnt Resulrs Additional Assurance ofOperability of Systems Conduslon ES-1.3 Switchover Procedure Con rrmoro Afenon Leuer issue Adequacy ofcurrent procedures during switchover &xnthc emergency water supply tank to thc eontahunent sump for long<can post~dent operations Commllmenl Changes to thc cmcrgency~ used forswitchover of the cmcrgency core cooling and containmcnt spray pumps to tbe rcdreutsncu Nanp willbc hnplcmcntaL These changes wi1I provide ssurance there willbe adequate sump volume, withlroper consideration ofinstrument bias and single>>failure criteria

+aatatcasr

ES-1.3 Switchover Procedure ESo1.3 Switchover Procedure issue resolved Implemented changes to ES-1.3 to incrcasc water injection, eliminated single-failure vulnerability, and account forrefueling water storage tank level bias

~noesis Refueling water storage tank level measurement bias

~ Accident analysis assumptions

~ Single-failure ESo1.3 Switchover Procedure Aeuons t

~ Refueling water storage tank level measurement bias

-Flow Induced errors (acoul level > indicjgtcd)

Resolution

'oved refueling pates stomge tank level transmitter tap

'nstrument uncertainty

~~

RRRRRRRRJI'S-1.3 Switchover Procedure Acuons

~ Accident analyses assumptions

-Rceriticality

-Containment pressure

-Long-tenn cooling Resolotloo

'ssumptions satislied ES-1.3 Switchover Procedure ES-1.3 Switchover Procedure Actions

'ingle-failure <g..

-One residual heat removal (RHR) pump supplied high-head emergency core cooling system (ECCS) pumps during transition

'esolution

-New transfer sotuencc ensures no loss ofinjection with single-failure Resolullon summa Eliminated refueling water supply tank level measurement bias

'et accident analyses limitations

~ Considered worst case, credible single active failure

~ Validated procedure and trained operating crews

+ Agggggdggr

Paul Scboepf Stan Fariow Joel Wiebe

-Jim Kobyra AIBlind tAcne Fitzpatrick N

ec feil a oii nip cnbng N7 Fibrous Material ln Containment N3 3ti hour Cooidown Nd RHR Suction Valve Auto<lose Ns Comprcsscd AirOvcrpressure Np Instrument Uncertaint Short Term Asscssmcnt Development Short Term Assessment Results Additional Assurance ofOperability of Systems Conclusion A enda ck Introduction Jcb IGnaseed Nl Rccircutatfon Sump Inventory Ns KS IDSwitchover Procedure Na Backleakaac to RWST Back-Leakage to Refueling Water Storage Tank Con irmato Action Letter issue Scat leak testing ofvalves may not be adequate to identify potential backllow from the containment to thc RWST during the LOCArecirculation phase Commitment Only two ofsix mini-flowrecirculation line valves have leakage verification tests. Justification willbe provided that the total leakage forthe six valves is

<10 gpm to ensure that Part l00 limitsare not exceeded ifcontainmcnt sump water werc to leak back to RWST during a design basis accident

~UCTaic Back.Leakage to Refueling Water Storage Tank r

issue resolved o Included fiowpaths in in-service testing program o Implemented new procedure: seat leakage testing ofvalves at each refueling outage to ensure < 10 gpm total leakage Back-Leakage to Refueling Water Storage Tank A~nal sla

'our back flowpaths

-Leak testing in place fortwo ofthe four paths

-Two paths not included in in.service testing program alcawasr cUcvalc Back-Leakage to Refueling Water Storage Tank Back4.eakage to Refueling Water Storage Tank Actions o Testing progranr results

-Tested valves already included ln testing program

-Added five valves pcr unit to testing program

-Test results issue resolved o Included flowpaths in in-scrvice testing program o Implemented new procedure:

seat leakage testing ofvalves*at each rcfucling outage to ensure < 10 gpm total leakage

Jcb Kln Paul Scboepf Stan Farlow Joel Wlebe Jim Kobyra AlBlind Cene Rtzpatrtctt A enda Introduction Nt Rcdrcutatton Sump lnwntory N4 KS IDSwitchover Procedure W

NX Rcdrculatton Sum Vcntins ibrous tc n

n nmcnt

<<S 36Jiour Coowown tte RHR Suction Valve AutoClose

<<5 Compressed AirOwrpressure

<<p instrument Unccrtatnty Short Term Asscssmcnt Dcvelopmcnt Short Terai Assessment Results Additional Assurance ofOperabNty of Systems Conduslon Reclrculatfon Sump Venting Con irmato Action Letter issue May not be adequate venting ofair underneath the roof

'f the containmcnt building recirculation sump Commitment Venting willbe rcinstallcd in the recirculation sump cover. The design willincorporate forcignmaterial exclusion requirements for thc sump ReclrculaVon Sump Venting

/ssue resolved Reinstalled recirculation sump cover vents with a design that prevents foreign material from entering through thc holes Reclrculatlon Sump Venting

~nial sls

'977/78 Alden Labs study o Vent holes added to sump cover in 1919 as an enhancement Reclrculatlon Sump Venting ReclrculaVon Sump Venting

~nal~ls Holes plugged in4996 and 1997 to address I/4" foreign material exclusion concern

~ctlons

~ Venting reinstalled o Design now incorporates foreign material exclusion provisions

ReclrculaVon Sump VenVng Issue resolved

'einstalled recirculation sump cover vents with a design that prevents foreign material from entering through the holes Stan Farlow Jod Wtsbc Jim Kobyra AlBlind Ceno Hispatrlck I3 hour Cooidowu RHR Suction Valve Auto@toss Is Comprssscdhlrovcrprcssurc Iti Instrument Uncertainty Short Term Asscssmeut Dcvdopmeut Short Term hsscssmcnt Results hddt ttouat Assurauco ofOperability or Systams Coodusiou A enda Cene Htspatrlck Introduction Jab Moesccd II Rcdrcutattoa Sump Inventory I4 ES IDSwitchover Procedure Ia Backtcakaee io RWST Paul Schoe r IT Hbrous Material In Contatnmcut Fibrous Materfal In Containment Fibrous Material In Containment Con irmalo Aclion Lerrer issue Fibrous material in containment building Commllmenl Removal offibrous material from containmcnt building that could clog the recirculation sump willbe complctcd

~nal sos

'nstallation ofcable tray fire stops

-Fibrous material used ai "damming material"

-Installation specification did not require removal of material in containment Fibrous Material In Containment Fibrous Material In Containment Acllons cllons

'emoved fibrctus damming material

-l2 locations in Unit I IS locations In Unit2

-Annulus and lnstnuncnt Room

'eviewed operating experience and regulatory information o Performed extensive walkdowns o Identified and addressed other fibrous insulation

Fibrous Naterfaf ln Contafnment Issue resolved Removed fibrous insulation material from containment building that could clog thc recirculation sump Cene Fttspatrtck Jcb Ktnssced Paul Scboc f Stan Fart ow Joel Wtcbc Jim Kobyrn hl Blind

" Cene Htspatrtck A enda 5n troduction Nt Redrculation Sump Inventory tt4 ES 13 Switchover Procedure

<<S

~ Bacldcakaae to RWST

<<3 Recirculation Sump Ycnttna trt Rbrous tatcrfsl tn Containmcnt

<<3 3@hour Coo!down on ve ttS Comprcsscd Airoverpressure ttp instrument Uncertainty Short Term Assessment Development Sbort Tenn Assasment Rauits Addldonal Assurance ofOperability of Systems Conduston 36.Hour Coofdown 36 Hour Cooldown Can mmata Action Letter issue Calculation needs to be performed that shows one train ofcooling water system is surtcient to rcmove the units from service Commitment Analyses willbc performed that willdemonstrate the capability to cooldown the units consistent with the design bash requiranents and necessary changes to procedures willbc completol Issue resolved Analyses completed to demonstrate 36-hour cooldown capability with onc train ofcooling 36 Hour Cooldown 36.Hour Cooldown

~nal sls o Original Westinghouse performance requirement fornormal cooldown

-Plant canbe eoolcd down in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> withonc train ofcooling

-Consequence:

cotnponcnt cooling water supply temperature can reach l20F during this evolution

~nial sls

'6 hour6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> cooldown analysis revisited for Unit2 uprate

-Design inspection issue: discrepancy in CCW heat exchanger type assumed in uptate cooldown calculation

-Original cooldown calculation contained heat exchanger modeling error

36 Hour Cooldown Actions

~ Demonstrated thermal hydraulic capability for a 36-hour cooldown 36-Hour Cooldown Actions e Component cooling water design temperature increased to 120'F for single train cooldown via deign change

-Equipment evaluations

-Piping evaluations

-Operating procedure change gmnaur 36.Hour Cooldown 36 Hour Cooldown ui ment evaluation Flow balance criteria increased slightly based on NSSS vendor recommendation to preserve heat trarisfer capability during 36-hour cooldown

-Safety injection pumps

-Centrifugal charging pumps

-Residual heat removal pumps Operability not challenged forprevious fiow limits based on GL 91-18

~tt ui ment evaluation cont.

e Planned non-Technical Specification radiation monitor replacement rescheduled - location of new monitors in lower temperature location 36.Hour Cooldown 36-Hour Coofdown

~ e Four minor pipe hanger moditications due to higher stresses associated with increased temperatures

~ Change driven by desire to handle 36-hour cooldown as a "nornial" condition - no changes required ifhandled as emergency condition fssue resolved Confirmed 36-hour cooldown capability with one train ofcooling water

0 0

Gene Htspatrtek Jeb Ktnaseed Paul Schoepf Stan Fartow Joel Wtebe Jim Kobyra At Blind Cene Fitzpatrick A enda introduction Nt Recirculation Sump inventory

<<4 ES 13 Switchover Procedure ea Baetdeakaae to RWST tran Reetreutatton Sump Venttna

<<1-Fibrous htaterhl in Containment ttd R16t Suction Yatve Au~ose Ns ompressed Air erpressure ep instrument Uncertainty Short Term Asussment Development Short Term Assessment Results Additional Assurance ofOperability of Systems Co net uslon Residual Heat Removal Suction Vahte Auto@lose Con u moto Action Letter issue Conflicts bctwcen operating procedures and Tcchnical Specilications forresidual heat removal system Commitment A technical specification change to allow operation in Mode 4 with the residual heat removal suction valves open and power removed is being processed.

Approval ofthis change by NRC willbc required prior to restart

~~ assrewasr rstrra le Residual Heat Removal Suction VaNe Auto@lose Residual Heat Removal Suction Valve Auto@lose Issue resolved Technical Specification amendment approved

'unction dcsigncd originallyto protect residual heat removal system from ovcrpressurc

'perational practice dcfcats thc auto-closure whcncvcr valves are open

-Concern forloss ofdecay heat removal

-Lowtemperature ovetpressure system operation e Impact on Tcchnical Specifications and Final Safety Analysis Report not identified Residual Meat Removal Suction Vahte Auto@lose Residual Heat Removal Suction Valve Auto@lose Actions

'ubmitted Technical Specification amendmcnt

-Removes surveillance requirement for valve a~losure

-Takes credit for low temperature ovetprcssure system protection forraided heat removal system

-Operating procedures, UFSAR and Tcchnical Specifications aligned Issue resolved Tcchnical Specification amendment approved

Gene Fitspatrick Jeb IQngseed Paul Sehoe f Sian Fartow Joel Wiebe Jim Kobyra AlBlind Gene Htspatrtck A Nnda introduction Nt Recirculation Sump fnventosy Ns ES IDSwltebowr Procedure Na Baetdeakage to RWST Ng Recirculation Sump Venting Fibrous Material in Containment NJ 3ts hour Cooldown V

N5 Com ressed AlrOve ressure Np nstrument neerta nry Short Term Assessment Dewtopment Short Term Assessment Results AddMonat Assurance ofOperabpdty of Systems Cond uston Compressed AlrOverpressure Con irmato Action Letter issue Adequacy ofpressure protection forsome components in thc compressed air system from equipment malfunction Commitment Ovcrprcssurc protection willbe provided downstream of thc 20 psig, 50 psig, and 85 psig control air regulators to mitigate the effects ofa postulated failed regulator Compressed AlrOverpressure Issue rei alved

'nstalled redundant, safety-grade reliefvalves and eliminated ovcrpressure potential o Eliminated potential forcommon-mode failure Compressed AlrOverpressure A~nal sls o System design

-Non-safety related

-"Failsafe" on loss ofair

-Activevalves change state on safety grade solenoid valve actuation

-Ovcrprcssurc protection forthe system but not for system loads Compressed AlrOverpressure A~nal sls

'nitial findings'.

-Potential common-mode failure ofequipment resulting from ovcrpressurization

-Many coinponents not rated forfullinitial pressure

-Component failures anticipated Compressed AlrOverpressure Issue resolved

'nstalled redundant safety grade reliefvalves and eliminated overprcssure potential o Eliminated potential forcommon-mode failure

0

Stan Fartow Instrument uncertainty o

bc Jim Kobyra AIBlind rt crm Asscssmcnt opmcnt Short Term Asscssmcnt Results AdditkinalAssurance ofOperability of Systems Cene Htzpatrick Conclusion A endg Cene Htspatrlck Introducdon Jcb Kingsccd gl Rcdrcutadon Sump Inventory gg KS IDSwitchover Procedure gg Backlcakagc to R%ST g2 Rcdrculatton Sump Venting Paul Schoepl ttr Hbrous Material ln Containmcnt g3 3&ear CooMown ttd RHR Suction YalvchutoClose Instrument UncertaInty Con trmoto Action Lc'tter Issue Instrument uncertainties incorporate! into proccdurcs and analyses Comnritment Emergency procedures and other important-to-safety procedures, calculations, or analyses willbc rcvicwed to account for instrument uncertainties lt is understood that resolution ofthis issue requires a long-tenn program continuing beyond restart Qmaicatr Instrument UncertaInty Instrument UncertaInty 4~nal sis

'reas for improvement

-Control usc ofInstrument uncertainties in calculations, procedures, and analysis

-Improve control ofuncertainty calculation inputs

-Process measurement error ca!culations

-Provide training to other disciplines

-Increase number ofparameters under formal control Issue resolution o Program elements

-Control use ofuncertainties

~ Ahninistrative control

~ Paramctcis used to assure Tcchnical Spedgcation ccmp4ancc

'ntegrate with nNmal operating procohimupgrade program that was committed to!n our NRC submittal AEFNRC I260H Instrument UncertaInty Instrument UncertaInty

'rogram ciemontg

-Plant specific methodology

'ethod to calculate Instmmcnt unccrtaindcs Rcfcicnce NRC Branch Tcchnical Posidcn HICB-12

-Review existing calculations w Ebminatc rcplicue caicidations

~ NRC Inspection raccdure 93807 Tralnmg X

o Instrument uncertainties under formal control

-Reactor trip and engineered safety feature actuation system sctpdnts

-Emergency and abnormal opcradng procohucs

-Operations, surveillance and test procedures

-Plant perfamancc data used in analysis

-Scipoints forplant alarms assodatcd withmoaitcdng Tcchnical Specigcation con pllance

lnstmment Uncertainty Actions corn leted

~ Reviewed level instrumentation forvelocity eifcct

~ Reviewed and rcviscd emergency operating procedures forswitchover to recirculation o Reviewed and rcviscd Technical Specification surveillance procedure used by operations

'enerated parameter list forTechnical Specification compliance Instrtrment Uncertainty ctions cpm leted cont.

~ Generated administrative control procedures

~ Reviewed EOP sctpoint documentation

~ Reviewed license bases

~ Addressed related non-programmatic unrcsolvcd issues from the inspection report

~ Complctcd plant spcciific methodology manual Instrlrment Uncertainty ahedule Complete all reviews and calculations in 1998 A enda Gene Htspatrkk introduction Jcb Kluasccd Nt Recirculation Suaip inventory N4 ES lDSwitchover Procedure SS Backteakaae to RWSP

<<S Recirculation Sump Vcndng Paul Scbocpr N

Hbrous titatcrtat ln Contalnuicnt SS 36.hour Cooldosrn e6 RHR Suction Valve Auto%lose Ns Coin pressed AirOvcrprcssure Stan Fartovr 09 tnsrrumcot ncertain Joel Wicbe Short Term Asscssincnt Dcvciopiucnt lla rt erin aleut is AlBlind Additional Assurance or Operability or Ssstccas Gene Htspatrtck Conclusion Development ofShort Term Assessment Corrective action process

-Investigatiori ofissue

-Root cause analy'sis

-Correction ofissue

-Actionto prevent recurrence Development ofShort Tenn Assessment o Purpose ofshort term assessment To determine whether similar issues may exist in other safety systems, and ifthey do, whether they affect system operability

Development ofShort Tenn Assessment Independent root cause analysis teams (CAL issues l-8)

-Root cause analyst

-Outside technical analyst(s)

-Individual knowledgeable ofissue Development ofShort Tenn Assessment

'enior management review ofcauses

-CALitems 1-8

-Causes

-Potential impact on operability

-Identified and discussed implications Result: Five issues with potential to impact operability Development ofShort Tenn Assessment o Root cause ofother design inspection issues

-Root cause analyst

-Outside technical analyst(s) o Allroot causes additionally reviewed by independent senior industry peers Development ofShort Tenn Assessment o Senior management review ofcauses

-Compared to CAL issue causes and short tenn assesQllcnt o Result

-No additional issues were identified

-Some specific actions added Development ofShort Tenn Assessment o Issues with potential to impact operability

-Analyses withptors or incorrect assumptions

-Non-safety related systems failure modes

-Lcvcl instrument bias duc to Bcrnoullieffec

-Containmcnt sump attribute not prescrvcd

-Improper application ofsingle failure criteria, A enda Ceno Htspatrtck Introdncdon Job IQnesccd et Rcrtrcutatlon Sump lnwntory ES IDSsiltcbovcr Procedure ea Backtcakaao to RWST

<<3 Rcrtrcutadon Sump Ycndng Paul Schocpf N

Hbrous htatcrtat ln Containment e3 36@our CooMosrn RHR Suction Yatvo AuorQosc

<<5 Compressed hlrovcrprcssure Stan Fartovr ep Instrument Uncertainty Itl cnt Jins Kobyra Short Term Asscssmcnt Results I

rance o para iyor Systems Ceno Htspatrtck Conduslon

0 0

Short Tenn Assessment Results Short Term Assessment Results c Engineering issues I. Analyses with errors or incorrect assumptions

2. Non-safety related systems failure modes
3. Level instrument bias duc to Bcrnoulli effec
4. Some contalnmcnt attributes not preserved S. Improper application ofsingle failure criteria

'esolution process

-Scope and deliverable

-Operations and engineering management

-Initialresults Indicated further expansion

-Closure defined documented reports Short Tenn Assessment Isragrem 10 root causes withpetanttat opcrabmty kiipact Exit&0kneAdge ISSR, Iavdlsncas, procedures, ate.)

Short Term Assessment Results-Issue Nf

~ Analyses crmts or incorrect assumptions

~nfinn safety analyses ofrecord

-Evaluate heat exchanger modeling

-Dctcrmine extent ofcalculation problems Short Tenn Assessment Results-Issue O1

'hort Tenn Assessment Results-Issue O1

~ Confirmation ofanalyses ofrecord

-Seven pcrsoir team to the NSSS offic

-IWcpthrcvtcwdfUnit I gt 2 analyses

-Minorfindings-Interface assumptions

-Analyses ofrecord-conservative

-ECCS, CTS, RHR, Containment, AFW,CCW

'afety-related heat exchangers will perform their function

-Residual heat removal heat exchanger

-Containment spray heat exchanger

-Component cooling water heat exchanger

-Spent fuel pool heat exchanger

-EDGjacket water and lube oil heat cxchangcrs

~ Counter cow versus TKhfAE

~ Csiculadoas revised

Short Tenn Assessment Results - Issue ¹1 Short Term Assessment Results -Issue ¹1

'ssuring confidence ofAEP calculations Total Reviewed Electrical 273 119 Mechanical 1529 6

Instrument 330 157 Structural 2410 294 Other 526 6

5068 632

'ssuring confidence ofAEP calculations

~ Recent calculation program efforts

-LBPRP

-MOVcalculations

-Electrical distribution calculations

-I&CInstrument uncertainty calculations

~ Peer review

-l71 Design Inspection calculations

-20 functional calculations Short Tenn Assessment Results - Issue ¹1 Short Term Assessment Results-Issue ¹1 Electrical Mechanical Other

'EP functional calculations Total Reviewed 32 3

79 16 28 3

139 22

'eer Review

-Team Inspection-Management involvement

-Additionto thc vcriTication Safety'related systems

-Emergency core cooling water

-Essential service water

-Containment spray

-Auxiliatyfccdwatcr

-Eicctrical distribution

-Chemical volume and control Short Term Assessment Results-Issue ¹1 Short Term Assessment Results -Issue ¹1

~ Peer review results

-Administrative issues

-Technical quest'tons raised (10)

-No effect on system operability We have confidence that AEP calculations are sufficiently conservative to assure system operability

~ Achieved through

-'The peer review results

-Our reconstitution programs

-Conclusion ofsafety system functional inspections performed on the ESW and electrical distribution aystctlls

Short Term Assessment Results-Issue ¹2 Short Tenn Assessment Results - Issue ¹2

'on-safety related system interface

-Effect on safety related system performance

-Selection process forrcvicw

~ Safety &,nan~ety related systems

. 'ignigcauce ofinterface withsafety related systems

~ Potentially unicvtcwed tost/failure modes

-Comparison with maintenance rule risk significance

'on-safety related system evaluations

-Modifiedcontrol air system

-Reactor control system

-Condcnsatc/

fcedwaterrmain stcam

-Circulating water

~

-Non-essential service water

.Electricaldistribution

-Pressuriscr heaters u No adverse effects Short Tenn Assessment Results - Issue ¹2 Short Tenn Assessment Results - Issue ¹3

'onclusion

-Postulated failures ofnon.safety related systems do not affect safety system operability e Appropriate application ofprocess measurement effects

-Team approach with industry consultants

-Compared AEP engineering guides to industry ttandards

-Appropriate process measuremcnt effect Bemoulli effect on level instrumentation

-Non.standard process location

-No guidance in engineering guides Short Tenn Assessment Results-Issue ¹3 Short Tenn Assessment Results - Issue ¹3 Bcmoulli effect on level instrumentation

-Allsafety relet@I level instruments cvalusted

-Condensate storage tank

'fcct is present but iaslgnigcaut

-Mid-loopRCS

'tfcct ls present but iasignigcant

-RVLlS iEtfcct is present and was tuctudot

-Level instruments appropriately account for Bcrnoulli effect bias e Bemoulli effect on level instrumentation

-idcC <<ngineering guide rcviscd

-Calculations account foithe flowinduced effects on process level instruments

Short Tenn Assessment Results - Issue ¹3 Short Tenn Assessment Results-Issue ¹3

'tructures as systems

-Structural and mechanical functions

-Functions may not bc survcilled

'tructures considered

-Containmcnt

-Auxiliarybuilding walls

-Control room complex

-Forebay and discharge vault o AuxiliaryBuildingInterior Walls

-HELBanalyses in 1996

-HELBboundary drawings Containment complex structure

-Structural integrity

-Multiplycompartments

-Interior flowpaths to support ECCS functions Short Tenn Assessment Results - Issue ¹0.,

Short Tenn Assessment Results - Issue ¹5 o Containment attributes

-Multkllsciplineinspection team

-Focused on perfonnance attributes

-Technical and housekeeping questions raised

-Actions were taken to disposition findings

-No new issues raised that affect operability Applicationofsingle failure criteria

-"Ftuiure to run" scenarios are considered ln analyses by both Westinghouse and AEP

-Crossied safety-related system evaluations

-Essential service water system

~ Normsl pocsatkxt

-AFW,CVCS, CCW, ESW, clectricat distribution o Emergency crossde Short Tenn Assessment Results o Conclusion

-Results firmlysupport our conclusion, there exists reasottabie assurance that the problems ofthe type found during the Design Inspection do not impact operability ofthe other safety systems A enda Cene Htrpstrkk latroductloa Jcb Klnasccd Nl Rcctreutsttoa Sump Inventory N4 ES LS Switchover Procedure NS Boctdcoksae to RWST Ns Recirculation Sump Ycnttna Paul Schocpf rrr Hbrous Mstcrtst la Contsfnmcnt NS SAeor Cooldown N6 RHR Suction ValveAu~

NS Compressed AlrOvcrprcssure Stoa Farhnr NN lastnuncnt Unccrtslnty Joel Wlebe Short Tenn Asscssmcnt Development AlBlind s~

  • ddt~A ~orOp r Mttyol S

toms

Cene HtspaMk Jcb IQngsced Paul Schocpf Stan Farfow Joel Wcbe Jim Kobyra AlBUnd A endN Introduction Nl Rcclrculadon Sump Inventory N4 KS IDSwitchover Procedure NN Backlcakage to RWST NI Rcclrculadon Sump Vcndng Ny Hbrous MatcrhLI ln Containment N3 36-hour CooMown Nd RHR Sucdon Valve AuloClose NS Comprcsscd AirOverpressure NP Instrument Uncertainty Short Torus Asscssmcnt Dcvelopmcnt Short Term Assessment Results Addidonal Amuran<<e ofOpcrabiUty of S

terna Conclusion

I r

/

~

,8 t

~4 h at' it V%p C'y

'V

~t S

"i C

'1<

0

I Confirmatory Action Letter Issue 1

Re i u

it Tt ittttt ttt g

N J>>U 8

inactive Sump 6t2' Active Sump 602-10'g8'-g

'6IO'4'eactor Cavity 1

11 1'umps used to cool the reactor and containment building may not have enough water supply to allow long-term operation of the systems.

AEP Commitment Analyses willbe performed to demonstrate that the 'recirculation sump level is adequate to prevent vortexing, or appropriate modifications willbe made.

I

~

~

('ontainmcnt Spr~y t(;rS) t~nvcr tfppcsc Cont.

(oritI:

Nozdcs Nozzle Uquld I'",.:., Steam Reactor,'ti(YS C

S Resolution

~ Analyses demonstrated emergency core cooling system/containment spray system operability.

~ Determined that sump level willremain above 602'0" throughout long-term recirculation phase.

~ Submitted Technical Specification amendment to credit more existing ice mass and other contributing sources of water in sump inventory calculations.

vh vh Fan stalnveU Accumuhtor Rooms Inactive Sump Nozzle ice via Melt RelueUng and Canal Condensed Orahs Steam Active Sump Reactor Cavity 4>>t 47z>>Y

I

~

r I

Confirmatory Action Letter Issue 4 I

R i

tt i tt t.ower

('.ont.

Nor~los

tfppcr, Cttntri-Noxztcs' rett.llnlttclltspnly t( 1st hmnnutators tcc Steam ttcactor li('('8

(.out;ult Systrnn

('undcnscr rs t(WZt'g~+Ltt Current procedures implementing switchover from the Refueling Water Storage Tank (RWST) to the containment sump may not be adequate for long-term, post-accident operations.

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g asltarcaN steers re JOWLS AEP Commjtment Changes to the emergency procedure used for switchover of the emergency core cooling and containment spray pumps to the recirculation sump willbe implemented.

These changes willprovide assurance there willbe adequate sump volume, with proper consideration of instrument bias and single failure criteria.

Resolution

~ Prepared, validated and trained all operating crews on revisions to ES-1.3 "Transfer to Cold Leg Recirculation". '

Revision reasonably assures an adequate recirculation sump level and eliminates the potential single failure vulnerability that existed during the transition from injection to recirculation phase.

~ RWST water level tap was relocated to account for the bias that may have existed.

~ The RWST, recirculation sump, ECCS and CTS pumps are operable with ES-1.3

. Revision 5.

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Confirmatory Action Letter Issue S Wa W T

'-F R i Tl i ii Testing of Mini-FlowRecirculation Lines may not be adequate to assure that back-leakage to RWST willnot exceed acceptable levels during a design basis accident.

AEP Commitment Only two of six mini-flowrecirculation line valves have leakage verification tests.

Justification willbe provided that the total leakage for the six valves is less than 10 gallons per minute (gpm) to ensure that Part 100 limits are not exceeded ifcontainment sump water were to leak back to the RWST during a design basis accident.

Resolution

~ Testing of the valves not previously tested showed that total leakage for these paths back to the RWST was well below 10 gpm value in the UFSAR.

~ Included affected flow paths in the In-Service Testing program.

~ Implemented new procedures: seat leakage testing of valves at each refueling outage to ensure < 10 gpm total leakage.

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Confirmatory Action Letter Issue 2 T

I Venting of air underneath the roof of the containment building recirculation sump may not be adequate.

AEP Commitment Venting willbe re-installed in the recirculation sump cover. The design will incorporate foreign material exclusion requirements for the sump.

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~ Venting has been reinstalled in the

~

recirculation sump cover in both TTnits.

~ Vents incorporate screening to satisfy the

'oreign material exclusion requirements.

~ Recirculation sumps have been returned to their approved design configuration.

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Confirmatory Action Letter Issue 7 l

1 I

11 Fibrous material located in containment buildings may clog the recirculation sump.

AEP Commitment Removal of fibrous material from containment that could clog the recirculation sump willbe completed.

Resolution

~ Containment inspections were conducted in Units 1 and 2.

~ identified and removed unencapsulated fibrous insulation materials from 12 locations in Unit 1, 15 locations in Unit 2, in the aiuxulus and instrument rooms.

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Confirmatory Action Letter Issue 3 1

1 lf Calculation needs to be performed that shows, one train of cooling water is sufficient to remove the units from service.

AEP Commitment Analyses willbe performed that will demonstrate the capability to cool down the units consistent with design basis requirements and necessary changes to procedures willbe completed.

Resolution

~ Thermal hydraulic analysis concluded that a single train of residual heat removal/component cooling water/essential service water is capable of cooling down the reactor coolant system in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

~ Operating procedure revisions were made to reflect a higher maximum component cooling water supply temperature limit (increased to 120'F).

Four pipe supports were also modified.

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  • Confirmatory Action Letter Issue tl lH I

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Conflicts between operating procedures and Technical Specifications for Residual Heat Removal Suction Valve Autoclosure Interlock.

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Heal fxcrraeger Ivrvveer Cornea Welvr AEP Commitment ATechnical Specification change to allow operation in Mode 4 with the RHR suction valves open and power removed is being processed.

Approval of this change by the NRC willbe required prior to restart.

Resolution

~ Submitted a proposed Technical Specification change to the NRC that eliminates the need for the RHR Suction Valve Autoclosure interlock when in a shutdown cooling configuration. The Technical Specification change has been approved by the NRC.

~ 200 Air Confirmatory Action Letfer Issue 5 Overpressure protection for some components served by the compressed air system may not be adequate in the event of a postulated air regulator failure.

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/Valve 500 Alr AEP Commifmenf Overpressure protection willbe provided downstream of the 20 psig, 50 psig, and 85 psig control air regulators to mitigate the effects of a postulated failed regulator.

AeCrIarcr 050 Atr Q AacrAIcur Resolution

~ Installed redundant, safety-grade relief valves on all of the control headers (20 psig, 50 psig, and 85 psig) and eliminated overpressure potential.

~ Eliminated potential for common-mode failure due to overpressurization.

~ Safety related systems and components supported by the control air system are operable.

Confirmatory Action Letter Issue g 1

I I

1 I

Need to incorporate instrument uncertainties into procedures and analyses.

AEP Commitment Emergency procedures and other important-to-safety procedures, calculations, or analyses willbe reviewed to account for instrument uncertainties.

Resoiution

~ Actions completed

- Reviewed level instrumentation For velocity effect.

- Reviewed and revised emergency operating procedures for switchover to recirculation.

- Reviewed and revised technical specification surveillance procedure used by Operations.

- Generated parameter list for technical specification compliance.

- Generated Administrative control procedures.

- Reviewed EOP Setpoint Documentation.

- Reviewed License Bases.

- Addressed all related non-programmatic Unresolved Issues from the inspection report.

- Completed Plant Specific Methodology Manual.

~ Continuing Actions

- Developed a plan to:

- control instrument uncertainty and incorporate it into procedures, calculations, and analyses.

- complete reviews, training, and calculations by December 1, 1998.

- Checklist, based on current NRC guidelines, willbe used to review existing and future instrument uncertainty calculations.

- Developing a plant specific methodology manual to calculate instrument uncertainties; manual willbe an expansion of existing engineering guide.

- Developing administrative controls to ensure that instrument uncertainties are considered whenever procedures, calculations and analyses are developed or revised.

-'ntegrating instrument uncertainty program with the upgraded normal operating procedure and emergency operating procedure reviews.

Purpose To assess whether issues similar to the eight listed in the confirmatory action letter (CAL) may exist in other safety systems, and ifthey do, to determine whether they affect system operability.

Roof Cause Analysis of other Oesign Inspection Issues Root causes of other issues raised during the design inspection that were not included in the CALwere also reviewed.

'oot Cause Investigation and Evaluation ol CALissues Independent teams comprised of AEP Nuclear Generation Group and outside technical analyst(s) conducted root cause evaluations of the eight CAL issues.

Independent Review by Senior Industry Peers Allfinal root cause analyses were reviewed by independent senior industry peers.

Senior Management Review and Action A group of senior managers and staff reviewed the root causes of the CALand AE issues.

Action plans were developed to further assess those issues that had the potential to create operability concerns in other systems.

Identified Five Engineering Issues Senior management endorsed action plans for five engineering issues identified for short-term assessment that had both generic implications and were deemed likely to affect safety-related system operability.

~ Some analyses were found to contain errors and incorrect assumptions.

~ Some containment attributes, such those related to sump performance, were not adequately preserved.

~ Failure to consider a credible failure mode on a non-safety-related system interfacing with a safety-related system.

~ Failure to consider level instrument bias due to Bernoulli effect.

~ improper application of single failure criterion.

Evaluation and Revietv Each engineering issue was evaluated and reviewed by experienced teams of engineering and management personnel.

Each evaluation considered existing system assessments, design assessments, safety analyses and reports.

These documents helped focus review efforts in specific areas of vulnerability.

Conclusion The short-term assessment provides reasonable assurance that issues of the type found during the design inspection do not impact the operability of other safety systems at Cook Nuclear Plant.

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CISCTRK Charts Matrices represent a series of critical reviews condu'cted to provide reasonable assurance that safety systems willperform their intended functions. Included in the matrices are short term assessments conducted after the design inspection and previously performed safety system functional inspections (SSFI). These reviews were performed by the NRC, contractor, and AEP Nuclear Generation Group staffs.

Conclusion Matrices firmlysupport the conclusion that there is reasonable assurance that the safety systems are capable of fulfillingtheir intended design function.

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