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{{#Wiki_filter: | {{#Wiki_filter:b IU '[..i L.1 i l e. c. | ||
b IU '[. .i L.1 i | . wTi Li: a WAs 3 | ||
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NORTHERN | :e | ||
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Septtsaber 12, 1977 thb &b h Mr. 1. G. Xeppler, Director R2gion III office of Inspection and Enforcement United States Nuclear Regulaton Cosamission 799 Roosevelt Road Glen Ellyn, IL | g,, | ||
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NORTHERN STATES POWER COMPANY Ponticello Nuc1 car Generating Plant | |||
.% nticello,FN 55362 9 | |||
Septtsaber 12, 1977 thb &b h Mr. 1. G. Xeppler, Director R2gion III office of Inspection and Enforcement United States Nuclear Regulaton Cosamission 799 Roosevelt Road Glen Ellyn, IL 60137 | |||
==Dear Mr. Keppler:== | ==Dear Mr. Keppler:== | ||
MATICEl.ID NJCIIAR GDiERATING PIMir Docket No. 50-263 License No. DPR-22 Previous correspondence with your office on Septcseher 15, 1975, discussed re-porting of refueling outage valve leakage pmblems. | |||
MATICEl.ID NJCIIAR GDiERATING PIMir Docket No. 50-263 License No. DPR-22 Previous correspondence with your office on | For the current refueling outage we will report penetration and isolation valve leakage rates which ex-cced the acceptance criteria outlined in section 4.7.A.2.f of the Technical Specification in a similar anaer. | ||
outage we will report penetration and isolation valve leakage rates which ex-cced the acceptance criteria outlined in section 4.7.A.2.f of the Technical Specification in a similar anaer. Excessive Icakage rates will be reported within 24 hours or no later than the first working day following the event, Office of Inspection and by telephone and | Excessive Icakage rates will be reported within 24 hours or no later than the first working day following the event, Office of Inspection and by telephone and telecopy to the Director, Region III,d within 14 days following Enforcement. | ||
In acconlance with these reporting nquimments, notification is herchy nede that the fo11cming valves were found to leak in excess of th'c acceptance criteria for local leak tests specified in Section 4.7.A.2.f of the Technical .epecifi-cations: | A Licensee Event Report will be submitte rep::ii of all Icaking valves. | ||
Main Steam Drain Isolation Valve, FD 2373 | In acconlance with these reporting nquimments, notification is herchy nede that the fo11cming valves were found to leak in excess of th'c acceptance criteria for local leak tests specified in Section 4.7.A.2.f of the Technical.epecifi-cations: | ||
Main Steam Outboart) Isolation Valve, AD 2-86A-Yours yery truly, M | Main Steam Drain Isolation Valve, FD 2373 Main Steam Outboart) Isolation Valve, AD 2-86A-Yours yery truly, M | ||
. L. R. Eliason. | |||
Plant Manager 8y3202 | |||
AD | ~ | ||
AD s | |||
Minnesota Pollution Control Agency | 05 gg Dinctor, Office of Management Information 6 cc: | ||
Program Contml G. Charnoff Minnesota Pollution Control Agency Attn: | |||
J. W. Fennan - | |||
1ile Copy sent bv telcennier to Reppler., | 1ile Copy sent bv telcennier to Reppler., | ||
thW $: 9 L LSg 9 | |||
p z. | |||
.m m- | |||
,}} | |||
Latest revision as of 02:27, 14 December 2024
Text
b IU '[..i L.1 i l e. c.
. wTi Li: a WAs 3
_3
- e
_a, g.,
g,,
m...
- (
w a
. uw.&
NORTHERN STATES POWER COMPANY Ponticello Nuc1 car Generating Plant
.% nticello,FN 55362 9
Septtsaber 12, 1977 thb &b h Mr. 1. G. Xeppler, Director R2gion III office of Inspection and Enforcement United States Nuclear Regulaton Cosamission 799 Roosevelt Road Glen Ellyn, IL 60137
Dear Mr. Keppler:
MATICEl.ID NJCIIAR GDiERATING PIMir Docket No. 50-263 License No. DPR-22 Previous correspondence with your office on Septcseher 15, 1975, discussed re-porting of refueling outage valve leakage pmblems.
For the current refueling outage we will report penetration and isolation valve leakage rates which ex-cced the acceptance criteria outlined in section 4.7.A.2.f of the Technical Specification in a similar anaer.
Excessive Icakage rates will be reported within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or no later than the first working day following the event, Office of Inspection and by telephone and telecopy to the Director, Region III,d within 14 days following Enforcement.
A Licensee Event Report will be submitte rep::ii of all Icaking valves.
In acconlance with these reporting nquimments, notification is herchy nede that the fo11cming valves were found to leak in excess of th'c acceptance criteria for local leak tests specified in Section 4.7.A.2.f of the Technical.epecifi-cations:
Main Steam Drain Isolation Valve, FD 2373 Main Steam Outboart) Isolation Valve, AD 2-86A-Yours yery truly, M
. L. R. Eliason.
Plant Manager 8y3202
~
AD s
05 gg Dinctor, Office of Management Information 6 cc:
Program Contml G. Charnoff Minnesota Pollution Control Agency Attn:
J. W. Fennan -
1ile Copy sent bv telcennier to Reppler.,
thW $: 9 L LSg 9
p z.
.m m-
,